IR 05000373/2021013

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County Station Biennial Problem Identification and Resolution Inspection Report 05000373/2021013 and 05000374/2021013
ML22019A284
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 01/20/2022
From: Kenneth Riemer
NRC/RGN-III/DRP/B1
To: Rhoades D
Exelon Generation Co, Exelon Nuclear
References
IR 2021013
Download: ML22019A284 (15)


Text

January 20, 2022

SUBJECT:

LASALLE COUNTY STATION - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000373/2021013 AND 05000374/2021013

Dear Mr. Rhoades:

On December 20, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your LaSalle County Station and discussed the results of this inspection with Mr. Van Fleet, and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety-conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

No findings or violations of more than minor significance were identified during this inspection. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Signed by Riemer, Kenneth on 01/20/22 Kenneth R. Riemer, Chief Branch 1 Division of Reactor Projects Docket Nos. 05000373 and 05000374 License Nos. NPF-11 and NPF-18

Enclosure:

As stated

Inspection Report

Docket Numbers: 05000373 and 05000374 License Numbers: NPF-11 and NPF-18 Report Numbers: 05000373/2021013 and 05000374/2021013 Enterprise Identifier: I-2021-013-0017 Licensee: Exelon Generation Company, LLC Facility: LaSalle County Station Location: Marseilles, IL Inspection Dates: November 29, 2021 to December 17, 2021 Inspectors: J. Bozga, Senior Reactor Inspector G. Hansen, Sr. Emergency Preparedness Inspector G. Hausman, Senior Reactor Inspector P. Smagacz, Resident Inspector Approved By: Kenneth R. Riemer, Chief Branch 1 Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at LaSalle County Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

(1) The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.

Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted a five-year review of the 125V DC systems and Core Standby Cooling systems.

Operating Experience, Self-Assessments and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits and self-assessments.

Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

INSPECTION RESULTS

Assessment 71152B Based on the samples reviewed, the team determined that the licensees' performance in each of these areas adequately supported nuclear safety.

Effectiveness of Problem Identification:

Overall, the licensee was effective at identifying issues at a low threshold and was properly entering them into the Corrective Action Program (CAP) as required by procedures. The inspectors determined that the station was generally effective at identifying negative trends that could potentially impact nuclear safety, at an appropriate threshold and at a healthy rate, team interviewed personnel, reviewed documents, walked down portions of the plant, and assessed licensee problem identification. Staff were encouraged to identify issues and felt comfortable raising concerns with management. However, there were numerous descriptions of the workforce feeling that very low-level items never get fixed, even though numerous condition reports are entered year after year or every time certain surveillances are performed.

The inspectors reviewed root cause and apparent cause evaluations and determined those evaluations were adequate. The inspectors noted that adding more detail to the event timelines will aid in an independent reviewer understanding all known facts. For example, during the review of the root cause report for the refuel bridge mast foreign material issue (AR 4407109), a statement troubleshooting was performed, and fuel moves recommenced was made. This statement could have been expounded upon and detailed the troubleshooting efforts, what was or was not identified, and the criteria for recommencing with fuel moves. Also, detailed descriptions on the actual physical limitations of the refuel mast after each failure would have aided an independent reviewer.

Effectiveness of Prioritization and Evaluation of Issues:

In depth reviews of a risk-informed sampling of Action Requests (ARs), work orders (WOs),and cause evaluations were completed, including 5-year reviews of issues associated with the 125V DC Battery Systems and Core Standby Cooling Systems. The inspectors identified that the licensee generally, appropriately prioritized and evaluated issues for resolution.

The inspectors also noted that while issue evaluations were generally sound, there were several examples where additional research was needed to understand the technical basis, primarily due to a lack of clear documentation. This theme had previously been identified in earlier licensee self-assessments and CAP audits and continued to be a concern.

Effectiveness of Corrective Actions:

The inspectors concluded that the licensee was generally effective in developing Corrective Actions that were appropriately focused to correct the identified problem and correct conditions adverse to quality. For issues considered significant conditions adverse to quality, the licensee took action to address the root and contributing causes and to preclude repetition. Corrective actions were generally completed in a timely manner and in accordance with procedural requirements commensurate with the safety significance of the issue.

