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: 1. Abnormal Occurrence Report No. 50-313/74-9
: 1. Abnormal Occurrence Report No. 50-313/74-9
,
: 2. Report Date:    10/25/74            3. Occurrence Date:        10/17/74
: 2. Report Date:    10/25/74            3. Occurrence Date:        10/17/74
: 4. Facility:    Arkansas Nuclear One-Unit 1 Russe 11ville, Arkansas
: 4. Facility:    Arkansas Nuclear One-Unit 1 Russe 11ville, Arkansas
                                      ,
   .            5.
   .            5.
Identification of Occurrence: Crack in the socket weld on reactor coolant drain line (CCA-13-1-1-1/2) located between "B" steam generator and "B" reactor coolant pump. The socket weld is located just upstream of Valve RitD-8B                                                            a
Identification of Occurrence: Crack in the socket weld on reactor coolant drain line (CCA-13-1-1-1/2) located between "B" steam generator and "B" reactor coolant pump. The socket weld is located just upstream of Valve RitD-8B                                                            a
: 6. Conditiv.s Prior to Occurrence:
: 6. Conditiv.s Prior to Occurrence:
Steady-State Power        X              Reactor Power                            ~
Steady-State Power        X              Reactor Power                            ~
1669      Wth Ilot Standby                              Net. Output          550      We
1669      Wth Ilot Standby                              Net. Output          550      We Cold Shutdown                            Percent of Full. Power      65 %
                                                                                                .
Cold Shutdown                            Percent of Full. Power      65 %
Refueling Shutdown Routine Startup Operation O
Refueling Shutdown Routine Startup Operation O
Routine Shutdown                                                                '
Routine Shutdown                                                                '
Operation                              ,
Operation                              ,
                                                                ' "
Load Changes During Routine Power Operation          .
Load Changes During Routine Power Operation          .
Other (Specify)
Other (Specify) 7    Description of Occurrence:                                -
                                                                                                        .
7    Description of Occurrence:                                -
                                                                                  .
1
1
* A one (1) hour leak rate calculation, indicating a 2.15 gpm leakage, was completed at 1245 on October 17,~1974.      An immediate investigation com-menced. An entry was made into the reactor building and a leak was four.d in the vicinity of the cold leg drain on loop 8, "B" reactor coolant pump.        3 At that time, it was r.ot possible to identify an exact cause of leakage, whether it was a defective weld, valve bonnet leak, packing, etc. Load reduction and shutdown commenced.
* A one (1) hour leak rate calculation, indicating a 2.15 gpm leakage, was completed at 1245 on October 17,~1974.      An immediate investigation com-menced. An entry was made into the reactor building and a leak was four.d in the vicinity of the cold leg drain on loop 8, "B" reactor coolant pump.        3 At that time, it was r.ot possible to identify an exact cause of leakage, whether it was a defective weld, valve bonnet leak, packing, etc. Load reduction and shutdown commenced.
                                                                                                        .
At hot shutdown, a leak was found in the coupling to 1-1/2 inch pipe t. eld of the drain. At that time, the situation was identified as an abnormal          '
At hot shutdown, a leak was found in the coupling to 1-1/2 inch pipe t. eld of the drain. At that time, the situation was identified as an abnormal          '
degradation of the Reactor Coolant Pressure Coundary, s  /
degradation of the Reactor Coolant Pressure Coundary, s  /
     %)
     %)
800415073'7                                    .
800415073'7                                    .
                                                                                                  ..
July 5, 1974                      NSP-10, Rev. O                  Page 1 of 3
July 5, 1974                      NSP-10, Rev. O                  Page 1 of 3
                                                                  .


