IR 05000424/2015008: Difference between revisions

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| issue date = 05/07/2015
| issue date = 05/07/2015
| title = IR 05000424/2015-008 and 05000425/2015-008, Vogtle, Units 1 and 2  NRC Problem Identification and Resolution Inspection Report
| title = IR 05000424/2015-008 and 05000425/2015-008, Vogtle, Units 1 and 2  NRC Problem Identification and Resolution Inspection Report
| author name = Masters A D
| author name = Masters A
| author affiliation = NRC/RGN-II/DRP/RPB7
| author affiliation = NRC/RGN-II/DRP/RPB7
| addressee name = Taber B K
| addressee name = Taber B
| addressee affiliation = Southern Nuclear Operating Co, Inc
| addressee affiliation = Southern Nuclear Operating Co, Inc
| docket = 05000424, 05000425
| docket = 05000424, 05000425
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=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:UNITED STATES May 7, 2015
[[Issue date::May 7, 2015]]


Mr. Brian Vice President - Vogtle Southern Nuclear Operating Company, Inc.
==SUBJECT:==
 
VOGTLE ELECTRIC GENERATING PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000424/2015008 AND 05000425/2015008
Vogtle Electric Generating Plant 7821 River Road Waynesboro, GA 30830
 
SUBJECT: VOGTLE ELECTRIC GENERATING PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000424/2015008 AND 05000425/2015008


==Dear Mr. Taber:==
==Dear Mr. Taber:==
On April 2, 2015, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your Vogtle Electric Generating Plant Units 1 and 2. The enclosed report documents the inspection findings, which were discussed on April 2, 2015, with Mr. G. Saxon and other members of your staff.
On April 2, 2015, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your Vogtle Electric Generating Plant Units 1 and 2. The enclosed report documents the inspection findings, which were discussed on April 2, 2015, with Mr. G. Saxon and other members of your staff.


On the basis of the samples selected for review, the inspectors concluded that, in general, problems were properly identified, evaluated, and corrected. In reviewing your corrective action program, the inspectors assessed how well your staff identified problems at a low threshold, your staff's implementation of the station's process for prioritizing and evaluating these problems, and the effectiveness of corrective actions taken by the station to resolve these problems. In each of these areas, the inspectors determined that your staff's performance was adequate to support nuclear safety.
On the basis of the samples selected for review, the inspectors concluded that, in general, problems were properly identified, evaluated, and corrected. In reviewing your corrective action program, the inspectors assessed how well your staff identified problems at a low threshold, your staffs implementation of the stations process for prioritizing and evaluating these problems, and the effectiveness of corrective actions taken by the station to resolve these problems. In each of these areas, the inspectors determined that your staffs performance was adequate to support nuclear safety.


The inspectors also evaluated other processes your staff used to identify issues for resolution.
The inspectors also evaluated other processes your staff used to identify issues for resolution.


These included your use of audits and self-assessments to identify latent problems and your incorporation of lessons learned from industry operating experience into station programs, processes, and procedures. The inspectors determined that your station's performance in each of these areas supported nuclear safety.
These included your use of audits and self-assessments to identify latent problems and your incorporation of lessons learned from industry operating experience into station programs, processes, and procedures. The inspectors determined that your stations performance in each of these areas supported nuclear safety.


Finally, the inspectors determined that your station's management maintains a safety-conscious work environment adequate to support nuclear safety. Based on the inspectors' observations, your employees are willing to raise concerns related to nuclear safety through at least one of the several means available. In accordance with 10 CFR 2.390 of the NRC's "Agency Rules of Practice and Procedure," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). Adams is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Finally, the inspectors determined that your stations management maintains a safety-conscious work environment adequate to support nuclear safety. Based on the inspectors observations, your employees are willing to raise concerns related to nuclear safety through at least one of the several means available. In accordance with 10 CFR 2.390 of the NRCs Agency Rules of Practice and Procedure, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). Adams is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA By Reinaldo Rodriguez For/ Anthony D. Masters, Chief Reactor Projects Branch 7 Division of Reactor Projects Docket Nos. 50-424, 50-425 License Nos. NPF-68, NPF-81  
Sincerely,
/RA By Reinaldo Rodriguez For/
Anthony D. Masters, Chief Reactor Projects Branch 7 Division of Reactor Projects Docket Nos. 50-424, 50-425 License Nos. NPF-68, NPF-81


===Enclosure:===
===Enclosure:===
IR 05000424/2015008, 05000425/2015008  
IR 05000424/2015008, 05000425/2015008 w/Attachment: Supplementary Information


===w/Attachment:===
REGION II==
Supplementary Information cc Distribution via ListServ
Docket Nos.: 50-424, 50-425 License Nos.: NPF-68, NPF-81 Report Nos.: 05000424/2015008 and 05000425/2015008 Licensee: Southern Nuclear Operating Company, Inc. (SNC)
Facility: Vogtle Electric Generating Plant, Units 1 and 2 Location: Waynesboro, GA 30830 Dates: March 16 - April 2, 2015 Inspectors: Wesley Deschaine, Resident Inspector Sequoyah (Team Leader)
Shani Lewis, Project Engineer Natasha Childs, Resident Inspector Oconee Ryan Taylor, Senior Project Inspector Approved by: Anthony D. Masters, Chief Reactor Projects Branch 7 Division of Reactor Projects Enclosure


=SUMMARY=
=SUMMARY=
IR 05000424/2015008 and 05000425/2015008; March 16 - April 2, 2015; Vogtle Electric Generating Plant, Units 1 and 2; Biennial Inspection of the Problem Identification and Resolution
IR 05000424/2015008 and 05000425/2015008; March 16 - April 2, 2015; Vogtle Electric


Program.
Generating Plant, Units 1 and 2; Biennial Inspection of the Problem Identification and Resolution Program.


The inspection was conducted by two resident inspectors, a senior project inspector, and a project engineer. No findings were identified. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 5.
The inspection was conducted by two resident inspectors, a senior project inspector, and a project engineer. No findings were identified. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 5.


Identification and Resolution of Problems The inspectors concluded that, in general, problems were properly identified, evaluated, prioritized, and corrected. The licensee was effective at identifying problems and entering them into the corrective action program (CAP) for resolution, as evidenced by the relatively few number of deficiencies identified by external organizations (including the NRC) that had not been previously identified by the licensee, during the review period. Generally, prioritization and evaluation of issues were adequate, formal root cause evaluations for significant problems were adequate, and corrective actions specified for problems were acceptable. Overall, corrective actions developed and implemented for issues were generally effective and implemented in a timely manner.
Identification and Resolution of Problems The inspectors concluded that, in general, problems were properly identified, evaluated, prioritized, and corrected. The licensee was effective at identifying problems and entering them into the corrective action program (CAP) for resolution, as evidenced by the relatively few number of deficiencies identified by external organizations (including the NRC) that had not been previously identified by the licensee, during the review period. Generally, prioritization and evaluation of issues were adequate, formal root cause evaluations for significant problems were adequate, and corrective actions specified for problems were acceptable. Overall, corrective actions developed and implemented for issues were generally effective and implemented in a timely manner.


