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| | issue date = 01/27/2012 | | | issue date = 01/27/2012 |
| | title = Summary of the Staff'S Review of the Steam Generator Tube Inservice Inspection Refueling Outage 25 | | | title = Summary of the Staff'S Review of the Steam Generator Tube Inservice Inspection Refueling Outage 25 |
| | author name = Paige J C | | | author name = Paige J |
| | author affiliation = NRC/NRR/DORL/LPLII-2 | | | author affiliation = NRC/NRR/DORL/LPLII-2 |
| | addressee name = Nazar M | | | addressee name = Nazar M |
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| =Text= | | =Text= |
| {{#Wiki_filter:UNITED NUCLEAR REGULATORY WASHINGTON, D.C. 20555-0001 January 27, 2012 Mr. Mano Nazar Executive Vice President and Chief Nuclear Officer Florida Power and Light Company P.O. Box 14000 Juno Beach, Florida 33408-0420 TURKEY POINT UNIT 3 - | | {{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 January 27, 2012 Mr. Mano Nazar Executive Vice President and Chief Nuclear Officer Florida Power and Light Company P.O. Box 14000 Juno Beach, Florida 33408-0420 |
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| | ==SUBJECT:== |
| | TURKEY POINT UNIT 3 - |
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| ==SUMMARY== | | ==SUMMARY== |
| OF THE STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 (TAC NO. ME6351) | | OF THE STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 (TAC NO. ME6351) |
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| ==Dear Mr. Nazar:== | | ==Dear Mr. Nazar:== |
| By letters dated April 19 and November 23,2011 (Agencywide Documents Access and Management Systems (ADAMS) Accession Nos. ML11119A006 and ML 11340A074), Florida Power and Light Co. (FPL) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. These reports were submitted in accordance with Turkey Point Unit 3 Technical Specifications (TSs) Sections 4.4.5.1, 4.4.5.2 and 6.9.1.8. A summary of the NRC staff's evaluation of the Turkey Point Unit 3 Fall 2010 Refueling Outage 25 SG tube inspection results is enclosed. | | |
| Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML 110030005). | | By letters dated April 19 and November 23,2011 (Agencywide Documents Access and Management Systems (ADAMS) Accession Nos. ML11119A006 and ML11340A074), Florida Power and Light Co. (FPL) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. These reports were submitted in accordance with Turkey Point Unit 3 Technical Specifications (TSs) Sections 4.4.5.1, 4.4.5.2 and 6.9.1.8. |
| The NRC staff concluded that FPL provided the information required by the Turkey Point Unit 3 TSs and that no addition ollow-up is required at this time. Since ely, // ( ///7 /t'son c. | | A summary of the NRC staff's evaluation of the Turkey Point Unit 3 Fall 2010 Refueling Outage 25 SG tube inspection results is enclosed. Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML110030005). The NRC staff concluded that FPL provided the information required by the Turkey Point Unit 3 TSs and that no addition ollow-up is required at this time. |
| L/PPlant Licensing Branch 11-2 Division of Operating Reactor licensing Office of Nuclear Reactor Regulation Docket No. 50-250 | | Since ely, ~. // |
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| | /t'son pa;ge,'pJ:/;.:::- |
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| | L/PPlant Licensing Branch 11-2 Division of Operating Reactor licensing Office of Nuclear Reactor Regulation Docket No. 50-250 |
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| ==Enclosure:== | | ==Enclosure:== |
| | As stated cc w/encl: Distribution via Listserv |
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| As stated cc w/encl: Distribution via Listserv UNITED NUCLEAR REGULATORY WASHINGTON, D.C. 20555-0001
| | UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 |
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| ==SUMMARY== | | ==SUMMARY== |
| OF THE U.S. NUCLEAR REGULATORY COMMISSION STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 FLORIDA POWER AND LIGHT COMPANY TURKEY POINT UNIT 3 DOCKET NO. 50-250 By letters dated April 19 and November 23, 2011 (Agencywide Documents Access and Management Systems Accession Nos. ML 11119A006 and ML 11340A074), Florida Power and Light Co. (FPL, the licensee) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML 110030005). | | OF THE U.S. NUCLEAR REGULATORY COMMISSION STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 FLORIDA POWER AND LIGHT COMPANY TURKEY POINT UNIT 3 DOCKET NO. 50-250 By letters dated April 19 and November 23, 2011 (Agencywide Documents Access and Management Systems Accession Nos. ML11119A006 and ML11340A074), Florida Power and Light Co. (FPL, the licensee) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML110030005). |