                                                                                                  - _  __
                                      ,-.
            .
    *
              .
                                                                                                      -
    ,
     +  ~l
     +  ~l
     \~_a' Abnormal Occurrence Report No. 50-313/74-9                              Sheet 2
     \~_a' Abnormal Occurrence Report No. 50-313/74-9                              Sheet 2
: 8. Designation of Apparent Cause of Occurrence:
: 8. Designation of Apparent Cause of Occurrence:
Design                                Procedure
Design                                Procedure bbnufre.ture                          Unusual Service Condition Including Installation /                          Environmental Construction Component Failure Operator                __
  -
Other (Sptsify)      X Examination of the affected area was conducted by a qualified metal-lurgist, a consultant from Bechtel Engineering. A check of ferrite content of the weld revealed no abnormalities. A dimensional check of the clearance required for the fit up of a socket type weld was dona after the weld was ground out. This check revealed a more than adequate clearance between the coupling and the pipe. The existence of fatigue stress is being considered. Vibration readings were taken
bbnufre.ture                          Unusual Service Condition Including Installation /                          Environmental Construction Component Failure Operator                __
Other (Sptsify)      X
                                                                                                            ,
Examination of the affected area was conducted by a qualified metal-lurgist, a consultant from Bechtel Engineering. A check of ferrite content of the weld revealed no abnormalities. A dimensional check of the clearance required for the fit up of a socket type weld was dona after the weld was ground out. This check revealed a more than adequate clearance between the coupling and the pipe. The existence of fatigue stress is being considered. Vibration readings were taken
('"'N                for further analysis to determine the -possible existence of fatigue stress failure.                                                                    --
('"'N                for further analysis to determine the -possible existence of fatigue stress failure.                                                                    --
: 9. Analysis of Occurrence:
: 9. Analysis of Occurrence:
There were no safety implications or haz:rd to the health and safety of plant per;onnel or the public, due to prompt identification of the Icak and cooldown to cold shutdown conditions.                                              2
There were no safety implications or haz:rd to the health and safety of plant per;onnel or the public, due to prompt identification of the Icak and cooldown to cold shutdown conditions.                                              2
                                                                                     ~
                                                                                     ~
                                                                                                                .
s
s
                                                               ~
                                                               ~
            .
                                                            '
: 10. Corrective Action:
: 10. Corrective Action:
The socket weld filler material on the affected weld was completely                  ';
The socket weld filler material on the affected weld was completely                  ';
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Qualified welders, working under a QA program, were used to p<:rform
Qualified welders, working under a QA program, were used to p<:rform
* this repair. ANO QA/QC inspectors witnessed the entire repair. A leak test was performed with no discrepancies noted.                              -
* this repair. ANO QA/QC inspectors witnessed the entire repair. A leak test was performed with no discrepancies noted.                              -
                      .
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: i.                July 5,      a.t                    NSP-10, Rev. O                  Page 2 of 3          -i l
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: i.                July 5,      a.t                    NSP-10, Rev. O                  Page 2 of 3          -i
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                                                        *


                                                                               ~
                                                                               ~
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: e.  .
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Sheet 3
Sheet 3
: 11. Failure Mta:
: 11. Failure Mta:
  ,
The three other similar welds on drain lines in the reactor coolant system were visually checked _ with no indications noted.        A further analysis of the situation is required to determine if the additional investigation is necessary. The results are to be forwarded upon availability.
The three other similar welds on drain lines in the reactor coolant system were visually checked _ with no indications noted.        A further analysis of the situation is required to determine if the additional investigation is necessary. The results are to be forwarded upon availability.
                                                                                                                  -.
                                                                                                               -        j 12    Reviews and Approvals:
                .
                                                                                                               -        j
                                                      .
12    Reviews and Approvals:
Reviewed and Approved by: Plant Safety Committee Yes (X)      No ( )
Reviewed and Approved by: Plant Safety Committee Yes (X)      No ( )
Plant Superintendent
Plant Superintendent
Line 125: Line 81:
Approved by            ' # / M -,- ,f .,,[        [ Date: / 8 - Z s '- 7t /
Approved by            ' # / M -,- ,f .,,[        [ Date: / 8 - Z s '- 7t /
                                   /          a/fet "Re'vla Co 15e                  '
                                   /          a/fet "Re'vla Co 15e                  '
                                                                                                      '
g
g
                                             ~'      '
                                             ~'      '
        .
Approved by-                          '
Approved by-                          '
                                                        ,
fnager of htfc' lear ServGs Date: /0/    I
fnager of htfc' lear ServGs Date: /0/    I
                                                                                                   / /Y
                                                                                                   / /Y
                                                                                                  '
                                                                                                                 ~2 Approved by: h'72,','p/                  , ,/mf'        Date:
                                                                                                                 ~2 Approved by: h'72,','p/                  , ,/mf'        Date:
                                   /
                                   /
Director of Power Prod:.tction                  h"- 1s- 7f Approved by:      ]
Director of Power Prod:.tction                  h"- 1s- 7f Approved by:      ]
                                  .
                                          '
                                                                   )-            Date:      /[    '
                                                                   )-            Date:      /[    '
M Senior Vice Prdsident                                              ~
M Senior Vice Prdsident                                              ~
                    .
t
t
!          4
!          4
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NM
NM
                                                                                         .                      ~
                                                                                         .                      ~
July S, 1974                          NSP-10, Rev. O
July S, 1974                          NSP-10, Rev. O Pace t of 7
                                                                    "
Pace t of 7
_              -}}
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Revision as of 00:48, 1 February 2020

AO 50-313/74-09:on 741017,leak Found on Cold Leg Drain Loop of Reactor Coolant Pump.Cause Unknown.Socket Weld Filler Matl Applied to Weld & Single Root Pass Made.Leak Test Performed;No Discrepancies Noted
ML19326B388
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 10/25/1974
From: Cavanaugh W, Phillips J, Rueter D
ARKANSAS POWER & LIGHT CO.
To:
Shared Package
ML19326B382 List:
References
NUDOCS 8004150757
Download: ML19326B388 (4)


Text

.

w/

1. Abnormal Occurrence Report No. 50-313/74-9
2. Report Date: 10/25/74 3. Occurrence Date: 10/17/74
4. Facility: Arkansas Nuclear One-Unit 1 Russe 11ville, Arkansas

. 5.

