ML17308A228: Difference between revisions

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| issue date = 05/29/1986
| issue date = 05/29/1986
| title = Forwards Response to Violations Noted in Insp Repts 50-335/86-07 & 50-389/86-06.Corrective Actions:Procedure Changes Generated to Enhance Schedule of Surveillances
| title = Forwards Response to Violations Noted in Insp Repts 50-335/86-07 & 50-389/86-06.Corrective Actions:Procedure Changes Generated to Enhance Schedule of Surveillances
| author name = WOODY C O
| author name = Woody C
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name = GRACE J N
| addressee name = Grace J
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| docket = 05000335, 05000389
| docket = 05000335, 05000389
Line 14: Line 14:
| page count = 5
| page count = 5
}}
}}
See also: [[followed by::IR 05000335/1986007]]


=Text=
=Text=
{{#Wiki_filter:~lii{VFLORIOAPOV'lER&LIGHTCOMPANYeY2L-86-225Dr.3.NelsonCraceRegionalAdministrator,RegionIIU.S.NuclearRegulatoryCommissionSuite2900101MariettaStreet,N.V/.Atlanta,Ceorgia30323DearDr.Crace:Re:St.LucieUnit1and2DocketNos.50-335and50-389InsectionReort86-07and86-06FloridaPowerRLightCompanyhasreviewedthesubjectinspectionreport,andaresponseisattached.Thereisnoproprietaryinformationinthereport.Verytrulyyours,C.O.%'oodyGroupVicePresidentNuclearEnergyCOW/SAV:deAttachmentcc:HaroldF.Reis,EsquirePNS-LI-86-1698606100307860529PDRADOCN050003358PDRL3:1PEOPLE...SERVINGPEOPLI.  
{{#Wiki_filter:~
ATTACHMENTL-86-225Re:St.LucieUnitIand2DocketNos.50-335and50-389InsectionReort86-07and86-06FINDINGUnitsIand2TechnicalSpecification(TS)6.8.1.crequiresthatproceduresbeimplementedforsurveillanceandtestactivitiesofsafety-relatedequipment.Contrarytotheabove,AdministrativeOperatingProceduresIand2-0010125,ScheduleofPeriodic,TestsChecksandCalibrationsand0010127,ReactorEngineeringScheduleofPeriodicTestsandReports,werenotadequatelyimplementedinthatthefollowingsurveillancetestswerenotperformedwithinthespecifiedtimeintervals.a.OnSeptember29,1985,the25percenttimeextensionwasexceededforthequarterlymainsteamisolationvalve(MSIV)part-strokesurveillancetestrequriedbyUnitITS0.7.1.5.b.On3anuary10,1986,the25percenttimeextensionwasexceededfortheautomaticactuationlogicmonthlysurveillancetest,requiredbyUnit2TSTable0.3-2,fortheauxiliaryfeedwateractuationsystem(AFAS).c.OnFebruary7,1986,the25percenttimeextensionwasexceededforthemonthlysetpointcalculationandadjustmentofthefixedincorealarmsystemrequiredbyUnit2TS0.2.1.0.d.OnFebruary13,1986,the25percenttimeextensionwasexceededforthesemi-annualengineeredsafetyfeaturesactuationsystem(ESFAS)relaysurveillancetestrequiredbyUnit2TSTable0.3-2.L3:I  
lii {                           FLORIOA POV'lER & LIGHT COMPANY V
eY2 L-86-225 Dr. 3. Nelson Crace Regional Administrator, Region II U. S. Nuclear Regulatory Commission Suite 2900 101 Marietta Street, N.V/.
L-86-225Re:St.LucieUnit1and2DocketNos.50-335and50-389InsectionReort86-07and86-06Page2RESPONSE1.FPLconcurswiththeviolation.2.Thereasonfortheviolationisasfollows:a.Thequarterlymainsteamisolationvalve(MSIV)part-strokesurveillancetestrequiredbyUnit1TechnicalSpecification0.7.1.5exceededthe25'6extensiontimeduetoacognitivepersonnelerror.Theoperatorreviewedonlythesemi-annual,annual,and18-monthsurveillances,andinadvertentlyneglectedthequarterlylist.b.TheAuxiliaryFeedwaterActuationLogicmonthlysurveillancetestrequiredbyUnit2TechnicalSpecificationTable0.3-2exceededthe25%extensiontimeduetoacognitivepersonnelerror.InstrumentationandControlDepartmentpersonnelerroneouslyappliedadatetothePlantcworkOrder(PNO)forcompletionthatwasinexcessofthe2596extension.c.TheFixedIncoreAlarmSystemmonthlysetpointcalculationandadjustmentrequiredbyUnit2TechnicalSpecification0.2.1.0exceededthe25'Yoextensiontimeduetoanon-licensedutilitypersonnelerror.Thepersonnelerrorwasanoversightinreadingthesurveillanceschedule.d.TheEngineeredSafetyFeaturesActuationSystem(ESFAS)relaysemi-annualsurveillancetestrequiredbyUnit2TechnicalSpecificationsTable0.3-2exceededthe259oextensiontimeduetoanoversightinincludingthissurveillanceinthesemi-annualchecksheet.3.Thecorrectivestepstakenweretoperformtherequiredsurveillances.Thosepersonnelinvolvedwerecounseledonthenecessitytoperformsurveillancesduringtherequiredinterval.Thoseproceduresinvolvedwererevisedasnecessary.L3:1  
Atlanta, Ceorgia 30323
L-86-225Re:St.LucieUnitIand2DocketHos.50-335and50-389InsectionReort86-07and86-06Page30.Thecorrectivestepswhichwillorhavebeentakentoavoidfurtherviolationswere:a.QualityControlperformedareviewoftheirlogtoidentifyanyproblemareas,especiallyUnit2,andgeneratedprocedurechangestoenhancethescheduleofsurveillances.b.FPLconsidersthisitemcomplete,however,basedonSt.Lucie'spastperformance,wehavereviewedthesurveillanceprogramandfoundthatthefollowingprogramaticchangesarenecessarytoensurecontinuedhighperformance:l.EachDepartmentwillhavetheirownschedulingprocedure.2.Anindividualwillbeassignedineachdepartmenttooverseethesurveillancecompletion.5.Fullcomplianceforitem3wasachievedonApril8,1986.ItemOaabovewascompletedonMay9,1986.ItemObisexpectedtobecompletedonAugust15,1986.L3:1
 
