ML19031C033: Difference between revisions

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Director, Office          of Management Information and          Program Control The Energy People 95-2001 300M 8-7'
Director, Office          of Management Information and          Program Control The Energy People 95-2001 300M 8-7'


    .  '"
*~ *~  Report Number :
*~ *~  Report Number :
       , Report Date:
       , Report Date:
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Facility:
Facility:
7ji15/04L
7ji15/04L
                                 . 4-,r/78" 3/9/78 Salem Generating Station
                                 . 4-,r/78" 3/9/78 Salem Generating Station l">
* l">
Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Missed Surveillance:          Non-Radwaste Sampling for Suspended Solids Analysis CONDITIONS PRIOR TO OCCURRENCE:
Missed Surveillance:          Non-Radwaste Sampling for Suspended Solids Analysis CONDITIONS PRIOR TO OCCURRENCE:

Latest revision as of 13:11, 2 February 2020

04/06/1978 Letter Reportable Occurrence on Non-Radwaste Sampling for Suspended Solids Analysis
ML19031C033
Person / Time
Site: Salem  PSEG icon.png
Issue date: 04/06/1978
From: Librizzi F
Public Service Electric & Gas Co
To: Grier B
NRC/IE, NRC Region 1
References
LER 1978-015-04
Download: ML19031C033 (2)


Text

OPS~G

  • Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone 201 /622-7000 Mr. Boyce H. Grier Director of USNRC Off ice of Inspections and Enforcements Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406 0

\J1

Dear Mr. Grier:

LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 78-15/04L Pursuant to the requirements of Salem Generating Station Unit No. 1 Environmental Technical Specifications, we are submitting Licensee Event Report for Reportable Occurrence 78-15/04L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours,

-)

,;/)' L l VL l:_l'"'l --"\

F. P. Librizzi General Manager -

Electric Production CC: Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control The Energy People 95-2001 300M 8-7'

  • ~ *~ Report Number :

, Report Date:

Occurrence Date:

Facility:

7ji15/04L

. 4-,r/78" 3/9/78 Salem Generating Station l">

Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Missed Surveillance: Non-Radwaste Sampling for Suspended Solids Analysis CONDITIONS PRIOR TO OCCURRENCE:

N/A DESCRIPTION OF OCCURRENCE:

On the occasions summarized below, treated effluent was released from the non-radioactive liquid waste treatment basin, but a sample was not collected for suspended solids analysis.

January 1, 2, 7, 10, 14, 15, 16, 21, 24, 25, 26, 27, 28, 29, 30 February 7, 21 (Ref.: Section 2.2.2 of Appendix "B" to Operating License DPR-70)

The missing samples were identified upon records review in light of Occurrence 78-10/04L.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

The cause of this occurrence was personnel error. Corrective action as stated in LER 78-10/04L had not yet been implemented.

ANALYSIS OF OCCURRENCE:

N/A CORRECTIVE ACTION:

Responsibility to collect samples was re-assigned from demineralizer plant operator (day shift) to midnight shift Health Physics Technician.

FAILURE DATA:

N/A Prepared by_,....~~T~."-'L~*--S~p~e=n~c~e=r=--~~~~

Manage Statior SORC Meeting No. 14-78

_,....~~~~~~~~~~