The inspectors determined that overall, audits and self-assessments were adequate in identifying deficiencies and areas for improvement in the CAP, and appropriate corrective actions were developed to address the issues identified. Operating experience usage was found to be generally acceptable and integrated into the licensee's processes for performing and managing work and plant operations.
The inspectors determined that overall, audits and self-assessments were adequate in identifying deficiencies and areas for improvement in the CAP, and appropriate corrective actions were developed to address the issues identified. Operating experience usage was found to be generally acceptable and integrated into the licensees processes for performing and managing work and plant operations.


Based on discussions and interviews conducted with plant employees from various departments, the inspectors determined that personnel at the site felt free to raise safety concerns to management and use the CAP to resolve those concerns.
Based on discussions and interviews conducted with plant employees from various departments, the inspectors determined that personnel at the site felt free to raise safety concerns to management and use the CAP to resolve those concerns.
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's CAP procedures which described the administrative process for initiating and resolving problems primarily through the use of condition reports (CRs). To verify that problems were being properly identified, appropriately characterized, and entered into the CAP, the inspectors reviewed CRs that had been issued between February 2013 and February 2015, including a detailed review of selected CRs associated with the following risk-significant systems: Emergency Diesel Generators (EDGs), Nuclear Service Cooling Water (NSCW), 125VDC Electrical, and 4160V Electrical systems. Where possible, the inspectors independently verified that the corrective actions were implemented as intended. The inspectors also reviewed selected common causes and generic concerns associated with root cause evaluations (RCE) to determine if they had been appropriately addressed. To help ensure that samples were reviewed across all cornerstones of safety identified in the Reactor Oversight Process (ROP), the inspectors selected a representative number of CRs that were identified and assigned to the major plant departments, including operations, maintenance, engineering, health physics, chemistry, emergency preparedness, and security. These CRs were reviewed to assess each department's threshold for identifying and documenting plant problems, thoroughness of evaluations, and adequacy of corrective actions. The inspectors reviewed selected CRs, verified corrective actions were implemented, and attended meetings where CRs were evaluated for significance to determine whether the licensee was identifying, accurately characterizing, and entering problems into the CAP at an appropriate threshold. Plant walkdowns of equipment within the selected systems listed above and other plant areas were conducted by inspectors to assess the material condition and to identify deficiencies that had not been previously entered into the CAP. The inspectors reviewed CRs, maintenance history, corrective actions (CAs), completed work orders (WOs) for the systems, and reviewed associated system health reports. These reviews were performed to verify that problems were being properly identified, appropriately characterized, and entered into the CAP. Items reviewed generally covered a two-year period of time; however, in accordance with the inspection procedure, a five-year review was performed for selected systems for age-related issues. Control Room walk-downs were also performed to assess the main control room (MCR) deficiency list and to ascertain if deficiencies were entered into the CAP and tracked to resolution. Operator workarounds (OWA) and operator burden screenings were reviewed, and the inspectors verified compensatory measures for deficient equipment which were being implemented in the field.
The inspectors reviewed the licensees CAP procedures which described the administrative process for initiating and resolving problems primarily through the use of condition reports (CRs). To verify that problems were being properly identified, appropriately characterized, and entered into the CAP, the inspectors reviewed CRs that had been issued between February 2013 and February 2015, including a detailed review of selected CRs associated with the following risk-significant systems: Emergency Diesel Generators (EDGs), Nuclear Service Cooling Water (NSCW), 125VDC Electrical, and 4160V Electrical systems. Where possible, the inspectors independently verified that the corrective actions were implemented as intended. The inspectors also reviewed selected common causes and generic concerns associated with root cause evaluations (RCE) to determine if they had been appropriately addressed. To help ensure that samples were reviewed across all cornerstones of safety identified in the Reactor Oversight Process (ROP), the inspectors selected a representative number of CRs that were identified and assigned to the major plant departments, including operations, maintenance, engineering, health physics, chemistry, emergency preparedness, and security. These CRs were reviewed to assess each departments threshold for identifying and documenting plant problems, thoroughness of evaluations, and adequacy of corrective actions. The inspectors reviewed selected CRs, verified corrective actions were implemented, and attended meetings where CRs were evaluated for significance to determine whether the licensee was identifying, accurately characterizing, and entering problems into the CAP at an appropriate threshold.
 
Plant walkdowns of equipment within the selected systems listed above and other plant areas were conducted by inspectors to assess the material condition and to identify deficiencies that had not been previously entered into the CAP. The inspectors reviewed CRs, maintenance history, corrective actions (CAs), completed work orders (WOs) for the systems, and reviewed associated system health reports. These reviews were performed to verify that problems were being properly identified, appropriately characterized, and entered into the CAP. Items reviewed generally covered a two-year period of time; however, in accordance with the inspection procedure, a five-year review was performed for selected systems for age-related issues.
 
Control Room walk-downs were also performed to assess the main control room (MCR)deficiency list and to ascertain if deficiencies were entered into the CAP and tracked to resolution. Operator workarounds (OWA) and operator burden screenings were reviewed, and the inspectors verified compensatory measures for deficient equipment which were being implemented in the field.


The inspectors conducted a detailed review of selected CRs to assess the adequacy of the root cause and apparent cause evaluations of the problems identified. The inspectors reviewed these evaluations against the descriptions of the problem described in the CRs and the guidance in licensee procedure NMP-GM-002-GL03, "Cause Analysis and Corrective Actions Guideline.The inspectors assessed if the licensee had adequately determined the cause(s) of identified problems, and had adequately addressed operability, reportability, common cause, generic concerns, extent-of-condition, and extent-of-cause. The review also assessed if the licensee had appropriately identified and prioritized corrective actions to prevent recurrence.
The inspectors conducted a detailed review of selected CRs to assess the adequacy of the root cause and apparent cause evaluations of the problems identified. The inspectors reviewed these evaluations against the descriptions of the problem described in the CRs and the guidance in licensee procedure NMP-GM-002-GL03, Cause Analysis and Corrective Actions Guideline. The inspectors assessed if the licensee had adequately determined the cause(s) of identified problems, and had adequately addressed operability, reportability, common cause, generic concerns, extent-of-condition, and extent-of-cause. The review also assessed if the licensee had appropriately identified and prioritized corrective actions to prevent recurrence.


The inspectors reviewed selected industry operating experience (OE) items, including NRC generic communications, to verify that they had been appropriately evaluated for applicability and that issues identified through these reviews had been entered into the CAP.
The inspectors reviewed selected industry operating experience (OE) items, including NRC generic communications, to verify that they had been appropriately evaluated for applicability and that issues identified through these reviews had been entered into the CAP.
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The inspectors reviewed site trend reports, to determine if the licensee effectively trended identified issues and initiated appropriate corrective actions when adverse trends were identified.
The inspectors reviewed site trend reports, to determine if the licensee effectively trended identified issues and initiated appropriate corrective actions when adverse trends were identified.