Identification of Occurrence: Crack in the socket weld on reactor coolant drain line (CCA-13-1-1-1/2) located between "B" steam generator and "B" reactor coolant pump. The socket weld is located just upstream of Valve RitD-8B a

6. Conditiv.s Prior to Occurrence:

Steady-State Power X Reactor Power ~

1669 Wth Ilot Standby Net. Output 550 We Cold Shutdown Percent of Full. Power 65 %

Refueling Shutdown Routine Startup Operation O

Routine Shutdown '

Operation ,

Load Changes During Routine Power Operation .

Other (Specify) 7 Description of Occurrence: -

1

  • A one (1) hour leak rate calculation, indicating a 2.15 gpm leakage, was completed at 1245 on October 17,~1974. An immediate investigation com-menced. An entry was made into the reactor building and a leak was four.d in the vicinity of the cold leg drain on loop 8, "B" reactor coolant pump. 3 At that time, it was r.ot possible to identify an exact cause of leakage, whether it was a defective weld, valve bonnet leak, packing, etc. Load reduction and shutdown commenced.

At hot shutdown, a leak was found in the coupling to 1-1/2 inch pipe t. eld of the drain. At that time, the situation was identified as an abnormal '

degradation of the Reactor Coolant Pressure Coundary, s /

%)

800415073'7 .

July 5, 1974 NSP-10, Rev. O Page 1 of 3

+ ~l

\~_a' Abnormal Occurrence Report No. 50-313/74-9 Sheet 2

8. Designation of Apparent Cause of Occurrence:

Design Procedure bbnufre.ture Unusual Service Condition Including Installation / Environmental Construction Component Failure Operator __

Other (Sptsify) X Examination of the affected area was conducted by a qualified metal-lurgist, a consultant from Bechtel Engineering. A check of ferrite content of the weld revealed no abnormalities. A dimensional check of the clearance required for the fit up of a socket type weld was dona after the weld was ground out. This check revealed a more than adequate clearance between the coupling and the pipe. The existence of fatigue stress is being considered. Vibration readings were taken

('"'N for further analysis to determine the -possible existence of fatigue stress failure. --

9. Analysis of Occurrence:

There were no safety implications or haz:rd to the health and safety of plant per;onnel or the public, due to prompt identification of the Icak and cooldown to cold shutdown conditions. 2

~

s

~

10. Corrective Action:

The socket weld filler material on the affected weld was completely ';

ground out. The 1-1/2 inch pipe was reinserted in the socket and a single root pass was made. The surface of the coupling and the single root pass were dye penetrant checked with no indications evident.

Qualified welders, working under a QA program, were used to p<:rform

  • this repair. ANO QA/QC inspectors witnessed the entire repair. A leak test was performed with no discrepancies noted. -

1 i

7s )

\

%J

i. July 5, a.t NSP-10, Rev. O Page 2 of 3 -i l

~

e. .

l'

/

Abnormal Occurrence Report No.

Sheet 3

11. Failure Mta:

The three other similar welds on drain lines in the reactor coolant system were visually checked _ with no indications noted. A further analysis of the situation is required to determine if the additional investigation is necessary. The results are to be forwarded upon availability.

- j 12 Reviews and Approvals:

Reviewed and Approved by: Plant Safety Committee Yes (X) No ( )

Plant Superintendent

\ ) Yes (X) No ( )

V ._

Reference:

JWA-621 Date: 10/24/74 Reviewed by Date: O f (

Licensing Supervisor 3

Approved by ' # / M -,- ,f .,,[ [ Date: / 8 - Z s '- 7t /

/ a/fet "Re'vla Co 15e '

g

~' '

Approved by- '

fnager of htfc' lear ServGs Date: /0/ I

/ /Y

~2 Approved by: h'72,','p/ , ,/mf' Date:

/

Director of Power Prod:.tction h"- 1s- 7f Approved by: ]

)- Date: /[ '

M Senior Vice Prdsident ~

t

! 4

NM

. ~

July S, 1974 NSP-10, Rev. O Pace t of 7

_ -