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Line 30: |
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| If you have any questions on the above, call me at 618-244-6000. | | If you have any questions on the above, call me at 618-244-6000. |
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| e 21/0513 M14154847068 ÷>13018165151 Wm _Nutherm 5>01 South 11th Street Mount Vernon, IL62064 Phone:618-244-6000 Fexc6l8.244.6641l Decembe 18, 2015 Docmet Control Ds U.S. Nuclear Regulatory Commision Washington, DC 20555 Str~eet: Notificatieniunder 1OCFR 21.21 (d)(3)('ii) for Modre Industres RTD Transmitter Pursuant to 10CFR 21.21 (d) (3) (ii), Nutherm International, Inc. is providing written notification of the identification ofa potential defect found in Moore industries RID Transmitter Part Number:.RBT/3W20-40/4-2OMAI1 17ACI-EZ84.06-LNP-VTD [EX]. | | e 21/0513 M14154847068 ÷>13018165151 Wm _Nutherm 5>01 South 11th Street Mount Vernon, IL62064 Phone:618-244-6000 Fexc6l8.244.6641l Decembe 18, 2015 Docmet Control Ds U.S. Nuclear Regulatory Commision Washington, DC 20555 Str~eet: Notificatieniunder 10CFR 21.21 (d)(3)('ii) for Modre Industres RTD Transmitter Pursuant to 10CFR 21.21 (d) (3) (ii), Nutherm International, Inc. is providing written notification of the identification ofa potential defect found in Moore industries RID Transmitter Part Number:.RBT/3W20-40/4-2OMAI1 17ACI-EZ84.06-LNP-VTD [EX]. |
| The following information is required per 100FR 21.21 (d) (4) | | The following information is required per 100FR 21.21 (d) (4) |
| (i) Name and address of the individual or individuals informing the Commission. | | (i) Name and address of the individual or individuals informing the Commission. |
Line 75: |
Line 75: |
| If you have any questions on the above, call me at 618-244-6000. | | If you have any questions on the above, call me at 618-244-6000. |
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| e 21/0513 M14154847068 ÷>13018165151 Wm _Nutherm 5>01 South 11th Street Mount Vernon, IL62064 Phone:618-244-6000 Fexc6l8.244.6641l Decembe 18, 2015 Docmet Control Ds U.S. Nuclear Regulatory Commision Washington, DC 20555 Str~eet: Notificatieniunder 1OCFR 21.21 (d)(3)('ii) for Modre Industres RTD Transmitter Pursuant to 10CFR 21.21 (d) (3) (ii), Nutherm International, Inc. is providing written notification of the identification ofa potential defect found in Moore industries RID Transmitter Part Number:.RBT/3W20-40/4-2OMAI1 17ACI-EZ84.06-LNP-VTD [EX]. | | e 21/0513 M14154847068 ÷>13018165151 Wm _Nutherm 5>01 South 11th Street Mount Vernon, IL62064 Phone:618-244-6000 Fexc6l8.244.6641l Decembe 18, 2015 Docmet Control Ds U.S. Nuclear Regulatory Commision Washington, DC 20555 Str~eet: Notificatieniunder 10CFR 21.21 (d)(3)('ii) for Modre Industres RTD Transmitter Pursuant to 10CFR 21.21 (d) (3) (ii), Nutherm International, Inc. is providing written notification of the identification ofa potential defect found in Moore industries RID Transmitter Part Number:.RBT/3W20-40/4-2OMAI1 17ACI-EZ84.06-LNP-VTD [EX]. |
| The following information is required per 100FR 21.21 (d) (4) | | The following information is required per 100FR 21.21 (d) (4) |
| (i) Name and address of the individual or individuals informing the Commission. | | (i) Name and address of the individual or individuals informing the Commission. |
|
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Category:Deficiency Report (per 10CFR50.55e and Part 21)
