IR 05000373/2023012

From kanterella
Jump to navigation Jump to search
County Station - Biennial Problem Identification and Resolution Inspection Report 05000373/2023012 and 05000374/2023012
ML24017A120
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 01/18/2024
From: Robert Ruiz
NRC/RGN-III/DORS/RPB1
To: Rhoades D
Constellation Energy Generation, Constellation Nuclear
References
IR 2023012
Download: ML24017A120 (1)


Text

January 18, 2024

SUBJECT:

LASALLE COUNTY STATION - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000373/2023012 AND 05000374/2023012

Dear David P. Rhoades:

On December 15, 2023, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your LaSalle County Station and discussed the results of this inspection with John Van Fleet, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations problem identification and resolution program to confirm that the station was complying with NRC regulations and licensee standards. The team identified a finding in problem identification, implementation of the process for prioritizing and evaluating these problems, and the effectiveness of corrective actions taken to resolve these problems. Specifically, the team identified a finding with an associated non-cited violation for the failure to follow the requirements of the ASME OM code following a documented test failure of the Unit 1 residual heat removal discharge C heat exchanger relief valve. The details of this issue are discussed in the report.

The team also evaluated the stations effectiveness in identifying, prioritizing, evaluating, and correcting problems, reviewed licensee audits and self-assessments, and its use of industry and NRC operating experience information. The results of these evaluations are in the enclosure.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews, the team found no evidence of challenges to your organizations safety-conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy. If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at LaSalle County Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at LaSalle County Station.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Signed by Ruiz, Robert on 01/18/24 Robert Ruiz, Chief Reactor Projects Branch 1 Division of Operating Reactor Safety Docket Nos. 05000373 and 05000374 License Nos. NPF-11 and NPF-18

Enclosure:

As stated

Inspection Report

Docket Numbers: 05000373 and 05000374 License Numbers: NPF-11 and NPF-18 Report Numbers: 05000373/2023012 and 05000374/2023012 Enterprise Identifier: I-2023-012-0011 Licensee: Constellation Nuclear Facility: LaSalle County Station Location: Marseilles, IL Inspection Dates: November 27, 2023 to December 15, 2023 Inspectors: E. Magnuson, Reactor Inspector J. Meszaros, Resident Inspector N. Shah, Senior Project Engineer M. Siddiqui, Reactor Inspector Approved By: Robert Ruiz, Chief Reactor Projects Branch 1 Division of Operating Reactor Safety Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at LaSalle County Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Comply with ASME Code Requirements Following Test Failure Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green [P.2] - 71152B Systems NCV 05000373,05000374/2023012-01 Evaluation Open/Closed The inspectors identified a finding of very low safety significance (Green) and an associated non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (10 CFR)

Part 50.55a (f)(4)(ii) for the licensees failure to perform inservice tests to verify the operational readiness of valves whose function is required for safety. Specifically, the licensee failed to perform inservice testing on two additional relief valves from valve group R105, following the set-pressure testing failure of 1E12-F025C, and failed to perform the cause-and-effect evaluation of the testing failure.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 03.04)

(1) The inspectors performed a biennial assessment of the effectiveness of the licensees Problem Identification and Resolution program, use of operating experience, self-assessments and audits, and safety-conscious work environment.
  • Problem Identification and Resolution Effectiveness: The inspectors assessed the effectiveness of the licensees Problem Identification and Resolution program in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted a 5-year review of the core standby cooling systems. The inspection also included a selective review of past NRC observations, violations (including non-cited) and findings documented in the licensees Corrective Action Program.
  • Operating Experience: The inspectors assessed the effectiveness of the licensees processes for use of operating experience.
  • Self-Assessments and Audits: The inspectors assessed the effectiveness of the licensees identification and correction of problems identified through audits and self-assessments.
  • Safety-Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

INSPECTION RESULTS

Assessment 71152B Assessment of the Corrective Action Program Effectiveness of Problem Identification Overall, the station was effective at identifying issues at a low threshold and was properly entering them into the corrective action program (CAP) as required by station procedures.

During interviews, workers were familiar with how to enter issues into the CAP and stated that they were encouraged to use it to document issues. During plant walkdowns, the team observed that issues were being identified in the field and that they were being properly addressed in the CAP. The team determined that the station was generally effective at identifying negative trends that could potentially impact nuclear safety. For the areas reviewed, the team did not identify any issues in problem identification.

