ML17301A182: Difference between revisions

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| issue date = 03/29/1985
| issue date = 03/29/1985
| title = Responds to NRC 850228 Ltr Re Violations Noted in Insp Repts 50-335/85-04 & 50-389/85-04.Corrective Actions:Pump & Valve Summary Book Updated to Indicate Current Status of Surveillance & Test Activities of safety-related Equipment
| title = Responds to NRC 850228 Ltr Re Violations Noted in Insp Repts 50-335/85-04 & 50-389/85-04.Corrective Actions:Pump & Valve Summary Book Updated to Indicate Current Status of Surveillance & Test Activities of safety-related Equipment
| author name = WILLIAMS J W
| author name = Williams J
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name = GRACE J N
| addressee name = Grace J
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| docket = 05000335, 05000389
| docket = 05000335, 05000389
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| page count = 3
| page count = 3
}}
}}
See also: [[followed by::IR 05000335/1985004]]


=Text=
=Text=
{{#Wiki_filter:~5APg3~9,c/7FLORIDAPOWER&LIGHTCOMPANYNN291S86L-85-127Dr.3.NelsonGraceRegionalAdministrator,RegionIIU.S.NuclearRegulatoryCommission,Suite2900101MariettaStreetN.W.Atlanta,Georgia30323DearDr.Grace:Re:St.LucieUnits1and2DocketNos.50-335,50-389InsectionReort335/85-00and389/85-00FloridaPower4LightCompanyhasreviewedthesubjectinspectionreportandaresponseisattached.Thereisnoproprietaryinformationinthereport.Verytrulyyours,IGroupViresidentNuclearEnergy3WW/SAY/jsAttachmentcc:HaroldF.Reis,EsquirePNS-LI-85-125ve85082203348504-16PDRADOCK05000335PEOPlE...SERVINGPEOPLE
{{#Wiki_filter:FLORIDA POWER & LIGHT COMPANY
ATTACHMENTRe:St.Lucie:Units1and2DocketNos.-50-335,50-389IEInsectionRert335/85-00and389/85-00FindingTechnicalSpecification6.8.l.c.(Units1and2)requiresthatproceduresbeimplementedforsurveillanceandtestactivities,ofsafety-relatedequipment.Paragraphs8.2.5.Band8.2.8.AofAdministrativeProcedure0010132,theapplicableprocedureforinservicetesting(IST)ofASMEpumpsandvalves,requiresthatentriesbemadeinthecontrolroom"PumpandValveSummary"booktoindicatethecurrentstatusoftesting.Contrarytotheabove,on3anuary30,1985,procedure0010132hadnotbeenproperlyimplementedinthatentriesindicatingtestingstatushadnotbeenmadefor:Unit1Chargingpump1B,3uly1980;Unit2Hydrazinepumps2Aand2B,April-3une1980;Unit2HighPressureSafetyInjection(HPSI)pump2A,3anuary-February1980;andUnit2LowPressureSafetyInjection(LPSI)pump2A,3anuary-February1980..Response1.FPLconcurswiththefinding.2.ThereasonforthefindingwaspersonneloversightinthattheentrieswerenotmadeinPumpandValveSummaryBooktoindicatethecurrentstatusofthetestingasrequiredbyprocedure.3.ThePumpandValveSummaryBookhasbeenupdatedtoindicatethecurrentstatusofsurveillanceandtestactivitiesofsafety-relatedequipment.0.FPLismakingappropriateprocedurechangestomodifythemethodandresponsibilityformaintainingthepumpssummarydata.5.Fullcomplianceisexpectedtobeachievedby3une30,1985.
                                  ~5 APg 3
}}
                                                ~9,   c/         NN 2 9 7              1S86 L-85-127 Dr. 3. Nelson Grace Regional Administrator, Region II U. S. Nuclear Regulatory Commission, Suite 2900 101 Marietta Street N.W.
Atlanta, Georgia 30323
 
==Dear Dr. Grace:==
 
Re:   St. Lucie Units 1 and 2 Docket Nos. 50-335, 50-389 Ins ection Re ort 335/85-00 and 389/85-00 Florida Power 4 Light Company has reviewed the subject inspection report and a response is attached.
There is no proprietary information in the report.
Very truly yours, I
Group Vi      resident Nuclear Energy 3 W W/SAY/js Attachment cc:   Harold F. Reis, Esquire PNS-LI-85-125v e 8508220334 8504-16 PDR    ADOCK 05000335 PEOPlE... SERVING PEOPLE
 