MONTHYEARML24107A6972024-04-12012 April 2024 Engine Systems, Inc Part 21 Report Re EMD Cylinder Liner Water Leak ML22301A1742022-10-28028 October 2022 Global Nuclear Fuel Americas, LLC (GNF) - Part 21 60-Day Interim Report Notification: GNF3 Raised Water Rod (SC-22-04 Rt) ML21225A0812021-08-0404 August 2021 Lake Engineering Co., Final Report Per 10 CFR Part 21 Degraded Snubber SF1154 Hydraulic Fluid Batch No. 17BLVS293 ML21014A2342020-12-0707 December 2020 Fourth Interim Notification Per 10 CFR Part 21 Re Degraded Snubber SF1154 Hydraulic Fluid Batch No. 17BLVS293 ML20304A1612020-10-14014 October 2020 Lake Engineering Co., Degraded Snubber SF1154 Hydraulic Fluid Batch No. 16DLVS852 Final Report Per 10 CFR Part 21 ML20097B6912020-03-20020 March 2020 Second Interim Notification Per 10 CFR Part 21: Degraded Snubber SF1154 Hydraulic Fluid Batch No. 16DLVS852 ML20108F5302020-03-20020 March 2020 10CFR21 Reporting of Defects and Non-Compliance - Engine Systems, Inc. Report No. 10CFR21-0129, Rev. 0, Test Stand Deficiency - EMD Fuel Injectors P/N H40084720 ML20049A0752020-02-11011 February 2020 C&D Technologies, Inc. -10 CFR Part 21 Evaluation Regarding Container Failure in KCR-07 Batteries ML19347A4262019-12-10010 December 2019 General Atomics - Reportable Occurrence Under 10CFR21: Reported Failure in Analog High Range Radiation Monitor (RP-2C) ML19002A2042018-12-21021 December 2018 to Engine Systems, Inc., Part 21 Report Re Emd Fuel and Soakback Pumps - Potentially Undertorqued Cover Bolts ML18354A7422018-12-0404 December 2018 Engine Systems, Inc., Submittal of 1OCFR21 Reporting of Defects and Non-Compliance - Report No. 1OCFR21-0123, Rev. 0 - Emo Fuel and Soakback Pumps - Potentially Undertorqued Cover Bolts ML18353A4282018-11-30030 November 2018 Engine Systems, Inc., 10CFR21-0123, Rev. 0, for a 10CFR21 Reportable Condition on Emd Fuel and Soakback Pumps ML18078A5362018-01-31031 January 2018 Crane Nuclear, Inc. - Interim Report for 10 CFR Part 21 Investigation Report Notification of Xomox Plug Valve High Torsional Stress in Stem (Update) ML17194A8252017-07-11011 July 2017 Part 21 Report Re Wedge Pin Failure in Anchor Darling Motor Operated Double Disc Gate Valves with Threaded Stem to Upper Wedge Connections ML17090A4002017-03-24024 March 2017 Part 21 - Failure of Power Supplies to Meet Voltage Stability Specifications ML17086A0222017-03-23023 March 2017 Part 21 - Failure of Power Supplies to Meet Voltage Stability Specifications ML17081A4532017-03-20020 March 2017 Part 21 - Plastic Jar Dedication Sampling ML17039A5692017-02-0303 February 2017 Final Part 21 Report on Defect, Potential for Test Induced Damage 0867F Series Main Steam Safety Relief Valves ML17026A4142017-01-20020 January 2017 C&D Technologies, Inc. - Part 21 - Plastic Jar Dedication Sampling ML17026A4132017-01-11011 January 2017 Part 21 - Failure of Power Supplies to Meet Voltage Stability Specifications ML16061A0092016-02-22022 February 2016 Curtiss Wright - Part 21 Notification - Potential Defect in Okonite Tape Splices, Per James A. Fitzpatrick ML16055A1222016-02-22022 February 2016 Curtiss-Wright Corp. - Potential Defect in Okonite Tape Splices, Per James A. Fitzpatrick Nuclear Power Plant ML16039A2692016-02-0303 February 2016 Nutherm International, Inc. - Potential Issue Regarding Incorrect Industrial Irradiation Dose, Per Cooper, Oconee, Fitzpatrick, Point Beach, Brunswick, and Susquehanna ML15357A0412015-12-18018 December 2015 Nutherm International, Inc. - Potential Part 21 Report Involving RTD Transmitter, Per Fitzpatrick ML15187A1722015-06-30030 June 2015 Interim Part 21 Report - Potential Test Induced Defect in 0867F Main Steam Safety Relief Valves ML15134A0172015-05-0101 May 2015 Part 21 Report Regarding Potential Test Induced Defect in a 0867F Main Steam Safety Relief Valves ML15077A4222015-03-17017 March 2015 Curtiss Wright Flow Control Co., Interim Part 21 Report - Potential Test Induced Defect in a 0867F Main Steam Safety Relief Valves ML15022A6502015-01-20020 January 2015 Letter from Steven R. Eisenberg USNRC 10CFR Part 21 Notification ML14210A0102014-07-23023 July 2014 Part 21 - Unseating of Valve Spring on Scram Solenoid Pilot Valve ML14204A7082014-07-23023 July 2014 Enclosure 2, Description of Closure Evaluation, Non-Proprietary Information - Class I (Public) ML14204A7072014-07-23023 July 2014 Completed Evaluation of Part 21 Potentially Reportable