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| {{Adams|number = ML093451499}} | | {{Adams |
| | | number = ML093451499 |
| | | issue date = 12/11/2009 |
| | | title = IR 05000373-09-007, 05000374-09-007 on 11/02/09 - 11/20/09 for LaSalle County, Units 1 and 2, Problem Identification and Resolution Inspection |
| | | author name = Riemer K |
| | | author affiliation = NRC/RGN-III/DRP/B2 |
| | | addressee name = Pardee C |
| | | addressee affiliation = Exelon Generation Co, LLC, Exelon Nuclear |
| | | docket = 05000373, 05000374 |
| | | license number = NPF-011, NPF-018 |
| | | contact person = |
| | | document report number = IR-09-007 |
| | | document type = Inspection Report, Letter |
| | | page count = 34 |
| | }} |
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| {{IR-Nav| site = 05000373 | year = 2009 | report number = 007 }} | | {{IR-Nav| site = 05000373 | year = 2009 | report number = 007 }} |
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| =Text= | | =Text= |
| {{#Wiki_filter: | | {{#Wiki_filter:ber 11, 2009 |
| [[Issue date::December 11, 2009]]
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| Mr. Charles Senior Vice President, Exelon Generation Company, LLC President and Chief Nuclear Officer (CNO), Exelon Nuclear 4300 Winfield Road Warrenville, IL 60555
| | ==SUBJECT:== |
| | LASALLE COUNTY STATION, UNITS 1 AND 2 PROBLEM IDENTIFICATION AND RESOLUTION (PI&R) INSPECTION 05000373/2009007; 05000374/2009007 |
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| SUBJECT: LASALLE COUNTY STATION, UNITS 1 AND 2 PROBLEM IDENTIFICATION AND RESOLUTION (PI&R) INSPECTION 05000373/2009007; 05000374/2009007
| | ==Dear Mr. Pardee:== |
| | On November 23, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution (PI&R) inspection at the LaSalle County Station Units 1 and 2. The enclosed report documents the inspection results, which were discussed on November 23, 2009, with members of your staff. |
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| | The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license. |
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| | The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. |
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| | The inspection concluded that your staff was effective at identifying problems and incorporating them into the corrective action program. In general, issues were appropriately prioritized, evaluated, and corrected, audits and self-assessments were thorough and probing, and operating experience was appropriately screened and disseminated. Your staff was aware of the importance of having a strong safety-conscious work environment and expressed a willingness to raise safety issues. |
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| ==Dear Mr. Pardee:==
| | No findings or violations were identified during this inspection. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC=s document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). |
| On November 23, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution (PI&R) inspection at the LaSalle County Station Units 1 and 2. The enclosed report documents the inspection results, which were discussed on November 23, 2009, with members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. The inspection concluded that your staff was effective at identifying problems and incorporating them into the corrective action program. In general, issues were appropriately prioritized, evaluated, and corrected, audits and self-assessments were thorough and probing, and operating experience was appropriately screened and disseminated. Your staff was aware of the importance of having a strong safety-conscious work environment and expressed a willingness to raise safety issues. No findings or violations were identified during this inspection. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC=s document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
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| Sincerely,/RA/ | | Sincerely, |
| Kenneth Riemer, Chief Branch 2 Division of Reactor Projects Docket No. 50-373; 50-374 License No. NPF-11; NPF-18 | | /RA/ |
| | Kenneth Riemer, Chief Branch 2 Division of Reactor Projects Docket No. 50-373; 50-374 License No. NPF-11; NPF-18 |
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| ===Enclosure:=== | | ===Enclosure:=== |
| Inspection Report 05000373/2009007; 05000374/2009007 | | Inspection Report 05000373/2009007; 05000374/2009007 w/Attachment: Supplemental Information |
| | |
| | REGION III== |
| | Docket Nos: 05000373; 05000374 License Nos: NPF-11; NPF-18 Report No: 05000373/2009007; 05000374/2009007 Licensee: Exelon Generation Company, LLC Facility: LaSalle County Station, Units 1 and 2 Location: Marseilles, IL Dates: November 2-20, 2009 Inspectors: N. Shah, Project Engineer - Team Lead F. Ramirez, Resident Inspector - LaSalle C. Scott, Reactor Engineer D. Swarzc, Reactor Engineer Observers: Jane Yesinowki, Illinois Emergency Management Agency Approved by: Kenneth Riemer, Chief Branch 2 Enclosure |
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| | =SUMMARY OF FINDINGS= |
| | IR 05000373/2009007; 05000374/2009007 (November 2, 2009 - November 20, 2009), |
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| | LaSalle County Station Units 1 and 2; Biennial Baseline Inspection of the Identification and Resolution of Problems. |
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| | This team inspection was performed by three regional inspectors and the site resident inspector. |
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| | No findings or violations were identified. |
| | |
| | Identification and Resolution of Problems Overall, the corrective action program (CAP) was being effectively implemented. Issues were identified at a low threshold, evaluated and corrected. Self-assessments and audits by Nuclear Oversight (NOS) were thorough and critical of the assessed areas. Operating experience was recognized as valuable and was effectively communicated. Interviews with licensee staff and a review of the Employee Concerns Program (ECP) indicated that the licensee had a positive safety culture environment that encouraged identification of issues in the CAP. |
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| | However, the inspectors identified several areas of concern that may negatively impact the licensees ability to identify and resolve issues. In some cases, these issues had been recognized by the licensee, but effective corrective action had not been taken. Briefly, the issues were: |
| | * The current CAP performance indicators were not always effectively used or sufficient to monitor the program. Although the licensee was aware of these issues, CAP staff appeared willing to live with the shortcomings and had not formally taken corrective action. |
| | * There were some examples of long-standing issues that were either not corrected or not evaluated. In some cases, the licensee had identified the issues, but had not evaluated why previous corrective actions were ineffective. |
| | * There were several examples where the review of operating experience (OE) in cause evaluations were not documented in accordance with licensee procedures. Additionally, there was no formal requirement to evaluate whether the failure to use OE was a precursor during the evaluation of events. Although the licensee had identified these issues in the CAP, the corrective actions were somewhat limited. |
| | * Issues that were reviewed by the ECP, but not captured in a formal case file, were not always well documented. This resulted in some uncertainty regarding whether potentially significant issues were appropriately dispositioned. |
| | |
| | ===NRC-Identified=== |
| | and Self-Revealed Findings |
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| | ===Cornerstone: Mitigating Systems=== |
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| ===w/Attachment:===
| | None. |
| Supplemental Information cc w/encl: Distribution via ListServ Enclosure U. S. NUCLEAR REGULATORY COMMISSION REGION III Docket Nos: 05000373; 05000374 License Nos: NPF-11; NPF-18 Report No: 05000373/2009007; 05000374/2009007 Licensee: Exelon Generation Company, LLC Facility: LaSalle County Station, Units 1 and 2 Location: Marseilles, IL Dates: November 2-20, 2009 Inspectors: N. Shah, Project Engineer - Team Lead F. Ramirez, Resident Inspector - LaSalle C. Scott, Reactor Engineer D. Swarzc, Reactor Engineer Observers: Jane Yesinowki, Illinois Emergency Management Agency
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| Approved by: Kenneth Riemer, Chief Branch 2 Enclosure
| | ===Licensee-Identified Violations=== |
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| =SUMMARY OF FINDINGS=
| | No violations of significance were identified. |
| ...........................................................................................................1 | |
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| =REPORT DETAILS= | | =REPORT DETAILS= |
| .......................................................................................................................3
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| ==OTHER ACTIVITIES== | | ==OTHER ACTIVITIES== |
| ......................................................................................................3
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| {{a|4OA2}} | | {{a|4OA2}} |
| ==4OA2 Problem Identification and Resolution== | | ==4OA2 Problem Identification and Resolution== |
| {{IP sample|IP=IP 71152B}} | | {{IP sample|IP=IP 71152B}} |
| ..................................................3 | | The activities documented in Sections |
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| | ===.1 through .4 constituted one biennial sample of=== |
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| | Problem Identification and Resolution (PI&R) as defined in Inspection Procedure (IP) 71152. |
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| | ===.1 Assessment of the Corrective Action Program Effectiveness=== |
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| | ====a. Inspection Scope==== |
| | The inspectors reviewed the licensees corrective action program (CAP) implementing procedures and attended CAP program meetings to assess the implementation of the CAP. |
| | |
| | The inspectors selectively reviewed risk and safety-significant issues entered in the CAP since the last NRC PI&R inspection in November 2007. The selection of issues ensured an adequate review of issues across the NRC cornerstones. The inspectors included issues identified through NRC generic communications, department self-assessments, licensee audits, operating experience reports, and NRC documented findings as part of this assessment. The inspectors also reviewed a selection of completed root, apparent and common cause evaluations. |
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| | The inspectors performed a more extensive review of the licensees control of cabling located in underground vaults, and corrective actions and temporary modifications that had been open for greater than one year. The review of the cabling located inside underground vaults consisted of a five year search of related issues identified in the CAP and discussions with appropriate licensee staff to assess the licensees efforts in addressing identified concerns. |
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| | During the reviews, the inspectors evaluated whether the licensee staffs actions were in compliance with the facilitys CAP and 10 CFR Part 50, Appendix B requirements. |
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| | Specifically, the inspectors evaluated if licensee personnel were identifying plant issues at the proper threshold, if these issues were entered into the CAP in a timely manner, and if these issues were appropriately resolved. The inspectors also evaluated whether root, apparent, and common cause evaluations were assigned and performed as appropriate. The inspectors also evaluated the timeliness and effectiveness of corrective actions for selected issue reports, completed investigations, and NRC-identified issues. |
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| | b. Assessment |
| | : (1) Effectiveness of Problem Identification Overall, the CAP program was effectively implemented in that issues were identified at a low threshold, evaluated and corrected. Workers were encouraged to identify issues and were familiar with the various avenues available (NRC, ECP, CAP, etc.). This was evident by the large number of CAP items generated annually, which were reasonably distributed across the various departments. A shared computerized database was used for creating individual reports and for subsequent management of the processes of issue evaluation and response. This included determining the issues significance, addressing such matters as regulatory compliance and reporting, and assigning any actions deemed necessary or appropriate. |
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| | However, the inspectors noted that the licensee performance indicators for monitoring the CAP program were not being effectively utilized. The inspectors identified that there was no requirement to investigate instances where indicators identified poor performance. For example, the inspectors noted that no Action Requests (ARs) had been initiated for several indicators that were either in the yellow or red band (indicating poor performance) during the past year. During interviews, licensee CAP staff commented that some of these indicators, because of how they were defined, may be inaccurately reporting performance. However, the inspectors could not find any CAP entries identifying these indicators so that they could be corrected. The inspectors questioned the efficacy of the indicators when no effort was made to evaluate instances when poor performance was identified or to revise those considered inaccurate. The licensee issued AR 993280 to evaluate this issue. |
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| | The inspectors determined that the station was generally effective at trending low level issues to prevent larger issues from developing. The licensee also used the CAP to document instances where previous corrective actions were ineffective or were inappropriately closed. |
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| | Findings No findings of significance were identified. |
| | : (2) Effectiveness of Prioritization and Evaluation of Issues The inspectors concluded that the station was generally effective at prioritizing and evaluating issues commensurate with the safety significance of the identified problem. |
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| | The inspectors determined that CAP screening meetings were generally thorough and maintained a high standard for approving actions. |
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| | The majority of issues were of low level and were either closed to trend or at a level appropriate for a condition evaluation. Some of these issues were closed to a work request or to another CAP report, but the inspectors noted that both the parent and daughter documents had the necessary verbiage to document the interrelationship. |
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| | The inspectors also had no concerns with those assigned an apparent, root or common cause evaluation. There were no items in the operations, engineering, or maintenance backlogs that were risk significant, individually or collectively. |
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| | Root, apparent and common cause evaluations were generally thorough; however, the inspectors did identify two examples where the level of review was less than appropriate: |
| | * AR 882701 was written to perform a common cause evaluation for an adverse trend regarding issues with work orders/packages. The evaluation identified that this issue had been recurring since 2003, but did not address why previous corrective actions were ineffective. |
| | * AR 784631 was written after the NRC resident inspectors had observed a high radiation barrier (fenced enclosure) that had been built adjacent to the Unit 1 safety-related Standby Gas Treatment System piping. The barrier was in contact with the piping (potentially raising a concern regarding the seismic analysis), but there was no licensee evaluation supporting this condition. Subsequently, the barrier was removed, but there was no documentation for its removal. |
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| | The licensee captured the above issues in the CAP as AR Nos. 996319 and 995883. |
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| | The inspectors determined that the licensee was generally effective at evaluating equipment functionality requirements after a degraded or non-conforming issue was identified. The inspectors reviewed Maintenance Rule action plans associated with systems currently in (a)(1) and for those returning to a(2) status within the last two years. No issues were identified from this review. |
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| | The inspectors also concluded that the licensee had been effectively managing underground cabling. |
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| | Findings No findings of significance were identified. |
| | : (3) Effectiveness of Corrective Actions The inspectors concluded that corrective actions for identified deficiencies were generally timely and adequately implemented, commensurate with their safety significance. The inspectors also concluded that sampled corrective actions assignments for selected NRC documented violations were generally effective and timely. However the inspectors did notice some untimely corrective actions as described below. |
| | * AR 840401 was written after the NRC identified a non-safety hanger attached to a safety related cable tray. In the evaluation, the licensee failed to note that the same issue had been previously identified about four years earlier (AR 352075)and that corrective actions had not been taken. |
| | * The inspectors noted that the licensee had not taken appropriate action to address potential preconditioning due to inappropriate work scheduling (for example, scheduling a post-maintenance test just prior to a surveillance test)despite having two prior NRC-identified instances of such, associated with the main steam isolation valves and reactor core isolation cooling systems. |
| | * AR 856961 was written to address oscillations observed on a Unit 1 control rod drive flow control valve. Although a work order was written to address this, it remained open for over two years. The inspectors did not identify any CAP item evaluating why the work order was open for so long. |
| | * AR 736409 was written to address high dose rates associated with a radioactive waste sample sink. The AR was closed to a work order, but there was no documentation that the work was actually performed. |
| | * The inspectors noted that work orders associated with the removal of temporary modifications, did not contain the necessary cross-referencing as required by procedure (i.e., neither the work order nor the temporary modification paperwork referenced the other). |
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| | The licensee wrote ARs 989540, 995336, 995957 and 988746, respectively, to address the above issues. |
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| | The inspectors also identified that numerous, recurring issues (since 2006) with the Units 1 and 2 gaseous and particulate radiation monitors used for reactor leak detection had not been resolved. The issues were varied and potentially affected the reliability of the monitors. Although these monitors were nonsafety-related, they were required by Technical Specifications. The licensee had performed past cause evaluations that had recommended corrective actions, but these actions had not been implemented. |
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| | Additionally, the licensee had not evaluated whether the issues significantly impacted the ability of the monitors to detect primary system leakage. The licensee subsequently identified that the monitors would perform the Technical Specification function and wrote AR 989527 to address this issue. |
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| | The licensee had 19 open corrective actions that were greater than one year old, with the oldest being 731 days old. The inspectors verified that the open actions were appropriate, that work orders were in place (and scheduled) for final implementation of the action, and that plant operation or risk was not adversely affected. |
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| | Findings No findings of significance were identified. |
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| | ===.2 Assessment of the Use of Operating Experience=== |
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| | ====a. Inspection Scope==== |
| | The inspectors reviewed the licensees implementation of the facilitys OE program. |
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| | Specifically, the inspectors reviewed implementing OE program procedures, observed daily station and pre-job briefings to observe the use of OE information, and selectively reviewed completed evaluations of OE issues and events. The intent of the review was to determine whether the licensee was effectively integrating OE experience into the performance of daily activities, whether evaluations of issues were proper and conducted by qualified personnel, whether the licensees program was sufficient to prevent future occurrences of previous industry events, and whether the licensee effectively used the information in developing departmental assessments and facility audits. The inspectors also assessed if corrective actions, as a result of OE experience, were identified and effectively implemented. |
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| | b. Assessment The inspectors concluded that the station appropriately screened OE information for applicability, and used the information for corrective and preventative actions to identify and prevent similar issues. The inspectors observed that OE was discussed as part of the daily station and pre-job briefings and was effectively disseminated across the various plant departments. During interviews with the inspectors, licensee staff generally commented favorably on the use of OE in their daily activities. |
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| | Although OE was considered as part of root, apparent and common cause evaluations, the inspectors identified that these reviews were not always documented in accordance with CAP procedures. The licensee had identified several examples during self-assessments conducted in 2008 and 2009 and had taken corrective action. |
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| | A subsequent licensee review, conducted prior to the NRC PI&R inspection, had identified no additional issues. However, the inspectors identified several examples where OE potentially applicable to the station was either not reviewed or the review was not documented as required. These examples occurred after the licensee self-assessments were completed, and were not identified in the licensees effectiveness review. The licensee initiated AR 995934 to evaluate this issue. |