Effectiveness of Prioritization and Evaluation of Issues In-depth reviews of a risk-informed sampling of action requests (ARs), work orders (WOs),and root and apparent cause and condition evaluations were completed. The team determined that the licensee had established a low threshold for entering deficiencies into the CAP, that the issues were generally being appropriately prioritized and evaluated for resolution, and that corrective actions (CAs) were implemented to mitigate the future risk of issues occurring that could affect overall system operability and/or reliability.

The inspectors noted that issues were properly screened, with most either classified as Conditions Adverse to Quality (CAQ) or Non-Corrective Action Program (NCAP) items.

Through a selective review of CAP and NCAP items, the inspectors found no issues either with the assigned level of evaluation or the proposed corrective actions. Issues having potential operability concerns were properly addressed through the screening process and during control room observations, and accompaniment of non-licensed operators during daily rounds; the inspectors did not identify any significant operator workarounds or similar deficiencies.

While most CAP products were acceptable, the inspectors identified some minor examples where the process requirements were not met. These included, but were not limited to:

  • A Corrective Action Program Evaluation (CAPE) for AR 4011747 did not have a required effectiveness review as an assigned action.
  • AR 4468596 had an incorrect significance level assigned.
  • The effectiveness review for root cause evaluation (RCE) associated with AR 4406976 was assigned within 3 months after implementation of the corrective actions to prevent recurrence, which was too early to assess their effectiveness.

The inspectors noted that similar examples were noted in recent licensee self-assessments and audits of the CAP and that actions were being taken by the licensee to reinforce the CAP standards and expectations. The licensee also captured the above inspector-identified examples in the CAP.

The inspectors did a selective review of issues identified by the NRC either documented as observations, or for which findings or other enforcement was issued. These issues were properly documented and screened in the CAP and corrective actions were appropriate and timely scheduled.

Issue evaluations were generally sound and of good quality. Most issues were screened as low significance and were assigned a work group evaluation (the lowest level of review);more significant issues were assigned a CAPE, or if highly significant, a root cause evaluation. Through a selective review, the inspectors verified that the assigned evaluations were consistent with the significance of the issue as defined in the licensees process.

Most evaluations were generally thorough and consistent with the expectations in licensee procedures; however, the inspectors did identify some CAPEs and RCE evaluations where the quality and depth of the review was less than thorough. Examples included:

  • The CAPE for AR 4479498, 1A RR Pump Failed to Downshift and Tripped to 0 Speed, concluded that the event was caused by loose terminal studs on the high speed to low speed auto transfer relay (i.e., GE HFA relays). Specifically, during maintenance on these relays, there was no action to verify the stud tightness prior to returning to service, resulting in some of the connections either being loose or becoming so over time. As a corrective action, the associated maintenance procedures/work packages for the GE HFA relays were revised to include steps to verify the tightness of the terminal stud connections. The inspectors noted that the extent of condition review for this CAPE did not consider other relays that were susceptible to the same condition. As a result, the licensee subsequently identified other relays that should also have been addressed by similar corrective actions.
  • The CAPE for AR 4407880, Spurious Group 4 Signal Causes VG/VR Actuations, identified that the event was primarily due to a technician not using the appropriate controls (i.e., self-check, questioning attitude), when performing maintenance on the system, resulting in the spurious signal; however, the CAPE also discussed issues with the work planning and coordination as having played a significant role. These work planning issues were not identified as a contributing cause and therefore, no action was assigned to identify and address any organizational learnings.

The licensee captured each of these examples in the CAP and had assigned appropriate corrective actions to address the concern.

The inspectors identified a finding of very low safety significance (Green) and an associated non-cited violation (NCV), for the failure to follow ASME code requirements following the set-pressure testing failure of residual heat removal pump discharge relief valve 1E12-F025C. This issue is discussed in more detail later in the report.

Assessment 71152B Five Year Review of the Core Standby Cooling System (CSCS)

The inspectors performed an expanded 5-year review of the Units 1 and 2 CSCS; specifically, by performing system walkdowns; evaluating condition reports and work orders; and interviewing personnel responsible for working on the system. The inspectors also reviewed a sample of aging management actions associated with the Unit 1 high pressure core spray (HPCS) room cooler piping, including condition reports, piping replacement plans, and work orders. Overall, the inspectors determined that the licensee was effectively managing issues associated with this system.