Condition Notification: Unseating of Valve Spring on SSPV W3F1-2014-0026, Notification of Potential Part 21 Report of Time-Delay Relays Spurious Actuation2014-04-11011 April 2014 Notification of Potential Part 21 Report of Time-Delay Relays Spurious Actuation ML14079A0282014-03-13013 March 2014 Part 21 - Allen Bradley Type 700RTC Relay Spuriously De-Energizing ML13238A2532013-08-21021 August 2013 Notification of Potential Part 21 Report - Foxboro Power Supply Potential Failures Due to Defective the Wraps and Holders ML13165A3422013-06-12012 June 2013 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers ML13127A0122013-05-0303 May 2013 Notification of Potential Interim Part 21 Report of Defect in a Relief Valve Bellows ML13093A1532013-04-0202 April 2013 Part 21 Report - Foxboro Power Supply Potential Failures Due to Defective Tie Wraps and Holders ML13064A0122013-02-25025 February 2013 Notification of Potential Part 21 Report Re Wedge Pin Failure of an Anchor/Darling Double-Disc Gate Valve ML13044A0752013-02-0808 February 2013 Part 21 - Completed Evaluation for Potential Error in Main Steam Line High Flow Calculational Methodology ML13042A0962013-02-0808 February 2013 Completed Evaluation of Part 21 Potentially Reportable Condition Notification: Error in Main Steam Line High Flow Calculational Methodology ML12348A1362012-12-13013 December 2012 Part 21 60-Day Interim Report Notification: Adequacy of Design Change in Am Magne-Blast Circuit Breakers ML12352A1232012-12-13013 December 2012 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers ML12347A3082012-12-12012 December 2012 Part 21 60-Day Interim Report Notification: Error in Main Steam Line High Flow Calculational Methodology ML12319A0122012-09-27027 September 2012 Error in Main Steam Line High Flow Calculational Methodology ML12319A0112012-09-27027 September 2012 Part-21 Report - Faulty Master Trip Units, Slave Units, and Resistance Temperature Detectors ML12177A0562012-06-21021 June 2012 Part 21 - Reliability Degradation of Resistors in Trip Units and Readout Assemblies ML12163A1302012-06-0606 June 2012 Part 21 Report - Failure of CRD Collet Retainer Tube/Outer Tube Weld ML12158A4472012-06-0606 June 2012 Part 21 60-Day Interim Report Notification - Closufailure of CRD Collet Retainer Tube/Outer Tube Weld ML12094A3712012-04-0202 April 2012 Part 21 Report - Rosemount Pressure Transmitters with Nonzero Based Calibrations ML12040A2832012-02-0707 February 2012 Notification of Potential Part 21 - Failure to Include Seismic Input in Reactor Control Blade Customer Guidance 2024-04-12
[Table view] Category:Letter
MONTHYEARIR 05000333/20240032024-11-12012 November 2024 Integrated Inspection Report 05000333/2024003 ML24317A1432024-11-0404 November 2024 Constellation Energy Generation, LLC, 2024 Annual Report - Guarantees of Payment of Deferred Premiums IR 05000333/20240902024-10-29029 October 2024 Final Significance Determination of a White Finding with Assessment Follow-Up and Notice of Violation; Inspection Report 05000333/2024090 JAFP-24-0055, Response to Request for Additional Information for License Amendment Request to Add Temporary Change to TS 3.3.2.1, Condition C, Control Rod Block Instrumentation2024-10-29029 October 2024 Response to Request for Additional Information for License Amendment Request to Add Temporary Change to TS 3.3.2.1, Condition C, Control Rod Block Instrumentation IR 05000333/20244022024-10-28028 October 2024 Material Control and Accounting Program Inspection Report 05000333/2024402 (Cover Letter Only) ML24276A1332024-10-17017 October 2024 Issuance of Amendment No. 357 Revise Technical Specifications to Adopt TSTF-529, Clarify Use and Application Rules, Revision-4, and Administrative Changes ML24282B0302024-10-11011 October 2024 Project Manager Assignment RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24207A0192024-10-0909 October 2024 SE Addendum Related to the License Amendment