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| | The inspectors also noted that the licensees staff was not required to evaluate whether the failure to use OE was a contributing cause of an event. Instead, the staff was only required to identify OE related to an event and use any insights gained in developing the corrective actions. The inspectors noted that several of the licensees root, apparent and common cause evaluations had identified OE that may have prevented the event had it been appropriately evaluated. The licensee initiated AR 995981 to evaluate this issue. |
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| | Findings No findings of significance were identified. |
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| | ===.3 Assessment of Self-Assessments and Audits=== |
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| | ====a. Inspection Scope==== |
| | The inspectors reviewed selected focused area self-assessments, check-in self-assessments, root cause effectiveness reviews, and NOS audits. The inspectors evaluated whether these audits and self-assessments were being effectively managed, adequately covered the subject areas, and whether identified issues were appropriately captured in the CAP. In addition, the inspectors also interviewed licensee personnel regarding the implementation of the audit and self-assessment programs. |
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| | b. Assessment The inspectors concluded that self-assessments and audits were typically accurate, thorough, and effective at identifying issues and enhancement opportunities at an appropriate threshold level. The inspectors concluded that these audits and self-assessments were completed by personnel knowledgeable in the subject area. |
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| | The inspectors considered the quality of the NOS audits to be thorough and critical. |
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| | The self-assessments were acceptable but, as expected, they were not at the same level of quality as the audits. The inspectors observed that CAP items had been initiated for issues identified through the NOS audits and self-assessments. |
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| | Findings No findings of significance were identified. |
| | |
| | ===.4 Assessment of Safety-Conscious Work Environment (SCWE)=== |
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| | ====a. Inspection Scope==== |
| | The inspectors interviewed selected members of the licensees staff to determine if there were any impediments of a SCWE. In addition, the inspectors discussed the implementation of the ECP with the ECP coordinators, and reviewed 2007 - 2009 ECP activities to identify any emergent issues or potential trends. In addition, the inspectors reviewed the facilitys ECP implementing procedures, interviewed the licensee ECP coordinators, and reviewed licensee safety culture surveys. The licensees programs to publicize the CAP and ECP programs were also reviewed. |
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| | b. Assessment The inspectors determined that the plant staff were aware of the importance of having a strong SCWE and expressed a willingness to raise safety issues. No one interviewed had experienced retaliation for safety issues raised, or knew of anyone who had failed to raise issues. All persons interviewed had an adequate knowledge of the CAP and ECP process. These results were similar to the findings of the licensees safety culture surveys. Based on these interviews, the inspectors concluded that there was no evidence of an unacceptable SCWE. |
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| | The inspectors determined that the ECP process was being effectively implemented. |
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| | The review of the selected ECP issues indicated that site personnel were appropriately using the CAP and ECP to identify concerns. However, during the interviews most station personnel did not know where the ECP office was located, although they could identify the ECP personnel. This did not appear to have a detrimental affect, based on the number of ECP issues currently in the system. |
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| | However, the inspectors observed that ECP issues not captured in a formal case file, were not always well documented. This resulted in some uncertainty regarding whether potentially significant issues were appropriately dispositioned. For example, there was one issue regarding a plant individual who exhibited signs of aberrant behavior while on shift. Although this concern was documented by the ECP staff, a formal case record was not opened. The inspectors could find no record of whether this concern was reviewed by the security staff as required by the site Security plan. Subsequently, the inspectors verified that this had occurred; however, the lack of a written record made it somewhat difficult to confirm. The ECP staff acknowledged this issue and was developing corrective actions. However, due to the potential to release confidential information, this observation was not captured in the CAP. |
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| | Findings No findings of significance were identified. |
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| {{a|4OA6}} | | {{a|4OA6}} |
| ==4OA6 Management Meetings.......................................................................................== | | ==4OA6 Management Meetings== |
| .9
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| | ===.1 Exit Meeting Summary=== |
| | * On November 23, 2009, the inspectors presented the inspection results to Mr. Wozniak and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary. |
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| | ATTACHMENT: |
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| =SUPPLEMENTAL INFORMATION= | | =SUPPLEMENTAL INFORMATION= |
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| ==KEY POINTS OF CONTACT== | | ==KEY POINTS OF CONTACT== |
| .....................................................................................................1 | | |
| | Licensee |
| | : [[contact::J. Bashor]], Engineering Director |
| | : [[contact::L. Blunk]], Operations Training Manager |
| | : [[contact::A. Byers]], Performance Improvement Specialist |
| | : [[contact::K. Ihnen]], Nuclear Oversight Manager |
| | : [[contact::B. Rash]], Maintenance Director |
| | : [[contact::T. Simpkin]], Regulatory Assurance Manager |
| | : [[contact::K. Taber]], Operations Director |
| | : [[contact::J. Vergara]], Senior Regulatory Specialist |
| | : [[contact::H. Vinyard]], Work Management Director |
| | : [[contact::D. Wozniak]], Site Vice President |
| | Nuclear Regulatory Commission |
| | : [[contact::K. Riemer]], Chief, Branch 2, Division of Reactor Projects |
| | |
| ==LIST OF ITEMS== | | ==LIST OF ITEMS== |
| OPENED, CLOSED AND DISCUSSED.........................................................1
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| ==LIST OF DOCUMENTS REVIEWED==
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| .........................................................................................2
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| ==LIST OF ACRONYMS==
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| : [[US]] [[]]
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| ED..................................................................................................19
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| Enclosure
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| : [[SUMMAR]] [[Y]]
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| : [[OF]] [[]]
| |
| : [[FINDIN]] [[]]
| |
| : [[GS]] [[]]
| |
| : [[IR]] [[05000373/2009007; 05000374/2009007 (November 2, 2009 - November 20, 2009), LaSalle County Station Units 1 and 2; Biennial Baseline Inspection of the Identification and Resolution of Problems. This team inspection was performed by three regional inspectors and the site resident inspector. No findings or violations were identified. Identification and Resolution of Problems Overall, the corrective action program (]]
| |
| CAP) was being effectively implemented. Issues were identified at a low threshold, evaluated and corrected. Self-assessments and audits by Nuclear Oversight (NOS) were thorough and critical of the assessed areas. Operating experience was recognized as valuable and was effectively communicated. Interviews with
| |
| licensee staff and a review of the Employee Concerns Program (ECP) indicated that the
| |
| licensee had a positive safety culture environment that encouraged identification of issues in the CAP. However, the inspectors identified several areas of concern that may negatively impact the licensee's ability to identify and resolve issues. In some cases, these issues had been
| |
| recognized by the licensee, but effective corrective action had not been taken. Briefly, the
| |
| issues were: The current
| |
| : [[CAP]] [[performance indicators were not always effectively used or sufficient to monitor the program. Although the licensee was aware of these issues,]]
| |
| CAP staff appeared willing to live with the shortcomings and had not formally taken corrective action. There were some examples of long-standing issues that were either not corrected or not evaluated. In some cases, the licensee had identified the issues, but had not evaluated why previous corrective actions were ineffective. There were several examples where the review of operating experience (OE) in cause evaluations were not documented in accordance with licensee procedures. Additionally, there was no formal requirement to evaluate whether the failure to use OE was a precursor during the evaluation of events. Although the licensee had identified these
| |
| issues in the
| |
| : [[CAP]] [[, the corrective actions were somewhat limited. Issues that were reviewed by the]]
| |
| ECP, but not captured in a formal case file, were not always well documented. This resulted in some uncertainty regarding whether potentially significant issues were appropriately dispositioned.
| |
| Enclosure
| |
| : [[A.]] [[]]
| |
| NRC-Identified and Self-Revealed Findings Cornerstone: Mitigating Systems None. B. Licensee-Identified Violations No violations of significance were identified.
| |
| Enclosure
| |
| : [[REPORT]] [[]]
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| : [[DETAIL]] [[S 4.]]
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| : [[OTHER]] [[]]
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| : [[ACTIVI]] [[TIES]]
| |
| : [[4OA]] [[2 Problem Identification and Resolution (71152B) The activities documented in Sections .1 through .4 constituted one biennial sample of Problem Identification and Resolution (]]
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| PI&R) as defined in Inspection Procedure
| |
| (IP) 71152. .1 Assessment of the Corrective Action Program Effectiveness a. Inspection Scope The inspectors reviewed the licensee's corrective action program (CAP) implementing procedures and attended
| |
| : [[CAP]] [[program meetings to assess the implementation of the]]
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| : [[CAP.]] [[The inspectors selectively reviewed risk and safety-significant issues entered in the]]
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| : [[CAP]] [[since the last]]
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| NRC PI&R inspection in November 2007. The selection of issues ensured
| |
| an adequate review of issues across the
| |
| : [[NRC]] [[cornerstones. The inspectors included issues identified through]]
| |
| NRC generic communications, department self-assessments, licensee audits, operating experience reports, and NRC documented findings as part of
| |
| this assessment. The inspectors also reviewed a selection of completed root, apparent
| |
| and common cause evaluations. The inspectors performed a more extensive review of the licensee's control of cabling located in underground vaults, and corrective actions and temporary modifications that had been open for greater than one year. The review of the cabling located inside
| |
| underground vaults consisted of a five year search of related issues identified in the CAP
| |
| and discussions with appropriate licensee staff to assess the licensee's efforts in
| |
| addressing identified concerns. During the reviews, the inspectors evaluated whether the licensee staff's actions were in compliance with the facility's
| |
| : [[CAP]] [[and 10]]
| |
| CFR Part 50, Appendix B requirements. Specifically, the inspectors evaluated if licensee personnel were identifying plant issues
| |
| at the proper threshold, if these issues were entered into the CAP in a timely manner,
| |
| and if these issues were appropriately resolved. The inspectors also evaluated whether
| |
| root, apparent, and common cause evaluations were assigned and performed as appropriate. The inspectors also evaluated the timeliness and effectiveness of corrective actions for selected issue reports, completed investigations, and
| |
| : [[NRC]] [[-identified issues. b. Assessment (1) Effectiveness of Problem Identification Overall, the]]
| |
| : [[CAP]] [[program was effectively implemented in that issues were identified at a low threshold, evaluated and corrected. Workers were encouraged to identify issues and were familiar with the various avenues available (NRC,]]
| |
| : [[ECP]] [[,]]
| |
| CAP, etc.). This was
| |
| evident by the large number of CAP items generated annually, which were reasonably
| |
| Enclosure distributed across the various departments. A shared computerized database was used for creating individual reports and for subsequent management of the processes of issue
| |
| evaluation and response. This included determining the issue's significance, addressing such matters as regulatory compliance and reporting, and assigning any actions deemed necessary or appropriate. However, the inspectors noted that the licensee performance indicators for monitoring the CAP program were not being effectively utilized. The inspectors identified that there
| |
| was no requirement to investigate instances where indicators identified poor
| |
| performance. For example, the inspectors noted that no Action Requests (ARs) had been initiated for several indicators that were either in the yellow or red band (indicating poor performance) during the past year. During interviews, licensee CAP staff
| |
| commented that some of these indicators, because of how they were defined, may be
| |
| inaccurately reporting performance. However, the inspectors could not find any CAP
| |
| entries identifying these indicators so that they could be corrected. The inspectors questioned the efficacy of the indicators when no effort was made to evaluate instances when poor performance was identified or to revise those considered inaccurate. The
| |
| licensee issued
| |
| : [[AR]] [[993280 to evaluate this issue. The inspectors determined that the station was generally effective at trending low level issues to prevent larger issues from developing. The licensee also used the]]
| |
| CAP to document instances where previous corrective actions were ineffective or were inappropriately closed. Findings No findings of significance were identified. (2) Effectiveness of Prioritization and Evaluation of Issues The inspectors concluded that the station was generally effective at prioritizing and evaluating issues commensurate with the safety significance of the identified problem. The inspectors determined that CAP screening meetings were generally thorough and
| |
| maintained a high standard for approving actions.
| |
|
| |
|
| The majority of issues were of low level and were either closed to trend or at a level appropriate for a condition evaluation. Some of these issues were closed to a work request or to another CAP report, but the inspectors noted that both the parent and
| | ===OPENED, CLOSED AND DISCUSSED=== |
| daughter documents had the necessary verbiage to document the interrelationship.
| | |
| The inspectors also had no concerns with those assigned an apparent, root or common
| | ===Opened and Closed=== |
| cause evaluation. There were no items in the operations, engineering, or maintenance
| | |
| backlogs that were risk significant, individually or collectively. Root, apparent and common cause evaluations were generally thorough; however, the inspectors did identify two examples where the level of review was less than appropriate: AR 882701 was written to perform a common cause evaluation for an adverse trend regarding issues with work orders/packages. The evaluation identified that this issue had been recurring since 2003, but did not address why previous
| | None. |
| corrective actions were ineffective.
| |
| Enclosure
| |
| : [[AR]] [[784631 was written after the]]
| |
| NRC resident inspectors had observed a high radiation barrier (fenced enclosure) that had been built adjacent to the Unit 1 safety-related Standby Gas Treatment System piping. The barrier was in contact
| |
| with the piping (potentially raising a concern regarding the seismic analysis), but
| |
| there was no licensee evaluation supporting this condition. Subsequently, the barrier was removed, but there was no documentation for its removal. The licensee captured the above issues in the
| |
| : [[CAP]] [[as]]
| |
| AR Nos. 996319 and 995883.
| |
| The inspectors determined that the licensee was generally effective at evaluating equipment functionality requirements after a degraded or non-conforming issue was
| |
| identified. The inspectors reviewed Maintenance Rule action plans associated with
| |
| systems currently in (a)(1) and for those returning to a(2) status within the last two years. No issues were identified from this review.
| |
| The inspectors also concluded that the licensee had been effectively managing
| |
| underground cabling.
| |
| Findings
| |
| No findings of significance were identified.
| |
| (3) Effectiveness of Corrective Actions The inspectors concluded that corrective actions for identified deficiencies were generally timely and adequately implemented, commensurate with their safety significance. The inspectors also concluded that sampled corrective actions
| |
| assignments for selected
| |
| : [[NRC]] [[documented violations were generally effective and timely. However the inspectors did notice some untimely corrective actions as described below.]]
| |
| : [[AR]] [[840401 was written after the]]
| |
| : [[NRC]] [[identified a non-safety hanger attached to a safety related cable tray. In the evaluation, the licensee failed to note that the same issue had been previously identified about four years earlier (]]
| |
| AR 352075) and that corrective actions had not been taken. The inspectors noted that the licensee had not taken appropriate action to address potential preconditioning due to inappropriate work scheduling (for example, scheduling a post-maintenance test just prior to a surveillance test)
| |
| despite having two prior NRC-identified instances of such, associated with the
| |
| main steam isolation valves and reactor core isolation cooling systems.
| |
| : [[AR]] [[856961 was written to address oscillations observed on a Unit 1 control rod drive flow control valve. Although a work order was written to address this, it remained open for over two years. The inspectors did not identify any]]
| |
| : [[CAP]] [[item evaluating why the work order was open for so long.]]
| |
| : [[AR]] [[736409 was written to address high dose rates associated with a radioactive waste sample sink. The]]
| |
| AR was closed to a work order, but there was no documentation that the work was actually performed.
| |
| Enclosure The inspectors noted that work orders associated with the removal of temporary modifications, did not contain the necessary cross-referencing as required by procedure (i.e., neither the work order nor the temporary modification paperwork
| |
| referenced the other). The licensee wrote ARs 989540, 995336, 995957 and 988746, respectively, to address the above issues. The inspectors also identified that numerous, recurring issues (since 2006) with the Units 1 and 2 gaseous and particulate radiation monitors used for reactor leak detection
| |
| had not been resolved. The issues were varied and potentially affected the reliability of
| |
| the monitors. Although these monitors were nonsafety-related, they were required by
| |
| Technical Specifications. The licensee had performed past cause evaluations that had recommended corrective actions, but these actions had not been implemented. Additionally, the licensee had not evaluated whether the issues significantly impacted the ability of the monitors to detect primary system leakage. The licensee subsequently
| |
| identified that the monitors would perform the Technical Specification function and wrote
| |
| AR 989527 to address this issue. The licensee had 19 open corrective actions that were greater than one year old, with the oldest being 731 days old. The inspectors verified that the open actions were
| |
| appropriate, that work orders were in place (and scheduled) for final implementation of
| |
| the action, and that plant operation or risk was not adversely affected.
| |
| Findings
| |
| No findings of significance were identified. .2 Assessment of the Use of Operating Experience a. Inspection Scope The inspectors reviewed the licensee's implementation of the facility's
| |
| : [[OE]] [[program. Specifically, the inspectors reviewed implementing]]
| |
| OE program procedures, observed daily station and pre-job briefings to observe the use of OE information, and selectively
| |
| reviewed completed evaluations of OE issues and events. The intent of the review was
| |
| to determine whether the licensee was effectively integrating OE experience into the
| |
| performance of daily activities, whether evaluations of issues were proper and conducted by qualified personnel, whether the licensee's program was sufficient to prevent future occurrences of previous industry events, and whether the licensee
| |
| effectively used the information in developing departmental assessments and facility audits. The inspectors also assessed if corrective actions, as a result of OE experience,
| |
| were identified and effectively implemented. b. Assessment The inspectors concluded that the station appropriately screened OE information for applicability, and used the information for corrective and preventative actions to identify
| |
| and prevent similar issues. The inspectors observed that OE was discussed as part of
| |
| the daily station and pre-job briefings and was effectively disseminated across the
| |
| Enclosure various plant departments. During interviews with the inspectors, licensee staff generally commented favorably on the use of
| |
| : [[OE]] [[in their daily activities. Although]]
| |
| OE was considered as part of root, apparent and common cause evaluations, the inspectors identified that these reviews were not always documented in accordance with CAP procedures. The licensee had identified several examples during
| |
| self-assessments conducted in 2008 and 2009 and had taken corrective action.