Assessment 71152B Assessment of Operating Experience and Self-Assessments and Audits Assessment of Operating Experience and Self-Assessment and Audits Based on the samples reviewed, the team determined that licensee performance in the use of Operating Experience (OE) and Self-Assessments and Audits adequately supported nuclear safety.

Use of Operating Experience The licensee routinely screened industry and NRC OE information for station applicability.

Based on these initial screenings, the licensee-initiated actions in the CAP to fully evaluate the impact, if any, to the station. When applicable, actions were developed and implemented in a timely manner to prevent similar issues from occurring. During interviews, licensee staff stated that operating experience lessons-learned were communicated during work briefings and department meetings and incorporated into plant operations.

The inspectors did identify one example of OE that was reviewed by licensee staff and deemed as not applicable to the site but was lacking sufficient documentation to support that conclusion. Specifically, AR 467770, OPEX Review 52007 Vulnerability. The licensee documented this issue in the CAP and reopened the evaluation to add the supporting basis. The inspectors reviewed the additional information and had no further issues.

Although the use of operating experience was seen as valuable, the inspectors identified some instances where it was not properly evaluated as a contributing cause in CAPE or root cause evaluations. Specifically, both the CAPE and root cause guidance procedures stated that OE should be reviewed to determine if there were similar industry events that could provide insights on the issue, including corrective actions, and whether this OE was a missed opportunity for the licensee to have taken prior action to prevent the event. The inspectors identified several examples where the licensee had identified potentially applicable OE but had not fully documented associated learnings from the event, or whether it was a missed opportunity. The inspectors also noted that the licensee had made a similar observation in a prior self-assessment and had identified an adverse trend. This trend was documented in AR 4723092 and the inspectors examples were added to the AR. The inspectors reviewed the AR and noted that the corrective actions, while in-progress, appeared appropriate.

No findings or violations were identified.

Self-Assessments and Audits The inspectors reviewed several audits and self-assessments and deemed those sampled as thorough and intrusive with regards to following up with the issues that were identified.

No findings or violations were identified.

Assessment 71152B Assessment of the Safety-Conscious Work Environment Assessment of Safety-Conscious Work Environment The team reviewed the stations programs to establish and maintain a safety-conscious work environment and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews, workers at the station expressed freedom to raise and enter safety concerns through any one of the various avenues available to them, and the team encountered no indications of a chilled work environment.

Workers expressed favorable opinions of the Employee Concerns Program (ECP) during interviews. While most workers felt no need to engage the ECP, the inspectors noted that there were still several issues documented in the program. Through a selective review, the inspectors concluded that these issues were appropriately handled and identified no adverse trends. The inspectors did note however, that some staff were unaware of where the ECP offices were onsite. This was despite several signs posted throughout the station describing the ECP office location. This was discussed with the ECP coordinator who planned to address this during routine plant department outreach meetings.

Based on the interview results and a review of the ECP issues, the most common issues at the station involved resources and a perception that lower-level CAP issues were not addressed timely. Licensee management was fully aware of these issues, as they had been identified prior in various station self-assessments and audits and in the previous NRC PI&R biennial inspection. The inspectors noted that the licensee had taken action to address these issues. The inspectors also noted that these issues had not had a significant impact on station performance nor had they discouraged licensee staff from raising concerns.

Overall, the inspectors found no evidence of challenges to the licensees safety-conscious work environment, as licensee employees were willing to raise nuclear safety concerns through at least one of several means available.

No violations or findings were identified.

Failure to Comply with ASME Code Requirements Following Test Failure Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green [P.2] - 71152B Systems NCV 05000373,05000374/2023012-01 Evaluation Open/Closed The inspectors identified a finding of very low safety significance (Green) and an associated non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (10 CFR)

Part 50.55a (f)(4)(ii) for the licensees failure to perform inservice tests to verify the operational readiness of valves whose function is required for safety. Specifically, the licensee failed to perform inservice testing on two additional relief valves from valve group R105, following the set-pressure testing failure of 1E12-F025C, and failed to perform the cause-and-effect evaluation of the testing failure.

