ML18086A457: Difference between revisions

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| issue date = 05/01/1981
| issue date = 05/01/1981
| title = Forwards LER 81-038/03L-0
| title = Forwards LER 81-038/03L-0
| author name = STEELE W J, UDERITZ R A
| author name = Steele W, Uderitz R
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| addressee name = GRIER B H
| addressee name = Grier B
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
| docket = 05000272
| docket = 05000272
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:5 Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 May 1, 1981 Mr. Boyce H. Grier Director of USNRC Off ice of Inspection and Enforcement Region i 631 Park Avenue King of Prussia, Pennsylvania 19406  
{{#Wiki_filter:PS~G Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 May 1, 1981 Mr. Boyce H. Grier Director of USNRC Off ice of Inspection and Enforcement Region i 631 Park Avenue King of Prussia, Pennsylvania                       19406


==Dear Mr. Grier:==
==Dear Mr. Grier:==
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 81-38/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 81-38/03L.
 
This report is required within thirty (30) days of the occurrence.
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 81-38/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 81-38/03L. This report is required within thirty (30) days of the occurrence.
Sincerely yours, c----.. dt/li&r R. A. Uderilz General Manager -Nuclear Production CC: Director, Office of Inspection and Enforcement (30 copies) Director, Office of Management Information and Program Control (3 copies) 4/J!1 () I ;-, C *-* r ' r* , .-C. r* ;! n 1 !. n O* 508'() ---L '"" ."001 1350'.11 4 80
Sincerely yours, c----
(  
                                                                          ~      ..   ~
'-... Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 Mr. Boyce H. Grier Director of USNRC May 1, 1981 Off ice of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406  
dt/li&r R. A. Uderilz General Manager -
Nuclear Production CC:       Director, Office of Inspection and Enforcement (30 copies)
Director, Office of Management Information and Program Control (3 copies) 5 4/J!1 ()   I ;-, ~ C *-* r ' r* , .- C. r* ;! 1n    n
                    ~*
O*       508'()                           -- -       L
                                                                                                        '"" ."001 1350'.11 4 80
 
('-...
:~ PS~G Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 May 1, 1981 Mr. Boyce H. Grier Director of USNRC Off ice of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania                     19406


==Dear Mr. Grier:==
==Dear Mr. Grier:==
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 81-38/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 81-38/cr3L.
 
This report is required within thirty (30) days of the occurrence.
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 81-38/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 81-38/cr3L. This report is required within thirty (30) days of the occurrence.
Sincerely yours, c-*-A't:cM:/ R. A. Uderrtz General Manager Nuclear Production CC: Director, Office of Inspection and Enforcement (30 copies) Director, Office of Management Information and Program Control (3 copies) g:, 2001 1350:1.) 4-80
Sincerely yours, c-*-
*, Report Number: Report Date: May 1, 1981 Occurrence Date: 4/04/81 Facility:
A't:cM:/
Salem Generating Station, Unit 1 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
R. A. Uderrtz General Manager Nuclear Production CC:       Director, Office of Inspection and Enforcement (30 copies)
Director, Office of Management Information and Program Control (3 copies) g:, 2001 1350:1.) 4-80
 