No. 338 for Implementation of the Alternative Source Term (DPO-2021-001) ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing JAFP-24-0051, Reply to Preliminary White Finding and Apparent Violation in NRC Inspection Report 05000333/2024011; EA-24-0882024-10-0303 October 2024 Reply to Preliminary White Finding and Apparent Violation in NRC Inspection Report 05000333/2024011; EA-24-088 ML24270A0742024-09-30030 September 2024 Individual Notice of Consideration of Issuance of Amendments to Renewed Facility Operating Licenses, Proposed No Significant Hazards Consideration Determination, & Opportunity for a Hearing (EPID L-2024-LLA-0134) - LTR ML24270A1452024-09-26026 September 2024 Notice of Enforcement Discretion for James A. Fitzpatrick Nuclear Power Plant JAFP-24-0046, Request for Enforcement Discretion for Technical Specification (TS) 3.3.2.1 Control Rod Block Instrumentation2024-09-25025 September 2024 Request for Enforcement Discretion for Technical Specification (TS) 3.3.2.1 Control Rod Block Instrumentation JAFP-24-0047, License Amendment Request – Temporary Addition to TS 3.3.2.1 Condition C, Control Rod Block Instrumentation to Support Upgrade to Rod Worth Minimizer Software2024-09-25025 September 2024 License Amendment Request – Temporary Addition to TS 3.3.2.1 Condition C, Control Rod Block Instrumentation to Support Upgrade to Rod Worth Minimizer Software JAFP-24-0045, Supplemental Information for License Amendment Request to Revise Technical Specifications to Adopt TSTF-529, Clarify Use and Application Rules, Revision 4, and Administrative Changes to the Technical Specifications2024-09-20020 September 2024 Supplemental Information for License Amendment Request to Revise Technical Specifications to Adopt TSTF-529, Clarify Use and Application Rules, Revision 4, and Administrative Changes to the Technical Specifications IR 05000333/20240112024-09-19019 September 2024 Follow-up to Inspection Procedure 71153 Report 05000333/2024011 and Preliminary White Finding and Apparent Violation JAFP-24-0044, Core Operating Limits Report Cycle 272024-09-16016 September 2024 Core Operating Limits Report Cycle 27 JAFP-24-0043, Revision to Commitment Relating to Resolution of Anchor Darling Double Disc Gate Valve Part 21 Issues2024-09-12012 September 2024 Revision to Commitment Relating to Resolution of Anchor Darling Double Disc Gate Valve Part 21 Issues ML24165A0382024-09-0404 September 2024 Issuance of Amendment No. 356 Update Fuel Handling Accident Analysis 05000333/LER-2024-002, Reactor Protection System Electric Power Monitoring System Trip Caused Primary Containment Isolation2024-09-0404 September 2024 Reactor Protection System Electric Power Monitoring System Trip Caused Primary Containment Isolation IR 05000333/20240052024-08-29029 August 2024 Updated Inspection Plan for James A. Fitzpatrick Nuclear Power Plant (Report 05000333/2024005) 05000333/LER-2024-001-01, EDG Lube Oil Check Valve Bonnet Cap Leak Due to Failed Gasket2024-08-21021 August 2024 EDG Lube Oil Check Valve Bonnet Cap Leak Due to Failed Gasket ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition IR 05000333/20240022024-08-0707 August 2024 Integrated Inspection Report 05000333/2024002 JAFP-24-0034, 10 CFR 50.46 Annual Report2024-07-31031 July 2024 10 CFR 50.46 Annual Report ML24208A0492024-07-30030 July 2024 Notice of Consideration of Issuance of Amendments to Facility Operating Licenses and Proposed No Significant Hazards Consideration Determination (Letter) JAFP-24-0036, Supplement to License Amendment Request to Update the Technical Specification Bases to Change the Fuel Handling Accident Analysis2024-07-29029 July 2024 Supplement to License Amendment Request to Update the Technical Specification Bases to Change the Fuel Handling Accident Analysis JAFP-24-0033, Response to Request for Information Pertaining to a Licensed Operator Positive Fitness-For-Duty Test2024-07-23023 July 2024 Response