5-year Reviews of the 125V DC Systems and Core Standby Cooling Systems:

The inspectors performed an expanded 5-year review of the Units 1 and 2 125 Vdc system; specifically, by performing system walk-downs and evaluating condition reports, engineering changes, and work orders. The inspectors also interviewed the system engineer responsible for this system. Overall, the inspectors determined that the licensee was effectively managing issues associated with this system.

As part of the review of the Core Standby Cooling System, the team identified a condition report (AR 4406388) which was associated with the use of operability limits (ASME Section III Appendix F) for determination of pressure boundary integrity/continued operation of FAC component 2RA023, a 4" tee in the reactor bottom head drain line 2RR28B-4. The inspection of this condition report will continue as a Selected Issue for Follow-Up (71152 inspection procedure) during NRC inspections in 2022.

Operating Experience, Self-Assessment and Audits:

The inspectors reviewed operating experience captured in the CAP and sampled operating experience from NRC, industry, vendors, and third-party groups. Overall, for the samples selected, the licensee was generally performing the appropriate assessments for station applicability. Through interviews and observations at selected station meetings, the inspectors also concluded that operating experience was being appropriately used in daily plant activities.

The inspectors determined that the licensee was adequately performing self-assessments and audits in accordance with licensee procedures and implementing corrective actions as needed. The inspectors did note not all self-assessment templates developed included sufficient guidance to ensure consistent evaluations. This was specifically identified in security self-assessments where one assessment included a discussion on the quantity of records reviewed, but other assessments contained blanket statements of passing.

Safety Conscious Work Environment:

As part of the NRCs safety conscious work environment evaluation during the PI&R biennial inspection, NRC inspectors completed a limited scope inspection sample of an assessment performed by the licensee that evaluated human performance behaviors exhibited during the recent refueling outage, L1R18, and the potential impact on safety conscious work environment at the site. The inspectors performed an independent review that evaluated the licensees internal assessment of the sites SCWE program and the actions that were developed and implemented in response to the licensees identified areas for improvement to promote a healthy organizational safety conscious work environment. The NRC inspectors reviewed licensee evaluation records, internal organizational assessment survey results, training plans, and conducted interviews with the Employee Concerns Program Manager, Organizational Effectiveness Manager, and management staff from various departments.

No violations or findings were identified.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On December 20, 2021, the inspectors presented the biennial problem identification and resolution inspection results to Mr. Van Fleet, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71152B Calculations L-003447 LaSalle Units 1 and 2, 125Vdc System Analysis Dated 002