| |
| A subsequent licensee review, conducted prior to the
| |
| : [[NRC]] [[]]
| |
| PI&R inspection, had
| |
| identified no additional issues. However, the inspectors identified several examples
| |
| where OE potentially applicable to the station was either not reviewed or the review was not documented as required. These examples occurred after the licensee self-assessments were completed, and were not identified in the licensee's effectiveness
| |
| review. The licensee initiated
| |
| : [[AR]] [[995934 to evaluate this issue. The inspectors also noted that the licensee's staff was not required to evaluate whether the failure to use]]
| |
| OE was a contributing cause of an event. Instead, the staff was only required to identify OE related to an event and use any insights gained in developing the corrective actions. The inspectors noted that several of the licensee's root, apparent
| |
| and common cause evaluations had identified OE that may have prevented the event
| |
| had it been appropriately evaluated. The licensee initiated AR 995981 to evaluate this
| |
| issue. Findings No findings of significance were identified. .3 Assessment of Self-Assessments and Audits a. Inspection Scope The inspectors reviewed selected focused area self-assessments, check-in self-assessments, root cause effectiveness reviews, and NOS audits. The inspectors evaluated whether these audits and self-assessments were being effectively managed, adequately covered the subject areas, and whether identified issues were appropriately
| |
| captured in the CAP. In addition, the inspectors also interviewed licensee personnel
| |
| regarding the implementation of the audit and self-assessment programs. b. Assessment The inspectors concluded that self-assessments and audits were typically accurate, thorough, and effective at identifying issues and enhancement opportunities at an
| |
| appropriate threshold level. The inspectors concluded that these audits and
| |
| self-assessments were completed by personnel knowledgeable in the subject area. The inspectors considered the quality of the NOS audits to be thorough and critical.
| |
| The self-assessments were acceptable but, as expected, they were not at the same level of quality as the audits. The inspectors observed that
| |
| : [[CAP]] [[items had been initiated for issues identified through the]]
| |
| NOS audits and self-assessments. Findings No findings of significance were identified.
| |
| Enclosure .4 Assessment of Safety-Conscious Work Environment (SCWE) a. Inspection Scope The inspectors interviewed selected members of the licensee's staff to determine if there were any impediments of a
| |
| : [[SCWE.]] [[In addition, the inspectors discussed the implementation of the]]
| |
| : [[ECP]] [[with the]]
| |
| : [[ECP]] [[coordinators, and reviewed 2007 - 2009]]
| |
| : [[ECP]] [[activities to identify any emergent issues or potential trends. In addition, the inspectors reviewed the facility's]]
| |
| : [[ECP]] [[implementing procedures, interviewed the licensee]]
| |
| : [[ECP]] [[coordinators, and reviewed licensee safety culture surveys. The licensee's programs to publicize the]]
| |
| : [[CAP]] [[and]]
| |
| : [[ECP]] [[programs were also reviewed. b. Assessment The inspectors determined that the plant staff were aware of the importance of having a strong]]
| |
| : [[SC]] [[]]
| |
| WE and expressed a willingness to raise safety issues. No one interviewed had experienced retaliation for safety issues raised, or knew of anyone who had failed to
| |
| raise issues. All persons interviewed had an adequate knowledge of the
| |
| : [[CAP]] [[and]]
| |
| ECP process. These results were similar to the findings of the licensee's safety culture surveys. Based on these interviews, the inspectors concluded that there was no
| |
| evidence of an unacceptable
| |
| : [[SCWE.]] [[The inspectors determined that the]]
| |
| : [[ECP]] [[process was being effectively implemented. The review of the selected]]
| |
| : [[ECP]] [[issues indicated that site personnel were appropriately using the]]
| |
| : [[CAP]] [[and]]
| |
| : [[ECP]] [[to identify concerns. However, during the interviews most station personnel did not know where the]]
| |
| ECP office was located, although they could
| |
| identify the ECP personnel. This did not appear to have a detrimental affect, based on
| |
| the number of
| |
| : [[ECP]] [[issues currently in the system. However, the inspectors observed that]]
| |
| ECP issues not captured in a formal case file, were not always well documented. This resulted in some uncertainty regarding whether potentially significant issues were appropriately dispositioned. For example, there was one issue regarding a plant individual who exhibited signs of aberrant behavior while on
| |
| shift. Although this concern was documented by the ECP staff, a formal case record
| |
| was not opened. The inspectors could find no record of whether this concern was
| |
| reviewed by the security staff as required by the site Security plan. Subsequently, the inspectors verified that this had occurred; however, the lack of a written record made it somewhat difficult to confirm. The ECP staff acknowledged this issue and was
| |
| developing corrective actions. However, due to the potential to release confidential
| |
| information, this observation was not captured in the CAP. Findings No findings of significance were identified.
| |
| Enclosure
| |
| : [[4OA]] [[6 Management Meetings .1 Exit Meeting Summary On November 23, 2009, the inspectors presented the inspection results to Mr. Wozniak and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.]]
| |
| : [[ATTACH]] [[MENT:]]
| |
| : [[SUPPLE]] [[]]
| |
| : [[MENTAL]] [[]]
| |
| : [[INFORM]] [[]]
| |
| : [[ATION]] [[Attachment]]
| |
| : [[SUPPLE]] [[]]
| |
| : [[MENTAL]] [[]]
| |
| : [[INFORM]] [[]]
| |
| : [[ATION]] [[]]
| |
| : [[KEY]] [[]]
| |
| : [[POINTS]] [[]]
| |
| : [[OF]] [[]]
| |
| CONTACT Licensee J. Bashor, Engineering Director L. Blunk, Operations Training Manager
| |
| A. Byers, Performance Improvement Specialist
| |
| K. Ihnen, Nuclear Oversight Manager
| |
| B. Rash, Maintenance Director
| |
| T. Simpkin, Regulatory Assurance Manager K. Taber, Operations Director J. Vergara, Senior Regulatory Specialist
| |
| : [[H.]] [[Vinyard, Work Management Director]]
| |
| : [[D.]] [[Wozniak, Site Vice President Nuclear Regulatory Commission K. Riemer, Chief, Branch 2, Division of Reactor Projects]]
| |
| : [[LIST]] [[]]
| |
| : [[OF]] [[]]
| |
| : [[ITEMS]] [[]]
| |
| : [[OPENED]] [[,]]
| |
| : [[CLOSED]] [[]]
| |
| : [[AND]] [[]]
| |
| DISCUSSED Opened and Closed None.
| |
| Attachment | | Attachment |
| : [[LIST]] [[]]
| |
| : [[OF]] [[]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| : [[ED]] [[The following is a list of documents reviewed during the inspection. Inclusion on this list does not imply that the]]
| |
| : [[NRC]] [[inspectors reviewed the documents in their entirety, but rather, that selected sections of portions of the documents were evaluated as part of the overall inspection effort. Inclusion of a document on this list does not imply]]
| |
| NRC acceptance of the document or
| |
| any part of it, unless this is stated in the body of the inspection report.
| |
| : [[PLANT]] [[]]
| |
| : [[PROCED]] [[URES Number Description or Title Date or Revision]]
| |
| : [[LS]] [[-]]
| |
| : [[AA]] [[-1012 Safety Culture Monitoring Revision]]
| |
| : [[0 EI]] [[-]]
| |
| : [[AA]] [[-101 Employee Concerns Program Revision]]
| |
| : [[8 EI]] [[-]]
| |
| : [[AA]] [[-1 Safety-Conscious Work Environment Revision]]
| |
| : [[2 EI]] [[-]]
| |
| : [[AA]] [[-101-1001 Employee Concerns Program Processes Revision]]
| |
| : [[8 LS]] [[-]]
| |
| : [[AA]] [[-1012 Safety Culture Monitoring Revision]]
| |
| : [[0 CC]] [[-]]
| |
| : [[AA]] [[-103 Configuration Control for Permanent Physical Plant Changes Revision]]
| |
| : [[19 AD]] [[-]]
| |
| : [[AA]] [[-2001 Management and Oversight of Supplemental Workforce Revision]]
| |
| : [[6 LS]] [[-]]
| |
| : [[AA]] [[-1001 Root Cause Analysis Manual Revision]]
| |
| : [[7 LS]] [[-]]
| |
| : [[AA]] [[-126-1007 Performance Improvement Toolbox Revision]]
| |
| : [[1 CC]] [[-]]
| |
| : [[AA]] [[-112 Temporary Configuration Changes Revision]]
| |
| : [[14 LS]] [[-]]
| |
| : [[AA]] [[-115-1004 Processing of]]
| |
| : [[NER]] [[s And]]
| |
| : [[NNOE]] [['s Revision]]
| |
| : [[0 LS]] [[-]]
| |
| : [[AA]] [[-115 Operating Experience Procedure Revisions 3,4,5 and]]
| |
| : [[10 LS]] [[-]]
| |
| : [[AA]] [[-115-1003 Processing of Significance Level]]
| |
| : [[3 OPEX]] [[Evaluations Revision 0]]
| |
| : [[LS]] [[-AA-115-1002 Processing of Significance Level]]
| |
| : [[2 OPEX]] [[Evaluations Revision 0]]
| |
| : [[LS]] [[-AA-115-1001 Processing of Significance Level]]
| |
| : [[1 OPEX]] [[Evaluations Revision 0]]
| |
| : [[LS]] [[-AA-115 Operating Experience Program Revision]]
| |
| : [[14 LOP]] [[-]]
| |
| : [[HS]] [[-01 Hydrogen Seal Oil System Startup and Operation Revision]]
| |
| : [[18 LOP]] [[-]]
| |
| : [[HS]] [[-03 Hydrogen Seal Oil System Shutdown Revision]]
| |
| : [[13 LOP]] [[-]]
| |
| : [[WL]] [[-01 Filling and Venting the Lake Makeup Piping Revision]]
| |
| : [[16 LOP]] [[-]]
| |
| : [[WL]] [[-01 Filling and Venting the Lake Makeup Piping Revision]]
| |
| : [[15 LOP]] [[-]]
| |
| : [[WL]] [[-13 Filling the Makeup Line with the Makeup Pump(s) Revision]]
| |
| : [[5 LIP]] [[-]]
| |
| : [[RH]] [[-602B Unit]]
| |
| : [[2 RHR]] [[Pump 2B/2C Flow Indication Calibration Revision 5]]
| |
| : [[LS]] [[-AA-125-1002 Common Cause Analysis Manual Revision]]
| |
| : [[6 LS]] [[-]]
| |
| AA-125-1003 Apparent Cause Evaluation Manual Revision 8
| |
| Attachment
| |
| : [[CORREC]] [[]]
| |
| : [[TIVE]] [[]]
| |
| : [[ACTION]] [[]]
| |
| : [[PROGRA]] [[M]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| : [[ED]] [[Number Description or Title Date or Revision 871625 L2R12-FME [Foreign Material] Accumulated Debris on Reactor Jet Pump 15 1/25/2009 732084 1A]]
| |
| : [[DG]] [[[Diesel Generator] Room Vent Supply Filter High D/P 2/5/2008 727393 Unit 1 Control Rod 18-39 Inoperable 1/27/2008 727361 Unit 1 Control Rod 18-23 Inoperable 1/26/2008 721332 Unit 1]]
| |
| : [[RR]] [[[Reactor Recirculation] Flow Change 1/11/2008]]
| |
| : [[970547 NOS]] [[[Nuclear Oversight] Identifies]]
| |
| : [[PI&R]] [[]]
| |
| : [[FASA]] [[[Focused Area Self-Assessment] Plan and Report Issues 9/25/2009 954832]]
| |
| : [[NOS]] [[]]
| |
| : [[ID]] [[:]]
| |
| : [[CAPR]] [[872750-14 Closure Issues 8/18/2009]]
| |
| : [[945993 LOA]] [[-]]
| |
| : [[PWR]] [[-101 Reference Error 7/10/2009 919749 Insufficient]]
| |
| : [[CA]] [[Closure Documentation 1/23/2009 901425]]
| |
| : [[CCA]] [[Actions not Created by Department 11/26/2008]]
| |
| : [[899233 IR]] [[891213 and]]
| |
| : [[IR]] [[891204 Incorrectly Closed to One Another 3/29/2009 680941 Off Scale Control Room Reading 10/6/2007 710857 Worker Alarmed]]
| |
| : [[MAF]] [[Portal Monitor 12/12/2007 694587 Low Level Issues]]
| |
| : [[EP]] [[Drills 3rd/4th Quarter Facilities 9/26/2007 709901]]
| |
| : [[6 MREM]] [[Emergent Dose was Received 12/10/2007 710836 Security-Weapons Cabinet at India Needs Anchored 12/12/2007 711281]]
| |
| : [[LS]] [[-AA-115 Review Needed for]]
| |
| : [[OE]] [[25417 12/12/2007 742353 Multiple]]
| |
| : [[TSI]] [[]]
| |
| : [[OK]] [[]]
| |
| : [[LED]] [['s not Lit 2/28/2008 731386 Reactor Building High Rad Alarm 2/4/2008 721355 Unit]]
| |
| : [[2 HWC]] [[[Hydrogen Water Chemistry] System Trip Due to High Hydrogen Pressure 1/12/2008 721319 Received Unexpected Unit 1]]
| |
| CRD [Control Rod Drive] HCU [Hydraulic Control Unit] Alarm for
| |
| Rod 42-51 1/12/2008 720249 Unexpected U1
| |
| : [[CRD]] [[Accumulator 54-23 Alarm 1/10/2008 872502 Shaw-Pipefitter Received Dose Rate Alarm in Drywell 1/26/2009 953952 Security-Vehicle Discovered Operable Without Key 8/16/2009 933571 Security Explosive Detector #1 and #2 Not Working Properly 6/21/2009 876268 Security-Live Round of Ammunition Declared at Check Point 2/4/2009 678960 Through Fault on L0104 Line Between Braidwood and LaSalle 9/15/2009 881434]]
| |
| TLD Ran Through X-Ray 2/17/2009 914174 NOS Finding in Corrective Action Effectiveness 4/30/2009
| |
| Attachment
| |
| : [[CORREC]] [[]]
| |
| : [[TIVE]] [[]]
| |
| : [[ACTION]] [[]]
| |
| : [[PROGRA]] [[M]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| : [[ED]] [[Number Description or Title Date or Revision]]
| |
| : [[914632 NOS]] [[]]
| |
| : [[ID]] [[:]]
| |
| : [[RCR]] [[[Root Cause Report] Checklist Answered Improperly 5/1/2009 913283]]
| |
| : [[NOS]] [[]]
| |
| : [[ID]] [[: No Evidence of Valve Inspection 11/30/2007 914165]]
| |
| : [[NOS]] [[]]
| |
| : [[ID]] [[:]]
| |
| : [[CAP]] [[Investigations Do Not Meet Some Admin Requirements 4/30/2009 848279: assignment 30 Address Issues Raised During]]
| |
| : [[FASA]] [[with]]
| |
| : [[RCR]] [[641194 Provide Guidance On Documenting]]
| |
| : [[OPEX]] [[Use in]]
| |
| : [[CAP]] [[Investigations 10/26/2009 848279: assignment 24/01 Address Issues Raised During]]
| |
| : [[FASA]] [[with]]
| |
