ML19031B515

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Licensee Event Report 1978 for Reportable Occurrence 78-30/03L Re Control Bank and Shutdown Rod Misalignment
ML19031B515
Person / Time
Site: Salem  PSEG icon.png
Issue date: 07/10/1978
From: Librizzi F
Public Service Electric & Gas Co
To: Grier B
NRC/IE, NRC Region 1
References
LER 1978-030-03L
Download: ML19031B515 (4)


Text

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PS~G Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101

  • Phone 201 /622-7000

'° r-* I July 10, 1978 CJ

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Mr. Boyce H. Grier -!'"l

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Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

LICENSE NO. DPR~70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 78-30/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 78-30/03L. This report is required within thirty (30) days of the occurrence.

Sinc::erely yours,

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F. P. Librizzi General Manager -

Electric Production CC: Director, Off ice and Enforcement of Insp~ctiq'lJ.lf.~m ~1fflitHJ ftlfDllLlVf.'J

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Director, Office of Management Information and Program Control

( 3 copies) 95-2001 300M 10-74 '

Report Number:

Report Date:

e 78-30/03L 7/10/78 Occurrence Date: 6/14/78 Facility: Salem Generating Station Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Control Bank and Shutdown Rod Misalignment Control Banks: A, B, C, D Shutdown Rods: lSAl 1SA3 CONDITIONS PRIOR TO OCCURRENCE:

Startup Mode 2; Reactor Power: 1%

DESCRIPTION OF OCCURRENCE:

At 0050 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br />, control room personnel identified control banks A, B, C and D and shutdown rods lSAl and 1SA3 as being greater than 12 steps below the bank demand position. Technical Specification 3.1.3.l(b) was implemented. At 0649 hours0.00751 days <br />0.18 hours <br />0.00107 weeks <br />2.469445e-4 months <br />, the reactor was tripped from 1% power to comply with the Action Statement. At 1145 hours0.0133 days <br />0.318 hours <br />0.00189 weeks <br />4.356725e-4 months <br />, the above control and shutdown rod position indicators had been recalibrated and Action Statement 3.1.3.1 was terminated.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

Control bank position indicators had not been calibrated at the operating position. When control banks A, B, C and D were with-drawn to the critical position, the indicators were greater than 12 steps from the bank demand.

Shutdown rods lSAl and 1SA3 position indicators had drifted to greater than 12 steps.

Non-linear scales and instrument drift was the cause of this occurrence.

ANALYSIS OF OCCURRENCE:

Technical Specification 3.1.3.1.b states that with more than one full or part length rod inoperable or misaligned from the bank demand posi-tion by more than + 12 steps (indicated position), be in Hot Standby within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

~-0 LER 78-30/03L In compliance with the above requirement, the unit was placed in Hot

  • I Standby within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and remained in that condition until the rod position indicators were returned to operable status at 1145 hours0.0133 days <br />0.318 hours <br />0.00189 weeks <br />4.356725e-4 months <br />.

CORRECTIVE ACTION:  !

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'I The rod position indicators on Control Banks A, B, C, D and Shutdown I Rods lSAl and lSA3 were recalibrated to within 12 steps of the bank position indicator. Comparison check confirmed operability.

FAILURE DATA:

N/A Prepared by T. L. Spencer

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Manager - Salem Generating Station SORC Meeting No. 39-78

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LICENSEE EVENT REPORT

,,,. - ~~NTROL BLOCK: .____.__..___.__._I-'-""""'"---CD 6

(PLEASE PRINT OR TYPE. REQUIRED INFORMATION!

I [il~] I N I 'J I s I G I s I 1 IG)I 0 I 0 I - I 0 I 0 I 0 I 0 I 0 I - I 0 I 0 101 4 11 I l I l I 1 181 I I0 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE :30 57 CAT 58 CON'T

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7 8

~~~~ LrJ© I o I s I o I o I o I 2 I 1 I 2 101 o I 6 I 1 I 4 I 1 I s IG)I o I 1 11. I o I7 I s 10 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@

lIITJ J During startup, the reactor operator identified control banks A, B, C,

[]ID D and shutdown rods lSAl and 1SA3 were found to be greater than 12 step§

~ from the bank demand position. Within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, reactor was manually ITTIJ tripped from 1% power to comply with T.S. Position indicators were re- J

[ill] calibrated and confirmed to be operable. This is the third.occurrence of this type.

CITiJ C£:ill 80 7 8 9 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SU8CODE COMPONENT CODE SUBCODE SUB CODE ITTIJ 7 8 9 I I IFI@ ~ w@ 1r1N1s1T1R1u1e 10 11 12 13 18 L!J 19

~@

20 SEQUENTIAL OCCURRENCE REPORT REVISION

(.":;\ LE R/RO CV ENT YEAR REPORT NO. CODE TYPE NO.

~ REPORT NUMBER I7 I 8 I 11 1013101 1_,.....I JolJI L1J L=1 LlJ 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN (.'.;;\ ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS ~ SUBMITTED FORM SUB. SUPPLIER MANUFACTURER L§J@L!J@ UJ@ ~@ I o I o I o I s401 lYJ@ LBJ@ [BJ@ I w I 1I2 Io I@

33 34 35 36 37 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @

QI£J The cause of this occurrence was instrument drift. Control banks were

[JJJJ calibrated at the bottom position. After withdrawal, non-linear ranges CIITI resulted in out of spec indication. Recalibration of control and shut-

!Jli] down rods corrected the greater than 12 step condition.

IJJI]

7 8 9 80

~

FACILITY STATUS  % POWER OTHER STATUS @ METHOD OF DISCOVERY DISCOVERY DESCRIPTION ~

[1E] ~@ I 0 I 0 I l 1@)11-_ _ _ N/_A_ __. Lg_JG)~I--'S~u.;.;.;;;;.r~v~e~i~l~l~a~n;;..:;..;;.c~e--'T~e~s~t~----------'

8 9 10 12 11 44 45 46 80 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY@ LOCATION OF RELEASE@

[2EJ ~@) W@) I....._.___N.._/A_ _ _....., N/A 8 9 10 11 44 45 80 PERSONNEL EXPOSURES ~

NUMBER (.:;::;\TYPE DESCRIPTION CD2l 1 o, o 1 0J0w@.____....:N=/=A:..___ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _____.

7 8 9 11 12 13 80 PERSONNEL INJURIES (,":;\

NUMBER DESCRIPTION~

~ I 0 I 0 I 0 l@i.._____-=N:;....;A;.::.....__ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ____,

8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY t4:j\

TYPE DESCRIPTION ~

[QI) ~@)L----'----~}~J/....:A~-----------------------'

7 8 9 10 80 PUBLICITY G\ NRCUSEONLY ISSUEDQ DESCRIPTION~ "'

ITTIJ Wei...____ _ _ _ _ _N......_A_ _ _ _ _ _ _ _ _ _ _ _ ___. II II I I I I II II I ~

8 9 10 68 69 80 c;;

NAME OF PREPARER _ _ _ _ _ T_._L_._s_.p~e_n_c_e_r______ *( 609) 36 5-7 000 0 Q.

PHONE: Salem Ext. 52 8 (j