June 11, 2020

Corrective Action 04062322 Replace Battery 2DC18E Cell 44 10/12/2017

Documents 04114041 Replace or Retest 1DC07E 03/12/2018

04144731 Generate Forced Outage Work Order for Battery 06/06/2018

Replacement

203137 U2 Division 1 Battery Replacement 12/14/2018

04455972 Request WR to Replace 2DC16E K306 Relay 10/26/2021

04455973 Request WR to Replace 2DC23E K306 Relay 10/26/2021

1337255 TRM Appendix G, Table 2 Enhancements Needed 03/01/2012

141231 VR Supply Duct Access Repair Patch Not Installed Per 01/27/2003

Design

1518242 Ops Crew 6 4/17/13 LOOP Lessons Learned 04/17/2013

2387941 2E22-F369A Relief Valve Failed As-Found Test 09/29/2014

2530386 FAC Program - OE Review of Davis Besse Steam Rupture 05/19/2015

2618561 Degraded Condition Observed on CSCS Piping Line 01/28/2016

2HP55A-4

3990967 Degraded Condition Observed on CSCS Piping Line 03/29/2017

2HP54A-4

4048633 RM - 1C71A-K10C Failed to De-Energize During LOS-RP-Q2 09/03/2017

4099862 Limitation For 2HP55BB Per EC 403264 Flaw Evaluation 02/01/2018

4172339 Unit 2 LPCS Motor Cooler Inlet Pipe 2DG22A-1.5" is 09/12/2018

Degraded

4192778 2018 WANO AFI ER.2 11/06/2018

21635 VT-3 Exams Specified on Supports Exempted from 02/19/2019

Examination

25076 ACB 1414 Had a Lockout Trip While Performing LOS-AP-R2 03/01/2019

28241 Low Power TIP Set not Completed Due to TIPs OOS 03/10/2019

251021 Review Code Requirements for Replacement VY Cooling 05/22/2019

Coils

252624 Code Non-Conformance Identified For VY Coolers 05/29/2019

1(2)VY03A

Inspection Type Designation Description or Title Revision or

Procedure Date

257366 4.0 Critique IR on Tendon Surveillances 06/17/2019

258604 Late Surveillance (LIS-OG-408) 06/21/2019

261844 Cardox Tank Compressor Tripped on Thermal Overloads 07/04/2019

262090 NRC ID - Dry Pipe FP Lines not Sloped Per NFPA13 07/05/2019

265814 1RE026 Closed Light Did Not Illuminate During LOS-PC-Q1 07/21/2019

265960 Large Steam Leak Found Downstream of 1G33-F040 07/22/2019

266264 Performance Level 3 OPEX Review of ICES 456532 for 08/23/2019

Applicability to LaSalle

267062 MSIV Pilot Solenoid Leads Crossed 07/25/2019

267121 PCE Level 1 07/25/2019

270252 Historical 2C51-J004C App J Leakage Evaluations not Found 08/07/2019

271342 Unexpected MCR Alarm: Unit 1 Hydrogen Panel Trouble 08/12/2019

273172 Part 21 Flowserve Unqualified NDE Performance of 08/20/2019

Component

273349 NER NC-19-010-Y OE Review- Potential LaSalle 08/20/2019

Vulnerability

276944 Part 21 Contactors Failing to Release/Open When 09/05/2019

De-Energized

277173 NRC IN 2019-05: Over Pressurization of Alpha Sources 09/06/2019

280047 AT 04257366-04 Needs to be Reevaluated 09/17/2019

281169 LOS-SY-SR1 Revision Needed 09/22/2019

284443 Through Wall Leak on ST Piping in U2 Div 1 CSCS Pump 10/02/2019

Room

286161 Unacceptable Trend Identified on MSIV Timing Per 10/08/2019

LOS-PC-Q2

288235 NRC IN 2019-08 OPEX Regarding FAC Causing RX Scrams 10/16/2019

288344 NRC ID: NRC Question on 1G33-F040 10/16/2019

288357 Replace Piping 1DG23B-6" 10/16/2019

294984 NRC IN 19-09: Spent Fuel Cask Movement Issues 10/30/2019

295415 Revise EC 363524 to Extend VY Fan SBM C\S Replacement 11/07/2019

PM's

4305470 Biennial Safety Culture Self-Assessment 02/04/2020

4306254 Level 3 OPEX Review Requested #465166 Diablo Canyon 12/27/2019

Inspection Type Designation Description or Title Revision or

Procedure Date

Unit 2

4306904 1B RR Pump Lower Oil Reservoir Hi Level 12/30/2019

4307124 Level 3 OPEX Review Requested #464385 Salem Unit 2 12/31/2019

4307131 Level 3 OPEX Review Requested #458702 Hatch Unit 2 12/31/2019

4318198 L1R18 FAC; 1RH006 Low Wall Thickness 02/15/2020

4319242 L1R18 FAC; Component 1RH014 Low Wall Thickness 02/19/2020

22219 1ES010B Indicating Closed 02/28/2020

22221 1ES010C Indicating Closed 02/28/2020

28259 P21- Potential Deviation of Pressure Transmitters 03/20/2020

4330162 Rosemount Transmitters Part 21 for Changes in Heat Rise 03/27/2020

4343229 Flex Generator Issue at Quad: LaSalle has Similar Generator 05/14/2020