Description:

The residual heat removal (RHR) pump discharge relief valves (E12-F025A/B/C) at LaSalle station were normally closed valves and had a safety function to open to protect the RHR pump discharge piping in the event of an overpressure condition. The relief valves were set to relieve pressure at 500 psig, as listed in the updated final safety analysis report (UFSAR)

Section 6.3.2.2.12. The valves were also required to close to provide containment isolation for the RHR system.

The licensees American Society of Mechanical Engineers (ASME) Code of Record for Operation and Maintenance of Nuclear Power Plants, (OM) was the 2004 Edition with Addenda though 2006. The licensee categorized the relief valves as Category C valves and tested the relief valves in accordance with Mandatory Appendix 1 of the OM Code.

Mandatory Appendix I Paragraph I-1350(c)(1), required, for each valve tested for which the as-found set-pressure (first test actuation) exceeds the greater of either +/- tolerance limit of the Owner-established set-pressure acceptance criteria of I-1310(e) or +/- 3% of valve nameplate set-pressure, two additional valves shall be tested from the same valve group.

Additionally, Mandatory Appendix I Paragraph I-1350(c)(3) states, in part, the Owner shall evaluate the cause and effect of valves that fail to comply with the set-pressure acceptance criteria established in I-1350(c)(1).

On May 20, 2022, the 1E12-F025C failed to meet the as-found set-pressure testing acceptance criteria under Work Order (WO) 05240622-04, EWP MM Perform Testing of Relief Valve 1E12-F025C. The licensee had replaced the valve with a pre-tested relief valve and entered the issue into the corrective action program (CAP) as AR 4501066, 1E12-F025C WO#5240622-04.

The inspectors reviewed licensee Procedure LMP-GM-06, Bench Testing/Setting of ASME OM Class 2 and 3 Safety Relief Valves, Revision 36, and noted step E.2.3.3 stated, Initiate an Issue Report. Issue Report must specify that an Action Tracking Item be created for a Causal Evaluation of the failed as-found test. The Inspectors requested the casual evaluation of the failed as-found set-pressure test, and requested the WOs which performed the inservice testing of two additional relief valves as a result of the 1E12-F025C testing failure.

In response to the inspectors questions, the licensee determined they had failed to perform inservice testing on two additional relief valves, and had failed to perform the causal evaluation of the testing failure. The licensee determined they had inadequate WO closure documentation for WO 5240622-04 and had failed to determine the additional scope expansion testing requirements under AR 4501066.

Corrective Actions: The licensee entered this issue into their CAP and planned to perform the additional testing during outage L1R20.

Corrective Action References: AR 04720092, PI&R Issue - Missed Relief Valve Tests

Performance Assessment:

Performance Deficiency: The licensees failure to perform inservice tests to verify the operational readiness of relief valves, whose functions are required for safety, was a performance deficiency and contrary to 10 CFR 50.55a (f)(4)(ii). Specifically, the licensee failed to perform inservice testing on two additional relief valves from the R105 valve group, following the set-pressure testing failure of the 1E12-F025C valve, and failed to perform the cause-and-effect evaluation of the testing failure.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, when a relief valve fails as-found set-pressure testing, the licensee is required to test additional relief valves as a means to address any generic issues which could apply to similar valves in the valve group. The licensee failed to perform set-pressure testing on two additional valves within the valve group, and therefore failed to ensure the availability, reliability, and capability of those additional valves to perform their intended safety function.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors determined the finding was of very low safety significance (Green) because although the finding was a deficiency affecting the design or qualification of a mitigating structure, system, or component (SSC), the SSC maintained its operability and PRA functionality.

Cross-Cutting Aspect: P.2 - Evaluation: The organization thoroughly evaluates issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance. Specifically, when the 1E12-F025 set-pressure failure occurred, the organization did not thoroughly evaluate the issue to ensure compliance with all applicable ASME OM Code requirements.

Enforcement:

Violation: Title 10, CFR Part 50, 50.55a (f)(4)(ii) states, in part, Inservice tests to verify operational readiness of pumps and valves, whose function is required for safety, conducted during successive 120-month intervals must comply with the requirements of the latest edition and addenda of the ASME OM Code incorporated by reference in paragraph (a)(1)(iv) of this section 18 months before the start of the 120-month interval.

