ML19319E540

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AO 50-313/75-12:on 751229,svc Water Sys Valve CV-3821 to Decay Heat Cooler Failed to Automatically Open When Decay Heat Pump Started.Caused by Increase in Binding in Valve Packing or Seating Valve Hard Against Valve Seat
ML19319E540
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 01/13/1976
From: Rueter D
ARKANSAS POWER & LIGHT CO.
To:
Shared Package
ML19319E529 List:
References
NUDOCS 8004110803
Download: ML19319E540 (4)


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Abnormal Oc.rrence Report No. 50-313/75-12 2.

Report Date:

1/13/76 3.

Occurrence Date:

12/29/75 4

Facility:

Arkansas Nuclear One-Unit.1 Russellville, Arkansas 5.

Identification of Occurrence:

Service Water System Valve to Decay Heat Cooler, CV-382,1, failed to open.

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Conditions Prior to Occurrence:

Steady-State Power Reactor Power 0

MWth llot Standby Net Output 0

Mwe Cold Shutdown X

Percent of Full Power o

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Refueling Shutdown Load Changes During Routine Power Operation l

Routine Startup Operation Routine Shutdown Operation Other (specify) 3 i

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bescription of occurrence:

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At 1310 hours0.0152 days <br />0.364 hours <br />0.00217 weeks <br />4.98455e-4 months <br /> on December 29, 1975, the service water valve CV-3821 to j

decay heat cooler taika t: :pe... automatically when decay hsat pump was started. The valve, however, opened manually.

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March 4, 1975 NSP-10, Rev. 2 Page 2 of 4

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'N Abnormal Occurrence Report No.

50-313/75-12 8.

Designation 'of Apparent Cause of Occurrence:

Design Procedure I

t Manufacture Unusual Service Condition including iinvironmental Installation /

I Construction Component Failurc Operator Other (specify)

-X The cause was probably an increase in binding in the valve, packing or l

seating the valve hard against the valve seat manually.

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Analysis'of Occurrence:

Since cooling water is not needed until transfer of the decay heat pump to the reactor building sump during a LOCA, there was more than an adequate amount of time for the valve to be opened manually. This incident would not have affected the health and safety of th,e public.

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March 4, 1975 NSP-10, Rev. 2 Page 3 Of 4 i

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Abnormal. Occurrence Report No.

50-313'/75-12 i

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Corrective Action:

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A slight adjustment was made to the torque switch.

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Failuro Data:

None.

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' March 4, 1975 NSP-10, Rev. 2 Page a of 4 E

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