to Request for Information Pertaining to a Licensed Operator Positive Fitness-For-Duty Test IR 05000333/20244032024-07-18018 July 2024 Biennial Problem Identification and Resolution Inspection Report 05000333/2024403 (Cover Letter Only) IR 05000333/20244012024-07-15015 July 2024 Security Baseline Inspection 05000333/2024401 RS-24-070, Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions2024-07-12012 July 2024 Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions ML24190A1932024-07-0909 July 2024 Correction Letter of Amendment No. 355 Revise Technical Specifications Section 3.4.3.1, Safety Relief Valves Setpoint Lower Tolerance IR 05000333/20240102024-07-0808 July 2024 Commercial Grade Dedication Inspection Report 05000333/2024010 ML24184A1662024-07-0303 July 2024 Senior Reactor and Reactor Operator Initial License Examinations ML24136A1162024-06-26026 June 2024 Issuance of Amendment No. 355 Revise Technical Specifications Section 3.4.3.1, Safety Relief Valves Setpoint Lower Tolerance JAFP-24-0027, EDG Lube Oil Check Valve Bonnet Cap Leak Due to Failed Gasket2024-06-24024 June 2024 EDG Lube Oil Check Valve Bonnet Cap Leak Due to Failed Gasket ML24176A2412024-06-24024 June 2024 Licensed Operator Positive Fitness-for-Duty Test 05000333/LER-2024-001, EDG Lube Oil Check Valve Bonnet Cap Leak Due to Failed Gasket2024-06-24024 June 2024 EDG Lube Oil Check Valve Bonnet Cap Leak Due to Failed Gasket RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations JAFP-24-0026, Supplement to License Amendment Request to Modify Technical Specification Surveillance Requirement (SR) 3.4.3.1 Safety Relief Valves (Srvs) Setpoint Lower Tolerance2024-06-12012 June 2024 Supplement to License Amendment Request to Modify Technical Specification Surveillance Requirement (SR) 3.4.3.1 Safety Relief Valves (Srvs) Setpoint Lower Tolerance ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 IR 05000333/20240012024-05-0909 May 2024 Integrated Inspection Report 05000333/2024001 JAFP-24-0023, 2023 Annual Radiological Environmental Operating Report2024-05-0909 May 2024 2023 Annual Radiological Environmental Operating Report RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests JAFP-24-0020, 2023 Annual Radioactive Effluent Release Report2024-04-25025 April 2024 2023 Annual Radioactive Effluent Release Report JAFP-24-0019, 2023 REIRS Transmittal of NRC Form 52024-04-18018 April 2024 2023 REIRS Transmittal of NRC Form 5 ML24106A0152024-04-15015 April 2024 Request for Withholding Information from Public Disclosure Response to Request for Additional Information for License Amendment Request to Update the Technical Specification Bases to Change the Fuel Handling ML24107A6972024-04-12012 April 2024 Engine Systems, Inc Part 21 Report Re EMD Cylinder Liner Water Leak ML24103A2042024-04-12012 April 2024 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition 2024-09-04
[Table view] |
Text
'12/18/2015 l* AtTO P Part 21 (PAR) Event# 51612 Rep Org: NUTHERM INTERNATIONAL, INC Notification Date)I Time: 12118/2015 16:41 (EST)
Supplier: NUTHERM INTERNATIONAL, INC Event Date I Time: 12/18/2015 *(CST)
Last Modification: 12/18/2015 Region: 3 Docket #:
City: MOUNT VERNON Agreement State: Yes County: License #:
State: IL NRC Notified by: ADRIENNE SMITH Notifications: MARC FERDAS R1DO HQ Ops Officer: DONG HWA PARK PART 2 1/50.55 REACTORS EMAIL Emergency Class: NON EMERGENCY 10 CFR Section:
21.21 (d)(3)(i) DEFECTS AND NONCOMPLIANCE POTENTIAL PART 21 INVOLVING RTD TRANSMITTER The following is excerpted from a report submitted by Nutherm International, Inc.:
"The wire insulation in T2 transformer on the Moores Industry RTD transmitter Part Number: RBT/3W20-40/4-20MA/11I7AC/-EZ84.06-LNP-VTID [EX] was damaged during assembly. This damage reduced the insulation resistance and dielectric breakdown between the windings of the transformer. This resulted in early, catastrophic failure of the RTD transmitter.