| : [[RCR]] [[641194 Provide Guidance On Documenting]]
| |
| : [[OPEX]] [[Use in]]
| |
| : [[CAP]] [[Investigations 10/26/2009]]
| |
| : [[840401 NRC]] [[Identified Inspection Findings in Aux Building Ceiling 11/04/2008 352075 Mass Spectrometer Duct Attachment to Cable Tray Support 7/1/2005 344802 Design Changes Required Due to Re-Location of Equipment 6/15/2005 849004]]
| |
| : [[NRC]] [[Potential Finding Undersized Spray Nozzles 11/21/2008]]
| |
| : [[708358 PI&R]] [[Inspection-Untimely Corrective Actions for]]
| |
| CSCS [Component System Cooling Water] Valve
| |
| Replacements 12/6/2007
| |
| : [[709749 NCV]] [[[Non-Cited Violation] Associated with Diesel Fuel Storage Not Fully Addressed 12/10/2007 703553]]
| |
| : [[TS]] [[B3.8.3 Fuel Oil Capacity Required for Division 3 Inconsistent 11/21/2007]]
| |
| : [[699901 TS]] [[Bases 3.8.3 Fuel Oil Capacity for 7 days Inconsistent 11/12/2007 955205]]
| |
| : [[NRC]] [[2nd Quarter Inspection Report 8/19/2009]]
| |
| : [[699299 NRC]] [[]]
| |
| : [[ID]] [['d Wrong Location for New]]
| |
| : [[2DG]] [[117 Valve in]]
| |
| : [[LOP]] [[-DG-09M 11/12/2007]]
| |
| : [[708359 PI&R]] [[Inspection-No Site Investigation for L1R11]]
| |
| : [[JP]] [[[Jet Pump]]]
| |
| : [[RB]] [[[Riser Brace] Delays 12/6/2007 729732]]
| |
| : [[NRC]] [[-Identified Problem 1/31/2008]]
| |
| : [[735802 NRC]] [[Identifies]]
| |
| : [[GAP]] [[in]]
| |
| : [[FME]] [[Barrier Curtain 2/13/2008 741419 During]]
| |
| : [[NRC]] [[Walkdown, Whip Restraint was Identified Loose 2/26/2008]]
| |
| : [[772740 NRC]] [[1st Quarter Inspection Report-Green Findings with One]]
| |
| : [[NCV]] [[3/31/2008 786350 Security-Training Records With Administrative Errors 6/13/2008]]
| |
| : [[841567 NRC]] [[Identified Appendix R]]
| |
| : [[ELBP]] [[Light Indication Abnormalities 11/6/2008]]
| |
| : [[846783 NRC]] [[Triennial: Smoke Detectors Affect Any Other Functions 11/12/2008]]
| |
| ACE 839916 Security Negligent Weapon Discharge 7/30/2009
| |
| Attachment
| |
| : [[CORREC]] [[]]
| |
| : [[TIVE]] [[]]
| |
| : [[ACTION]] [[]]
| |
| : [[PROGRA]] [[M]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| : [[ED]] [[Number Description or Title Date or Revision]]
| |
| : [[ACE]] [[731403 Unposted High Radiation Area Identified in Unit 1 Reactor Building B]]
| |
| RHR [Residual Heat Removal]
| |
| Pump Room 2/4/2007
| |
| : [[ACE]] [[728969 Workers Instructed to Log Off]]
| |
| : [[ED]] [[[Electronic Dosimeter] Prior to Exceeding]]
| |
| : [[X.]] [[4 Mrem 1/30/2008]]
| |
| : [[ACE]] [[]]
| |
| : [[728710 CA]] [[s fro]]
| |
| : [[CCA]] [[325231 Are Ineffective 1/29/2008]]
| |
| : [[ACE]] [[723807 Broken Fuel Bundle Spacer 1/17/2008]]
| |
| : [[ACE]] [[907825 Contamination Discovered Outside a Posted]]
| |
| : [[CA]] [[[Contaminated Area] 4/15/2009]]
| |
| : [[ACE]] [[687105 Security Posting Not Properly Documented 10/19/2007]]
| |
| : [[ACE]] [[696564 Cask Shoring Makes Contact With]]
| |
| : [[HIC]] [[[high integrity container] During Loading 11/8/2007]]
| |
| : [[ACE]] [[758197 L1R12 Steam Affected Dose 8.579]]
| |
| : [[REM]] [[Over Estimate 4/2/2008]]
| |
| : [[RCE]] [[696281]]
| |
| : [[CCA]] [[Rolled Into Root Cause Following Management Challenge (Modifications Not Fully Incorporated due to Lack of Clear Standards) 11/8/2007]]
| |
| : [[RCE]] [[872750 Unit 2 Refuel Bridge Mast-Braided Wire Cable 1 of 2 Failed 1/27/2009]]
| |
| : [[RCE]] [[]]
| |
| : [[752478 EP]] [[Pre-Exercise]]
| |
| : [[DEP]] [[Failure to Classify in Timely Manner 3/19/2008]]
| |
| : [[RCE]] [[924205]]
| |
| : [[RR]] [[[Reactor Recirculation] Ganged Controller Malfunction 5/27/2009]]
| |
| : [[RCE]] [[868704 Elevated Dose Rates Identified During L2R12 1/19/2009 924999]]
| |
| : [[MRC]] [[Directed]]
| |
| : [[IR]] [[from]]
| |
| : [[EACE]] [[Review: 1B]]
| |
| : [[HD]] [[[Heater Drain] Bearing Failure 4/4/2009 927524]]
| |
| : [[MRC]] [[Rejection of]]
| |
| : [[ACE]] [[908791]]
| |
| : [[EHC]] [[Software Mod Not Performed 6/3/2009]]
| |
| : [[940703 LAS]] [[]]
| |
| : [[VE]] [[Root Cause Does not Address All Potential Causes 7/10/2009]]
| |
| : [[963546 RA]] [[-]]
| |
| : [[FRPT]] [[Deficiency-IR 848279-Issues with]]
| |
| : [[RCR]] [[641194 9/3/2009 916994 Ineffective]]
| |
| : [[CAPR]] [[Associated With]]
| |
| : [[LVDT]] [[Failure]]
| |
| : [[RCR]] [[5/7/2009]]
| |
| : [[CCE]] [[882701 Investigate Documentation Issues For Past 9 Months 2/19/2009]]
| |
| : [[CCE]] [[676417 Adverse Trend in Radiation Protection Performance Indicator 9/26/2007]]
| |
| : [[CCE]] [[914174]]
| |
| : [[NOS]] [[Finding In Corrective Action Effectiveness 4/30/2009]]
| |
| : [[CCE]] [[901038 Online Dose Estimating Accuracy Needs Improvement 4/1/2009 899020 Declining Reliability of Radiation Monitors Across Fleet 3/28/2009 936524 System]]
| |
| IQ Assessment Report 6/29/2009 898613 Operations Identified Adverse Trend 1(2)PL15J and 1(2)PL75J 3/27/2009
| |
| Attachment
| |
| : [[CORREC]] [[]]
| |
| : [[TIVE]] [[]]
| |
| : [[ACTION]] [[]]
| |
| : [[PROGRA]] [[M]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| : [[ED]] [[Number Description or Title Date or Revision]]
| |
| : [[CCE]] [[827168 2]]
| |
| : [[PL]] [[15J Trouble In Main Control Room 10/6/2008]]
| |
| : [[CCE]] [[693124 Rad Monitor Trend Pull]]
| |
| : [[ID]] [['s Need for Further Investigation 11/1/2007 894269]]
| |
| : [[2PL]] [[75J Particulate Channel Rad Hi Alarm 3/18/2009 844159]]
| |
| : [[NOS]] [[]]
| |
| : [[ID]] [[Enhancement for New Fuel Transfer Basket 11/12/2008 704754]]
| |
| : [[NOS]] [[]]
| |
| : [[ID]] [[]]
| |
| : [[FPR]] [[[Fire Protection Report] Descriptions, Drawings, and Pre-Fire Plan Issues 11/28/2007 692354 U2]]
| |
| : [[SFP]] [[[Spent Fuel Pool] Boraflex Panel Degradation Projections through 7/1/08 10/31/2007 880430 L2R12 Shaw Performance Common Cause Analysis (]]
| |
| : [[AT]] [[865420-02) 2/13/2009]]
| |
| : [[798029 NOS]] [[]]
| |
| : [[ID]] [[: Finding Refrigerant Control Deficiencies 7/16/2008 892574 1C]]
| |
| : [[CW]] [[[Circulating Water] Pump Failure to Start, Then Overcurrent Conditions 3/13/2009 859439 L2R12 Late Work Order Generated from]]
| |
| : [[PM]] [[12/22/2008]]
| |
| : [[856855 EP]] [[]]
| |
| : [[FASA]] [[843943-Deficiency in Augmentation Drills Time/Day 12/16/2008 759725 Break In Lake Make Up Line Following System Pump Start 04/05/2008 799885 Perform Root Cause On Unit]]
| |
| : [[1 MDRFP]] [[Work Window 07/24/2008 756083 Training]]
| |
| : [[INPO]] [[]]
| |
| : [[ATV]] [[Identified]]
| |
| : [[OJT]] [[/TPE As Team Identified Finding 03/28/2008 916375 Technician Performed Task Without Qualification 05/06/2009 889582 Adverse Trend In]]
| |
| : [[MMD]] [[Performance 03/06/2009 889584 Adverse Trend In]]
| |
| : [[EMD]] [[Performance 03/06/2009 889592 Adverse Trend In]]
| |
| : [[IMD]] [[Performance 03/06/2009 693812 Labeling Discrepancy During 1]]
| |
| : [[VX]] [[08C Troubleshooting 11/02/2007]]
| |
| : [[735952 OSHA]] [[Recordable-]]
| |
| : [[WELDTE]] [[C 02/14/2008 737285 Shaw- 3" Line Incorrectly Identified in Minor]]
| |
| : [[WO]] [[Revision 02/16/2008 738459 Generator Seal Oil Ingress 02/19/2008 836359 Leak Work Off Curve Is Off Track 10/27/2008 852498]]
| |
| : [[NOS]] [[]]
| |
| : [[ID]] [[: Corrective Actions For Transient Combustible Issues 12/04/2008 874657 Shaw - Sea Van Slides Off Of Truck Backing Into Refuel Pad 02/01/2009 878589 Coordination Issue Between Turbine Roll and Switching 02/10/2009 911322 Vibration Analysis Identifies Wiped Bearing(s) On 0]]
| |
| : [[VL]] [[03C 04/24/2009]]
| |
| : [[665602 OPEX]] [[- LaSalle County Station]]
| |
| SME Review of OE25373 08/28/2007
| |
| Attachment
| |
| : [[CORREC]] [[]]
| |
| : [[TIVE]] [[]]
| |
| : [[ACTION]] [[]]
| |
| : [[PROGRA]] [[M]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| : [[ED]] [[Number Description or Title Date or Revision 633803 Wiring of]]
| |
| : [[STS]] [[Controller 0]]
| |
| : [[TIC]] [[-VC002 Does Not Match Drawing 05/25/2007 633816 Wiring for]]
| |
| : [[STS]] [[Controller 0]]
| |
| : [[TIC]] [[-VC045 Does Not Match Drawing 05/25/2007 633809 Wiring for]]
| |
| : [[STS]] [[Controller 0]]
| |
| : [[TIC]] [[-VC003 Does Not Match Drawing 05/25/2007 885736 Troubleshooting A Controller Issue 02/26/2009]]
| |
| : [[771796 STS]] [[Controller Mod Enhancements 05/05/2008 889586 Adverse Trend In]]
| |
| : [[IMD]] [[Performance 03/06/2009]]
| |
| : [[858932 FME]] [[Plug Left In]]
| |
| : [[CRD]] [[10-11]]
| |
| : [[SSPV]] [[Exhaust Port 12/21/2008]]
| |
| : [[CCA]] [[889592-02 Adverse Trend In]]
| |
| : [[MWP]] [[Performance 03/18/2009]]
| |
| : [[RCE]] [[756083 Improper Implementation of Electrical Maintenance]]
| |
| : [[OJT]] [[/]]
| |
| : [[TPE]] [[04/25/2008]]
| |
| : [[CCA]] [[889582-02 Adverse Trend in]]
| |
| : [[MMD]] [[Performance 04/01/2009]]
| |
| : [[RCA]] [[916375 Unqualified]]
| |
| : [[IMD]] [[Technicians Performed]]
| |
| : [[LIS]] [[-]]
| |
| WS-201, Unit 2 Service Water Effluent Monitor
| |
| Calibration. 05/05/09 RCA 799885-03 Motor Driven Reactor Feed Pump Work Window Scope Expansion due to Less than Optimal Pump
| |
| Internal Component Design Specifications 07/20/2007
| |
| : [[CCA]] [[889586-02 Low Level Performance Issues in]]
| |
| : [[IMD]] [[Performance 04/03/2009]]
| |
| : [[RCA]] [[759725 Lake Makeup Line Leakage Due to Procedure Placekeeping Error 04/05/08]]
| |
| : [[CCA]] [[889584-02 Low Level Performance Issues in]]
| |
| : [[EMD]] [[03/27/2009]]
| |
| : [[ACE]] [[836359 Leak Work Curve is Off Track 10/27/2008]]
| |
| : [[ACE]] [[735952 Lost Time Accident- WeldTech Pipe Filter Struck by Tool 07/13/2008]]
| |
| : [[ACE]] [[693812 Unit 1 24/48]]
| |
| : [[VDC]] [[System B Battery Room Exhaust Fan Running with Clearance 11/02/07]]
| |
| : [[ACE]] [[]]
| |
| : [[858932 FME]] [[Plug Left In]]
| |
| : [[CRD]] [[10-11]]
| |
| : [[SSPV]] [[Exhaust Port 12/21/2008]]
| |
| : [[ACE]] [[911322 Vibration Analysis Identifies Wiped Bearings(s) on]]
| |
| : [[0VL]] [[03C 04/24/2009]]
| |
| : [[ACE]] [[878589-04 During Initial Turbine Roll Prior to Synchronization the Unit2 Turbine Tripped on Generator Lockout. 02/09/2009]]
| |
| : [[ACE]] [[874657-04 Cargo Container Slides Over the Side of a Flatbed Trailer 01/31/2009]]
| |
| ACE 852498-06 Inability to Arrest the Adverse Trend in the Transient Combustible Control 01/11/2009 ACE 737285 Condensate Booster System Line Incorrectly Identified and Removed 02/16/2008 492926 Assignment 2 Perform a Common Cause Analysis on Rod 26-35 double notch on withdraw. Validate latest revision
| |
| of
| |
| : [[LS]] [[-]]
| |
| ASA-125-1002 for CCA format. 9/1/2006 496876 Control Room Indication Bands Differ 6/5/2006
| |
| Attachment
| |
| : [[CORREC]] [[]]
| |
| : [[TIVE]] [[]]
| |
| : [[ACTION]] [[]]
| |
| : [[PROGRA]] [[M]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| ED Number Description or Title Date or Revision 496876 Assignment 2 Operations Services to Evaluate Referenced Indicators and Document Appropriate Bands for
| |
| Incorporation in
| |
| : [[T&]] [[]]
| |
| RM with Assistance from
| |
| Engineering as Required 9/21/2006 716812 Assignment 4 For Finding 2, verify all actions are complete and appropriate to prevent a future finding (IR 663732) 3/19/2008 764450 Assignment 2 Perform Common Cause Analysis on Reactivity management Performance Indicator Adverse
| |
| Trend. Validate latest revision of
| |
| : [[LS]] [[-]]
| |
| AA-125-1002
| |
| for
| |
| : [[CCA]] [[format. 5/23/2008 507829 Control Room Indicator Differences (Part 2) 7/10/2006 678869 1B]]
| |
| : [[DG]] [[Cooling Strainer Stuck in]]
| |
| : [[BW]] [[When System is in]]
| |
| : [[STBY]] [[10/2/2007 679684 U-2 Drywell Cooler Condensate Flow Rate Erratic Indication 10/4/2007]]
| |
| : [[680151 RWLC]] [[Level Setpoint Set Down Ramping Out too Soon upon Reset 10/4/2007 681645 Trng: 2]]
| |
| : [[ILT]] [[Students Fail Systems Final Exam 10/8/2007 681658 Trng:]]
| |
| : [[INPO]] [[Identifies Gap to Excellence in]]
| |
| : [[SIM]] [[Critiques 10/8/2007 681731 Possibility of New Fuel Failure on LaSalle Unit 1 10/8/2007 681885 Domestic Water Underground Valve Operator Box Full of Debris 10/9/2007 682781 1B Diesel Generator Load/Speed Drifts 10/10/2007 682796 1B Diesel Generator Voltage Regulator Adjustment Erratic 10/10/2007 683328 A]]
| |
| : [[VC]] [[Refrigeration Compressor Inop Due to Short Circuit 10/11/2007 683695 Received]]
| |
| : [[PPC]] [[Alarm for 'A']]
| |
| : [[RHR]] [[]]
| |
| : [[INOP]] [[10/12/2007 684937 2B]]
| |
| : [[DG]] [[Fuel Oil Sample Results 10/15/2007 696832]]
| |
| : [[NRC]] [[Preconditioning Question on 1-16-07 2E51-F019 Cycling 11/9/2007]]
| |
| : [[698423 ERO]] [[Exam Security Issue During Annual Requal training 11/13/2007 707328 Check-in Opex 12/4/2007 716812]]
| |
| : [[NRC]] [[Inspection Report 2007-004 - Green Findings and One Asso (NCV) 12/31/2007 727361 Unit 1 Control Rod 18-23 Inoperable 1/27/2008]]
| |
| : [[729156 NRC]] [[Insp]]
| |
| : [[RPT]] [[2007-006 - Green Findings Associated]]
| |
| : [[NCV]] [[s 1/30/2008 735550]]
| |
| : [[NRC]] [[Insp]]
| |
| : [[RPT]] [[2007-005 - Green Finding and Associated]]
| |
| : [[NCV]] [[2/13/2008]]
| |
| : [[741941 MSR]] [[Low Load]]
| |
| : [[VLV]] [[1B21-RSLLV2 Full Closed.]]