4357505 U1 EHC Pressure Low in Band with New Discharge Filter 07/18/2020

4362593 NRC Question on 2CW03A Piping Support 08/10/2020

4365890 RM - Step Change Reduction in U2 Jet Pump 15 Flow 08/27/2020

4366965 Degraded Piping Support 09/02/2020

4368035 LR Inspection of 2LP13B-3" Piping 09/08/2020

4368037 LR Inspection of 2LP23AA-1/2" Piping 09/08/2020

4368040 LR Inspection for 2LP19A-3" Piping 09/08/2020

4380329 SR 3.4.3.1 Jet Pump# 15 Curve No Conservative Change 10/28/2020

4382365 B DFP High Discharge Pressure 11/05/2020

4383488 2A RHR Seal Cooler Flow Low 11/10/2020

4389292 RM - JP 5/6 ACMP Flow Mismatch 12/10/2020

4391800 Loss of U2 Div 3 Water Leg Pump 12/23/2020

4391803 NRC IN 2020-04 - FP Mn Yard Buried Cast Iron Piping 12/17/2020

Failures

4404161 L2R18 FAC Component 2HJ016 Low Wall Thickness 02/23/2021

4404521 L2R18 FAC; 2RH004, Low Wall Thickness 02/24/2021

4404903 2DG01A Heat Exchanger Tubes Material Degradation 02/24/2021

4404903 2DG01A Heat Exchanger Tubes Material Degradation 02/26/2021

4405141 Unanticipated Does Rate Alarm in High Radiation Area 02/27/2021

4406388 FAC Inspection on 2RA023 not Performed 03/03/2021

4406519 NRC ID Failure to Write IR in Heat Exchanger Program 03/03/2021

4406519 NRC ID Failure to Write IR in Heat Exchanger Program 03/04/2021

Inspection Type Designation Description or Title Revision or

Procedure Date

4406544 NRC ID LR Selective Leaching Program Perf. Deficiencies 03/01/2021

4406555 L2R18 FAC; 2MS66B-RT-01, Low Wall Thickness 03/04/2021

4407109 Unit 2 Refuel Bridge Mast Issue During Fuel Moves 03/07/2021

4407109 Unit 2 Refuel Bridge Mast Issue During Fuel Moves 03/07/2021

4407388 "L" SRV Drop Test Failure 03/08/2021

4407915 "L" SRV Failed LOS-MS-R& Drop Test 03/10/2021

4407917 "R" SRV Failed Regulated Header Drop Test 03/10/2021

4409413 NRC Identified-NRC Questioned Weld Procedure 03/15/2021

Qualification

4417755 RM - Unit 2 Jet Pump #6 is not Within Jet Pump Curves 04/20/2021

22004 FAC RWCU Bottom Head Drain Lessons Learned 05/06/2021

23071 NRC IN 2021-01: Design Bases LLed Power Operated 05/11/2021

Valves

26705 RM - 2A RPS M/G Set Output Breaker Tripped 05/31/2021

27494 2A RPS MG Set Voltage Adjustment Pot Bad 06/04/2021

28890 L1R19 Class 1 Small Bore Pipe Socket Welds 06/11/2021

4433739 Tendon Grease Cap Area Unit 2 Concrete Inspections 07/07/2021

4441741 2021 PI&R SA Gap: OBJ 3A 08/20/2021

44447160 No Flow Thru U1 EHC Fullers Earth Filters Via Hydraulic 09/17/2021

Pump

4448905 10CFR Part 21. Ametek Equalize Relay 09/27/2021

Corrective Action 4465190 NRC ID- 2HP54A-4" UT Inspection Results Per WO-4621240 12/07/2021

Documents 4466247 NRC Identified Issue With L-003447 Rev. 002 12/13/2021

Resulting from 4466816 NRC ID - 2DG22A-1.5" Min Wall Design Limit 12/15/2021

Inspection 4467017 NRC Observation - 2021 PI&R - CR Type AR Generation 12/16/2021

4467039 NRC Observation - PI&R 2021 - Security Self-Assessments 12/16/2021

4467111 NRC Observation - PI&R 2021 - Enhancement Opportunity 12/16/2021

for RCR

Engineering 403264 Minimum Wall Thickness for Unit 2 Division 3 VY Cooler 1

Changes Piping for Extent of Condition

403264 Minimum Wall Thickness for Unit 2 Division 3 VY Cooler 2

Piping for Extent of Condition

28380 L2R18 FAC Min Wall Evaluation 4

Inspection Type Designation Description or Title Revision or

Procedure Date

28380 L2R18 FAC Min Wall Evaluation 5

Engineering LAS-02121 Failure Analysis of Limit Switch from LaSalle Station 08/14/2018

Evaluations LAS-24193 Failure Analysis of a Namco Limit Switch from LaSalle 11/16/2018

Station

LAS-62503 Failure Analysis of a Namco limit Switch from Lasalle Station 05/03/2019

LAS-93383 Failure Analysis of a NAMCO Limit Switch Assembly 06/13/2012

Miscellaneous 4405141 Rad Worker Behaviors Root Cause 05/27/2021

4407109 Root Cause Investigation Report for Unit 2 Refuel Bridge 06/25/2021

Mast Issue During Fuel Moves

IEEE STD 485- IEEE Recommended Practice for Sizing Lead-Acid Batteries 09/11/2003