The inspectors reviewed licensee audits and self-assessments, including those which focused on problem identification and resolution programs and processes, to verify that findings were entered into the CAP and to verify that these audits and assessments were consistent with the NRC's assessment of the licensee's CAP.
The inspectors reviewed licensee audits and self-assessments, including those which focused on problem identification and resolution programs and processes, to verify that findings were entered into the CAP and to verify that these audits and assessments were consistent with the NRCs assessment of the licensees CAP.


The inspectors attended various plant meetings to observe management oversight functions of the corrective action process. These included CR screening meetings and Management Review Committee (MRC) meetings.
The inspectors attended various plant meetings to observe management oversight functions of the corrective action process. These included CR screening meetings and Management Review Committee (MRC) meetings.
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Documents reviewed are listed in the Attachment.
Documents reviewed are listed in the Attachment.


b. Assessment Problem Identification The inspectors determined that the licensee was generally effective in identifying problems and entering them into the CAP and there was an appropriately low threshold for entering issues into the CAP. This conclusion was based on a review of the requirements for initiating CRs as described in licensee procedure NMP-GM-002-001, "Corrective Action Program Instructions," management's expectation that employees were encouraged to initiate CRs for any reason. Trending was generally effective in monitoring equipment performance. Site management was actively involved in the CAP and focused appropriate attention on significant plant issues. Based on reviews and walkdowns of accessible portions of the selected systems, the inspectors determined that system deficiencies were being identified and placed in the CAP.
b. Assessment Problem Identification The inspectors determined that the licensee was generally effective in identifying problems and entering them into the CAP and there was an appropriately low threshold for entering issues into the CAP. This conclusion was based on a review of the requirements for initiating CRs as described in licensee procedure NMP-GM-002-001, Corrective Action Program Instructions, managements expectation that employees were encouraged to initiate CRs for any reason. Trending was generally effective in monitoring equipment performance. Site management was actively involved in the CAP and focused appropriate attention on significant plant issues. Based on reviews and walkdowns of accessible portions of the selected systems, the inspectors determined that system deficiencies were being identified and placed in the CAP.


A performance deficiency was identified during the inspection associated with the site's failure to identify and correct the condition adverse to quality discovered during the failure analysis for the 2B EDG bridge transfer switch. Specifically, the failure analysis report concluded that the bridge transfer switch failed due to hardened and degraded grease not being properly removed during preventative maintenance (PM). The report also concludes that the PM procedure may be inadequate to remove the older grease and should be updated to mitigate future failures. The site has entered this issue into the CAP as CRs 10041480 and 10043156. However, because this performance deficiency did not adversely affect any ROP cornerstone objectives, the inspectors determined the issue was of minor significance and not subject to enforcement action in accordance with the NRC's Enforcement Policy.
A performance deficiency was identified during the inspection associated with the sites failure to identify and correct the condition adverse to quality discovered during the failure analysis for the 2B EDG bridge transfer switch. Specifically, the failure analysis report concluded that the bridge transfer switch failed due to hardened and degraded grease not being properly removed during preventative maintenance (PM). The report also concludes that the PM procedure may be inadequate to remove the older grease and should be updated to mitigate future failures. The site has entered this issue into the CAP as CRs 10041480 and 10043156. However, because this performance deficiency did not adversely affect any ROP cornerstone objectives, the inspectors determined the issue was of minor significance and not subject to enforcement action in accordance with the NRCs Enforcement Policy.


Problem Prioritization and Evaluation Based on the review of CRs sampled by the inspection team during the onsite period, the inspectors concluded that problems were generally prioritized and evaluated in accordance with the licensee's CAP procedures as described in the CR severity level determination guidance in NMP-GM-002-001. Each CR was assigned a priority level at the CAP coordinator (CAPCO) meeting, and adequate consideration was given to system or component operability and associated plant risk.
Problem Prioritization and Evaluation Based on the review of CRs sampled by the inspection team during the onsite period, the inspectors concluded that problems were generally prioritized and evaluated in accordance with the licensees CAP procedures as described in the CR severity level determination guidance in NMP-GM-002-001. Each CR was assigned a priority level at the CAP coordinator (CAPCO) meeting, and adequate consideration was given to system or component operability and associated plant risk.


The inspectors determined that station personnel had conducted root cause and apparent cause analyses in compliance with the licensee's CAP procedures and assigned cause determinations were appropriate, considering the significance of the issues being evaluated. A variety of formal causal-analysis techniques were used depending on the type and complexity of the issue consistent with NMP-GM-002-GL03.
The inspectors determined that station personnel had conducted root cause and apparent cause analyses in compliance with the licensees CAP procedures and assigned cause determinations were appropriate, considering the significance of the issues being evaluated. A variety of formal causal-analysis techniques were used depending on the type and complexity of the issue consistent with NMP-GM-002-GL03.


The inspectors identified three performance deficiencies associated with the licensee's prioritization and evaluation of issues. These issues were screened in accordance with Manual Chapter 0612, "Issue Screening," and were determined to be of minor significance and not subject to enforcement action in accordance with the NRC's Enforcement Policy.
The inspectors identified three performance deficiencies associated with the licensees prioritization and evaluation of issues. These issues were screened in accordance with Manual Chapter 0612, Issue Screening, and were determined to be of minor significance and not subject to enforcement action in accordance with the NRCs Enforcement Policy.
* The inspectors reviewed Corrective Action Report (CAR) 210971 associated with a NRC non-cited violation (NCV), and identified the following issues with the Apparent Cause Determination (ACD): o Technical Evaluation (TE) 860480 was a corrective action for Operations training to perform a Gap Analysis to address potential knowledge gaps identified by the apparent cause team. This action was one of several actions to resolve apparent cause #1 (AC1) and contributing cause #1 (CC1) of the ACD. The priority level of TE 860480 was downgraded from a level 2 to level 3 without following the process as outlined in section 4.6 of NMP-GM-002-001. Additionally, the apparent cause analysts did not follow the process outlined in NMP-GM-002-GL03 when initially assigning the corrective action. The licensee has entered these issues into the CAP as CRs 10047594 and 10047596.
* The inspectors reviewed Corrective Action Report (CAR) 210971 associated with a NRC non-cited violation (NCV), and identified the following issues with the Apparent Cause Determination (ACD):
o Technical Evaluation (TE) 860480 was a corrective action for Operations training to perform a Gap Analysis to address potential knowledge gaps identified by the apparent cause team. This action was one of several actions to resolve apparent cause #1 (AC1) and contributing cause #1 (CC1) of the ACD. The priority level of TE 860480 was downgraded from a level 2 to level 3 without following the process as outlined in section 4.6 of NMP-GM-002-001. Additionally, the apparent cause analysts did not follow the process outlined in NMP-GM-002-GL03 when initially assigning the corrective action. The licensee has entered these issues into the CAP as CRs 10047594 and 10047596.


o TE 853634 was a corrective action for the Chemistry department to perform a department stand down to discuss upcoming procedure changes as a result of the event. The action was one of several actions to resolve AC1 and CC1 of the ACD. The action due date was extended without following NMP-GM-002-001.
o   TE 853634 was a corrective action for the Chemistry department to perform a department stand down to discuss upcoming procedure changes as a result of the event. The action was one of several actions to resolve AC1 and CC1 of the ACD. The action due date was extended without following NMP-GM-002-001.