"It has been determined that no visual inspection of the transformer or testing after the transformer is installed will discover this defect. This defect can only be found by performing testing on the transformer prior to installation."
This temperature transmitter has been sent to Entergy Operations - Fitzpatrick.
0 2110513 M14154847068 .* 13018165151 501 SOUTh ELEVENTHI S.TREET MT., VERNON. ILLINlOIS 62884 PHONE 818-244-8000 FAX 618-244-8641 To, iJRc. o(p~.r-)J5 *e.n v& rom: A-t,.e.*v 5c- '..,.
Fux '3 I1o*/ &*-T 1- Pages Including Covon 9 Phone= _________ Date: IZl*/ r3 CC: Nutherm Project No: ,________,_____
Customer Project No:
If you have any questions on the above, call me at 618-244-6000.
e 21/0513 M14154847068 ÷>13018165151 Wm _Nutherm 5>01 South 11th Street Mount Vernon, IL62064 Phone:618-244-6000 Fexc6l8.244.6641l Decembe 18, 2015 Docmet Control Ds U.S. Nuclear Regulatory Commision Washington, DC 20555 Str~eet: Notificatieniunder 10CFR 21.21 (d)(3)('ii) for Modre Industres RTD Transmitter Pursuant to 10CFR 21.21 (d) (3) (ii), Nutherm International, Inc. is providing written notification of the identification ofa potential defect found in Moore industries RID Transmitter Part Number:.RBT/3W20-40/4-2OMAI1 17ACI-EZ84.06-LNP-VTD [EX].
The following information is required per 100FR 21.21 (d) (4)
(i) Name and address of the individual or individuals informing the Commission.
Wade Bowfin, Chairman of the Board Nutherm International, Inc.
501 South 11lth Street Mount Vernon, Illinois 62864 (ii) Identification of the facility, the activity, or the basic component supplied for such facility or such activity within the United States which fails to comply or contains a defect.
It has been identified that this temperature transmitter, RBT/3W20-40/4-20MA/1l17AC/-EZ84.06-
-LN-P-VTID [EX] as been sent to the following facility.
Entergy Operations - Fitzpatrick
('ill) Identification of the firm constructing the facility or supplying the basic component which fails to comply or contains a defect.
Nutherm International, Inc., 501 South 11th Street. Mount Vernon, Illinois 62864.
(iv) Nature of the defect or failure to comply and the safety hazard which is created or could be created by such defect or falture to comply.
The wire insulation in 12 trasformer on the Moores Industry RTD transmitter Part Number:
RBT/3W20-40/4-20MA/11l7AC/-EZ_4.06-LNP-VTD [EX] was damaged during assembly. This damage reduced the insulation resistance and dielectric breakdown between the windings of the transformer. This resulted in.early, catastrophic failure of the RTD trasmitter.
It has been determined that no visual inspection of the transformer or testing after the transformer is installed will discover this defect. This defect can only be found by performing testing on the transformer prior to installation.
(v) The date on which the information of such defect or failure to comply was obtained.
December 18, 2015
0 21/0513 M14154847068 ->13018165151 Page 2 December 18, 2015 (vi) In the case of a basic component which contains a defect or fails to comply, the number and location of these components in use at, supplied for, being supplied for, or may be supplied for, manufcurd or being manufactured for one or more facilities or activities subject to the regulations in this part.