Report Number:
Report Date:       May 1, 1981 Occurrence Date:   4/04/81 Facility:         Salem Generating Station, Unit 1 Public Service Electric & Gas Company Hancocks Bridge, New Jersey   08038 IDENTIFICATION OF OCCURRENCE:
Loss of Audible Fire Alarm CONDITIONS PRIOR TO OCCURRENCE:
Loss of Audible Fire Alarm CONDITIONS PRIOR TO OCCURRENCE:
Mode 5 -Rx Power 0% -Unit Load 0 MW DESCRIPTION OF OCCURRENCE:
Mode 5 - Rx Power 0% - Unit Load 0 MW DESCRIPTION OF OCCURRENCE:
While performing routine testing of the Fire Detection System IAW the Salem Generating Station Fire Fighting Manual, it was discovered that no audible alarm signals were being generated.
While performing routine testing of the Fire Detection System IAW the Salem Generating Station Fire Fighting Manual, it was discovered that no audible alarm signals were being generated. Action State-ment 3.3.3.6.a was entered at 1256.hours.
Action ment 3.3.3.6.a was entered at 1256.hours.
This occurrence constituted operation in a degraded mode IAW Technical Specification 6.9.1.9.b.
This occurrence constituted operation in a degraded mode IAW Technical Specification 6.9.1.9.b.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
Equipment Failure -A limit switch in the No. 14 Decoder in the Tone Generating System was binding and prevented th.e decoder from completing the sequential action necessary to generate the audible alarm. The limit switch had drifted out of adjustment.
Equipment Failure - A limit switch in the No. 14 Decoder in the Tone Generating System was binding and prevented th.e decoder from completing the sequential action necessary to generate the audible alarm. The limit switch had drifted out of adjustment.
ANALYSIS OF OCCURRENCE:
ANALYSIS OF OCCURRENCE:
Technical Specification requires that a fire watch patrol be established to inspect the zone(s) with the inoperable instrument(s) at least once per hour. CORRECTIVE ACTION: The 'decoder and its limit switch were readjusted, cycled several times and tested satisfactory.
Technical Specification 3~3.3.6.a requires that a fire watch patrol be established to inspect the zone(s) with the inoperable instrument(s) at least once per hour.
The Action Statement was terminated at 1526 hours. FAILURE DATA: Pyrotronics  
CORRECTIVE ACTION:
-Decoder -Model ZCP-4 Prepared By W. J. Steele Manager -Salem Generating Station SORC Meeting No. 81-30}}
The 'decoder and its limit switch were readjusted, cycled several times and tested satisfactory. The Action Statement was terminated at 1526 hours.
FAILURE DATA:
Pyrotronics - Decoder - Model ZCP-4 Prepared By     W. J. Steele Manager - Salem Generating Station SORC Meeting No.       81-30}}

Latest revision as of 09:13, 3 February 2020

Forwards LER 81-038/03L-0
ML18086A457
Person / Time
Site: Salem PSEG icon.png
Issue date: 05/01/1981
From: Steele W, Uderitz R
Public Service Enterprise Group
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18086A458 List:
References
NUDOCS 8105080360
Download: ML18086A457 (3)


Text

PS~G Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 May 1, 1981 Mr. Boyce H. Grier Director of USNRC Off ice of Inspection and Enforcement Region i 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 81-38/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 81-38/03L. This report is required within thirty (30) days of the occurrence.

Sincerely yours, c----

~ .. ~

dt/li&r R. A. Uderilz General Manager -

Nuclear Production CC: Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control (3 copies) 5 4/J!1 () I ;-, ~ C *-* r ' r* , .- C. r* ;! 1n n

~*

O* 508'() -- - L

'"" ."001 1350'.11 4 80

('-...

~ PS~G Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 May 1, 1981 Mr. Boyce H. Grier Director of USNRC Off ice of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 81-38/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 81-38/cr3L. This report is required within thirty (30) days of the occurrence.

Sincerely yours, c-*-

A't:cM:/

R. A. Uderrtz General Manager Nuclear Production CC: Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control (3 copies) g:, 2001 1350:1.) 4-80

Report Number:

Report Date: May 1, 1981 Occurrence Date: 4/04/81 Facility: Salem Generating Station, Unit 1 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Loss of Audible Fire Alarm CONDITIONS PRIOR TO OCCURRENCE:

Mode 5 - Rx Power 0% - Unit Load 0 MW DESCRIPTION OF OCCURRENCE:

While performing routine testing of the Fire Detection System IAW the Salem Generating Station Fire Fighting Manual, it was discovered that no audible alarm signals were being generated. Action State-ment 3.3.3.6.a was entered at 1256.hours.

This occurrence constituted operation in a degraded mode IAW Technical Specification 6.9.1.9.b.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

Equipment Failure - A limit switch in the No. 14 Decoder in the Tone Generating System was binding and prevented th.e decoder from completing the sequential action necessary to generate the audible alarm. The limit switch had drifted out of adjustment.

ANALYSIS OF OCCURRENCE:

Technical Specification 3~3.3.6.a requires that a fire watch patrol be established to inspect the zone(s) with the inoperable instrument(s) at least once per hour.

CORRECTIVE ACTION:

The 'decoder and its limit switch were readjusted, cycled several times and tested satisfactory. The Action Statement was terminated at 1526 hours0.0177 days <br />0.424 hours <br />0.00252 weeks <br />5.80643e-4 months <br />.

FAILURE DATA:

Pyrotronics - Decoder - Model ZCP-4 Prepared By W. J. Steele Manager - Salem Generating Station SORC Meeting No. 81-30