1997 for Stationary Applications

IEEE STD 946- IEEE Recommended Practice for the Design of 03/21/1985

1985 Safety-Related DC Auxiliary Power Systems for Nuclear

Power Generating Stations

NOSA-LAS-19-05 Engineering Design Control Audit Report 07/10/2019

NOSA-LAS-20-05 Engineering Programs Audit Report 07/15/2020

NOSA-LAS-21-05 LaSalle Corrective Action Program Audit Report 09/01/2021

OPEX Evaluation ICES 318466, Pin Hole Leak at Residual Heat Removal 11/25/2015

2570259-02 Service Water (RHRSW) Pipe Elbow

OPEX Evaluation LER 2017-003, Division 2 Residual Heat Removal Service 11/09/2017

4056244-02 Water System (RHRSW) Inoperable Due to an Inoperable

RHRSW Flow Control Valve (FCV) (Fermi 2)

OPEX Evaluation ESW Inop Due to Silt Buildup 04/29/2020

430760

NDE Reports20-141 Ultrasonic Exam of 2DG22A-1 1/2 09/08/2020

Procedures EI-AA-101 Employee Concerns Program 11

ER-AA-320 Maintenance Rule Implementation Per NEI 18-10 0

NISP-PI-02 Conduct of Self-Assessments and Benchmarks 0

NO-AA-10 Quality Assurance Topical Report 97

PI-AA-101 Conduct of Performance Improvement 2

PI-AA-1012 Safety Culture Monitoring 3

PI-AA-115 Operating Experience Program 5

PI-AA-120 Issue ID and Screening Process 11

Inspection Type Designation Description or Title Revision or

Procedure Date

PI-AA-120 Issue Identification and Screening Process 11

PI-AA-125-1001 Root Cause Analysis Manual 6

PI-AA-125-1003 Corrective Action Program Evaluation Manual 6

PI-AA-126-1001 Self-Assessments 5

Self-Assessments 4091749 RP Personnel Knowledge SA Report Assignment 07/02/2019

4113395 NRC SY Baseline Inspect-SA Report PASSPORT 06/06/2019

Assignment

4113396 NRC EP Baseline Inspect-SA Report PASSPORT 09/05/2019

Assignment

4192133 SA Report - M&TE Inventory Control, Access, & Handling 10/08/2019

4192133 Self-Assessment M&TE Inventory Control, Access, & 11/06/2018

Handling

4192145 SA Report Assignment - M&T Effectiveness of ACAD 17-01 10/02/2019

4192182 SA Report Assignment - NRC SY Baseline Inspection 12/18/2019

257452 Self-Assessment of SA/BM NISP-PI-02 Implementation 05/14/2020

4305470 Biennial Safety Culture Self-Assessment 02/04/2020

29347 LaSalle Pre-NRC Triennial Heat Sink 02/24/2021

29367 SA Report - Security Baseline Inspection 07/21/2021

29672 SA Report - RP Baseline Inspection 07/16/2021

29675 SA Report - EP Baseline Inspection/Performance Indicator 10/01/2021

Verification

4343239 Cyber Security Program Effectiveness Self-Assessment 05/14/2020

4362946 LaSalle M&T Comprehensive Self-Assessment Report 06/30/2021

4378794 2020 INPO Performance Based Evaluation Results 09/23/2021

4430137 2021 Preparation for NRC Problem Identification and 08/23/2021

Resolution (PI&R) Inspection

LaSalle Station Fleet Assessment Special Assessment Report 02/24/2020

01/27-31/2020

LaSalle Station Fleet Assessment T-6 Assessment Report (Maintenance) 04/16/2020

03/23-27/2020

LaSalle Station Fleet Assessment T-18 Assessment Report (Maintenance) 06/14/2021

05/17-21/2021

LaSalle Station Fleet Assessment Mid-Cycle Assessment Report 09/18/2019

Inspection Type Designation Description or Title Revision or

Procedure Date

08/16-28/2019 (Maintenance)

LaSalle Station Fleet Assessment Midcycle Assessment Debrief 11/15/2021

Work Orders 4866827 Unit 2 Refuel Bridge Contingency Repairs 03/07/2021

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