| |
| : [[RSLLV]] [[2 Full Open 2/28/2008 744606 Fluctuations Observed in Instantaneous Reactor Power 3/4/2008 748777]]
| |
| NOS ID: Porc Issues 3/12/2008
| |
| Attachment
| |
| : [[CORREC]] [[]]
| |
| : [[TIVE]] [[]]
| |
| : [[ACTION]] [[]]
| |
| : [[PROGRA]] [[M]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| : [[ED]] [[Number Description or Title Date or Revision]]
| |
| : [[759538 NRC]] [[-Identified:]]
| |
| : [[MSIV]] [[Preconditioning 4/4/2008 764450 Reactivity Management Performance Indicator Adverse Trend 4/17/2008]]
| |
| : [[784631 NRC]] [[Identified - Unit 1]]
| |
| : [[SBGT]] [[Line Contact with Scaffold 6/9/2008 786762 U2 in Drywell Inlet Pressure Low Alarm 6/16/2008 795700 Roof Runoff Water Pooling on Top of]]
| |
| : [[SEC]] [[/]]
| |
| : [[TSC]] [[]]
| |
| : [[DG]] [[Storage Tank 7/11/2008 803468 Request]]
| |
| : [[CCA]] [[be Performed on Configuration Control Events 8/4/2008 808859 1C]]
| |
| : [[RHR]] [[Suction Valve Tripped Thermal Overload 8/20/2008 812175]]
| |
| : [[NRC]] [[-Identified - Air Leakage Past Watertight Door 17 8/28/2008]]
| |
| : [[815803 NRC]] [[-Identified:]]
| |
| : [[CRD]] [[Drive Water]]
| |
| : [[PCV]] [[Bypass 9/9/2008 818563 Observed Increase in U2 Offgas Pre-Treat]]
| |
| : [[XE]] [[-133 Activity 9/16/2008 819234 2B21-F016 & 2B21-F019 Not Tested 9/18/2008 823046 Failed]]
| |
| : [[PMT]] [[For]]
| |
| : [[WO]] [[# 384652, 2B Fuel Pool Cooling]]
| |
| : [[PP]] [[9/26/2008 823530 Exceeded Thermal Limit During L1M18 Shutdown 9/28/2008 827452 Perform Root Cause Investigation for L1C12 Fuel Failures 10/7/2008 828198]]
| |
| : [[NOS]] [[]]
| |
| : [[ID]] [[: D Operations Declining Performance Trend 10/8/2008 833268]]
| |
| : [[SBLC]] [[Solution Temperature Low 10/20/2008]]
| |
| : [[837037 SBLC]] [[Solution Tank Temperature Low 10/28/2008 839821 Water in]]
| |
| : [[TSC]] [[/IS]]
| |
| : [[DG]] [[Storage Tank Sample 11/3/2008 843802]]
| |
| : [[CRD]] [[26-35 High Temp Alarm 11/12/2008 844283 Unexpected Group]]
| |
| : [[1 MSIV]] [[Half-Isolation Signal 11/12/2008 846571 "A"]]
| |
| : [[RR]] [[Pump Oil Level Alarm Causing Div 1 125V Ground Alarm 11/18/2008]]
| |
| : [[847325 LOS]] [[-]]
| |
| : [[DG]] [[-M2 Requires Procedure Change 11/19/2008]]
| |
| : [[848993 NRC]] [[Potential Finding; Transient Combustibles 11/24/2008 855280 Transient Combustible Compliance Issues 12/11/2008 855678 Ice Buildup on Top of the]]
| |
| : [[TSC]] [[/SEC]]
| |
| : [[DG]] [[Fuel Oil Storage Tank 12/12/2008 856949 U-1]]
| |
| : [[MSL]] [[Hi Rad Alarm Spike 12/16/2008 856961 1C11-R600 U1]]
| |
| : [[CRD]] [[]]
| |
| : [[FCV]] [[Oscillating in Auto 12/16/2008]]
| |
| : [[857522 NRC]] [[-Id'D: Reported Unavailability for]]
| |
| : [[RHR]] [[When Not Required 12/17/2008]]
| |
| : [[861035 NRC]] [[-Identified - Water Identified on a]]
| |
| : [[VC]] [[/VE Platform 12/29/2008 863045 Operations Crew 6 Clock Reset 1/6/2009 864514 2A]]
| |
| : [[RR]] [[]]
| |
| FCV Drifting While Locked-Up and Pumps Off 1/9/2009
| |
| Attachment
| |
| : [[CORREC]] [[]]
| |
| : [[TIVE]] [[]]
| |
| : [[ACTION]] [[]]
| |
| : [[PROGRA]] [[M]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| : [[ED]] [[Number Description or Title Date or Revision 865886 Div 2 Visual Annunciator Power Supply Failure 1/13/2009]]
| |
| : [[866819 CA]] [[Management Review Completed Late 1/14/2009 868063]]
| |
| : [[NRC]] [[-Identified - Standing Order Not Screened]]
| |
| : [[IAW]] [[50:59 10/17/2007 868501 Control Rod 34-59 Took 20 Minutes to Insert 1/19/2009 872750 U2]]
| |
| : [[RFB]] [[Mast - Braided Wire Load cable 1 of 2 Failed 1/28/2009 876016 A]]
| |
| : [[OB]] [[]]
| |
| : [[MSIV]] [[Accumulator Fails Drop Test 2/4/2009]]
| |
| : [[881009 EHC]] [[System]]
| |
| : [[HYD]] [[Fault Setting Incorrect 2/16/2009 883503 Untimely]]
| |
| : [[IR]] [[Resolution 9/21/2009 889586 Adverse Trend in]]
| |
| : [[IMD]] [[Performance 3/6/2009 898146 Additional Discrepancies with]]
| |
| : [[ISI]] [[Documentation 3/26/2009 900378 Hi-Rad Area around cask well drain needs to be disassembled and removed 3/31/2009 902423 Operator Work Around Board Meeting Results 4/3/2009 910096]]
| |
| : [[NRC]] [[-Identified Dry Sight Glass for]]
| |
| : [[VG]] [[Loop Seal 4/21/2009 919000 Perform a]]
| |
| : [[CCA]] [[for Level 5 Rm Events - 2008 5/13/2009]]
| |
| : [[919624 ACE]] [[Requested for]]
| |
| : [[IR]] [[908769,]]
| |
| : [[RO]] [[- Mode Switch Issue 5/14/2009 921752 2A]]
| |
| : [[RR]] [[]]
| |
| : [[FCV]] [[Actuator Seal Leakage 5/19/2009 923160 Unit 1 Scram Due to 1W]]
| |
| : [[MPT]] [[Lightning Arrestor Failure 5/22/2009]]
| |
| : [[924545 CH]] [[Identifies Possible Trends in Recent]]
| |
| : [[HU]] [[Performance 5/27/2009 925331 Adverse Trend in Even Free Clock Resets at LaSalle 5/29/2009 926304 Color Banding between Units does not Match 6/1/2009 926589 1B]]
| |
| : [[RR]] [[Pump Outer Seal Degrading 6/2/2009 930540 Request]]
| |
| : [[CCA]] [[on LaSalle Configuration Control Events 6/12/2009 934253 Observed Increase in U1 Offgas Pre-Treat Activities 6/23/2009]]
| |
| : [[955588 NRC]] [[Question on]]
| |
| : [[ARI]] [[Initiation During U2 Scram 8/20/2009 956315 Unit 1 and]]
| |
| : [[2 DEHC]] [[Surveillances Not Performed 8/21/2009 990437 Proc. Comp. Not Capturing Rod Moves During U-2]]
| |
| : [[CRD]] [[Cycling 11/8/2009]]
| |
| : [[993280 NRC]] [[]]
| |
| : [[IDD]] [[- Effectiveness of Performance Indicators Questioned 11/13/2009]]
| |
| : [[995883 NRC]] [[]]
| |
| : [[ID]] [[:]]
| |
| : [[WO]] [[Not found for High Radiation Barrier Removal 11/19/2009 995957 Contingency Package Left Open for Extended Period 11/19/2009 683820]]
| |
| : [[CDBI]] [[Lessons Learned]]
| |
| : [[LOCA]] [[Block Start Calculation 10/12/2007 691865 2B]]
| |
| RHR Seal Cooler Has a Low Flow Rate of 10.2 GPM 10/30/2007
| |
| Attachment
| |
| : [[CORREC]] [[]]
| |
| : [[TIVE]] [[]]
| |
| : [[ACTION]] [[]]
| |
| : [[PROGRA]] [[M]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| : [[ED]] [[Number Description or Title Date or Revision 692247 Conflicting Procedures Need Revision 10/31/2009 702329 Wrong Transducer Used for Test Results in Bad Data 11/21/2007]]
| |
| : [[705226 PI&R]] [[Insp -]]
| |
| : [[NRC]] [[Identified the Need for Better Documentation 11/29/2007 706551 Applicability of Dresden]]
| |
| : [[MOV]] [[Concern to LaSalle 12/3/2007 707882 Plant Walkdown with]]
| |
| : [[NRC]] [[12/6/2007 710706 1B]]
| |
| : [[DG]] [[Oil Cooler Outlet Temp Gauge 1E22-R531 Reads Low 12/12/2007 711140 System Trending Identifies Margin Issue 12/13/2007 714115 Revise Procedures]]
| |
| : [[LIS]] [[-PC-121(221) 12/20/2007 716242 Design Eng]]
| |
| : [[ID]] [[s Non-Conservative Step in]]
| |
| : [[CC]] [[-AA-112 Rev 12 12/28/2007 728597 1B21-F513B Moderate Packing Leak 1/29/2008 728626]]
| |
| : [[1ES]] [[002 Severe Packing Leak 1/29/2008 737253 Engineering Not Following Procedure]]
| |
| : [[ER]] [[-AA-340-2000 as Written 2/16/2008 770555 Hydrogen Found in Bearing 10 Casing 5/1/2008 791008 1E12-F042B Examine]]
| |
| : [[MOV]] [[Motor for Magnesium Rotor Degradation 6/27/2008 796221 1]]
| |
| : [[FP]] [[125]]
| |
| : [[RB]] [[Ring Header Stop Valve Minor Leak 7/14/2008 836452 U1 Small]]
| |
| : [[RCIC]] [[Turbine Steam Leak Previously Identified 10/27/2008 852332 Triennial]]
| |
| : [[EH&S]] [[Audit 2008 Findings and Recommendations 12/4/2008 864964 Extent of Condition Review for Unit 2 Spent Fuel Pool 1/9/2009 888535 Calibrate 2]]
| |
| : [[FI]] [[-FC038 Before Performing]]
| |
| : [[LOS]] [[-]]
| |
| : [[FC]] [[-Q1 on 5/25/2009 3/4/2009 912034 Replace the 1E12-F064C Valve in L1R15 4/27/2009]]
| |
| : [[926938 OE]] [[on Jet Pump Slip Joint Clamps Applicable to]]
| |
| : [[LSCS]] [[6/2/2009]]
| |
| : [[948170 NRC]] [[-Identified: No Emergency Restoration Att for Los-]]
| |
| : [[SC]] [[-Q1 7/31/2009]]
| |
| : [[953484 NRC]] [[Question:]]
| |
| : [[SBLC]] [[Availability During Surveillance 8/14/2009 955487 Boroscope]]
| |
| : [[MOV]] [[Motor for 2E12-F024B in L2R13 8/20/2009 968594 Active Oil Seepage from Thrust Bearing Oil Return Box Cover 9/22/2009 986109]]
| |
| : [[RM]] [[- Suspended U-1]]
| |
| : [[RR]] [[]]
| |
| : [[HPU]] [[Subloop Swap]]
| |
| : [[PMID]] [['s 10/29/2009 987190 B1]]
| |
| : [[RR]] [[]]
| |
| : [[HPU]] [[Subloop Discharge Pressure Found High 11/1/2009 988238]]
| |
| CAPR Unable to be Complied with, Needs Revision 11/03/2009
| |
| Attachment
| |
| : [[CORREC]] [[]]
| |
| : [[TIVE]] [[]]
| |
| : [[ACTION]] [[]]
| |
| : [[PROGRA]] [[M]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| : [[ED]] [[Number Description or Title Date or Revision]]
| |
| : [[ACE]] [[736609 Water Issues from Valve Bonnet Due to Insufficient Draining 2/14/2008]]
| |
| : [[ACE]] [[]]
| |
| : [[737220 IVVI]] [[(In-Vessel Visual Inspection) Examinations Performed with Expired Visual Acuity 2/7/2008]]
| |
| : [[ACE]] [[737253 System Engineering Failed to Use Empirical Data When Determining Tube-Plugging Limits 2/16/2008]]
| |
| : [[ACE]] [[757852 Spurious Technical Support Center Emergency Makeup Unit Start 4/1/2008]]
| |
| : [[ACE]] [[775338 2B Diesel Engine Trip Up with Lockout Reset 5/14/2008]]
| |
| : [[ACE]] [[851075 Late Identification of Degrading Trend on Control Valve #3]]
| |
| : [[LVDT]] [[12/1/2008]]
| |
| : [[ACE]] [[869141 Unit-2]]
| |
| : [[RPV]] [[Head Lift Stopped Due to High Indicated Weight 1/20/2009]]
| |
| : [[ACE]] [[870845 Replacement of 0]]
| |
| : [[VE]] [[04CA Compressor Due to Anomalous Head Temperatures 11/19/2008]]
| |
| : [[ACE]] [[909987]]
| |
| : [[NOS]] [[Identified Numerous Deficiencies in the Implementation of SystemIQ 2/20/2009]]
| |
| : [[CCA]] [[890184 E-5 to E-1 Stability Due to Negative Trend 4/8/2009]]
| |
| : [[CCA]] [[905332 Historical]]
| |
| : [[EHC]] [[Pump Performance 4/30/2009]]
| |
| : [[CCA]] [[914651 Human Performance Issues Identified in]]
| |
| : [[NOS]] [[Review 5/21/2009]]
| |
| : [[RCR]] [[742287 Failure of Turbine Speed Detection System While Synching the Generator to the Grid 4/28/2008]]
| |
| : [[RCR]] [[825873 Excessive Hydrogen Leakage on Unit 1 Main Generator Hydrogen Seal 10/30/2008]]
| |
| RCR 881009 Electro-Hydraulic Control (EHC) System Hydraulic Transmitter Fault Setting Incorrect Due to
| |
| Ineffective Review of Software File Changes 2/5/2009
| |
| : [[RCR]] [[920759 Abnormal Knocking Noise and High Vibrations on 0]]
| |
| : [[VE]] [[04CA Refrigeration Compressor 7/9/2009]]
| |
| : [[RCR]] [[923335 Untimely Recognition that No Steam Packing Exhauster Blower was Running 7/2/2009 886819 2C]]
| |
| : [[CD]] [[/CB Min Flow Failed Open,]]
| |
| : [[MCR]] [[Unexpected Alarm 2/28/2009 824848 Rod 34-31 Withdraw Speed is Too Fast 10/1/2008 683288 Thermography Identifies Minor Hotspot in 1W]]
| |
| : [[MPT]] [[Cabinet 10/11/2007 687932 A]]
| |
| : [[VE]] [[Oil Temperature Has Approached 155 Degrees F 10/22/2007 688935 Part 21 for 2B]]
| |
| : [[DG]] [[Air Start Solenoid Valve Never Installed 10/24/2007 696350 Bolted Bus Connections May Need Replacement 11/08/2007 699827 Emergent Work Impacts Work Planning Daily Planning 11/15/2007 709276]]
| |
| : [[0VE]] [[09]]
| |
| : [[YB]] [[Damper Failure 12/09/2007]]
| |
| : [[713811 FT]] [[-]]
| |
| VR026 Loop May be OOT 12/19/2007
| |
| Attachment
| |
| : [[CORREC]] [[]]
| |
| : [[TIVE]] [[]]
| |
| : [[ACTION]] [[]]
| |
| : [[PROGRA]] [[M]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| : [[ED]] [[Number Description or Title Date or Revision 713225 Potential Thread Engagement Issue on 2B D/G Emergency Stop 12/18/2007 723586 Unknown High Conductivity Input in]]
| |
| : [[RW]] [[Floor Drain 1/17/2008 729396]]
| |
| : [[NOS]] [[]]
| |
| : [[ID]] [[: Issues Regarding the 1A 24]]
| |
| : [[VDC]] [[Battery Charger 1/31/2008 736409]]
| |
| : [[0PL]] [[31J High Rad Area is Contaminated 2/14/2008 740511 Apparent Seat Leakage by 1E12-F064B 2/25/2008 741586 No]]
| |
| : [[EPN]] [[]]
| |
| : [[FW]] [[Process]]
| |
| : [[SPL]] [[Valve Isolation Valve Doesn't Isolate 2/27/2008 754492 Nesting on B Radwaste Crane Intermittent Issues 3/25/2008]]
| |
| : [[763535 ECP]] [[Probe for Unit 1 is Degrading 4/15/2008 778769 Did Not Receive]]
| |
| : [[ERO]] [[Page 5/23/2008 785154]]
| |
| : [[2VD]] [[05C Tripped 6/11/2008 861648 Temporary Catch Basin Used As A Permanent Solution 12/31/2008 863162]]
| |
| : [[OPEX]] [[Review of Susquehanna]]
| |
| : [[OE]] [[28038 1/06/2009 866492 Did Not Receive]]
| |
| : [[ERO]] [[Page on 1/12/2009 1/14/2009]]
| |
| : [[868523 SRM]] [[A Signal to Noise Ratio 1/19/2009 873905 Particulate Slightly Elevated in]]
| |
| : [[RCIC]] [[Turbine Oil 1/30/2009 934253 Observed Increase in U1 Offgas Pre-Treat Activities 6/23/2009 934958 A Train]]
| |
| : [[VE]] [[Inleakage Into]]
| |
| : [[CRE]] [[is Greater Than Allowed 6/24/2009 964856 Inaccurate Does Estimation on Work Task 9/14/2009 965049]]
| |
| : [[1PA]] [[06J Westinghouse 7300 Panel 9/15/2009 969345 Classification of]]
| |
| : [[MS]] [[Branch Piping & Components 9/23/2009 990192 U-1 Turb Bldg]]
| |
| : [[CAM]] [[Alarm 11/7/2009 991337 Miscellaneous Automatic Control System Power Failure 11/10/2009]]
| |
| : [[ACE]] [[681645]]
| |
| : [[2ILT]] [[Students Fail Systems Final Exam 12/07/2007]]
| |
| : [[ACE]] [[696564 Cask Shoring Makes Contact With]]