| Turkey Point Unit 3 has three Westinghouse Model 44F SGs. The SGs have tubes that were hydraulically expanded into the tubesheet and are supported by Type 405 stainless steel tube support plates with broached quatrefoil holes. The Unit 3 SGs were placed into operation in 1982, and have thermally treated Alloy 600 tubing. The licensee provided the scope, extent, methods, and results of their SG tube inspections in the documents referenced above. In addition, the licensee described corrective actions (e.g., tube plugging) taken in response to the inspection findings. | | Turkey Point Unit 3 has three Westinghouse Model 44F SGs. The SGs have tubes that were hydraulically expanded into the tubesheet and are supported by Type 405 stainless steel tube support plates with broached quatrefoil holes. The Unit 3 SGs were placed into operation in 1982, and have thermally treated Alloy 600 tubing. |
| As a result of its review of the above documents, the NRC staff has the following comments/observations: No crack-like indications were detected during the outage. Tubes R6 C45 and R7 C45 in SG B were plugged, but not stabilized. | | The licensee provided the scope, extent, methods, and results of their SG tube inspections in the documents referenced above. In addition, the licensee described corrective actions (e.g., |
| Both of these tubes had shallow wear indications attributed to a suspected foreign object near the upper edge of the 2 nd tube support plate on the cold leg side (02C). The tubes were plugged but not stabilized since the expected wear rate is low. The tubes surrounding R6 C45 and R7 C45A at the 02C location will be examined during the refueling outage for Cycle 27 in 2013 and during future inspections to monitor for degradation and for migration of the suspected foreign object. This required action has been documented in the plant's corrective action program. Enclosure | | tube plugging) taken in response to the inspection findings. |
| -2 The licensee summarized the scope of inspections (primary and secondary side) as required by Technical Specification 6.9.1.8, "Steam Generator Tube Inspection Report." Based on a review of the information provided, the staff concludes that the licensee provided the information required by their technical specifications.
| | As a result of its review of the above documents, the NRC staff has the following comments/observations: |
| In addition, the staff concludes that there are no technical issues that warrant follow-up action at this time since the inspections appear to be consistent with the objective of detecting potential tube degradation and the inspection results appear to be consistent with industry operating experience at similarly designed and operated units.
| | : 1. No crack-like indications were detected during the outage. |
| January 27,2012 Mr. Mano Nazar Executive Vice President and Chief Nuclear Officer Florida Power and Light Company P.O. Box 14000 Juno Beach, Florida 33408-0420 TURKEY POINT UNIT 3 -
| | : 2. Tubes R6 C45 and R7 C45 in SG B were plugged, but not stabilized. Both of these tubes had shallow wear indications attributed to a suspected foreign object near the upper edge of the 2nd tube support plate on the cold leg side (02C). The tubes were plugged but not stabilized since the expected wear rate is low. The tubes surrounding R6 C45 and R7 C45A at the 02C location will be examined during the refueling outage for Cycle 27 in 2013 and during future inspections to monitor for degradation and for migration of the suspected foreign object. This required action has been documented in the plant's corrective action program. |
| | Enclosure |
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| ==SUMMARY==
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| OF THE STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 (TAC NO. ME6351)
| | : 3. The licensee summarized the scope of inspections (primary and secondary side) as required by Technical Specification 6.9.1.8, "Steam Generator Tube Inspection Report." |
| | Based on a review of the information provided, the staff concludes that the licensee provided the information required by their technical specifications. In addition, the staff concludes that there are no technical issues that warrant follow-up action at this time since the inspections appear to be consistent with the objective of detecting potential tube degradation and the inspection results appear to be consistent with industry operating experience at similarly designed and operated units. |
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| ==Dear Mr. Nazar:==
| | ML110030005). The NRC staff concluded that FPL provided the information required by the Turkey Point Unit 3 TSs and that no additional follow-up is required at this time. |
| By letters dated April 19 and November 23, 2011 (Agencywide Documents Access and Management Systems (ADAMS) Accession Nos. ML 11119A006 and ML 11340A074), Florida Power and Light Co. (FPL) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. These reports were submitted in accordance with Turkey Point Unit 3 Technical Specifications (TSs) Sections 4.4.5.1, 4.4.5.2 and 6.9.1.8. A summary of the NRC staff's evaluation of the Turkey Point Unit 3 Fall 2010 Refueling Outage 25 SG tube inspection results is enclosed.