The licensees ASME Code of Record for Operation and Maintenance of Nuclear Power Plants, is the 2004 Edition with Addenda though 2006.

Paragraph ISTC-5240, Safety and Relief Valves, states, safety and relief valves shall meet the inservice testing requirements of Mandatory Appendix I. Mandatory Appendix I, Paragraph I-1350(c)(1), states, for each valve tested for which the as-found set-pressure (first test actuation) exceeds the greater of either +/- tolerance limit of the Owner-established set-pressure acceptance criteria of I-1310(e) or +/- 3% of valve nameplate set-pressure, two additional valves shall be tested from the same valve group. Additionally, Mandatory Appendix I Paragraph I-1350(c)(3) states, in part, the Owner shall evaluate the cause and effect of valves that fail to comply with the set-pressure acceptance criteria established in I-1350(c)(1).

Contrary to the above, as of December 15, 2023, the licensee failed to perform inservice tests to verify the operational readiness of valves whose function is required for safety, in accordance with the requirements of the 2004 ASME OM Code with Addenda through 2006. Specifically, following the set-pressure testing failure of safety-related relief valve 1E12-F025C, the licensee failed to perform inservice testing on two additional valves from the same (R105) valve group, and failed to evaluate the cause and effect of this valve that failed to comply with the set-pressure acceptance criteria established in I-350(c)(1).

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On December 15, 2023, the inspectors presented the biennial problem identification and resolution inspection results to John Van Fleet, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71152B Corrective Action 1297044 TSP#3 RPS Relay 1C71A-K10C Did Not Deenergize as