Nutherm International, Inc. has concluded its review of all procurements of the RBT/3W20-40/4-2OMA/l117AC/-EZ84.06-LNP-VTD [EX] transmitters and have found two (2) units with this potential defect shipped to customers. The following facility was determined to be impacted by this condition:
Entergy Operations - Fitzpatrick Purchase Order Nutherm Traceability Number Serial No.
0649 13945-O1R1 1/01 2326051 10444073 13818-OlR1 1/01 2377572 (vii) The corrective action which has been, is being, or will be taken; the name of the individual or
- organization responsible for the action; and the length of time that has been or will be taken to complete the action.
Initial actions of determining the units aff~ete were completed 12/18/2015. The impacted customer was notified of this condition 12/18/2015. Corrective actions to prevent installation of damaged transformers consist of testing the transformer prior to installation. Nutherm obtained a unit with this testing performed. Unit was found to be free of the nonconforming condition and was tested at Nutherm International, Inc. The unit was found to be defect free and conforming to all specifications and requirements. Commercial Grade Dedication of this unit was completed 12/18/2015 and shipped to Fitzpaltick on 12/18/2015. The manufacturer has completed corrective actions to prevent any further nonconforming transformers being installed into any transmitters.
(viii) Any advice related to the defect or failure to comply about the facility, activity, or basic component that has been, is being, or will be given to purchasers or licensees.
Replacement of the units listed above is suggested.
(ix) In the case of an early site permit, the entities to whom an early site permit was transferred.
,.Not applicable.
0 21(0513 M14154847068 ->13018165151 D04 Page 3 December 18, 2015 Sincerely, NUTHERM INTERNATIONAL, Inc, Wade Boli Chairman of Board WB/abs cc: Rich Apa, Supervisor, Purchaing, Entergy Operations - Fitzpatrick
'12/18/2015 l* AtTO P Part 21 (PAR) Event# 51612 Rep Org: NUTHERM INTERNATIONAL, INC Notification Date)I Time: 12118/2015 16:41 (EST)
Supplier: NUTHERM INTERNATIONAL, INC Event Date I Time: 12/18/2015 *(CST)
Last Modification: 12/18/2015 Region: 3 Docket #:
City: MOUNT VERNON Agreement State: Yes County: License #:
State: IL NRC Notified by: ADRIENNE SMITH Notifications: MARC FERDAS R1DO HQ Ops Officer: DONG HWA PARK PART 2 1/50.55 REACTORS EMAIL Emergency Class: NON EMERGENCY 10 CFR Section:
21.21 (d)(3)(i) DEFECTS AND NONCOMPLIANCE POTENTIAL PART 21 INVOLVING RTD TRANSMITTER The following is excerpted from a report submitted by Nutherm International, Inc.:
"The wire insulation in T2 transformer on the Moores Industry RTD transmitter Part Number: RBT/3W20-40/4-20MA/11I7AC/-EZ84.06-LNP-VTID [EX] was damaged during assembly. This damage reduced the insulation resistance and dielectric breakdown between the windings of the transformer. This resulted in early, catastrophic failure of the RTD transmitter.
"It has been determined that no visual inspection of the transformer or testing after the transformer is installed will discover this defect. This defect can only be found by performing testing on the transformer prior to installation."
This temperature transmitter has been sent to Entergy Operations - Fitzpatrick.
0 2110513 M14154847068 .* 13018165151 501 SOUTh ELEVENTHI S.TREET MT., VERNON. ILLINlOIS 62884 PHONE 818-244-8000 FAX 618-244-8641 To, iJRc. o(p~.r-)J5 *e.n v& rom: A-t,.e.*v 5c- '..,.