}}
==Dear Dr. Crace:==
 
Re: St. Lucie Unit 1 and 2 Docket Nos. 50-335 and 50-389 Ins ection Re ort 86-07 and 86-06 Florida Power R Light Company has reviewed the subject inspection report, and    a response is attached.
There is no proprietary information in the report.
Very truly yours, C. O. %'oody Group Vice President Nuclear Energy COW/SA V:de Attachment cc: Harold F. Reis, Esquire P NS-LI-86-169 8606100307 860529 PDR    ADOCN 05000335 8                      PDR L3:1                                                            PEOPLE...           PEOPLI.
 
ATTACHMENT                          L-86-225 Re: St. Lucie Unit I and 2 Docket Nos. 50-335 and 50-389 Ins ection Re ort 86-07 and 86-06 FINDING Units I and 2 Technical Specification (TS) 6.8.1.c requires that procedures      be implemented for surveillance and test activities of safety-related equipment.
Contrary to the above, Administrative Operating Procedures I and 2-0010125, Schedule  of Periodic, Tests Checks and Calibrations and 0010127, Reactor Engineering Schedule of Periodic Tests and Reports, were not adequately implemented in that the following surveillance tests were not performed within the specified time intervals.
: a. On September    29, 1985, the 25 percent time extension was exceeded for the quarterly main steam isolation valve (MSIV) part-stroke surveillance test requried by Unit I TS 0.7.1.5.
: b. On 3anuary    10, 1986, the 25 percent time extension was exceeded for the automatic actuation logic monthly surveillance test, required by Unit 2 TS Table 0.3-2, for the auxiliary feedwater actuation system (AFAS).
: c. On February 7, 1986, the 25 percent time extension was exceeded for the monthly setpoint calculation and adjustment of the fixed incore alarm system required by Unit 2 TS 0.2.1.0.
: d. On February    13, 1986, the 25 percent time extension was exceeded for the semi-annual engineered safety features actuation system (ESFAS) relay surveillance test required by Unit 2 TS Table 0.3-2.
L3:I
 