| |
| : [[HIC]] [[During Loading 12/14/2007]]
| |
| : [[ACE]] [[695614 Drywell Floor Drain Sump Fill-Up Rate/Pump Discharge Flow Recorder Failed 12/28/2007]]
| |
| : [[ACE]] [[748777]]
| |
| : [[NOD]] [[]]
| |
| : [[ID]] [['d Concerns With the Implementation of]]
| |
| LS-AA-106, Plant Operations Review Committee
| |
| (PORC) 4/30/2008
| |
| : [[ACE]] [[769736 The 2A]]
| |
| : [[DG]] [[Room Exhaust Damper]]
| |
| : [[2VD]] [[11]]
| |
| : [[YA]] [[/B Did Not Open As Expected 7/10/2008]]
| |
| : [[ACE]] [[869141 Unit-2]]
| |
| RPV Head Lift Stopped Due to High Indicated Weight 2/26/2009 ACE 890180 New Disc Installed in 2B21-F032A With Potential Weight Difference 4/16/2009
| |
| Attachment
| |
| : [[CORREC]] [[]]
| |
| : [[TIVE]] [[]]
| |
| : [[ACTION]] [[]]
| |
| : [[PROGRA]] [[M]]
| |
| : [[DOCUME]] [[]]
| |
| : [[NTS]] [[]]
| |
| : [[REVIEW]] [[]]
| |
| : [[ED]] [[Number Description or Title Date or Revision]]
| |
| : [[ACE]] [[900673 Low Service Water Pressure and Shutdown of 1A Service Water Pump Due to]]
| |
| FME (Foreign
| |
| Material Exclusion) Concerns From Dive Activity
| |
| in the Service Water Tunnel 5/05/2009
| |
| : [[ACE]] [[908791]]
| |
| : [[EHC]] [[Software Modification Not Performed 6/09/2009]]
| |
| : [[ACE]] [[954664 1]]
| |
| : [[ES]] [[065 Stem Disc Separation 10/01/2009]]
| |
| : [[ACE]] [[969479]]
| |
| : [[IMD]] [[Technician Exceeded the]]
| |
| : [[GL]] [[82-12 Overtime Guideline as Specified in]]
| |
| : [[LS]] [[-AA-119 10/29/2009]]
| |
| : [[RCE]] [[827452 L1C12 Nuclear Fuel Failures 11/06/2008]]
| |
| : [[OPERAT]] [[ING]]
| |
| : [[EXPERI]] [[]]
| |
| : [[ENCE]] [[Number Description or Title Date or Revision]]
| |
| : [[521373 OE]] [[23020 Potential for]]
| |
| : [[RCIC]] [[Water Hammer- Nine Mile Point 2 08/18/2006]]
| |
| : [[578711 MOV]] [[]]
| |
| : [[OPEX]] [[]]
| |
| : [[OE]] [[23797- Corporate Engineering Action Plan 01/12/2007 665602]]
| |
| : [[OPEX]] [[- LaSalle County Station]]
| |
| : [[SME]] [[Review of]]
| |
| : [[OE]] [[25373 08/28/2007]]
| |
| : [[669975 OPEX]] [[- LaSalle County Station Review of Green]]
| |
| : [[NER]] [[- 07-057 09/11/2007]]
| |
| : [[674693 IN]] [[2007-24 Summary of 2006]]
| |
| : [[FFD]] [[Performance Reports 09/24/2007 678868]]
| |
| : [[IN]] [[2007-29 Operability Effects of Temp Scaffolding 10/02/2007 684958 Fleet Review of Operating Experience Report 24759 10/15/2007 719685]]
| |
| : [[NER]] [[]]
| |
| : [[NC]] [[07-044 Rev 1 Red- Essential Service Water Piping 01/09/2008 736805]]
| |
| : [[NER]] [[]]
| |
| : [[NC]] [[-08-007 Yellow Fleet Actions-]]
| |
| : [[TMI]] [[High Rad Area Event 02/15/2008]]
| |
| : [[737688 NER]] [[]]
| |
| : [[NC]] [[-08-009 Yellow- Security Force Members Lapsed Quals 02/18/2008]]
| |
| : [[904247 IN]] [[2009-04 Age-Related Constant Support Degradation 04/07/2009 830408]]
| |
| : [[RIS]] [[2008-23]]
| |
| : [[GTRI]] [[for High Risk Radiological Material 10/13/2008]]
| |
| OE07-001 Operability Evaluation, Reactor Vessel Jet Pump 19 Instrumentation Line (IR 581231) Revision 2 OE07-002 Operability Evaluation, Emergency Diesel Generators, Diesel Fuel Storage Tanks, Diesel Fuel Day Tanks: Use of Ultra-Low-Sulfur Diesel
| |
| will Require Increased Fuel Storage Volume
| |
| (IR 612524) Revision 5
| |
| Attachment
| |
| : [[OPERAT]] [[]]
| |
| : [[ING]] [[]]
| |
| : [[EXPERI]] [[]]
| |
| : [[ENCE]] [[Number Description or Title Date or Revision]]
| |
| : [[OE]] [[08-003 Operability Evaluation, Unit 1 and 2 Division 3 Batteries 1]]
| |
| : [[DC]] [[18E and 2DC18E, Unit 1 and 2]]
| |
| : [[HPCS]] [[Pump Breakers 1]]
| |
| : [[AP]] [[07E (S35) and]]
| |
| : [[2AP]] [[07E-004 (S35) Alternate Breaker Sequence Possible during a]]
| |
| : [[LOOP]] [[-LOCA (IR 792505) Revision]]
| |
| : [[1 OE]] [[08-005 Operability Evaluation, 0]]
| |
| VE04CB, Refrigerant Compressor subject to internal damage due to
| |
| liquid refrigerant slugging during startup Revision
| |
| : [[5 OEE]] [[08-02 Operability Evaluation, Unit 1 and 2 Diesel Generators Air Inlet Temperature Rating Issues (]]
| |
| : [[IR]] [[744660,]]
| |
| : [[IR]] [[746204) Revision 0]]
| |
| : [[AUDITS]] [[,]]
| |
| : [[ASSESS]] [[]]
| |
| : [[MENTS]] [[]]
| |
| : [[AND]] [[]]
| |
| : [[SELF]] [[-ASSESSMENTS Number Description or Title Date or Revision]]
| |
| : [[NOSA]] [[-]]
| |
| : [[LAS]] [[-09-03 Security Plan,]]
| |
| : [[FFD]] [[, Access Authorization, and]]
| |
| : [[PADS]] [[(AR 858488) Revision]]
| |
| : [[2 NOSA]] [[-]]
| |
| : [[LAS]] [[-09-01 Corrective Action Program (AR 859231) Revision]]
| |
| : [[2 NOSA]] [[-]]
| |
| : [[LAS]] [[-09-06 LaSalle Radiation Protection Program (AR 862840) Revision 0 848279-03 Preparation for]]
| |
| : [[NRC]] [[]]
| |
| : [[PI&R]] [[Inspection 11/2-20/2009 848253-03 Security 848244-02]]
| |
| : [[SOER]] [[[Significant Operational Event Report] 01-1 Implementation Assessment 878991-02 Employee Concerns Program Check-In Assessment 10/2009 917330-02 Safety Culture Monitoring 6/5/09 Executive Review of Exelon Nuclear's Learning Programs August 2009 707328-04 Operating Experience Results Measurement Review 08/27/09 707328-04 Operating Experience Check-In Assessment 12/17/08 713021 Maintenance Functional Area Audit 2/6/2008 848238 Maintenance Rigging and Lifting Program Check-In Assessment 3/31/2009 912557-01 Mechanical Maintenance Document of Work Issues Check-In Assessment 12/15/2009 912590-01 Check-In Assessment to Review Documentation of Work Issues 12/29/09 908683-01 Low Level Performance Issues in]]
| |
| : [[IMD]] [[12/31/2009 907966 Management Directed Assessment Plan Maintenance Red Rating 09/15/09]]
| |
| : [[2007 AFI]] [[]]
| |
| CM.4-2 Fuel Failures Check-In Self-Assessment Report (861374) Performance Gap Resolution in L2R12 outage 12/30/2008
| |
| Attachment
| |
| : [[AUDITS]] [[,]]
| |
| : [[ASSESS]] [[MENTS]]
| |
| : [[AND]] [[]]
| |
| : [[SELF]] [[-ASSESSMENTS Number Description or Title Date or Revision]]
| |
| : [[ACE]] [[681645-02 2]]
| |
| : [[ILT]] [[Students Fail Systems Final Exam 9/28/2007]]
| |
| : [[ACE]] [[744606]]
| |
| : [[ACE]] [[- Investigation Fluctuations Observed in Instantaneous Reactor Power 3/4/2008]]
| |
| : [[ACE]] [[919624 Three Reactor Operators Fail to take Mode Switch to Shutdown during a Training Scenario 5/14/2009]]
| |
| CCA 919000-02 Level 5 Reactivity Management Issue Trends 6/4/2009 CCA 924545-02 Common Cause Analysis : Data Review of Items that Contain a Human Performance Element in
| |
| LaSalle Chemistry in 2009 6/18/2009
| |
| : [[CCA]] [[925331-02 Common Cause Analysis: Adverse Trend in LaSalle Event Free Clock Resets 1/1/- 6/1/2009]]
| |
| : [[CCA]] [[930540-02 Common Cause Analysis of LaSalle Configuration Control Events 9/2007 - 6/2009]]
| |
| : [[NOSA]] [[-]]
| |
| : [[LAS]] [[-07-07 Operations Functional Area (AR 576590) 11/12 - 11/30/2007]]
| |
| : [[RCE]] [[-727361-03 Unit 1 Channel Distortion Root Cause Report 2/23/2008]]
| |
| : [[RCE]] [[823530 Root Cause Investigation: Unplanned Thermal Limit]]
| |
| : [[LCO]] [[Entry During L1M18 Shutdown 11/11/2008]]
| |
| : [[RCE]] [[827452-02 Root Cause Investigation: L1C12 Nuclear Fuel Failures 11/6/2008]]
| |
| : [[RCE]] [[923160 Root Cause Investigation: Ground Across the Unit 1 West Main Power Transformer Surger (Lightning) Arrester resulting in a Scram 7/8/2009 707328]]
| |
| : [[OPEX]] [[Check-In Assessment 12/17/2008 828627-03]]
| |
| : [[2008 CREHP]] [[Program Assessment 1/21/2009 862824 Engineering Design Control Audit]]
| |
| : [[NOSA]] [[-LAS-09-05 8/20/2009 713027 Engineering Programs and Station Blackout Audit Report]]
| |
| : [[NOSA]] [[-]]
| |
| : [[LAS]] [[-08-05 7/2/2008 861376-01 Plant Systems - Performance Monitoring Check-In 6/30/2009 848177-02]]
| |
| : [[ISI]] [[Program Preparedness for L2R12]]
| |
| : [[NRC]] [[Inspection 1/29/2009]]
| |
| : [[CONDIT]] [[]]
| |
| : [[ION]] [[]]
| |
| : [[REPORT]] [[S]]
| |
| : [[GENERA]] [[TED]]
| |
| : [[DURING]] [[]]
| |
| : [[INSPEC]] [[TION Number Description or Title Date or Revision]]
| |
| : [[993280 NRC]] [[-]]
| |
| : [[IDD]] [[-Effectiveness of Performance Indicators Questioned 11/13/2009]]
| |
| : [[996319 NRC]] [[]]
| |
| : [[ID]] [[: Review of Maintenance Documentation]]
| |
| : [[CCA]] [[#882701 11/20/2009 995883]]
| |
| : [[NRC]] [[]]
| |
| : [[ID]] [[:]]
| |
| : [[WO]] [[[Work Order] Not Found for High Radiation Barrier Removal 11/19/2009]]
| |
| : [[996372 NRC]] [[]]
| |
| ID: WO 605660 Closed with No Work Performed 11/20/2009
| |
| Attachment
| |
| : [[CONDIT]] [[]]
| |
| : [[ION]] [[]]
| |
| : [[REPORT]] [[S]]
| |
| : [[GENERA]] [[TED]]
| |
| : [[DURING]] [[]]
| |
| : [[INSPEC]] [[TION Number Description or Title Date or Revision 995957 Contingency Package Left Open for Extended Period 11/18/2009]]
| |
| : [[989540 NRC]] [[]]
| |
| : [[ID]] [['D: Previously Identified Issue Waiting Resolution 11/5/2009]]
| |
| : [[989527 NRC]] [[]]
| |
| : [[PI&R]] [[1(2)PL15J and 1(2)PL75J Reliability 11/4/2009]]
| |
| : [[988746 NRC]] [[]]
| |
| : [[ID]] [[:]]
| |
| : [[CC]] [[-]]
| |
| : [[AA]] [[-112 Note Not Included in T-MOD Work Packages 11/4/2009 995934 Documentation Issues With Regard to]]
| |
| : [[CAP]] [[/]]
| |
| : [[OPE]] [[x Investigations 11/19/2009]]
| |
| : [[995581 NRC]] [[Recommendation Regarding]]
| |
| : [[OPE]] [[x Use In]]
| |
| : [[CAP]] [[Investigations 11/19/2009]]
| |
| : [[MISCEL]] [[LANEOUS Number Description or Title Date or Revision 816066 (A)(1) Action Plan Development]]
| |
| : [[RR]] [[-02 (Subloops) Revision 0 930416 (A)(1) Action Plan Development]]
| |
| : [[AN]] [[-01 (Unit 2) Revision 0 891409 (A)(1) Action Plan Development]]
| |
| : [[RE]] [[-03 Revision 0]]
| |
| : [[NES]] [[-MS-04.1 Seismic Prequalified Scaffolds Rev.]]
| |
| : [[5 IR]] [[995336 Exelon Nuclear Issue - Statement of Confirmation:]]
| |
| : [[NRC]] [[Id;]]
| |
| : [[IR]] [[Actions Not Smarter 11/18/2009 List of OpEvals, Associated]]
| |
| : [[IR]] [[and Status 2003 - 2009 Plan of the Day 11/4/2009]]
| |
| : [[SOC]] [[Package 11/13/2009 Summary of Open Work Arounds and Challenges 11/2007 - 11/2009 Work Orders Number Description or Title Date or Revision]]
| |
| : [[WO]] [[01240425 2A]]
| |
| : [[OTBD]] [[]]
| |
| : [[MSIV]] [['Slow Test']]
| |
| : [[P.B.]] [[Sticks 10/28/2009]]
| |
| : [[WO]] [[1071579 1B Diesel generator Load/Speed Drifts: Adjust Friction Drive, Replace Lid 7/2/2008]]
| |
| : [[WO]] [[1186297 1A]]
| |
| : [[RR]] [[]]
| |
| : [[FCV]] [[Movement with No Operator Input 1/14/2008]]
| |
| : [[WO]] [[844595 Fleet Work Package Documentation Continuation 806424 11/13/2008 Temporary and/or Permanent Plant Modifications Number Description or Title Date or Revision]]
| |
| : [[EC]] [[369811 Remove Internals from]]
| |
| : [[EFCV]] [[1G33-F389E Revision]]
| |
| : [[0 EC]] [[369496 Install Vibration Monitoring for Main Turbine Control Valves]]
| |
| CV2 and CV4 Revision 0
| |
| Attachment Temporary and/or Permanent Plant Modifications Number Description or Title Date or Revision EC 367757 Hook Up Instrumentation to Gather Data to See if an Offset is a More Viable Option for Main
| |
| Turbine Back Pressure Indicators 1/10/2008
| |
| : [[EC]] [[371362 Bypassing the Reactor Recirc Flow Control Valve]]
| |
| : [[LVDT]] [[to]]
| |
| : [[RVDT]] [[Mismatch Alarm. The]]
| |
| : [[RVDDT]] [[Signal has Degraded. 7/10/2008]]
| |
| : [[EC]] [[373691 Correct Various P&]]
| |
| : [[ID]] [[Drawing Errors Revision]]
| |
| : [[0 EC]] [[376196 Reduce]]
| |
| : [[OPS]] [[Burdens by Modifying]]
| |
| : [[RHR]] [[Interlocks 7/8/2009]]
| |
| : [[EC]] [[362940 Install Caldon Non-Intrusive Flow Measuring Instrument in Support of]]
| |
| : [[MWE]] [[Recovery Plan Revision 0]]
| |
| : [[EC]] [[369498 Replace Double Block Drain Valves 1B21-F032A/B/C & 1B21-F303A/B/C With Equivalent Two (2) Single Valve Assemblies in Series Using Drawing]]
| |
| : [[IT]] [[-7000-M-]]
| |
| : [[PP]] [[-32 Installation Details Revision]]
| |
| : [[1 EC]] [[376996 1(2)]]
| |
| : [[PA]] [[06J Westinghouse 7300 Panel-Power Supplies Revision]]
| |
| : [[0 EC]] [[348186]]
| |
| DWFDS Flow Tube Modification Revision 1
| |
| Attachment
| |
| : [[LIST]] [[]]
| |
| : [[OF]] [[]]
| |
| : [[ACRONY]] [[]]
| |
| : [[MS]] [[]]
| |
| : [[USED]] [[]]
| |
| : [[AR]] [[Action Request]]
| |
| : [[CAP]] [[Corrective Action Program]]
| |
| CFR Code of Federal Regulations DRP Division of Reactor Projects
| |
| ECP Employee Concerns Program
| |
| IN Information Notices
| |
| : [[IP]] [[Inspection Procedure]]
| |
| : [[MRC]] [[Management Review Committee]]
| |
| NCV Non-Cited Violation NOS Nuclear Oversight
| |
| NRC U.S. Nuclear Regulatory Commission
| |
| : [[OE]] [[Operating Experience]]
| |
| : [[PARS]] [[Publicly Available Records]]
| |
| : [[PI&R]] [[Problem Identification and Resolution]]
| |
| : [[SC]] [[]]
| |
| WE Safety-Conscious Work Environment
| |
| WO Work Order
| |
| C. Pardee -2-
| |
| In accordance with
| |
| : [[10 CFR]] [[2.390 of the]]
| |
| : [[NRC]] [['s "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the]]
| |
| : [[NRC]] [[Public Document Room or from the Publicly Available Records (]]
| |
| : [[PARS]] [[) component of the]]
| |
| : [[NRC]] [[=s document system (]]
| |
| : [[ADAMS]] [[).]]