There was no assessment of the potential impact of the extension and the appropriate level of management approval was not received. The licensee has entered this issue into the CAP as CR 100475594.
There was no assessment of the potential impact of the extension and the appropriate level of management approval was not received. The licensee has entered this issue into the CAP as CR 100475594.
* The inspectors reviewed CAR 211142 associated with an NRC NCV and identified the following issue with the Apparent Cause Determination: o The ACD report listed seven corrective actions to address AC1; none of the seven actions were assigned a priority level 2, which is not in accordance with NMP-GM-002-001. This procedure states that corrective actions assigned to address an apparent cause should be assigned a level 2 priority. The potential weakness in assigning the incorrect priority level is that the action could potentially be revised and/or receive due date extensions without receiving the appropriate levels of review appropriate for the significance. The licensee has entered this issue into the CAP as CR 10049368.
* The inspectors reviewed CAR 211142 associated with an NRC NCV and identified the following issue with the Apparent Cause Determination:
o The ACD report listed seven corrective actions to address AC1; none of the seven actions were assigned a priority level 2, which is not in accordance with NMP-GM-002-001. This procedure states that corrective actions assigned to address an apparent cause should be assigned a level 2 priority. The potential weakness in assigning the incorrect priority level is that the action could potentially be revised and/or receive due date extensions without receiving the appropriate levels of review appropriate for the significance. The licensee has entered this issue into the CAP as CR 10049368.


Corrective Actions Based on a review of corrective action documents, interviews with licensee staff, and verification of completed corrective actions, the inspectors determined that overall, corrective actions were timely, commensurate with the safety significance of the issues, and effective, in that conditions adverse to quality were corrected and non-recurring. For significant conditions adverse to quality, the corrective actions directly addressed the cause and effectively prevented recurrence in that a review of performance indicators, CRs, and effectiveness reviews demonstrated that the significant conditions adverse to quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence (CAPRs) were sufficient to ensure corrective actions were properly implemented and were effective.
Corrective Actions Based on a review of corrective action documents, interviews with licensee staff, and verification of completed corrective actions, the inspectors determined that overall, corrective actions were timely, commensurate with the safety significance of the issues, and effective, in that conditions adverse to quality were corrected and non-recurring. For significant conditions adverse to quality, the corrective actions directly addressed the cause and effectively prevented recurrence in that a review of performance indicators, CRs, and effectiveness reviews demonstrated that the significant conditions adverse to quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence (CAPRs) were sufficient to ensure corrective actions were properly implemented and were effective.
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No findings were identified.
No findings were identified.


2. Use of Operating Experience
===2. Use of Operating Experience===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors examined the licensee's use of industry OE to assess the effectiveness of how external and internal operating experience information was used to prevent similar or recurring problems at the plant. In addition, the inspectors selected operating experience documents (e.g., NRC generic communications, 10 CFR Part 21 reports, licensee event reports, vendor notifications, and plant internal operating experience items, etc.), which had been issued since February 2013, to verify whether the licensee had appropriately evaluated each notification for applicability to the Vogtle Electric Generating Plant, Units 1 and 2, and whether issues identified through these reviews were entered into the CAP.
The inspectors examined the licensees use of industry OE to assess the effectiveness of how external and internal operating experience information was used to prevent similar or recurring problems at the plant. In addition, the inspectors selected operating experience documents (e.g., NRC generic communications, 10 CFR Part 21 reports, licensee event reports, vendor notifications, and plant internal operating experience items, etc.), which had been issued since February 2013, to verify whether the licensee had appropriately evaluated each notification for applicability to the Vogtle Electric Generating Plant, Units 1 and 2, and whether issues identified through these reviews were entered into the CAP.


b. Assessment Based on a review of selected documentation related to operating experience issues, the inspectors determined that the licensee was generally effective in screening operating experience for applicability to the plant. Industry OE was evaluated at either the corporate or plant level depending on the source and type of the document. Relevant information was then forwarded to the applicable department for further action or informational purposes. OE issues requiring action were entered into the CAP for tracking and closure. In addition, operating experience was included in all apparent cause and root cause evaluations in accordance with licensee procedure NMP-GM-002-GL03.
b. Assessment Based on a review of selected documentation related to operating experience issues, the inspectors determined that the licensee was generally effective in screening operating experience for applicability to the plant. Industry OE was evaluated at either the corporate or plant level depending on the source and type of the document. Relevant information was then forwarded to the applicable department for further action or informational purposes. OE issues requiring action were entered into the CAP for tracking and closure. In addition, operating experience was included in all apparent cause and root cause evaluations in accordance with licensee procedure NMP-GM-002-GL03.
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No findings were identified.
No findings were identified.


3. Self-Assessments and Audits
===3. Self-Assessments and Audits===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed audit reports and self-assessment reports, including those which focused on problem identification and resolution, to assess the thoroughness and self-criticism of the licensee's audits and self-assessments, and to verify that problems identified through those activities were appropriately prioritized and entered into the CAP for resolution in accordance with licensee procedure NMP-GM-003, "Self-Assessment and Benchmark Procedure."
The inspectors reviewed audit reports and self-assessment reports, including those which focused on problem identification and resolution, to assess the thoroughness and self-criticism of the licensee's audits and self-assessments, and to verify that problems identified through those activities were appropriately prioritized and entered into the CAP for resolution in accordance with licensee procedure NMP-GM-003, Self-Assessment and Benchmark Procedure.


b. Assessment The inspectors determined that the scopes of assessments and audits were adequate. Self-assessments were generally detailed and critical, as evidenced by findings consistent with the inspector's independent review. The inspectors verified that CRs were created to document areas for improvement and findings resulting from the self-assessments, and verified that actions had been completed consistent with those recommendations. Generally, the licensee performed evaluations that were technically accurate.
b. Assessment The inspectors determined that the scopes of assessments and audits were adequate.
 
Self-assessments were generally detailed and critical, as evidenced by findings consistent with the inspectors independent review. The inspectors verified that CRs were created to document areas for improvement and findings resulting from the self-assessments, and verified that actions had been completed consistent with those recommendations. Generally, the licensee performed evaluations that were technically accurate.