L-86-225 Re: St. Lucie Unit 1 and 2 Docket Nos. 50-335 and 50-389 Ins ection Re ort 86-07 and 86-06 Page 2
 
===RESPONSE===
: 1. FPL concurs with the violation.
: 2. The reason  for the violation is as follows:
: a. The quarterly main steam isolation valve (MSIV) part-stroke surveillance test required by Unit 1 Technical Specification 0.7.1.5 exceeded the 25'6 extension time due to a cognitive personnel error. The operator reviewed only the semi-annual,         annual, and 18-month surveillances,     and inadvertently neglected the quarterly list.
: b. The  Auxiliary Feedwater Actuation Logic monthly surveillance test required by Unit 2 Technical Specification Table 0.3-2 exceeded the 25%
extension time due to a cognitive personnel error. Instrumentation and Control Department personnel erroneously applied a date to the Plant cwork Order (PNO) for completion that was in excess of the 2596 extension.
: c. The  Fixed Incore Alarm System monthly setpoint calculation and adjustment required by Unit 2 Technical Specification 0.2.1.0 exceeded the 25'Yo extension time due to a non-licensed utility personnel error. The personnel error was an oversight in reading the surveillance schedule.
: d. The Engineered Safety Features Actuation System (ESFAS) relay semi-annual surveillance test required by Unit 2 Technical Specifications Table 0.3-2 exceeded the 259o extension time due to an oversight in including this surveillance in the semi-annual check sheet.
: 3. The corrective steps taken were to perform the required surveillances. Those personnel involved were counseled on the necessity to perform surveillances during the required interval. Those procedures involved were revised as necessary.
L3:1
 
L-86-225 Re: St. Lucie Unit I and 2 Docket Hos. 50-335 and 50-389 Ins ection Re ort 86-07 and 86-06 Page 3
: 0. The corrective steps which    will or have been taken to avoid further violations were:
: a. Quality Control performed a review of their log to identify any problem areas, especially Unit 2, and generated procedure changes to enhance the schedule of surveillances.
: b. FPL considers    this item complete, however, based on St. Lucie's past performance, we have reviewed the surveillance program and found that the following programatic changes are necessary to ensure continued high performance:
: l. Each Department will have their own scheduling procedure.
: 2. An individual will be assigned in each department to oversee the surveillance completion.
: 5. Full compliance for item 3 was achieved on April 8, 1986. Item Oa above was completed on May 9, 1986. Item Ob is expected to be completed on August 15, 1986.
L3:1}}

Latest revision as of 08:59, 29 October 2019

Forwards Response to Violations Noted in Insp Repts 50-335/86-07 & 50-389/86-06.Corrective Actions:Procedure Changes Generated to Enhance Schedule of Surveillances
ML17308A228
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 05/29/1986
From: Woody C
FLORIDA POWER & LIGHT CO.
To: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
L-86-225, NUDOCS 8606100307
Download: ML17308A228 (5)


Text

~

lii { FLORIOA POV'lER & LIGHT COMPANY V

eY2 L-86-225 Dr. 3. Nelson Crace Regional Administrator, Region II U. S. Nuclear Regulatory Commission Suite 2900 101 Marietta Street, N.V/.

Atlanta, Ceorgia 30323

Dear Dr. Crace:

Re: St. Lucie Unit 1 and 2 Docket Nos. 50-335 and 50-389 Ins ection Re ort 86-07 and 86-06 Florida Power R Light Company has reviewed the subject inspection report, and a response is attached.

There is no proprietary information in the report.

