ML19031C033
ML19031C033 | |
Person / Time | |
---|---|
Site: | Salem |
Issue date: | 04/06/1978 |
From: | Librizzi F Public Service Electric & Gas Co |
To: | Grier B NRC/IE, NRC Region 1 |
References | |
LER 1978-015-04 | |
Download: ML19031C033 (2) | |
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Category:Letter
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Finney, USNRC Senior Resident Inspector, Salem (X24) Mr. P. Mulligan, Manager IV, NJBNE Mr. R. Braun, President and Chief Nuclear Officer — Nuclear Mr. T. Cachaza, Salem Commitment Tracking Coordinator Mr. L. Marabella, Corporate Commitment Tracking Coordinator Mr. D. Lafleur, Salem Regulatory Assurance NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION 01-2014) t, , .1 • '., LICENSEE EVENT REPORT (LER) 'S ree Page 2 or required number of digits/characters for each block) APPROVED BY OMB: NO. 3150-0104 EXPIRES: 0113112017 Estimated burden per response to comply with this mandatory collection request: 80 hours. Reported lessons learned are Incorporated Into the licensing process and fed back to Industry. 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Elevation Personnel Airlock Inoperable ML19031B0361978-08-24024 August 1978 LER 1978-044-03 for Salem Unit 1 Inoperability of No. 11 S/G Feedwater Flow Channel 2 ML19031A8951978-08-14014 August 1978 LER 1978-041-03 for Salem Unit 1 Excessive Quadrant Power Tilt Ratio During Power Escalation ML19031B0391978-08-0303 August 1978 LER 1978-040-03 for Salem Unit 1 Inoperability of Makeup Valve from Demineralized Water Plant ML19031B5121978-08-0202 August 1978 Licensee Event Report 1978 for Reportable Occurrence 78-39/03L Re No. 13 Containment Fan Foil Unit Inoperable ML19031B5111978-08-0202 August 1978 Licensee Event Report 1978 for Reportable Occurrence 78-38/03L Re No. 11 Steam Generator Flow Channel II Inoperable ML19031B1651978-07-20020 July 1978 LER 1978-035-03 for Salem Unit 1 Loss of Power to No. 2 Station Power Transformer ML19031B5131978-07-20020 July 1978 Licensee Event Report 1978 for Reportable Occurrence 78-36/03L Re Vital Bus Under Voltage Relay Setting Outside Technical Specification Limit ML19031C0301978-07-20020 July 1978 07/20/1978 Letter Reportable Occurrence on Non-Radwaste Sampling for Suspended Solids ML19031B1671978-07-12012 July 1978 LER 1978-026-03 for Salem Unit 1 Failure of Motor Operated Valve ML19031C0311978-07-12012 July 1978 07/12/1978 Letter Reportable Occurrence on Missed Surveillance of Monthly Functional Test of Steam Generator Blowdown Radiation Monitoring Channels ML19031B0401978-07-12012 July 1978 LER 1978-033-03 for Salem Unit 1 No. 11 Steam Generator Steam Flow Channel II ML19031B5151978-07-10010 July 1978 Licensee Event Report 1978 for Reportable Occurrence 78-30/03L Re Control Bank and Shutdown Rod Misalignment ML19031B0411978-06-30030 June 1978 LER 1978-027-03 for Salem Unit 1 Malfunctioning Exterior Door of Containment Entry Air Lock ML19031B5171978-06-30030 June 1978 No. 1 - Licensee Event Report 1978 for Reportable Occurrence 78-28/03L Re Inoperable 100 Ft. Elevation Air Lock Interior Door ML19031C0321978-06-28028 June 1978 06/28/1978 Letter Reportable Occurrence on Non-Radwaste Sampling for Suspended Solids Analysis ML19031A8191978-06-21021 June 1978 LER 1978-029-01 for Salem Unit 1 Inoperability of Two Power Range Channels During Training Startups ML19031B5191978-05-15015 May 1978 LER 1978-025-03 for Salem Generating Station Unit 1 Re Missed Tech. Specification Surveillance: 4.8.2.4.1 DC and 4.8.2.2 AC Breaker Alignment and Power Availability ML19031B5201978-05-10010 May 1978 LER Supplemental Report for Reportable Occurrence 77-43/03L Re Inoperable No 12 S/G Channel 3 Due to Failed Pressure Transmitter ML19031B5211978-04-27027 April 1978 04/27/1978 Letter Reportable Occurrence on Excessive Concentration of Iodine in Milk Sample Collected at Environmental Sampling Location ML19031B0421978-04-17017 April 1978 LER 1978-021-03 for Salem Unit 1 Missed Surveillance of Fluoride Sample ML19031A8961978-04-17017 April 1978 LER 1978-022-01 for Salem Unit 1 Seismic Test Results for NEMA 12 Enclosures ML19031B5221978-04-11011 April 1978 LER 1978-080-03 for Salem Unit 1 Inoperability of 1B Diesel ML19031C0331978-04-0606 April 1978 04/06/1978 Letter Reportable Occurrence on Non-Radwaste Sampling for Suspended Solids Analysis ML19031B5231978-04-0606 April 1978 LER 1977-042-03 for Salem Unit 1 Inoperability of Channel III Pressurizer Level ML19031A8971978-04-0606 April 1978 LER 1978-018-03 for Salem Unit 1 Excessive Trip Setpoint During Functional Test on PWR Range Channel N43 ML19031A8981978-04-0505 April 1978 LER 1978-017-03 for Salem Unit 1 Tilt Ratio During Power Escalation 2024-05-09 |
Text
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- Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone 201 /622-7000 Mr. Boyce H. Grier Director of USNRC Off ice of Inspections and Enforcements Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406 0
\J1
Dear Mr. Grier:
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 78-15/04L Pursuant to the requirements of Salem Generating Station Unit No. 1 Environmental Technical Specifications, we are submitting Licensee Event Report for Reportable Occurrence 78-15/04L.
This report is required within thirty (30) days of the occurrence.
Sincerely yours,
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,;/)' L l VL l:_l'"'l --"\
F. P. Librizzi General Manager -
Electric Production CC: Director, Office of Inspection and Enforcement (30 copies)
Director, Office of Management Information and Program Control The Energy People 95-2001 300M 8-7'
- ~ *~ Report Number :
, Report Date:
Occurrence Date:
Facility:
7ji15/04L
. 4-,r/78" 3/9/78 Salem Generating Station l">
Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Missed Surveillance: Non-Radwaste Sampling for Suspended Solids Analysis CONDITIONS PRIOR TO OCCURRENCE:
N/A DESCRIPTION OF OCCURRENCE:
On the occasions summarized below, treated effluent was released from the non-radioactive liquid waste treatment basin, but a sample was not collected for suspended solids analysis.
January 1, 2, 7, 10, 14, 15, 16, 21, 24, 25, 26, 27, 28, 29, 30 February 7, 21 (Ref.: Section 2.2.2 of Appendix "B" to Operating License DPR-70)
The missing samples were identified upon records review in light of Occurrence 78-10/04L.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
The cause of this occurrence was personnel error. Corrective action as stated in LER 78-10/04L had not yet been implemented.
ANALYSIS OF OCCURRENCE:
N/A CORRECTIVE ACTION:
Responsibility to collect samples was re-assigned from demineralizer plant operator (day shift) to midnight shift Health Physics Technician.
FAILURE DATA:
N/A Prepared by_,....~~T~."-'L~*--S~p~e=n~c~e=r=--~~~~
Manage Statior SORC Meeting No. 14-78
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