Fux '3 I1o*/ &*-T 1- Pages Including Covon 9 Phone= _________ Date: IZl*/ r3 CC: Nutherm Project No: ,________,_____
Customer Project No:
If you have any questions on the above, call me at 618-244-6000.
e 21/0513 M14154847068 ÷>13018165151 Wm _Nutherm 5>01 South 11th Street Mount Vernon, IL62064 Phone:618-244-6000 Fexc6l8.244.6641l Decembe 18, 2015 Docmet Control Ds U.S. Nuclear Regulatory Commision Washington, DC 20555 Str~eet: Notificatieniunder 10CFR 21.21 (d)(3)('ii) for Modre Industres RTD Transmitter Pursuant to 10CFR 21.21 (d) (3) (ii), Nutherm International, Inc. is providing written notification of the identification ofa potential defect found in Moore industries RID Transmitter Part Number:.RBT/3W20-40/4-2OMAI1 17ACI-EZ84.06-LNP-VTD [EX].
The following information is required per 100FR 21.21 (d) (4)
(i) Name and address of the individual or individuals informing the Commission.
Wade Bowfin, Chairman of the Board Nutherm International, Inc.
501 South 11lth Street Mount Vernon, Illinois 62864 (ii) Identification of the facility, the activity, or the basic component supplied for such facility or such activity within the United States which fails to comply or contains a defect.
It has been identified that this temperature transmitter, RBT/3W20-40/4-20MA/1l17AC/-EZ84.06-
-LN-P-VTID [EX] as been sent to the following facility.
Entergy Operations - Fitzpatrick
('ill) Identification of the firm constructing the facility or supplying the basic component which fails to comply or contains a defect.
Nutherm International, Inc., 501 South 11th Street. Mount Vernon, Illinois 62864.
(iv) Nature of the defect or failure to comply and the safety hazard which is created or could be created by such defect or falture to comply.
The wire insulation in 12 trasformer on the Moores Industry RTD transmitter Part Number:
RBT/3W20-40/4-20MA/11l7AC/-EZ_4.06-LNP-VTD [EX] was damaged during assembly. This damage reduced the insulation resistance and dielectric breakdown between the windings of the transformer. This resulted in.early, catastrophic failure of the RTD trasmitter.
It has been determined that no visual inspection of the transformer or testing after the transformer is installed will discover this defect. This defect can only be found by performing testing on the transformer prior to installation.
(v) The date on which the information of such defect or failure to comply was obtained.
December 18, 2015
0 21/0513 M14154847068 ->13018165151 Page 2 December 18, 2015 (vi) In the case of a basic component which contains a defect or fails to comply, the number and location of these components in use at, supplied for, being supplied for, or may be supplied for, manufcurd or being manufactured for one or more facilities or activities subject to the regulations in this part.
Nutherm International, Inc. has concluded its review of all procurements of the RBT/3W20-40/4-2OMA/l117AC/-EZ84.06-LNP-VTD [EX] transmitters and have found two (2) units with this potential defect shipped to customers. The following facility was determined to be impacted by this condition:
Entergy Operations - Fitzpatrick Purchase Order Nutherm Traceability Number Serial No.
0649 13945-O1R1 1/01 2326051 10444073 13818-OlR1 1/01 2377572 (vii) The corrective action which has been, is being, or will be taken; the name of the individual or
- organization responsible for the action; and the length of time that has been or will be taken to complete the action.
Initial actions of determining the units aff~ete were completed 12/18/2015. The impacted customer was notified of this condition 12/18/2015. Corrective actions to prevent installation of damaged transformers consist of testing the transformer prior to installation. Nutherm obtained a unit with this testing performed. Unit was found to be free of the nonconforming condition and was tested at Nutherm International, Inc. The unit was found to be defect free and conforming to all specifications and requirements. Commercial Grade Dedication of this unit was completed 12/18/2015 and shipped to Fitzpaltick on 12/18/2015. The manufacturer has completed corrective actions to prevent any further nonconforming transformers being installed into any transmitters.
(viii) Any advice related to the defect or failure to comply about the facility, activity, or basic component that has been, is being, or will be given to purchasers or licensees.
Replacement of the units listed above is suggested.
(ix) In the case of an early site permit, the entities to whom an early site permit was transferred.
,.Not applicable.
0 21(0513 M14154847068 ->13018165151 D04 Page 3 December 18, 2015 Sincerely, NUTHERM INTERNATIONAL, Inc, Wade Boli Chairman of Board WB/abs cc: Rich Apa, Supervisor, Purchaing, Entergy Operations - Fitzpatrick