Very truly yours, C. O. %'oody Group Vice President Nuclear Energy COW/SA V:de Attachment cc: Harold F. Reis, Esquire P NS-LI-86-169 8606100307 860529 PDR ADOCN 05000335 8 PDR L3:1 PEOPLE... PEOPLI.

ATTACHMENT L-86-225 Re: St. Lucie Unit I and 2 Docket Nos. 50-335 and 50-389 Ins ection Re ort 86-07 and 86-06 FINDING Units I and 2 Technical Specification (TS) 6.8.1.c requires that procedures be implemented for surveillance and test activities of safety-related equipment.

Contrary to the above, Administrative Operating Procedures I and 2-0010125, Schedule of Periodic, Tests Checks and Calibrations and 0010127, Reactor Engineering Schedule of Periodic Tests and Reports, were not adequately implemented in that the following surveillance tests were not performed within the specified time intervals.

a. On September 29, 1985, the 25 percent time extension was exceeded for the quarterly main steam isolation valve (MSIV) part-stroke surveillance test requried by Unit I TS 0.7.1.5.
b. On 3anuary 10, 1986, the 25 percent time extension was exceeded for the automatic actuation logic monthly surveillance test, required by Unit 2 TS Table 0.3-2, for the auxiliary feedwater actuation system (AFAS).
c. On February 7, 1986, the 25 percent time extension was exceeded for the monthly setpoint calculation and adjustment of the fixed incore alarm system required by Unit 2 TS 0.2.1.0.
d. On February 13, 1986, the 25 percent time extension was exceeded for the semi-annual engineered safety features actuation system (ESFAS) relay surveillance test required by Unit 2 TS Table 0.3-2.

L3:I

L-86-225 Re: St. Lucie Unit 1 and 2 Docket Nos. 50-335 and 50-389 Ins ection Re ort 86-07 and 86-06 Page 2

RESPONSE

1. FPL concurs with the violation.
2. The reason for the violation is as follows:
a. The quarterly main steam isolation valve (MSIV) part-stroke surveillance test required by Unit 1 Technical Specification 0.7.1.5 exceeded the 25'6 extension time due to a cognitive personnel error. The operator reviewed only the semi-annual, annual, and 18-month surveillances, and inadvertently neglected the quarterly list.
b. The Auxiliary Feedwater Actuation Logic monthly surveillance test required by Unit 2 Technical Specification Table 0.3-2 exceeded the 25%

extension time due to a cognitive personnel error. Instrumentation and Control Department personnel erroneously applied a date to the Plant cwork Order (PNO) for completion that was in excess of the 2596 extension.

c. The Fixed Incore Alarm System monthly setpoint calculation and adjustment required by Unit 2 Technical Specification 0.2.1.0 exceeded the 25'Yo extension time due to a non-licensed utility personnel error. The personnel error was an oversight in reading the surveillance schedule.
d. The Engineered Safety Features Actuation System (ESFAS) relay semi-annual surveillance test required by Unit 2 Technical Specifications Table 0.3-2 exceeded the 259o extension time due to an oversight in including this surveillance in the semi-annual check sheet.
3. The corrective steps taken were to perform the required surveillances. Those personnel involved were counseled on the necessity to perform surveillances during the required interval. Those procedures involved were revised as necessary.

L3:1

L-86-225 Re: St. Lucie Unit I and 2 Docket Hos. 50-335 and 50-389 Ins ection Re ort 86-07 and 86-06 Page 3

0. The corrective steps which will or have been taken to avoid further violations were:
a. Quality Control performed a review of their log to identify any problem areas, especially Unit 2, and generated procedure changes to enhance the schedule of surveillances.
b. FPL considers this item complete, however, based on St. Lucie's past performance, we have reviewed the surveillance program and found that the following programatic changes are necessary to ensure continued high performance:
l. Each Department will have their own scheduling procedure.
2. An individual will be assigned in each department to oversee the surveillance completion.
5. Full compliance for item 3 was achieved on April 8, 1986. Item Oa above was completed on May 9, 1986. Item Ob is expected to be completed on August 15, 1986.

L3:1