ATTACHMENT Re:     St. Lucie: Units 1 and 2 Docket Nos.- 50-335, 50-389 IE Ins ection Re rt 335/85-00 and 389/85-00 Finding Technical Specification 6.8.l.c. (Units 1 and 2) requires that procedures be implemented for surveillance and test activities, of safety-related equipment.
Paragraphs      8.2.5.B and 8.2.8.A of Administrative Procedure 0010132, the applicable  procedure  for inservice testing (IST) of ASME pumps and valves, requires that entries be made in the control room "Pump and Valve Summary" book to indicate the current status of testing.
Contrary to the above, on 3anuary 30, 1985,             procedure 0010132 had not been properly implemented in that entries indicating        testing status had not been made for: Unit 1 Charging pump 1B, 3uly 1980; Unit 2      Hydrazine pumps 2A and 2B, April-3une 1980; Unit 2 High Pressure Safety Injection      (HPSI) pump 2A, 3anuary-February 1980; and Unit 2 Low Pressure Safety Injection        (LPSI) pump 2A, 3anuary-February 1980..
 
===Response===
: 1. FPL concurs with the finding.
: 2. The reason for the finding was personnel oversight in that the entries were not made in Pump and Valve Summary Book to indicate the current status of the testing as required by procedure.
: 3. The Pump and Valve Summary Book has been updated to indicate the current status of surveillance and test activities of safety-related equipment.
: 0. FPL is making appropriate procedure changes to modify the method and responsibility for maintaining the pumps summary data.
: 5. Full compliance is expected to be achieved by 3une 30, 1985.}}

Latest revision as of 11:18, 29 October 2019

Responds to NRC 850228 Ltr Re Violations Noted in Insp Repts 50-335/85-04 & 50-389/85-04.Corrective Actions:Pump & Valve Summary Book Updated to Indicate Current Status of Surveillance & Test Activities of safety-related Equipment
ML17301A182
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 03/29/1985
From: Williams J
FLORIDA POWER & LIGHT CO.
To: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17301A181 List:
References
L-85-127, NUDOCS 8505220334
Download: ML17301A182 (3)


Text

FLORIDA POWER & LIGHT COMPANY

~5 APg 3

~9, c/ NN 2 9 7 1S86 L-85-127 Dr. 3. Nelson Grace Regional Administrator, Region II U. S. Nuclear Regulatory Commission, Suite 2900 101 Marietta Street N.W.

Atlanta, Georgia 30323

Dear Dr. Grace:

Re: St. Lucie Units 1 and 2 Docket Nos. 50-335, 50-389 Ins ection Re ort 335/85-00 and 389/85-00 Florida Power 4 Light Company has reviewed the subject inspection report and a response is attached.

There is no proprietary information in the report.

Very truly yours, I

Group Vi resident Nuclear Energy 3 W W/SAY/js Attachment cc: Harold F. Reis, Esquire PNS-LI-85-125v e 8508220334 8504-16 PDR ADOCK 05000335 PEOPlE... SERVING PEOPLE

ATTACHMENT Re: St. Lucie: Units 1 and 2 Docket Nos.- 50-335, 50-389 IE Ins ection Re rt 335/85-00 and 389/85-00 Finding Technical Specification 6.8.l.c. (Units 1 and 2) requires that procedures be implemented for surveillance and test activities, of safety-related equipment.

Paragraphs 8.2.5.B and 8.2.8.A of Administrative Procedure 0010132, the applicable procedure for inservice testing (IST) of ASME pumps and valves, requires that entries be made in the control room "Pump and Valve Summary" book to indicate the current status of testing.

Contrary to the above, on 3anuary 30, 1985, procedure 0010132 had not been properly implemented in that entries indicating testing status had not been made for: Unit 1 Charging pump 1B, 3uly 1980; Unit 2 Hydrazine pumps 2A and 2B, April-3une 1980; Unit 2 High Pressure Safety Injection (HPSI) pump 2A, 3anuary-February 1980; and Unit 2 Low Pressure Safety Injection (LPSI) pump 2A, 3anuary-February 1980..

Response

1. FPL concurs with the finding.
2. The reason for the finding was personnel oversight in that the entries were not made in Pump and Valve Summary Book to indicate the current status of the testing as required by procedure.
3. The Pump and Valve Summary Book has been updated to indicate the current status of surveillance and test activities of safety-related equipment.
0. FPL is making appropriate procedure changes to modify the method and responsibility for maintaining the pumps summary data.
5. Full compliance is expected to be achieved by 3une 30, 1985.