| |
| : [[ADAMS]] [[is accessible from the]]
| |
| NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
| |
| Sincerely,
| |
| /RA/
| |
| Kenneth Riemer, Chief
| |
| Branch 2
| |
| Division of Reactor Projects Docket No. 50-373; 50-374
| |
| License No.
| |
| : [[NPF]] [[-11;]]
| |
| NPF-18
| |
|
| |
|
| Enclosure: Inspection Report 05000373/2009007; 05000374/2009007 w/Attachment: Supplemental Information cc w/encl: Distribution via ListServ
| | ==LIST OF DOCUMENTS REVIEWED== |
| : [[DOCUME]] [[]]
| | |
| : [[NT]] [[]]
| |
| : [[NAME]] [[: G:\1-]]
| |
| : [[SECY]] [[\1-WORK]]
| |
| : [[IN]] [[]]
| |
| : [[PROGRE]] [[SS\LAS 2009]]
| |
| : [[007 PIR.DO]] [[C G Publicly Available G Non-Publicly Available G Sensitive G Non-Sensitive To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy]]
| |
| : [[OFFICE]] [[]]
| |
| : [[RIII]] [[N]]
| |
| : [[RIII]] [[E]]
| |
| : [[RIII]] [[]]
| |
| : [[RIII]] [[]]
| |
| : [[NAME]] [[]]
| |
| : [[NS]] [[hah:cms KRiemer]]
| |
| : [[DATE]] [[12/03/09 12/11/09]]
| |
| : [[OFFICI]] [[AL]]
| |
| : [[RECORD]] [[]]
| |
| : [[COPY]] [[Letter to C. Pardee from K. Riemer dated December 11, 2009]]
| |
| : [[SUBJEC]] [[T:]]
| |
| : [[LASALL]] [[E]]
| |
| : [[COUNTY]] [[]]
| |
| : [[STATIO]] [[N,]]
| |
| : [[UNITS]] [[1]]
| |
| : [[AND]] [[]]
| |
| : [[2 PROBLE]] [[M]]
| |
| : [[IDENTI]] [[FICATION]]
| |
| : [[AND]] [[]]
| |
| : [[RESOLU]] [[TION (PI&R)]]
| |
| : [[INSPEC]] [[]]
| |
| : [[TION]] [[05000373/2009007; 05000374/2009007]]
| |
| }} | | }} |
|
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Category:Inspection Report
MONTHYEARIR 05000373/20243012024-10-31031 October 2024 Initial License Examination Report 05000373/2024301 05000374/2024301 IR 05000373/20244042024-10-23023 October 2024 County Station – Security Baseline Inspection Report 05000373/2024404 and 05000374/2024404 IR 05000373/20244012024-09-27027 September 2024 County Station – Security Baseline Inspection Report 05000373/2024401 and 05000374/2024401 IR 05000373/20240052024-08-29029 August 2024 Updated Inspection Plan and Assessment Follow-Up Letter for Lasalle County Station (Report 05000373/2024005; 05000374/2024005) IR 05000373/20244022024-08-28028 August 2024 County Station - Cyber Security Inspection Report 05000373/2024402 and 05000374/2024402 IR 05000373/20240022024-08-13013 August 2024 County Station - Integrated Inspection Report 05000373/2024002 and 05000374/2024002 IR 05000373/20244202024-08-0505 August 2024 County Station - Security Baseline Inspection Report 05000373 2024420 and 05000374 2024420 IR 05000373/20240102024-05-29029 May 2024 County Station - Commercial Grade Dedication Inspection Report 05000373/2024010 and 05000374/2024010 IR 05000373/20240012024-05-13013 May 2024 County Station - Integrated Report 05000373/2024001 and 05000374/2024001 ML24131A1512024-05-13013 May 2024 County Station - Integrated Report 05000373/2024001 and 05000374/2024001 IR 05000373/20244032024-05-0202 May 2024 Public Lasalle County Station - Security Baseline Inspection Report 05000373/2024403 and 05000374/2024403; NRC Investigation Report No. 3-2023-006 IR 05000373/20230062024-02-28028 February 2024 Annual Assessment Letter for Lasalle County Station, Units 1 and 2 (Report 05000373/2023006; 05000374/2023006) IR 05000373/20230042024-01-24024 January 2024 County Station - Integrated Inspection Report 05000373/2023004 and 05000374/2023004 IR 05000373/20230122024-01-18018 January 2024 County Station - Biennial Problem Identification and Resolution Inspection Report 05000373/2023012 and 05000374/2023012 IR 05000373/20234022023-12-20020 December 2023 County Station - Security Baseline Inspection Report 05000373/2023402 and 05000374/2023402 IR 05000373/20230032023-11-0909 November 2023 County Station Integrated Inspection Report 05000373/2023003, 05000374/2023003, and 07200070/2023001 IR 05000373/20234012023-11-0707 November 2023 County Station Security Baseline Inspection Report 05000373/2023401 and 05000374/2023401 IR 05000374/20230102023-10-11011 October 2023 NRC Inspection Report 05000374/2023010 IR 05000373/20233012023-09-15015 September 2023 Errata to NRC Initial License Examination Report 05000373/2023301; 05000374/2023301 IR 05000373/20230052023-08-25025 August 2023 Updated Inspection Plan and Assessment Follow-Up Letter for LaSalle County Station (Report 05000373/2023005; 05000374/2023005) IR 05000373/20230022023-08-0101 August 2023 County Station - Integrated Inspection Report 05000373/2023002 and 05000374/2023002 IR 05000373/20230112023-06-26026 June 2023 County Station - Quadrennial Fire Protection Team Inspection Report 05000373/2023011 and 05000374/2023011 IR 05000373/20230012023-05-10010 May 2023 County Station - Integrated Inspection Report 05000373/2023001 and 05000374/2023001 IR 05000373/20220062023-03-0101 March 2023 Annual Assessment Letter for LaSalle County Station, Units 1 and 2 (Report 05000373/2022006 and 05000374/2022006) IR 05000373/20220042023-01-31031 January 2023 County Station - Integrated Inspection Report 05000373/2022004 and 05000374/2022004 IR 05000373/20224042022-12-21021 December 2022 County Station - Material Control and Accounting Program Inspection Report 05000373/2022404 and 05000374/2022404 IR 05000373/20225012022-12-0505 December 2022 County Station - Emergency Preparedness Biennial Exercise Inspection Report 05000373/2022501 and 05000374/2022501 IR 05000373/20224022022-11-17017 November 2022 County Station - Security Baseline Inspection Report 05000373/2022402 and 05000374/2022402 IR 05000373/20220032022-11-0101 November 2022 County Station - Integrated Inspection Report 05000373/2022003 and 05000374/2022003 IR 05000373/20220112022-11-0101 November 2022 County Station Design Basis Assurance Inspection (Teams) Inspection Report 05000373/2022011 and 05000374/2022011 IR 05000373/20224032022-09-15015 September 2022 County Station - Cyber Security Inspection Report 05000373/2022403 and 05000374/2022403 IR 05000373/20220052022-08-22022 August 2022 Updated Inspection Plan for Lasalle County Station (Report 05000373/2022005; 05000374/2022005) IR 05000373/20220022022-08-10010 August 2022 County Station - Integrated Inspection Report 05000373/2022002 and 05000374/2022002 IR 05000373/20224012022-05-18018 May 2022 County Station - Security Baseline Inspection Report 05000373/2022401 and 05000374/2022401 IR 05000373/20220012022-04-26026 April 2022 County Station - Integrated Inspection Report 05000373/2022001 and 05000374/2022001 ML22108A2802022-04-19019 April 2022 Information Request for an NRC Triennial Baseline Design Bases Assurance Inspection (Team) Inspection Report 05000373/2022011 05000374/20220 IR 05000373/20220102022-03-15015 March 2022 County Station License Renewal Phase 2 Report 05000373/2022010 IR 05000373/20210062022-03-0202 March 2022 Annual Assessment Letter (Report 05000373/2021006 and 05000374/2021006) IR 05000373/20210042022-02-0707 February 2022 County Station Integrated Inspection Report 05000373/2021004 and 05000374/2021004 IR 05000373/20210132022-01-20020 January 2022 County Station Biennial Problem Identification and Resolution Inspection Report 05000373/2021013 and 05000374/2021013 IR 05000373/20214022021-12-15015 December 2021 County Station - Security Baseline Inspection Report 05000373/2021402 and 05000374/2021402 IR 05000373/20210032021-11-0808 November 2021 County Station Integrated Inspection Report 05000373/2021003; 05000374/2021003 and 07200070/2021001 IR 05000373/20210022021-11-0101 November 2021 County Station Integrated Inspection Report 05000373/2021002 and 05000374/2021002 IR 05000373/20210122021-10-28028 October 2021 County Station- 50.59 Team Inspection Report 05000373/2021012 and 05000374/2021012 IR 05000373/20210052021-09-0101 September 2021 Updated Inspection Plan for Lasalle County Station, Units 1 and 2; Report 05000373/2021005 and 05000374/2021005 IR 05000373/20210112021-08-23023 August 2021 County Station - Design Basis Assurance Inspection (Programs) Inspection Report 05000373/2021011 and 05000374/2021011 IR 05000373/20215012021-06-16016 June 2021 County Station - Emergency Preparedness Biennial Exercise Inspection Report 05000373/2021501 and 05000374/2021501 IR 05000373/20214012021-05-18018 May 2021 County Station - Security Baseline Inspection Report 05000373/2021401 and 05000374/2021401 IR 05000373/20210012021-05-0404 May 2021 Lssalle County Station - Integrated Inspection Report 05000373/2021001 and 05000374/2021001 IR 05000374/20210102021-04-0505 April 2021 County Station - Post-Approval Site Inspection for License Renewal (Phase I) Report 05000374/2021010 2024-09-27
[Table view] Category:Letter
MONTHYEARIR 05000373/20243012024-10-31031 October 2024 Initial License Examination Report 05000373/2024301 05000374/2024301 IR 05000373/20244042024-10-23023 October 2024 County Station – Security Baseline Inspection Report 05000373/2024404 and 05000374/2024404 RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests 05000373/LER-2023-001-01, Air Circuit Breaker (Acb) Mechanically Operated Contacts (MOC) Switch Failed to Actuate2024-10-0909 October 2024 Air Circuit Breaker (Acb) Mechanically Operated Contacts (MOC) Switch Failed to Actuate ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing IR 05000373/20244012024-09-27027 September 2024 County Station – Security Baseline Inspection Report 05000373/2024401 and 05000374/2024401 ML24263A2062024-09-19019 September 2024 Request for Exemption from Certain Requirements of 10 CFR 72.212 and 10 CFR 72.214 for LaSalle County Station - Holtec MPC-68MCBS ML24260A0492024-09-16016 September 2024 Operator Licensing Examination Approval - Lasalle County Station, Unit 1 and 2, September 2024 RS-24-090, Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-09-12012 September 2024 Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 IR 05000373/20240052024-08-29029 August 2024 Updated Inspection Plan and Assessment Follow-Up Letter for Lasalle County Station (Report 05000373/2024005; 05000374/2024005) IR 05000373/20244022024-08-28028 August 2024 County Station - Cyber Security Inspection Report 05000373/2024402 and 05000374/2024402 ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 05000373/LER-2024-004-01, Emergency Diesel Generator Auto-Start and Load Due to Loss of System Auxiliary Transformer2024-08-22022 August 2024 Emergency Diesel Generator Auto-Start and Load Due to Loss of System Auxiliary Transformer IR 05000373/20240022024-08-13013 August 2024 County Station - Integrated Inspection Report 05000373/2024002 and 05000374/2024002 ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition IR 05000373/20244202024-08-0505 August 2024 County Station - Security Baseline Inspection Report 05000373 2024420 and 05000374 2024420 05000373/LER-2024-003-01, Supplement to Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.1.3 Completion Time Exceeded2024-07-31031 July 2024 Supplement to Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.1.3 Completion Time Exceeded ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification RS-24-064, Nuclear Radiological Emergency Plan Document Revisions2024-06-28028 June 2024 Nuclear Radiological Emergency Plan Document Revisions ML24178A2522024-06-27027 June 2024 County Station – Acknowledgement of Response to NRC Inspection Report 05000373/2024001 and 05000374/2024001 and Disputed Non-Cited Violation 05000373/LER-2024-004, Emergency Diesel Generator Auto-Start and Load Due to Loss of Station Auxiliary Transformer2024-06-19019 June 2024 Emergency Diesel Generator Auto-Start and Load Due to Loss of Station Auxiliary Transformer RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations 05000373/LER-2024-003, Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.1.3 Completion Time Exceeded2024-06-0606 June 2024 Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.1.3 Completion Time Exceeded IR 05000373/20240102024-05-29029 May 2024 County Station - Commercial Grade Dedication Inspection Report 05000373/2024010 and 05000374/2024010 ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 ML24142A3352024-05-21021 May 2024 Quad Cities—Information Request to Support the NRC Annual Baseline Emergency Action Level and Emergency Plan Changes 05000373/LER-2024-002, Reactor Protection System Half Scram Due to Motor Generator Set Electric Power Monitoring Assembly Output Breaker Trip2024-05-17017 May 2024 Reactor Protection System Half Scram Due to Motor Generator Set Electric Power Monitoring Assembly Output Breaker Trip RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report ML24131A1512024-05-13013 May 2024 County Station - Integrated Report 05000373/2024001 and 05000374/2024001 IR 05000373/20240012024-05-13013 May 2024 County Station - Integrated Report 05000373/2024001 and 05000374/2024001 RS-24-038, Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-05-0202 May 2024 Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests 05000373/LER-2024-001, Core Operating Limits Report Thermal Limits Exceeded2024-04-26026 April 2024 Core Operating Limits Report Thermal Limits Exceeded ML24108A1562024-04-15015 April 2024 Updated Final Safety Analysis Report (Ufsar), Revision 26 and Fire Protection Report (Fpr), Revision 11 ML24103A2042024-04-12012 April 2024 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition RS-24-002, Constellation Energy Generation, LLC - Annual Property Insurance Status Report2024-04-0101 April 2024 Constellation Energy Generation, LLC - Annual Property Insurance Status Report ML24071A2122024-03-12012 March 2024 County Station - Information Request for the Cyber-Security Baseline Inspection, Notification to Perform Inspection IR 05000373/20230062024-02-28028 February 2024 Annual Assessment Letter for Lasalle County Station, Units 1 and 2 (Report 05000373/2023006; 05000374/2023006) RS-24-014, Annual 10 CFR 50.46 Report of Emergency Core Cooling System Evaluation Model Changes and Errors2024-02-22022 February 2024 Annual 10 CFR 50.46 Report of Emergency Core Cooling System Evaluation Model Changes and Errors ML24018A0682024-02-0909 February 2024 Issuance of Amendment Nos. 262 and 247 Revised Design Bases of Lower Downcomer Braces ML24024A1332024-01-24024 January 2024 Confirmation of Initial License Examination IR 05000373/20230042024-01-24024 January 2024 County Station - Integrated Inspection Report 05000373/2023004 and 05000374/2023004 IR 05000373/20230122024-01-18018 January 2024 County Station - Biennial Problem Identification and Resolution Inspection Report 05000373/2023012 and 05000374/2023012 ML23354A2902024-01-0505 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0028 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) ML23360A6082023-12-27027 December 2023 County Station Request for Information for NRC Commercial Grade Dedication Inspection: Inspection Report 05000373/2024010 and 05000374/2024010 ML23278A1292023-12-14014 December 2023 Units 1 & 2; Limerick, Units 1 & 2; Nine Mile Point, Units 1 & 2; and Peach Bottom, Units 2 & 3 -Revision to Approved Alternatives to Use Boiling Water Reactor Vessel and Internals Project Guidelines ML23305A1402023-12-13013 December 2023 Units 1 & 2; Nine Mile Point, Unit 2; Peach Bottom, Units 2 & 3; and Quad Cities, Units 1 and 2 - Issuance of Amendments to Adopt Traveler TSTF-580 05000373/LER-2023-002, Turbine Stop Valve Limit Switch Failure Due to Lubricant Degradation2023-12-0404 December 2023 Turbine Stop Valve Limit Switch Failure Due to Lubricant Degradation 2024-09-06
[Table view] |
Inspection Report - LaSalle - 2009007 |
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Text
ber 11, 2009
SUBJECT:
LASALLE COUNTY STATION, UNITS 1 AND 2 PROBLEM IDENTIFICATION AND RESOLUTION (PI&R) INSPECTION 05000373/2009007; 05000374/2009007
Dear Mr. Pardee:
On November 23, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution (PI&R) inspection at the LaSalle County Station Units 1 and 2. The enclosed report documents the inspection results, which were discussed on November 23, 2009, with members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
The inspection concluded that your staff was effective at identifying problems and incorporating them into the corrective action program. In general, issues were appropriately prioritized, evaluated, and corrected, audits and self-assessments were thorough and probing, and operating experience was appropriately screened and disseminated. Your staff was aware of the importance of having a strong safety-conscious work environment and expressed a willingness to raise safety issues.