Documents Required

24099401 Results of Failure Analysis on RPV Limit Switch

20487 2C71A-K106G Relay Did Not Open During LOS-RP-Q2

4171578 Roll Up IR for RPS TSV Limit Switch Issues

265960 Large Steam Leak Found Downstream of 1G33-F040

4404903 2DG01A Heat Exchanger Tubes Material Degradation

4406519 NRC ID: Failure to Write IR 4406975 Damage in 2B33-F060B Rx Recirculation Flow Control Valve

4407109 Unit 2 Refuel Bridge Mast Issue During Fuel Moves

4407880 Spurious Group 4 Signal Causes VG/VR Actuations 03/10/2021

4407906 MSL Tunnel Temp Exceeds 135 F on U1 03/10/2021

4435863 NOSA-LAS-21-05 NOS Audit of LaSalle CAP

4455617 2A RPS Bearing Replacement 4.0 Critique

4460065 NRC MD 8.3 Revisions - NRC Incident Investigation Program

4468596 RM - U2 Radiochemistry Samples Ind. Presence of Fuel 12/28/2021

Defect

4468963 Level 3 OPEX Review for IRIS# 515757

447352 Level 3 OPEX Review for IRIS 515751

4474379 Level 3 OPEX Review for IRIS 513205

4478972 NOS ID: Parts Control Requires Management Attention

4479498 RM-1A RR Failed to Downshift and Tripped to 0 Speed

4480457 Level 3 OPEX Review for IRIS 513205

4480462 Level 3 OPEX Review for IRIS 518226

4481815 Trend IR 1B HX Partition Plate

4483962 Eval Required to Leave Scaffold in Place (RWCU Scaffolding)

4485486 Level 3 OPEX Review for IRIS# 515457

4487513 1WTO1PB 1B TBCCW Pump Degrading Seal

4487864 NOS ID: Gaps within CAPE 4407880-10 and Associated 03/28/2022

Actions

4496476 Trend - Incorrect IR Significance Level

Inspection Type Designation Description or Title Revision or

Procedure Date

4498422 LPCS Water Leg Pump Leak

4500996-42 Perform Risk Assessment for the Eaton Breakers

4501066 1E12-F025C WO#5240622-04

4507165 NOS ID: Continuing Issues with Parts Control in EMD Shop

22651 B Diesel Fire Pump Coolant Leak

23547 NRC ID: DBAI Design Analysis (EMD) Discrepancy

27147 NRC ID: DBAI Diesel Fuel

27147 NRC ID DBAI: Diesel Fuel Oil Level Calculation Errors

4530043 Shepard Calibrator Unsecured

4541790 Tagouts Self-Assessment Gap #1 12/09/2022

4541799 Tagouts Self-Assessment Gap #2 12/09/2022

4548783 FP SA Review of Completed Fire Protection Permits 01/17/2023

4548974 FP SA TRM 3.7.k 01/18/2023

4549245 FP SA Fire Drill in HRFA 01/19/2023

4549300 FP SA LMS-ZZ-03 01/19/2023

4549302 FP SA 0FP029 Valve Actuator 01/19/2023

4549364 FP SA LES-FP-05 No Dates 01/19/2023

4549541 FP SA LES-FP-05 2-22P-01 01/20/2023

4549546 FP SA LES-FP-05 2-17P-14 01/20/2023

4549548 FP SA 1-22P-06 01/20/2023

4549551 FP SA LES-FP-05 Det Zone 1-20 01/20/2023

4549568 FP SA Fire Drill 23-Q1-01 01/20/2023

4549615 FP SA Fire Brigade Participation 2021 01/20/2023

4551562 1A DG Speed Control Governor Not Responding

4556006 NRC ID: Fire Door Issue

4558566 Level 3 OPEX Review for IRIS# 543717

4559142 2E12-F064B Wont Stay Closed

4559305 U2 Auto Scram 03/04/2023

4564302 Trend in Non-Discretionary Clock Resets 2022 to 2023

4667295 Level 3 OPEX Review for IRIS #546271 04/03/2023

4671310 Site Trend in CAP Products Going Overdue

4674503 LaSalle County SO and EOC EMNET/NARS Phone Failure

4677770 OPEX Review IRIS 525007

Inspection Type Designation Description or Title Revision or

Procedure Date

4678390 2A Diesel B/D Starting Air Motors Inline Oiler Not Working

4679014 ILT 21-1 NRC Preliminary Results

4681955-08 Review of Fleet Events Requiring IRIS Reporting

4684120 Maintenance Trend: MMD Attention to Detail

4689109 2023 LaSalle Safety Culture Assessment

4689109-08 Biennial Fleet Safety Culture Self-Assessment

4689631 Level 3 OPEX Review for IRIS #561354 07/10/2023

4697410 Ops Obj 1 & 2 SA - Simulator UPS 08/19/2023

4697411 Ops Obj 1& 2 SA - Simulator Post-Event Testing 08/19/2023

4697412 Ops Obj 1& 2 SA - EO-I Qualification Book Cues 08/19/2023

4697413 Ops Obj 1 & 2 SA - Objective Alignment 08/19/2023

4697414 Ops Obj 1 & 2 SA - Operator Fundamentals Reference 08/19/2023

4697415 Ops Obj 1 & 2 SA - Objective Implementation 08/19/2023

4697416 Ops Obj 1 & 2 SA - PBIG Development 08/19/2023

4702449 Level 3 OPEX Review for IRIS# 561471 09/14/2023

AR 04192778 2018 WANO AFI ER.2 11/07/2018

AR 04443175 Potential Floatable Material (Snake) Found in U1 RB 08/28/2021