| | Sincerely, IRA! |
| Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML 11 0030005).
| | Jason C. Paige, Project Manager Plant Licensing Branch 11-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-250 |
| The NRC staff concluded that FPL provided the information required by the Turkey Point Unit 3 TSs and that no additional follow-up is required at this time. Sincerely, IRA! Jason C. Paige, Project Manager Plant Licensing Branch 11-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-250 | |
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| ==Enclosure:== | | ==Enclosure:== |
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| As stated cc w/encl: Distribution via Listserv Distribution: | | As stated cc w/encl: Distribution via Listserv Distribution: |
| PUBLIC LPL2-2 RtF RidsNrrDorlLpl2-2 RidsN rrLABClayton RidsOgcRp RidsAcrsAcnwMailCenter RidsNrrDorlDpr RidsRgn2MailCenter CHunt, NRR KKarwoski. | | PUBLIC LPL2-2 RtF RidsNrrDorlLpl2-2 RidsN rrLABClayton RidsOgcRp RidsAcrsAcnwMailCenter RidsNrrDorlDpr RidsRgn2MailCenter CHunt, NRR KKarwoski. NRR RidsNrrPMTurkeyPoint RidsNrrDeEsgb ADAMSAccession NO.:ML11361A381 *8~ymemo OFFICE LPL2-2/PM LPL2-2/LA ESGB/BC (A) LPL2-2/BC LPL2-2/PM NAME JPaige BClayton VCusumano* DBroaddus JPaige (FSaba for) |
| NRR RidsNrrPMTurkeyPoint RidsNrrDeEsgb ADA MSA ccession NO.:ML 11361A381 | | DATE 12/28/11 12/28/11 12112111 1127112 1127/12}} |
| *8 OFFICE LPL2-2/PM LPL2-2/LA ESGB/BC (A) LPL2-2/BC LPL2-2/PM NAME JPaige BClayton VCusumano* | |
| DBroaddus JPaige (FSaba for) DATE 12/28/11 12/28/11 12112111 1127112 1127/12 OFFICIAL RECORD COPY}} | |
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Category:Letter
MONTHYEARML24023A0342024-02-0505 February 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0038 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) L-2024-010, Point Units 3 and 4, Seabrook, Duane Arnold, and Point Beach Units 1 and 2, Nuclear Property Insurance - 10 CFR 50.54(w)(3)2024-01-25025 January 2024 Point Units 3 and 4, Seabrook, Duane Arnold, and Point Beach Units 1 and 2, Nuclear Property Insurance - 10 CFR 50.54(w)(3) ML23341A2102024-01-22022 January 2024 LTR-23-0216-1 - Closure Letter - 2.206 Petition for License Renewal Plant Reactor Pressure Vessel Embrittlement ML23320A3062024-01-22022 January 2024 Issuance of Amendment Nos. 298 and 291 Regarding Revising the Fire Protection Program in Support of Reactor Coolant Pump Seal Replacement Project L-2024-007, Inservice Inspection Program Owner'S Activity Report (OAR-1)2024-01-18018 January 2024 Inservice Inspection Program Owner'S Activity Report (OAR-1) L-2023-173, Quality Assurance Topical Report (FPL-1) Revision 30 Update2023-12-15015 December 2023 Quality Assurance Topical Report (FPL-1) Revision 30 Update L-2023-166, Turkey Points Units 3 and 4, Correction to the 2022 Annual Radioactive Effluent Release Report2023-12-0606 December 2023 Turkey Points Units 3 and 4, Correction to the 2022 Annual Radioactive Effluent Release Report ML23340A0332023-12-0101 December 2023 FPL to Fws, Comments Submitted by Florida Power and Light on the Species Status Assessment Accompanying the September 20, 2023 Proposed Threatened Species Status with Section 4(d) Rule for the Miami Cave Crayfish L-2023-172, Supplement to Exemption Request Regarding Enhanced Weapons. Firearms Background Checks. and Security Event Notifications Final Rule2023-11-29029 November 2023 Supplement to Exemption Request Regarding Enhanced Weapons. Firearms Background Checks. and Security Event Notifications Final Rule L-2023-155, Supplement to Response to Request for Additional Information, Revised NextEra Common Emergency Plan, and Revised Site-Specific Emergency Plan Annexes Regarding License Amendment Request for Common Emergency Plan Consistent with NUREG-06542023-11-28028 November 2023 Supplement to Response to Request for Additional Information, Revised NextEra Common Emergency Plan, and Revised Site-Specific Emergency Plan Annexes Regarding License Amendment Request for Common Emergency Plan Consistent with NUREG-0654, ML23333A0152023-11-27027 November 2023 Attachment G - Arcadis Memo Re FPL Year 4 Raasr Final (June 2, 2023, Appended to Derm letter)-1 ML23333A0102023-11-27027 