No findings or violations were identified during this inspection. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC=s document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Kenneth Riemer, Chief Branch 2 Division of Reactor Projects Docket No. 50-373; 50-374 License No. NPF-11; NPF-18
Enclosure:
Inspection Report 05000373/2009007; 05000374/2009007 w/Attachment: Supplemental Information
REGION III==
Docket Nos: 05000373; 05000374 License Nos: NPF-11; NPF-18 Report No: 05000373/2009007; 05000374/2009007 Licensee: Exelon Generation Company, LLC Facility: LaSalle County Station, Units 1 and 2 Location: Marseilles, IL Dates: November 2-20, 2009 Inspectors: N. Shah, Project Engineer - Team Lead F. Ramirez, Resident Inspector - LaSalle C. Scott, Reactor Engineer D. Swarzc, Reactor Engineer Observers: Jane Yesinowki, Illinois Emergency Management Agency Approved by: Kenneth Riemer, Chief Branch 2 Enclosure
SUMMARY OF FINDINGS
IR 05000373/2009007; 05000374/2009007 (November 2, 2009 - November 20, 2009),
LaSalle County Station Units 1 and 2; Biennial Baseline Inspection of the Identification and Resolution of Problems.
This team inspection was performed by three regional inspectors and the site resident inspector.
No findings or violations were identified.
Identification and Resolution of Problems Overall, the corrective action program (CAP) was being effectively implemented. Issues were identified at a low threshold, evaluated and corrected. Self-assessments and audits by Nuclear Oversight (NOS) were thorough and critical of the assessed areas. Operating experience was recognized as valuable and was effectively communicated. Interviews with licensee staff and a review of the Employee Concerns Program (ECP) indicated that the licensee had a positive safety culture environment that encouraged identification of issues in the CAP.
However, the inspectors identified several areas of concern that may negatively impact the licensees ability to identify and resolve issues. In some cases, these issues had been recognized by the licensee, but effective corrective action had not been taken. Briefly, the issues were:
- The current CAP performance indicators were not always effectively used or sufficient to monitor the program. Although the licensee was aware of these issues, CAP staff appeared willing to live with the shortcomings and had not formally taken corrective action.
- There were some examples of long-standing issues that were either not corrected or not evaluated. In some cases, the licensee had identified the issues, but had not evaluated why previous corrective actions were ineffective.
- There were several examples where the review of operating experience (OE) in cause evaluations were not documented in accordance with licensee procedures. Additionally, there was no formal requirement to evaluate whether the failure to use OE was a precursor during the evaluation of events. Although the licensee had identified these issues in the CAP, the corrective actions were somewhat limited.
- Issues that were reviewed by the ECP, but not captured in a formal case file, were not always well documented. This resulted in some uncertainty regarding whether potentially significant issues were appropriately dispositioned.
NRC-Identified
and Self-Revealed Findings
Cornerstone: Mitigating Systems
None.
Licensee-Identified Violations
No violations of significance were identified.
REPORT DETAILS
OTHER ACTIVITIES
4OA2 Problem Identification and Resolution
The activities documented in Sections
.1 through .4 constituted one biennial sample of
Problem Identification and Resolution (PI&R) as defined in Inspection Procedure (IP) 71152.
.1 Assessment of the Corrective Action Program Effectiveness
a. Inspection Scope
The inspectors reviewed the licensees corrective action program (CAP) implementing procedures and attended CAP program meetings to assess the implementation of the CAP.
The inspectors selectively reviewed risk and safety-significant issues entered in the CAP since the last NRC PI&R inspection in November 2007. The selection of issues ensured an adequate review of issues across the NRC cornerstones. The inspectors included issues identified through NRC generic communications, department self-assessments, licensee audits, operating experience reports, and NRC documented findings as part of this assessment. The inspectors also reviewed a selection of completed root, apparent and common cause evaluations.
The inspectors performed a more extensive review of the licensees control of cabling located in underground vaults, and corrective actions and temporary modifications that had been open for greater than one year. The review of the cabling located inside underground vaults consisted of a five year search of related issues identified in the CAP and discussions with appropriate licensee staff to assess the licensees efforts in addressing identified concerns.
During the reviews, the inspectors evaluated whether the licensee staffs actions were in compliance with the facilitys CAP and 10 CFR Part 50, Appendix B requirements.
Specifically, the inspectors evaluated if licensee personnel were identifying plant issues at the proper threshold, if these issues were entered into the CAP in a timely manner, and if these issues were appropriately resolved. The inspectors also evaluated whether root, apparent, and common cause evaluations were assigned and performed as appropriate. The inspectors also evaluated the timeliness and effectiveness of corrective actions for selected issue reports, completed investigations, and NRC-identified issues.
b. Assessment
- (1) Effectiveness of Problem Identification Overall, the CAP program was effectively implemented in that issues were identified at a low threshold, evaluated and corrected. Workers were encouraged to identify issues and were familiar with the various avenues available (NRC, ECP, CAP, etc.). This was evident by the large number of CAP items generated annually, which were reasonably distributed across the various departments. A shared computerized database was used for creating individual reports and for subsequent management of the processes of issue evaluation and response. This included determining the issues significance, addressing such matters as regulatory compliance and reporting, and assigning any actions deemed necessary or appropriate.
However, the inspectors noted that the licensee performance indicators for monitoring the CAP program were not being effectively utilized. The inspectors identified that there was no requirement to investigate instances where indicators identified poor performance. For example, the inspectors noted that no Action Requests (ARs) had been initiated for several indicators that were either in the yellow or red band (indicating poor performance) during the past year. During interviews, licensee CAP staff commented that some of these indicators, because of how they were defined, may be inaccurately reporting performance. However, the inspectors could not find any CAP entries identifying these indicators so that they could be corrected. The inspectors questioned the efficacy of the indicators when no effort was made to evaluate instances when poor performance was identified or to revise those considered inaccurate. The licensee issued AR 993280993280to evaluate this issue.
The inspectors determined that the station was generally effective at trending low level issues to prevent larger issues from developing. The licensee also used the CAP to document instances where previous corrective actions were ineffective or were inappropriately closed.
Findings No findings of significance were identified.
- (2) Effectiveness of Prioritization and Evaluation of Issues The inspectors concluded that the station was generally effective at prioritizing and evaluating issues commensurate with the safety significance of the identified problem.
The inspectors determined that CAP screening meetings were generally thorough and maintained a high standard for approving actions.
The majority of issues were of low level and were either closed to trend or at a level appropriate for a condition evaluation. Some of these issues were closed to a work request or to another CAP report, but the inspectors noted that both the parent and daughter documents had the necessary verbiage to document the interrelationship.
The inspectors also had no concerns with those assigned an apparent, root or common cause evaluation. There were no items in the operations, engineering, or maintenance backlogs that were risk significant, individually or collectively.
Root, apparent and common cause evaluations were generally thorough; however, the inspectors did identify two examples where the level of review was less than appropriate:
- AR 882701882701was written to perform a common cause evaluation for an adverse trend regarding issues with work orders/packages. The evaluation identified that this issue had been recurring since 2003, but did not address why previous corrective actions were ineffective.
- AR 784631784631was written after the NRC resident inspectors had observed a high radiation barrier (fenced enclosure) that had been built adjacent to the Unit 1 safety-related Standby Gas Treatment System piping. The barrier was in contact with the piping (potentially raising a concern regarding the seismic analysis), but there was no licensee evaluation supporting this condition. Subsequently, the barrier was removed, but there was no documentation for its removal.
The licensee captured the above issues in the CAP as AR Nos. 996319 and 995883.
The inspectors determined that the licensee was generally effective at evaluating equipment functionality requirements after a degraded or non-conforming issue was identified. The inspectors reviewed Maintenance Rule action plans associated with systems currently in (a)(1) and for those returning to a(2) status within the last two years. No issues were identified from this review.
The inspectors also concluded that the licensee had been effectively managing underground cabling.
Findings No findings of significance were identified.
- (3) Effectiveness of Corrective Actions The inspectors concluded that corrective actions for identified deficiencies were generally timely and adequately implemented, commensurate with their safety significance. The inspectors also concluded that sampled corrective actions assignments for selected NRC documented violations were generally effective and timely. However the inspectors did notice some untimely corrective actions as described below.
- AR 840401840401was written after the NRC identified a non-safety hanger attached to a safety related cable tray. In the evaluation, the licensee failed to note that the same issue had been previously identified about four years earlier (AR 352075352075and that corrective actions had not been taken.
- The inspectors noted that the licensee had not taken appropriate action to address potential preconditioning due to inappropriate work scheduling (for example, scheduling a post-maintenance test just prior to a surveillance test)despite having two prior NRC-identified instances of such, associated with the main steam isolation valves and reactor core isolation cooling systems.
- AR 856961856961was written to address oscillations observed on a Unit 1 control rod drive flow control valve. Although a work order was written to address this, it remained open for over two years. The inspectors did not identify any CAP item evaluating why the work order was open for so long.
- AR 736409736409was written to address high dose rates associated with a radioactive waste sample sink. The AR was closed to a work order, but there was no documentation that the work was actually performed.
- The inspectors noted that work orders associated with the removal of temporary modifications, did not contain the necessary cross-referencing as required by procedure (i.e., neither the work order nor the temporary modification paperwork referenced the other).
The licensee wrote ARs 989540, 995336, 995957 and 988746, respectively, to address the above issues.
The inspectors also identified that numerous, recurring issues (since 2006) with the Units 1 and 2 gaseous and particulate radiation monitors used for reactor leak detection had not been resolved. The issues were varied and potentially affected the reliability of the monitors. Although these monitors were nonsafety-related, they were required by Technical Specifications. The licensee had performed past cause evaluations that had recommended corrective actions, but these actions had not been implemented.
Additionally, the licensee had not evaluated whether the issues significantly impacted the ability of the monitors to detect primary system leakage. The licensee subsequently identified that the monitors would perform the Technical Specification function and wrote AR 989527989527to address this issue.
The licensee had 19 open corrective actions that were greater than one year old, with the oldest being 731 days old. The inspectors verified that the open actions were appropriate, that work orders were in place (and scheduled) for final implementation of the action, and that plant operation or risk was not adversely affected.
Findings No findings of significance were identified.
.2 Assessment of the Use of Operating Experience
a. Inspection Scope
The inspectors reviewed the licensees implementation of the facilitys OE program.
Specifically, the inspectors reviewed implementing OE program procedures, observed daily station and pre-job briefings to observe the use of OE information, and selectively reviewed completed evaluations of OE issues and events. The intent of the review was to determine whether the licensee was effectively integrating OE experience into the performance of daily activities, whether evaluations of issues were proper and conducted by qualified personnel, whether the licensees program was sufficient to prevent future occurrences of previous industry events, and whether the licensee effectively used the information in developing departmental assessments and facility audits. The inspectors also assessed if corrective actions, as a result of OE experience, were identified and effectively implemented.
b. Assessment The inspectors concluded that the station appropriately screened OE information for applicability, and used the information for corrective and preventative actions to identify and prevent similar issues. The inspectors observed that OE was discussed as part of the daily station and pre-job briefings and was effectively disseminated across the various plant departments. During interviews with the inspectors, licensee staff generally commented favorably on the use of OE in their daily activities.
Although OE was considered as part of root, apparent and common cause evaluations, the inspectors identified that these reviews were not always documented in accordance with CAP procedures. The licensee had identified several examples during self-assessments conducted in 2008 and 2009 and had taken corrective action.
A subsequent licensee review, conducted prior to the NRC PI&R inspection, had identified no additional issues. However, the inspectors identified several examples where OE potentially applicable to the station was either not reviewed or the review was not documented as required. These examples occurred after the licensee self-assessments were completed, and were not identified in the licensees effectiveness review. The licensee initiated AR 995934995934to evaluate this issue.
The inspectors also noted that the licensees staff was not required to evaluate whether the failure to use OE was a contributing cause of an event. Instead, the staff was only required to identify OE related to an event and use any insights gained in developing the corrective actions. The inspectors noted that several of the licensees root, apparent and common cause evaluations had identified OE that may have prevented the event had it been appropriately evaluated. The licensee initiated AR 995981995981to evaluate this issue.
Findings No findings of significance were identified.
.3 Assessment of Self-Assessments and Audits
a. Inspection Scope
The inspectors reviewed selected focused area self-assessments, check-in self-assessments, root cause effectiveness reviews, and NOS audits. The inspectors evaluated whether these audits and self-assessments were being effectively managed, adequately covered the subject areas, and whether identified issues were appropriately captured in the CAP. In addition, the inspectors also interviewed licensee personnel regarding the implementation of the audit and self-assessment programs.
b. Assessment The inspectors concluded that self-assessments and audits were typically accurate, thorough, and effective at identifying issues and enhancement opportunities at an appropriate threshold level. The inspectors concluded that these audits and self-assessments were completed by personnel knowledgeable in the subject area.
The inspectors considered the quality of the NOS audits to be thorough and critical.
The self-assessments were acceptable but, as expected, they were not at the same level of quality as the audits. The inspectors observed that CAP items had been initiated for issues identified through the NOS audits and self-assessments.
Findings No findings of significance were identified.
.4 Assessment of Safety-Conscious Work Environment (SCWE)
a. Inspection Scope
The inspectors interviewed selected members of the licensees staff to determine if there were any impediments of a SCWE. In addition, the inspectors discussed the implementation of the ECP with the ECP coordinators, and reviewed 2007 - 2009 ECP activities to identify any emergent issues or potential trends. In addition, the inspectors reviewed the facilitys ECP implementing procedures, interviewed the licensee ECP coordinators, and reviewed licensee safety culture surveys. The licensees programs to publicize the CAP and ECP programs were also reviewed.
b. Assessment The inspectors determined that the plant staff were aware of the importance of having a strong SCWE and expressed a willingness to raise safety issues. No one interviewed had experienced retaliation for safety issues raised, or knew of anyone who had failed to raise issues. All persons interviewed had an adequate knowledge of the CAP and ECP process. These results were similar to the findings of the licensees safety culture surveys. Based on these interviews, the inspectors concluded that there was no evidence of an unacceptable SCWE.
The inspectors determined that the ECP process was being effectively implemented.
The review of the selected ECP issues indicated that site personnel were appropriately using the CAP and ECP to identify concerns. However, during the interviews most station personnel did not know where the ECP office was located, although they could identify the ECP personnel. This did not appear to have a detrimental affect, based on the number of ECP issues currently in the system.
However, the inspectors observed that ECP issues not captured in a formal case file, were not always well documented. This resulted in some uncertainty regarding whether potentially significant issues were appropriately dispositioned. For example, there was one issue regarding a plant individual who exhibited signs of aberrant behavior while on shift. Although this concern was documented by the ECP staff, a formal case record was not opened. The inspectors could find no record of whether this concern was reviewed by the security staff as required by the site Security plan. Subsequently, the inspectors verified that this had occurred; however, the lack of a written record made it somewhat difficult to confirm. The ECP staff acknowledged this issue and was developing corrective actions. However, due to the potential to release confidential information, this observation was not captured in the CAP.
Findings No findings of significance were identified.
4OA6 Management Meetings
.1 Exit Meeting Summary
- On November 23, 2009, the inspectors presented the inspection results to Mr. Wozniak and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- J. Bashor, Engineering Director
- L. Blunk, Operations Training Manager
- A. Byers, Performance Improvement Specialist
- K. Ihnen, Nuclear Oversight Manager
- B. Rash, Maintenance Director
- T. Simpkin, Regulatory Assurance Manager
- K. Taber, Operations Director
- J. Vergara, Senior Regulatory Specialist
- H. Vinyard, Work Management Director
- D. Wozniak, Site Vice President
Nuclear Regulatory Commission
- K. Riemer, Chief, Branch 2, Division of Reactor Projects
LIST OF ITEMS
OPENED, CLOSED AND DISCUSSED
Opened and Closed
None.
Attachment
LIST OF DOCUMENTS REVIEWED