AR 04498641 Eng. Trend - Leadership Behaviors in Department 05/09/2022

Improvement

AR 04500996 0VE02CA Tripped 05/20/2022

AR 04505734 Trend in DC Battery Corrosion Issues 06/15/2022

AR 04513209 L1M24 Critical Path Delay - 35 Hours 07/27/2022

AR 04536886 NRC RIS 2022-22 Op Leakage Inconsistent w/Op Eval Proc 11/14/2022

AR 04549213 Level 3 OPEX Review for IRIS# 543773 01/19/2023

AR 04558586 Potential Trend: L2R19 Failed Welds 03/02/2023

AR 04701066 RM - LOS-RP-SA4 1C71A-K10G Didnt De-Energize as 09/07/2023

Expected

AR 04720620 1HP55A-4" Pipe Section Replacement 11/30/2023

AR 2612886 Scope Add Process Not Implemented Properly 01/15/2016

AR 2618747 LOS-LP-Q1 and A RHR Inoperable is This Necessary? 01/29/2016

AR 2625698 1A RHR Inoperable Due to Low Pressure 02/13/2016

AR 2628070 Indication Identified on 1DG02A-10" 02/18/2016

AR 2628951 Line 1DG05A-4" Was Not Cut in The Correct Location Per EC 02/19/2016

Inspection Type Designation Description or Title Revision or

Procedure Date

AR 2629265 Rejectable Indication in 1DG02A-10" Weld 3 WO 01326732-02 02/20/2016

AR 2632624 Division 2 CSCS Issues 02/27/2016

AR 2693331 LOS-RH-SR1 2B RHR PMP Seal Cooler Flowrate Pre-Test 07/15/2016

Data

AR 2694139 Low Flow Going Through 2B RHR Pump Seal Cooler 07/18/2016

AR 2695103 License Renewal (LR) Inspections for Selective Leaching 07/21/2016

AR 2715787 Pipe Downstream of 2E12-F407A is Degraded 09/14/2016

AR 2716369 Maintenance Rule Unavailability Exceeded for 2-CSCS-DG-06 09/15/2016

AR 2716731 (A)(1) Action Plan Not Completed Per Schedule 09/14/2016

AR 3954418 Troubleshoot Cause of Flow Increase 12/16/2016

AR 3971853 2E12-F386B, Hand Wheel Found Detached Upon Arrival 02/08/2017

AR 3985811 Maintenance Rule (A)(1) Determination for LAS-0-DG-01 03/15/2017

AR 3988392 Engineer Evaluate Trend in DG Cooling Water Flow 03/22/2017

AR 3997974 IR Not Written in a Timely Manner 04/07/2017

AR 3998308 NDE 1VY03A 2.5" Supply Header UT Readings Below Min. 04/14/2017

AR 4024726 NOS ID: Non-Consequential Errors in CSCS Hydraulic Model 06/22/2017

AR 4056244 Level 3 OPEX Review Requested LER 3412017003 Fermi 2 09/27/2017

AR 4098488 Data Points Do Not Support Welding for 2HP55BB Line 01/29/2018

AR 4104349 LAS-2-VY-02 Mrule Hours Criteria Exceeded 02/15/2018

AR 4130434 NOS ID: Active Leak from Drain Line 04/24/2018

AR 4182775 Preconditioning Eval Request for LOS-RH-Q2, ATT. 1A 10/12/2018

AR 4221635 VT-3 Exams Specified on Supports Exempted from 02/19/2019

Examination

AR 4233316 2B DG Coolant Leak 03/27/2019

AR 4236791 CMO Failed to Perform GL 89-13 RHR HX Inspection 04/05/2019

AR 4257023 Existing Cooler Housing Has Sag 06/14/2019

AR 4286478 Isolated pit identified on CSCS discharge pipe 1RH83BA-24" 10/09/2019

AR 4288357 Replace Piping 1DG23B-6" 10/16/2019

AR 4288399 Flooring and Piping Support Degradation in U2 CSCS Pump 10/16/2019

Room

AR 4316736 Visual Exam Results for ISI Component HPCS DG Cooler 1 02/10/2020

AR 4322965 Pipe Wall Leak Immediately Downstream of 1FC045B 03/02/2020

AR 4345863 Extent of condition UT inspection on 2DG23B-6" 05/26/2020

Inspection Type Designation Description or Title Revision or

Procedure Date

AR 4379968 Localized Corrosion Spots Identified on 1HP54A Piping 10/27/2020

AR 4382738 Extent of Condition UT Inspection on 1HP54A-4" 11/06/2020

AR 4401929 2A RHR Pump Seal Cooler Flow Low 02/12/2021

AR 4404903 2DG01A Heat Exchanger Tubes Material Degradation 02/26/2021

AR 4410959 NOS ID Final Weld not Inspected in WO 4677538-29 03/23/2021

AR 4444012 UT inspection on 1RH83BB-24" 09/01/2021

AR 4477278 NOS ID: Insulation on Valve 2FC045A Crushed 02/10/2022

AR 4477292 NOS ID: Pipe Support Severely Corroded, Actions Untimely 02/10/2022

AR 4503287 Level 3 OPEX Review for IRIS# 459111 06/01/2022

AR 4505723 Level 3 OPEX Review for IRIS# 493320 and 500237 06/15/2022

AR 4511506 Level 3 OPEX Review for IRIS# 529028 07/18/2022

AR 4520825 Snake in U1 RB Lower Raceway 09/06/2022

AR 4538390 LOS-DG-SR7 Acceptance Criteria Not Met 11/21/2022

AR 4549215 Level 3 OPEX Review for IRIS# 541158 01/19/2023

AR 4549219 Level 3 OPEX Review for IRIS# 542416 01/19/2023

AR UT inspection UT Inspection Results on 1HP52A-10" 10/28/2020

results on

1HP52A-10"