November 2023 Attachment B - 11/07/2022 - Waterkeeper Scoping Comments-1 L-2023-146, Part 73 Exemption Request Regarding Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Final Rule2023-11-16016 November 2023 Part 73 Exemption Request Regarding Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Final Rule L-2023-078, License Amendment Request 278, Incorporate Advanced Fuel Products, Extend Surveillance Intervals and 10 CFR 50.46 Exemption Request to Facilitate Transition to 24-Month Fuel Cycles2023-11-15015 November 2023 License Amendment Request 278, Incorporate Advanced Fuel Products, Extend Surveillance Intervals and 10 CFR 50.46 Exemption Request to Facilitate Transition to 24-Month Fuel Cycles IR 05000250/20230032023-11-0909 November 2023 Integrated Inspection Report 05000250/2023003 and 05000251/2023003 ML23310A1342023-11-0404 November 2023 10 CFR 2.206 Petition - LTR-23-0216-1 Petition Amendment; Turkey Point Subsequent Renewal with Petitioner 11/04/2023 ML24016A2622023-10-25025 October 2023 Subsequent License Renewal Updated List of Threatened and Endangered Species That May Occur in Your Proposed Project Location or May Be Affected Project L-2023-077, License Amendment Request 277 Updated Spent Fuel Pool Criticality Analysis2023-10-11011 October 2023 License Amendment Request 277 Updated Spent Fuel Pool Criticality Analysis ML23346A1322023-10-0606 October 2023 Communication from C-10 Research & Education Foundation Regarding NextEra Common Emergency Fleet Plan License Amendment Request and Related Documents Subsequently Published IR 05000250/20230102023-09-29029 September 2023 Biennial Problem Identification and Resolution Inspection Report 05000250/2023010 and 05000251/2023010 ML23234A1922023-09-27027 September 2023 Issuance of Amendment Nos. 297 and 290 Regarding Conversion to Improved Standard Technical Specifications ML23265A5492023-09-22022 September 2023 Transmittal of WCAP-18830-P/NP Turkey Point Fuel Storage Criticality Analysis for 24 Month Cycles to Support a License Amendment Request from FPL - License Amendment Request 277 Updated Spent Fuel Pool Criticality Analysis ML23243A9522023-09-0808 September 2023 Notice of Availability of the Draft Environmental Impact Statement for the Turkey Point Nuclear Generating Unit Numbers 3 and 4 Subsequent License Renewal Application ML23243A9542023-09-0808 September 2023 Notice of Availability of the Draft Environmental Impact Statement for the Turkey Point Nuclear Generating Unit Numbers 3 and 4 Subsequent License Renewal Application ML23243A9532023-09-0808 September 2023 Notice of Availability of the Draft Environmental Impact Statement for the Turkey Point Nuclear Generating Unit Numbers 3 and 4 Subsequent License Renewal Application ML23243A9552023-09-0808 September 2023 Notice of Availability of the Draft Environmental Impact Statement for the Turkey Point Nuclear Generating Unit Numbers 3 and 4 Subsequent License Renewal Application - Tribe- Section 106 Letters ML23199A2352023-09-0505 September 2023 Letter to EPA-Turkey Point Nuclear Generating Station, Units 3 and 4 - Notice of Availability of Draft Site-Specific Environmental Impact Statement for Subsequent License Renewal ML23199A2482023-09-0505 September 2023 Ltr to Florida Power and Light Co - Turkey Point Nuclear Generating Units 3 and 4 - Notice of Availability of Draft Site-Specific Environmental Impact Statement for Subsequent License Renewal L-2023-110, Response to Requests for Additional Information Regarding License Amendment Request No. 276, Revise Fire Protection Program in Support of Reactor Coolant Pump Seal Replacement Project2023-08-25025 August 2023 Response to Requests for Additional Information Regarding License Amendment Request No. 276, Revise Fire Protection Program in Support of Reactor Coolant Pump Seal Replacement Project IR 05000250/20230052023-08-21021 August 2023 Updated Inspection Plan for Turkey Point, Units 3 & 4 (Report 05000250/2023005 and 05000251/2023005) L-2023-115, Inservice Inspection Program Owner'S Activity Report (OAR-1)2023-08-21021 August 2023 Inservice Inspection Program Owner'S Activity Report (OAR-1) L-2023-114, Proposed Turkey Point Units 6 and 7; Seabrook Station; Point Beach Units 1 