====c. Findings====
====c. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
During the course of the inspection, the inspectors assessed the station's safety-conscious work environment (SCWE) through review of the stations Employee Concerns Program (ECP) and interviews with various departmental personnel. The inspectors reviewed a sample of ECP issues to verify that concerns were being properly reviewed and identified deficiencies were being resolved and entered into the CAP when appropriate.
During the course of the inspection, the inspectors assessed the stations safety-conscious work environment (SCWE) through review of the stations Employee Concerns Program (ECP) and interviews with various departmental personnel. The inspectors reviewed a sample of ECP issues to verify that concerns were being properly reviewed and identified deficiencies were being resolved and entered into the CAP when appropriate.


b. Assessment Based on the interviews conducted and the CRs reviewed, the inspectors determined that licensee management emphasized the need for all employees to identify and report problems using the appropriate methods established within the administrative programs, including the CAP and ECP. These methods were readily accessible to all employees.
b. Assessment Based on the interviews conducted and the CRs reviewed, the inspectors determined that licensee management emphasized the need for all employees to identify and report problems using the appropriate methods established within the administrative programs, including the CAP and ECP. These methods were readily accessible to all employees.


Based on discussions conducted with a sample of plant employees from various departments, the inspectors determined that employees felt free to raise issues, and that management encouraged employees to place issues into the CAP for resolution. The inspectors did not identify any reluctance on the part of the licensee staff to report safety concerns.
Based on discussions conducted with a sample of plant employees from various departments, the inspectors determined that employees felt free to raise issues, and that management encouraged employees to place issues into the CAP for resolution. The inspectors did not identify any reluctance on the part of the licensee staff to report safety concerns.
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====c. Findings====
====c. Findings====
No findings were identified.
No findings were identified.
 
{{a|4OA6}}
{{a|4OA6}}
==4OA6 Exit==
==4OA6 Exit==


=====Exit Meeting Summary=====
===Exit Meeting Summary===


On April 2, 2015, the inspectors presented the inspection results to Mr. G. Saxon and other members of the site staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection.
On April 2, 2015, the inspectors presented the inspection results to Mr. G. Saxon and other members of the site staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection.


ATTACHMENT:
ATTACHMENT:  


=SUPPLEMENTARY INFORMATION=
=SUPPLEMENTARY INFORMATION=
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===Licensee personnel===
===Licensee personnel===
:  
:
: [[contact::G. Saxon]], Plant Manager  
: [[contact::G. Saxon]], Plant Manager
: [[contact::G. Gunn]], Regulatory Affairs Manager  
: [[contact::G. Gunn]], Regulatory Affairs Manager
: [[contact::J. Wade]], Site Design Engineering Manager  
: [[contact::J. Wade]], Site Design Engineering Manager
: [[contact::K. Morrow]], Licensing Engineer  
: [[contact::K. Morrow]], Licensing Engineer
: [[contact::K. Walden]], Licensing Engineer  
: [[contact::K. Walden]], Licensing Engineer
: [[contact::M. Carstensen]], Engineer  
: [[contact::M. Carstensen]], Engineer
: [[contact::M. Cline]], Site CAPCO  
: [[contact::M. Cline]], Site CAPCO
: [[contact::N. Koteel]], Fleet PI Manager  
: [[contact::N. Koteel]], Fleet PI Manager
: [[contact::T. Thompson]], Site System Engineering Manager  
: [[contact::T. Thompson]], Site System Engineering Manager
: [[contact::T. Simmons]], PI Manager  
: [[contact::T. Simmons]], PI Manager
: [[contact::T. Moorer]], Director EHS  
: [[contact::T. Moorer]], Director EHS
===NRC personnel===
:
: [[contact::A. Alen]], Resident Inspector
: [[contact::M. Cain]], Senior Resident Inspector


===NRC personnel===
:
: [[contact::A. Alen]], Resident Inspector
: [[contact::M. Cain]], Senior Resident Inspector 
==LIST OF REPORT ITEMS==
==LIST OF REPORT ITEMS==