Corrective Action 4233263 PI&R Identified Issue - Gaps Identified with RCR 4406976

Documents 4720087 PI&R Issue - IR 4468596 Incorrect Significance Level

Resulting from 4720092 PI&R Issue - Missed Relief Valve Tests

Inspection 4720279 PI&R Issue - Legacy Effectiveness Reviews Not Assigned

21459 PI&R Issue - NRC PI&R Identified LVL 3 OPX Issue

22116 PI&R Issue - NRC PI&R Question Regarding

CAPE 4479498-07

22154 PI&R Issue - Revise Policy Guidance 139 for Quorum

23257 PI&R Identified Issue - Clarify CA from CAPE 4011747

23263 PI&R Identified Issue - Gaps Identified with RCR 4406976 12/13/2023

23313 PI&R Identified Issues - IR How Discovered Incorrectly Coded

23516 PI&R Inspection Issue - Cause from CAPE not Addressed 12/14/2023

by CA

23611 PI&R Inspection Identified - HPCS Degraded Piping 12/14/2023

24263 PI&R - NRC Ops Review Lists No Operability Concerns

Inspection Type Designation Description or Title Revision or

Procedure Date

Engineering 633646 Lost Parts Evaluation L2R18 002

Changes 637157 Line Kill for RT Heat Exchanger Vent Leaks

EC 624352 2VY03A Cooler Tubing Inlet Riser Repair Evaluation 05/23/2018

TCC 634296 TCCP Temp Setpoint Change for 2B RHR WS Strainer

DPS 2E12-N501 From 4 psid to 6 psid

Miscellaneous LaSalle Nuclear Safety Culture Review Meeting Minutes 10/9/2023

IST-LAS-BDOC- LaSalle County Generating Station - Inservice Testing Basis 03/01/2019

V-26 Document - 1E12-F025C

TP22-2-028 BWROG Reactivity Controls Review Committee (RCRC) 0

Guidelines for Excellence

NDE Reports Technical Report Long Range Guided Wave Ultrasonic Pipe Screening Results 07/05/2022

AH1543-

41060080

Technical Report Long Range Guided Wave Ultrasonic Pipe Screening Results 07/05/2022

AH1548-

41076266

Technical Report Long Range Guided Wave Ultrasonic Pipe Screening Results 09/29/2011

AM1261-343593,

AM1295-344407

Technical Report Long Range Guided Wave Ultrasonic Pipe Screening Results 11/21/2012

AM3116-430677

Technical Report Long Range Guided Wave Ultrasonic Pipe Screening Results 11/20/2013

AM4103-535476

Technical Report Long Range Guided Wave Ultrasonic Pipe Screening Results 01/13/2014

AM4103-535476R

Procedures EI-AA-1 Safety Conscious Work Environment Revision 4

LEP-HC-103 Refuel Bridge Preventative Maintenance Revision 18

LGA-002 Secondary Containment Control 11

LOS-NB-R2 Reactor Vessel Leakage Test 26

LOS-RD-SR3 Control Rod Operations 27

OP-AA-108-115 Operability Determinations Revision 27

OP-AA-300-1540 Reactivity Management Administration 21

PI-AA-115 Operating Experience Program Revision 6

PI-AA-125-1001 Root Cause Analysis Manual Revision 7

Inspection Type Designation Description or Title Revision or

Procedure Date

PI-AA-125-1003 Corrective Action Program Evaluation Manual

PI-AA-125-1004 Effectiveness Review Manual Revision 2

Self-Assessments NOSA-LAS-22-01 Maintenance Functional Area Audit Report 02/23/2033

Work Orders 1741625-03 EM EWP Special Test 2C71-K4B1 Agastat Relay MR-90 03/09/2021

5166843-01 RXS - Perform Foreign Material Inspection of Jet Pumps 02/17/2023

5168984-03 RXS - Inspect & Clean Unit 2 Bottom Head Drain 02/27/2023

256192-01 RXS Perform Ultrasonic Fuel Cleaning in L2R19 02/23/2023

16