and 2 - Official Service List Update2023-08-17017 August 2023 Proposed Turkey Point Units 6 and 7; Seabrook Station; Point Beach Units 1 and 2 - Official Service List Update IR 05000250/20230022023-08-14014 August 2023 Integrated Inspection Report 05000250/2023002 and 05000251/2023002 L-2023-098, and Point Beach Units 1 and 2 - Response to Request for Additional Information Regarding License Amendment Request for Common Emergency Plan Consistent with NUREG-0654, Revision 22023-08-0707 August 2023 and Point Beach Units 1 and 2 - Response to Request for Additional Information Regarding License Amendment Request for Common Emergency Plan Consistent with NUREG-0654, Revision 2 ML23242A0922023-08-0606 August 2023 Request for Withholding Information from Public Disclosure for Turkey Point Nuclear Generating Unit Nos. 3 and 4 ML23201A0872023-08-0303 August 2023 Audit Plan in Support of Review of License Amendment ML23198A2702023-08-0303 August 2023 Issuance of the Site-Specific Environmental Impact Statement Scoping Process Summary Report Associated with the Turkey Point Nuclear Generating Unit Numbers 3 and 4, Subsequent License Renewal Application, Environmental Report Supplement 2 L-2023-094, Response to Requests for Additional Information Regarding License Amendment Request No. 276, Revise Fire Protection Program in Support of Reactor Coolant Pump Seal Replacement Project2023-07-27027 July 2023 Response to Requests for Additional Information Regarding License Amendment Request No. 276, Revise Fire Protection Program in Support of Reactor Coolant Pump Seal Replacement Project ML23178A1872023-07-25025 July 2023 Review of the Spring 2022 Steam Generator Tube Inspections During Refueling Outage No. 33 ML23188A1242023-07-20020 July 2023 Acknowledgment of Temporary Suspension Request for License Request for License Amendment Request Reactor Protection System, Engineered Safety Features System, and Nuclear Instrumentation System ML23200A0672023-07-18018 July 2023 Tp 2023 RQ Inspection Notification Letter ML23173A0812023-07-17017 July 2023 Supplement to Regulatory Audit Plan in Support of Review of License Amendment Request Supporting Digital Instrumentation & Control Modernization Project (EPID L-2022-LLA-0105) - Non-Proprietary L-2023-087, Florida Power & Light/Nextera Energy, Results of the Safety Culture Program Effectiveness Review, March 20, 2023 (ADAMS Accession No. ML22340A452)2023-06-29029 June 2023 Florida Power & Light/Nextera Energy, Results of the Safety Culture Program Effectiveness Review, March 20, 2023 (ADAMS Accession No. ML22340A452) 2024-02-05
[Table view] Category:Inservice/Preservice Inspection and Test Report
MONTHYEARL-2024-007, Inservice Inspection Program Owner'S Activity Report (OAR-1)2024-01-18018 January 2024 Inservice Inspection Program Owner'S Activity Report (OAR-1) L-2023-115, Inservice Inspection Program Owner'S Activity Report (OAR-1)2023-08-21021 August 2023 Inservice Inspection Program Owner'S Activity Report (OAR-1) L-2022-149, U4R33 Steam Generator Tube Inspection Report2022-10-0404 October 2022 U4R33 Steam Generator Tube Inspection Report L-2022-109, Inservice Inspection Program - Owner'S Activity Report (OAR-1)2022-06-27027 June 2022 Inservice Inspection Program - Owner'S Activity Report (OAR-1) L-2022-035, Fifth Ten-Year Inservice Inspection Interval Relief Request No. 10 Part-II2022-03-10010 March 2022 Fifth Ten-Year Inservice Inspection Interval Relief Request No. 10 Part-II L-2022-027, Inservice Inspection Program Owner'S Activity Report (OAR-1)2022-02-17017 February 2022 Inservice Inspection Program Owner'S Activity Report (OAR-1) L-2021-183, Fifth Ten-Year Inservice Inspection Interval Relief Request No. 102021-09-30030 September 2021 Fifth Ten-Year Inservice Inspection Interval Relief Request No. 10 L-2021-042, Inservice Inspection Program Owner'S Activity Report (OAR-1)2021-02-15015 February 2021 Inservice Inspection Program Owner'S Activity Report (OAR-1) L-2020-126, ln-Service Inspection Program Owner'S Activity Report (OAR-1)2020-07-24024 July 2020 ln-Service Inspection Program Owner'S Activity Report (OAR-1) L-2020-074, Response to Request for Additional Information for Relief Request No. 62020-04-15015 April 2020 