===Opened and Closed===
===Opened and Closed===
None
 
None


===Closed===
===Closed===
: None
 
None
 
===Discussed===
===Discussed===


None
None


==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
===Procedures===
 
: NMP-GM-003-001, Self-Assessment Instructions for Focused Area Self-Assessment (FASA),
: Version 4.0
: NMP-GM-003, Self-Assessment and Benchmark Procedure, Version 21.1
: NMP-GM-002-005, Corrective Action Program Trending, Version 2.0
: NMP-GM-002-002, Effectiveness Review Instructions, Version 4.2
: 83308-C, Testing of Safety Related NSCW System Coolers, Version 31.3
: NMP-AD-012, Operability Determinations and Functionality Assessments, Version 12.4
: NMP-ES-002, System Monitoring and Health Reporting, Version 17.0
: NMP-ES-002-005, System Monitoring, Version 45.0
: NMP-GM-002, Corrective Action Program, Versions 13, 13.1, 17, 21, 29, 30.1, and 33
: NMP-GM-002-001, Corrective Action Program Instructions, Versions 30.1 and 33.1
: NMP-GM-002-F42, Fleet Keywords for the Corrective Action Program, Version 6.0
: NMP-GM-002-GL03, Cause Analysis and Corrective Actions Guideline, Version 25.0
: NMP-GM-008, Operating Experience Program, Version 16.0
: NMP-OS-006, Operations Performance Indicators, Version 16.1
: NMP-OS-006-002, Aggregate Operator Impact Review Instruction, Version 2.0
: NMP-ES-035-007, Fleet Fire Watch Instruction, Version 2.0
: NMP-ES-035-007, Fleet Fire Watch Instruction, Version 1.0
: 13145A-1, Diesel Generator Train A, Version 6.3
: NMP-ES-005, Scoping and Importance Determination for Equipment Reliability, Version 13.0
: NMP-ES-005-001, Scoping and Importance Determination for Equipment Reliability - Single
: Point Vulnerability, Version 7.0
===Condition Reports===
: 666516
: 666519
: 879125
: 886738
: 787908
: 736458
: 736457
: 10009629
: 10022663
: 10005548
: 10013422
: 10005644
: 138108
: 152044
: 164740
: 538849
: 597467
: 750553
: 751415
: 753454
: 755107
: 756528
: 757218
: 758675
: 768834
: 783161
: 800397 
: 2927
: 2929
: 818370
: 818742
: 830348
: 835222
: 836212
: 837899
: 838044
: 838871
: 2803
: 847696
: 847715
: 853151
: 854169
: 854169
: 854171
: 865135
: 885259
: 886940
: 887102
: 897154
: 900250
: 1026761
: 10003891
: 10003897
: 10011167
: 10013699
: 10014081
: 10014381
: 10015498
: 10015985
: 10017123
: 10017506
: 10019402
: 10028619
: 10033287
: 10035756
: 10039801
: 10002493
: 445343
: 459265
: 794843
: 617317
: 825470
: 10041480
: 10041025
: 29822
: 766880   
: Technical Evaluations906704
: 910486
: 798369
: 908394
: 337844
: 908404
: 668572
: 668563
: 737677
: 737675
: 836852
: 849687
: 853634
: 853638
: 853645
: 853645
: 853687
: 858192
: 858193
: 858193
: 858201
: 858201
: 858202
: 858202
: 858717
: 860480
: 860480
: 860488
: 865927
: 868157
: 868157
: 882472
: 2477
: 882477
: 882479
: 882482
: 882482
: 909344
: 909356
: 909668
: 911975
: 835105
: 675693
: Corrective Action Reports
: 212916
: 249529
: 249304
: 210270
: 213052
: 256024
: 208164
: 195060
: 210112
: 210971
: 211089
: 211142
: 213395
: 255666
: 255857
===Work Orders===
: SNC586376
: SNC586566
: SNC567223
: SNC567222
: SNC602033 SNC621555 SNC629405 SNC631008 SNC631027 
: SNC632292
: SNC632880
: SNC637929 SNC642581 SNC619779 SNC589884
: SNC589884
: SNC619778
: SNC624725
: SNC624726 SNC624738 SNC524759 SNC624767
: SNC646897
: SNC640825 SNC564818
: SNC638913 SNC528990
: Self-Assessments Nuclear Oversight (NOS) audit of the CAP, Fleet-CAP-2014, April 7, 2014 Nuclear Oversight Special CAP audit, Fleet-Special
: CAP-2015 FASA Self-Assessment, Implementation of Interim Cyber Security Milestones 1-7, 5/13/2013 Drawings 1X4DB133-1, Nuclear Service Cooling Water System P&ID, Version 54.0
: 1X4DB133-2, Nuclear Service Cooling Water System P&ID, Version 60.0
: 1X4DB134, Nuclear Service Cooling Water System P&ID, Version 31.0
: 1X3D-AA-G01A, Main one line Class 1E 125V DC and 120V vital AC systems, version 10.0 1X3D-AA-H01A, One line Class 1E 125V DC Train A, version 17.0
===Other Documents===
: Failure Analysis of Square D Tap Switch Class 9831, 2B EDG, Date 11/24/2014
: MRC package for 3-18-2015
: CAPCO (CR daily screening) meeting package for 2/26/2015
: CAPCO (CR daily screening) meeting package for 3/18/2015 FP LCO Package, LCO Number: 1-14-026
: FP LCO Package, LCO Number: 2-13-169
: DC-1806, Design Bases for Class 1E dc system, Version 13
: System Health Report - Unit 1 1804 - 4160 Volt Alternating Current System System Health Report - Unit 2 1804 - 4160 Volt Alternating Current System
: DC-1202, Nuclear Service Cooling Water (NSCW) System Design Bases, Version 13
: DC-1202A, Nuclear Service Cooling Towers Design Bases, Revision 11
: DC-2105, NSCW Cooling Towers and Warehouses Design Bases, Version 7
: ELV-01212, Vogtle Electric Generating Plant Response to Generic Letter 89-13, dated January 25, 1990
: FSAR Chapter 9, Section 9.2.1, Nuclear Service Cooling Water System
: LCV-0716-C, Correspondence from CK McCoy to USNRC, Vogtle Electric Generating Plant Revised Reply to a Notice of Violation, dated April 1, 1996
: NL-04-1762, Correspondence from Don Grissette to USNRC regarding additional information concerning generic letter 96-06, dated November 5, 2004 System Health Reports, Unit 1 NSCW, Q1-2013 through Q4-2014
: System Health Reports, Unit 2 NSCW, Q1-2013 through Q4-2014
: VEGP-LR-IMP-12, Vogtle Electric Generating Plant - Units 1&2, Generic Letter 89-13 Program License Renewal Implementation Package, dated May 15, 2009 V-LO-TX-06101, Operations Lesson Plan - Nuclear Service Cooling Water System, Revision 7.1
: X4C1202V43, Flow Calculation for the Unit 2 NSCW System, Revision 7
: CRs Generated
: 10042617, Tunnel 2T2A incandescent lighting out - three fixtures
: 10042633, NSCW Electrical Receptacle deficiency - open-hot
: 10043020, Loose Penetration Labels
: 10043156, Vogtle Failure Analysis Report tracking
: 10043415, 1R18 Work Order SNC564478 is work complete but in schedule status in MAXIMO
: 10043439, IRT closure documents do not capture all actions that are outstanding.
: 10043450, PI&R inspection finding on work orders were not cancelled per
: NMP-GM-006-GL01
: 10043501, Log-keeping practices need improvement
: 10047591, CA TE extended without following
: NMP-GM-002-001
: 10047594, Failure to follow
: NMP-GM-002-GL03 for training corrective action
: 10047596, CA downgraded without following
: NMP-GM-002-001, section 4.6
: 10048988, Corrective action priority inconsistency from causal analysis
}}
}}

Latest revision as of 04:17, 20 December 2019

IR 05000424/2015-008 and 05000425/2015-008, Vogtle, Units 1 and 2 NRC Problem Identification and Resolution Inspection Report
ML15127A591
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 05/07/2015
From: Masters A
Reactor Projects Branch 7
To: Taber B
Southern Nuclear Operating Co
References
IR 2015008
Download: ML15127A591 (16)


Text

UNITED STATES May 7, 2015

SUBJECT:

VOGTLE ELECTRIC GENERATING PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000424/2015008 AND 05000425/2015008

Dear Mr. Taber:

On April 2, 2015, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your Vogtle Electric Generating Plant Units 1 and 2. The enclosed report documents the inspection findings, which were discussed on April 2, 2015, with Mr. G. Saxon and other members of your staff.

On the basis of the samples selected for review, the inspectors concluded that, in general, problems were properly identified, evaluated, and corrected. In reviewing your corrective action program, the inspectors assessed how well your staff identified problems at a low threshold, your staffs implementation of the stations process for prioritizing and evaluating these problems, and the effectiveness of corrective actions taken by the station to resolve these problems. In each of these areas, the inspectors determined that your staffs performance was adequate to support nuclear safety.

The inspectors also evaluated other processes your staff used to identify issues for resolution.

These included your use of audits and self-assessments to identify latent problems and your incorporation of lessons learned from industry operating experience into station programs, processes, and procedures. The inspectors determined that your stations performance in each of these areas supported nuclear safety.