Response to Request for Additional Information for Relief Request No. 6 L-2020-056, Fifth Ten-Year Inservice Inspection Interval Relief Request No. 62020-03-30030 March 2020 Fifth Ten-Year Inservice Inspection Interval Relief Request No. 6 L-2019-175, Steam Generator Tube Inspection Report2019-09-25025 September 2019 Steam Generator Tube Inspection Report ML19189A3532019-07-0808 July 2019 Inservice Inspection Program: Owner'S Activity Report (OAR-1) L-2019-018, Submittal of Inservice Inspection Program Owner'S Activity Report (OAR-1)2019-02-0707 February 2019 Submittal of Inservice Inspection Program Owner'S Activity Report (OAR-1) L-2018-232, Metamic Inservice Surveillance Campaign Summary Report2018-12-13013 December 2018 Metamic Inservice Surveillance Campaign Summary Report L-2017-132, Inservice Inspection Program Owner'S Activity Reports2017-07-20020 July 2017 Inservice Inspection Program Owner'S Activity Reports L-2016-138, Inservice Inspection Program Owner'S Activity Report for Fifth Inservice Inspection Interval2016-07-12012 July 2016 Inservice Inspection Program Owner'S Activity Report for Fifth Inservice Inspection Interval L-2016-139, Fifth 10-Year Interval Inservice Testing Program Plan2016-07-0606 July 2016 Fifth 10-Year Interval Inservice Testing Program Plan L-2016-044, Inservice Inspection Program Owner'S Activity Report2016-02-26026 February 2016 Inservice Inspection Program Owner'S Activity Report L-2015-223, Fifth Ten-Year Interval Inservice Testing (IST) Program Relief Request No. PR-01-Resubmittal2015-09-25025 September 2015 Fifth Ten-Year Interval Inservice Testing (IST) Program Relief Request No. PR-01-Resubmittal L-2015-101, Submittal of Fifth Ten-Year Inservice Inspection (ISI) Interval Relief Request No. 32015-06-0808 June 2015 Submittal of Fifth Ten-Year Inservice Inspection (ISI) Interval Relief Request No. 3 L-2015-098, Fifth Ten-Year Interval Inservice Testing (IST) Program, Relief Request No. PR-012015-05-12012 May 2015 Fifth Ten-Year Interval Inservice Testing (IST) Program, Relief Request No. PR-01 L-2015-040, Submittal of Fifth 10 Year Interval Inservice Inspection (ISI) Program Plan2015-03-11011 March 2015 Submittal of Fifth 10 Year Interval Inservice Inspection (ISI) Program Plan ML15077A2142015-03-0202 March 2015 Inservice Inspection Plan - Fifth Inspection Interval, Relief Request No. 1, Revision 1 L-2015-020, Closeout of the Fourth Ten-Year Inservice Inspection (ISI) Interval Relief Requests Nos. 15, 16, 172015-02-13013 February 2015 Closeout of the Fourth Ten-Year Inservice Inspection (ISI) Interval Relief Requests Nos. 15, 16, 17 L-2015-012, Inservice Inspection Program Owner'S Activity Report (OAR-1)2015-01-16016 January 2015 Inservice Inspection Program Owner'S Activity Report (OAR-1) L-2014-105, Inservice Inspection Plan - Fifth Inspection Interval, Unit 3 Relief Request No. 1 - Response to Follow-up Request for Additional Information2014-04-14014 April 2014 Inservice Inspection Plan - Fifth Inspection Interval, Unit 3 Relief Request No. 1 - Response to Follow-up Request for Additional Information L-2014-096, Inservice Inspection Plan - Fifth Inspection Interval Unit 3 Relief Request No. 12014-04-0404 April 2014 Inservice Inspection Plan - Fifth Inspection Interval Unit 3 Relief Request No. 1 L-2014-040, Letter Regarding Inservice Testing Program-Extension of Interval for Turkey Point, Units 3 and 42014-02-13013 February 2014 Letter Regarding Inservice Testing Program-Extension of Interval for Turkey Point, Units 3 and 4 L-2013-113, Inservice Inspection Plan Submittal of Relief Request No. 122013-05-24024 May 2013 Inservice Inspection Plan Submittal of Relief Request No. 12 L-2012-435, Inservice Inspection Program Fourth Interval-Third Period-First Refueling Outage Owner'S Activity Report (OAR-1)2012-12-0303 December 2012 Inservice Inspection Program Fourth Interval-Third Period-First Refueling Outage Owner'S Activity Report (OAR-1) L-2012-214, License Renewal Commitment, Submittal of Pressurizer Surge Line Welds Inspection Program2012-05-16016 May 2012 License Renewal Commitment, Submittal of Pressurizer Surge Line Welds Inspection Program ML11361A3812012-01-27027 January 2012 Summary of the Staff'S Review