Finally, the inspectors determined that your stations management maintains a safety-conscious work environment adequate to support nuclear safety. Based on the inspectors observations, your employees are willing to raise concerns related to nuclear safety through at least one of the several means available. In accordance with 10 CFR 2.390 of the NRCs Agency Rules of Practice and Procedure, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). Adams is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA By Reinaldo Rodriguez For/

Anthony D. Masters, Chief Reactor Projects Branch 7 Division of Reactor Projects Docket Nos. 50-424, 50-425 License Nos. NPF-68, NPF-81

Enclosure:

IR 05000424/2015008, 05000425/2015008 w/Attachment: Supplementary Information

REGION II==

Docket Nos.: 50-424, 50-425 License Nos.: NPF-68, NPF-81 Report Nos.: 05000424/2015008 and 05000425/2015008 Licensee: Southern Nuclear Operating Company, Inc. (SNC)

Facility: Vogtle Electric Generating Plant, Units 1 and 2 Location: Waynesboro, GA 30830 Dates: March 16 - April 2, 2015 Inspectors: Wesley Deschaine, Resident Inspector Sequoyah (Team Leader)

Shani Lewis, Project Engineer Natasha Childs, Resident Inspector Oconee Ryan Taylor, Senior Project Inspector Approved by: Anthony D. Masters, Chief Reactor Projects Branch 7 Division of Reactor Projects Enclosure

SUMMARY

IR 05000424/2015008 and 05000425/2015008; March 16 - April 2, 2015; Vogtle Electric

Generating Plant, Units 1 and 2; Biennial Inspection of the Problem Identification and Resolution Program.

The inspection was conducted by two resident inspectors, a senior project inspector, and a project engineer. No findings were identified. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 5.

Identification and Resolution of Problems The inspectors concluded that, in general, problems were properly identified, evaluated, prioritized, and corrected. The licensee was effective at identifying problems and entering them into the corrective action program (CAP) for resolution, as evidenced by the relatively few number of deficiencies identified by external organizations (including the NRC) that had not been previously identified by the licensee, during the review period. Generally, prioritization and evaluation of issues were adequate, formal root cause evaluations for significant problems were adequate, and corrective actions specified for problems were acceptable. Overall, corrective actions developed and implemented for issues were generally effective and implemented in a timely manner.

The inspectors determined that overall, audits and self-assessments were adequate in identifying deficiencies and areas for improvement in the CAP, and appropriate corrective actions were developed to address the issues identified. Operating experience usage was found to be generally acceptable and integrated into the licensees processes for performing and managing work and plant operations.

Based on discussions and interviews conducted with plant employees from various departments, the inspectors determined that personnel at the site felt free to raise safety concerns to management and use the CAP to resolve those concerns.

REPORT DETAILS

4OA2 Problem Identification and Resolution

1. Corrective Action Program Effectiveness

a. Inspection Scope

The inspectors reviewed the licensees CAP procedures which described the administrative process for initiating and resolving problems primarily through the use of condition reports (CRs). To verify that problems were being properly identified, appropriately characterized, and entered into the CAP, the inspectors reviewed CRs that had been issued between February 2013 and February 2015, including a detailed review of selected CRs associated with the following risk-significant systems: Emergency Diesel Generators (EDGs), Nuclear Service Cooling Water (NSCW), 125VDC Electrical, and 4160V Electrical systems. Where possible, the inspectors independently verified that the corrective actions were implemented as intended. The inspectors also reviewed selected common causes and generic concerns associated with root cause evaluations (RCE) to determine if they had been appropriately addressed. To help ensure that samples were reviewed across all cornerstones of safety identified in the Reactor Oversight Process (ROP), the inspectors selected a representative number of CRs that were identified and assigned to the major plant departments, including operations, maintenance, engineering, health physics, chemistry, emergency preparedness, and security. These CRs were reviewed to assess each departments threshold for identifying and documenting plant problems, thoroughness of evaluations, and adequacy of corrective actions. The inspectors reviewed selected CRs, verified corrective actions were implemented, and attended meetings where CRs were evaluated for significance to determine whether the licensee was identifying, accurately characterizing, and entering problems into the CAP at an appropriate threshold.

Plant walkdowns of equipment within the selected systems listed above and other plant areas were conducted by inspectors to assess the material condition and to identify deficiencies that had not been previously entered into the CAP. The inspectors reviewed CRs, maintenance history, corrective actions (CAs), completed work orders (WOs) for the systems, and reviewed associated system health reports. These reviews were performed to verify that problems were being properly identified, appropriately characterized, and entered into the CAP. Items reviewed generally covered a two-year period of time; however, in accordance with the inspection procedure, a five-year review was performed for selected systems for age-related issues.

Control Room walk-downs were also performed to assess the main control room (MCR)deficiency list and to ascertain if deficiencies were entered into the CAP and tracked to resolution. Operator workarounds (OWA) and operator burden screenings were reviewed, and the inspectors verified compensatory measures for deficient equipment which were being implemented in the field.

The inspectors conducted a detailed review of selected CRs to assess the adequacy of the root cause and apparent cause evaluations of the problems identified. The inspectors reviewed these evaluations against the descriptions of the problem described in the CRs and the guidance in licensee procedure NMP-GM-002-GL03, Cause Analysis and Corrective Actions Guideline. The inspectors assessed if the licensee had adequately determined the cause(s) of identified problems, and had adequately addressed operability, reportability, common cause, generic concerns, extent-of-condition, and extent-of-cause. The review also assessed if the licensee had appropriately identified and prioritized corrective actions to prevent recurrence.

The inspectors reviewed selected industry operating experience (OE) items, including NRC generic communications, to verify that they had been appropriately evaluated for applicability and that issues identified through these reviews had been entered into the CAP.

The inspectors reviewed site trend reports, to determine if the licensee effectively trended identified issues and initiated appropriate corrective actions when adverse trends were identified.

The inspectors reviewed licensee audits and self-assessments, including those which focused on problem identification and resolution programs and processes, to verify that findings were entered into the CAP and to verify that these audits and assessments were consistent with the NRCs assessment of the licensees CAP.

The inspectors attended various plant meetings to observe management oversight functions of the corrective action process. These included CR screening meetings and Management Review Committee (MRC) meetings.

Documents reviewed are listed in the Attachment.

b. Assessment Problem Identification The inspectors determined that the licensee was generally effective in identifying problems and entering them into the CAP and there was an appropriately low threshold for entering issues into the CAP. This conclusion was based on a review of the requirements for initiating CRs as described in licensee procedure NMP-GM-002-001, Corrective Action Program Instructions, managements expectation that employees were encouraged to initiate CRs for any reason. Trending was generally effective in monitoring equipment performance. Site management was actively involved in the CAP and focused appropriate attention on significant plant issues. Based on reviews and walkdowns of accessible portions of the selected systems, the inspectors determined that system deficiencies were being identified and placed in the CAP.

A performance deficiency was identified during the inspection associated with the sites failure to identify and correct the condition adverse to quality discovered during the failure analysis for the 2B EDG bridge transfer switch. Specifically, the failure analysis report concluded that the bridge transfer switch failed due to hardened and degraded grease not being properly removed during preventative maintenance (PM). The report also concludes that the PM procedure may be inadequate to remove the older grease and should be updated to mitigate future failures. The site has entered this issue into the CAP as CRs 10041480 and 10043156. However, because this performance deficiency did not adversely affect any ROP cornerstone objectives, the inspectors determined the issue was of minor significance and not subject to enforcement action in accordance with the NRCs Enforcement Policy.