of the Steam Generator Tube Inservice Inspection Refueling Outage 25 L-2011-254, Inservice Inspection Program Fourth Interval-Second Period-Third Refueling Outage Owner'S Activity Report (OAR-1)2011-08-0505 August 2011 Inservice Inspection Program Fourth Interval-Second Period-Third Refueling Outage Owner'S Activity Report (OAR-1) L-2011-119, Submittal of Steam Generator Tube Inspection Report2011-04-19019 April 2011 Submittal of Steam Generator Tube Inspection Report L-2011-042, Inservice Inspection Program Fourth Interval-Second Period-Third Refueling Outage Owner'S Activity Report (OAR-1)2011-02-0707 February 2011 Inservice Inspection Program Fourth Interval-Second Period-Third Refueling Outage Owner'S Activity Report (OAR-1) L-2010-250, Fourth Inservice Inspection Interval, Relief Request No. 9, Visual Examination of Containment Liner Repair2010-10-27027 October 2010 Fourth Inservice Inspection Interval, Relief Request No. 9, Visual Examination of Containment Liner Repair L-2010-042, Inservice Inspection Program Fourth Interval-Second Period-Second Refueling Outage Owner'S Activity Report (OAR-1)2010-02-26026 February 2010 Inservice Inspection Program Fourth Interval-Second Period-Second Refueling Outage Owner'S Activity Report (OAR-1) L-2009-167, Inservice Inspection Program Fourth Interval-Second Period-Second Refueling Outage Owner'S Activity Report (OAR-1)2009-08-0606 August 2009 Inservice Inspection Program Fourth Interval-Second Period-Second Refueling Outage Owner'S Activity Report (OAR-1) L-2008-003, Inservice Inspection Report2008-01-10010 January 2008 Inservice Inspection Report L-2007-036, Inservice Inspection Report2007-03-0808 March 2007 Inservice Inspection Report L-2006-158, Inservice Inspection Record2006-06-28028 June 2006 Inservice Inspection Record L-2006-062, Response to Request for Additional Information Regarding Steam Generator Tube Plugging Inservice Inspection Report2006-02-27027 February 2006 Response to Request for Additional Information Regarding Steam Generator Tube Plugging Inservice Inspection Report L-2005-190, 2005 Inservice Inspection Report2005-09-0808 September 2005 2005 Inservice Inspection Report L-2005-137, Steam Generator Tube Plugging Inservice Inspection 12-Month Special Report2005-06-17017 June 2005 Steam Generator Tube Plugging Inservice Inspection 12-Month Special Report L-2005-046, Refueling Outage Summary of Inservice Inspection Examinations.2005-02-15015 February 2005 Refueling Outage Summary of Inservice Inspection Examinations. L-2004-217, Steam Generator Tube Plugging Inservice Inspection 12-Month Special Report2004-10-12012 October 2004 Steam Generator Tube Plugging Inservice Inspection 12-Month Special Report L-2004-046, Inservice Inspection (ISI) Program Missing Pages from Fpl'S Letter L-2004-046, Dated March 11, 20042004-04-29029 April 2004 Inservice Inspection (ISI) Program Missing Pages from Fpl'S Letter L-2004-046, Dated March 11, 2004 L-2004-043, Submittal of Fourth 10-year Testing Interval IST Program, Revision 0, Beginning February 22, 2004 for Turkey Point Unit 3 and April 15, 2004 for Turkey Point Unit 42004-03-11011 March 2004 Submittal of Fourth 10-year Testing Interval IST Program, Revision 0, Beginning February 22, 2004 for Turkey Point Unit 3 and April 15, 2004 for Turkey Point Unit 4 L-2004-025, Transmittal of Inservice Inspection Report2004-01-30030 January 2004 Transmittal of Inservice Inspection Report 2024-01-18
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UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 January 27, 2012 Mr. Mano Nazar Executive Vice President and Chief Nuclear Officer Florida Power and Light Company P.O. Box 14000 Juno Beach, Florida 33408-0420
SUBJECT:
TURKEY POINT UNIT 3 -
SUMMARY
OF THE STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 (TAC NO. ME6351)
Dear Mr. Nazar:
By letters dated April 19 and November 23,2011 (Agencywide Documents Access and Management Systems (ADAMS) Accession Nos. ML11119A006 and ML11340A074), Florida Power and Light Co. (FPL) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. These reports were submitted in accordance with Turkey Point Unit 3 Technical Specifications (TSs) Sections 4.4.5.1, 4.4.5.2 and 6.9.1.8.
A summary of the NRC staff's evaluation of the Turkey Point Unit 3 Fall 2010 Refueling Outage 25 SG tube inspection results is enclosed. Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML110030005). The NRC staff concluded that FPL provided the information required by the Turkey Point Unit 3 TSs and that no addition ollow-up is required at this time.
Since ely, ~. //
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L/PPlant Licensing Branch 11-2 Division of Operating Reactor licensing Office of Nuclear Reactor Regulation Docket No. 50-250
Enclosure:
As stated cc w/encl: Distribution via Listserv
UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001
SUMMARY
OF THE U.S. NUCLEAR REGULATORY COMMISSION STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 FLORIDA POWER AND LIGHT COMPANY TURKEY POINT UNIT 3 DOCKET NO. 50-250 By letters dated April 19 and November 23, 2011 (Agencywide Documents Access and Management Systems Accession Nos. ML11119A006 and ML11340A074), Florida Power and Light Co. (FPL, the licensee) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML110030005).
Turkey Point Unit 3 has three Westinghouse Model 44F SGs. The SGs have tubes that were hydraulically expanded into the tubesheet and are supported by Type 405 stainless steel tube support plates with broached quatrefoil holes. The Unit 3 SGs were placed into operation in 1982, and have thermally treated Alloy 600 tubing.
The licensee provided the scope, extent, methods, and results of their SG tube inspections in the documents referenced above. In addition, the licensee described corrective actions (e.g.,
tube plugging) taken in response to the inspection findings.
As a result of its review of the above documents, the NRC staff has the following comments/observations:
- 1. No crack-like indications were detected during the outage.
- 2. Tubes R6 C45 and R7 C45 in SG B were plugged, but not stabilized. Both of these tubes had shallow wear indications attributed to a suspected foreign object near the upper edge of the 2nd tube support plate on the cold leg side (02C). The tubes were plugged but not stabilized since the expected wear rate is low. The tubes surrounding R6 C45 and R7 C45A at the 02C location will be examined during the refueling outage for Cycle 27 in 2013 and during future inspections to monitor for degradation and for migration of the suspected foreign object. This required action has been documented in the plant's corrective action program.
Enclosure
-2
- 3. The licensee summarized the scope of inspections (primary and secondary side) as required by Technical Specification 6.9.1.8, "Steam Generator Tube Inspection Report."
Based on a review of the information provided, the staff concludes that the licensee provided the information required by their technical specifications. In addition, the staff concludes that there are no technical issues that warrant follow-up action at this time since the inspections appear to be consistent with the objective of detecting potential tube degradation and the inspection results appear to be consistent with industry operating experience at similarly designed and operated units.
ML110030005). The NRC staff concluded that FPL provided the information required by the Turkey Point Unit 3 TSs and that no additional follow-up is required at this time.
Sincerely, IRA!
Jason C. Paige, Project Manager Plant Licensing Branch 11-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-250
Enclosure:
As stated cc w/encl: Distribution via Listserv Distribution:
PUBLIC LPL2-2 RtF RidsNrrDorlLpl2-2 RidsN rrLABClayton RidsOgcRp RidsAcrsAcnwMailCenter RidsNrrDorlDpr RidsRgn2MailCenter CHunt, NRR KKarwoski. NRR RidsNrrPMTurkeyPoint RidsNrrDeEsgb ADAMSAccession NO.:ML11361A381 *8~ymemo OFFICE LPL2-2/PM LPL2-2/LA ESGB/BC (A) LPL2-2/BC LPL2-2/PM NAME JPaige BClayton VCusumano* DBroaddus JPaige (FSaba for)
DATE 12/28/11 12/28/11 12112111 1127112 1127/12