Problem Prioritization and Evaluation Based on the review of CRs sampled by the inspection team during the onsite period, the inspectors concluded that problems were generally prioritized and evaluated in accordance with the licensees CAP procedures as described in the CR severity level determination guidance in NMP-GM-002-001. Each CR was assigned a priority level at the CAP coordinator (CAPCO) meeting, and adequate consideration was given to system or component operability and associated plant risk.

The inspectors determined that station personnel had conducted root cause and apparent cause analyses in compliance with the licensees CAP procedures and assigned cause determinations were appropriate, considering the significance of the issues being evaluated. A variety of formal causal-analysis techniques were used depending on the type and complexity of the issue consistent with NMP-GM-002-GL03.

The inspectors identified three performance deficiencies associated with the licensees prioritization and evaluation of issues. These issues were screened in accordance with Manual Chapter 0612, Issue Screening, and were determined to be of minor significance and not subject to enforcement action in accordance with the NRCs Enforcement Policy.

  • The inspectors reviewed Corrective Action Report (CAR) 210971 associated with a NRC non-cited violation (NCV), and identified the following issues with the Apparent Cause Determination (ACD):

o Technical Evaluation (TE) 860480 was a corrective action for Operations training to perform a Gap Analysis to address potential knowledge gaps identified by the apparent cause team. This action was one of several actions to resolve apparent cause #1 (AC1) and contributing cause #1 (CC1) of the ACD. The priority level of TE 860480 was downgraded from a level 2 to level 3 without following the process as outlined in section 4.6 of NMP-GM-002-001. Additionally, the apparent cause analysts did not follow the process outlined in NMP-GM-002-GL03 when initially assigning the corrective action. The licensee has entered these issues into the CAP as CRs 10047594 and 10047596.

o TE 853634 was a corrective action for the Chemistry department to perform a department stand down to discuss upcoming procedure changes as a result of the event. The action was one of several actions to resolve AC1 and CC1 of the ACD. The action due date was extended without following NMP-GM-002-001.

There was no assessment of the potential impact of the extension and the appropriate level of management approval was not received. The licensee has entered this issue into the CAP as CR 100475594.

  • The inspectors reviewed CAR 211142 associated with an NRC NCV and identified the following issue with the Apparent Cause Determination:

o The ACD report listed seven corrective actions to address AC1; none of the seven actions were assigned a priority level 2, which is not in accordance with NMP-GM-002-001. This procedure states that corrective actions assigned to address an apparent cause should be assigned a level 2 priority. The potential weakness in assigning the incorrect priority level is that the action could potentially be revised and/or receive due date extensions without receiving the appropriate levels of review appropriate for the significance. The licensee has entered this issue into the CAP as CR 10049368.

Corrective Actions Based on a review of corrective action documents, interviews with licensee staff, and verification of completed corrective actions, the inspectors determined that overall, corrective actions were timely, commensurate with the safety significance of the issues, and effective, in that conditions adverse to quality were corrected and non-recurring. For significant conditions adverse to quality, the corrective actions directly addressed the cause and effectively prevented recurrence in that a review of performance indicators, CRs, and effectiveness reviews demonstrated that the significant conditions adverse to quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence (CAPRs) were sufficient to ensure corrective actions were properly implemented and were effective.

c. Findings

No findings were identified.

2. Use of Operating Experience

a. Inspection Scope

The inspectors examined the licensees use of industry OE to assess the effectiveness of how external and internal operating experience information was used to prevent similar or recurring problems at the plant. In addition, the inspectors selected operating experience documents (e.g., NRC generic communications, 10 CFR Part 21 reports, licensee event reports, vendor notifications, and plant internal operating experience items, etc.), which had been issued since February 2013, to verify whether the licensee had appropriately evaluated each notification for applicability to the Vogtle Electric Generating Plant, Units 1 and 2, and whether issues identified through these reviews were entered into the CAP.

b. Assessment Based on a review of selected documentation related to operating experience issues, the inspectors determined that the licensee was generally effective in screening operating experience for applicability to the plant. Industry OE was evaluated at either the corporate or plant level depending on the source and type of the document. Relevant information was then forwarded to the applicable department for further action or informational purposes. OE issues requiring action were entered into the CAP for tracking and closure. In addition, operating experience was included in all apparent cause and root cause evaluations in accordance with licensee procedure NMP-GM-002-GL03.

c. Findings

No findings were identified.

3. Self-Assessments and Audits

a. Inspection Scope

The inspectors reviewed audit reports and self-assessment reports, including those which focused on problem identification and resolution, to assess the thoroughness and self-criticism of the licensee's audits and self-assessments, and to verify that problems identified through those activities were appropriately prioritized and entered into the CAP for resolution in accordance with licensee procedure NMP-GM-003, Self-Assessment and Benchmark Procedure.

b. Assessment The inspectors determined that the scopes of assessments and audits were adequate.

Self-assessments were generally detailed and critical, as evidenced by findings consistent with the inspectors independent review. The inspectors verified that CRs were created to document areas for improvement and findings resulting from the self-assessments, and verified that actions had been completed consistent with those recommendations. Generally, the licensee performed evaluations that were technically accurate.

c. Findings

No findings were identified.

4. Safety-Conscious Work Environment

a. Inspection Scope

During the course of the inspection, the inspectors assessed the stations safety-conscious work environment (SCWE) through review of the stations Employee Concerns Program (ECP) and interviews with various departmental personnel. The inspectors reviewed a sample of ECP issues to verify that concerns were being properly reviewed and identified deficiencies were being resolved and entered into the CAP when appropriate.

b. Assessment Based on the interviews conducted and the CRs reviewed, the inspectors determined that licensee management emphasized the need for all employees to identify and report problems using the appropriate methods established within the administrative programs, including the CAP and ECP. These methods were readily accessible to all employees.

Based on discussions conducted with a sample of plant employees from various departments, the inspectors determined that employees felt free to raise issues, and that management encouraged employees to place issues into the CAP for resolution. The inspectors did not identify any reluctance on the part of the licensee staff to report safety concerns.

c. Findings

No findings were identified.

4OA6 Exit

Exit Meeting Summary

On April 2, 2015, the inspectors presented the inspection results to Mr. G. Saxon and other members of the site staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection.

ATTACHMENT:

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

G. Saxon, Plant Manager
G. Gunn, Regulatory Affairs Manager
J. Wade, Site Design Engineering Manager
K. Morrow, Licensing Engineer
K. Walden, Licensing Engineer
M. Carstensen, Engineer
M. Cline, Site CAPCO
N. Koteel, Fleet PI Manager
T. Thompson, Site System Engineering Manager
T. Simmons, PI Manager
T. Moorer, Director EHS

NRC personnel

A. Alen, Resident Inspector
M. Cain, Senior Resident Inspector

LIST OF REPORT ITEMS

Opened and Closed

None

Closed

None

Discussed

None

LIST OF DOCUMENTS REVIEWED