ML18153C070: Difference between revisions

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{{#Wiki_filter:* OPERATING DATA REPORT
{{#Wiki_filter:*
* CORRECTED COPY* 01/05/90 DOCKET NO.: 50-281 DATE: -1,...,0,.....,./.,,..,05,,.....,/""'"89=------
* CORRECTED COPY*
COMPLETED BY: Linda A. Warren TELEPHONE:  
01/05/90 OPERATING DATA REPORT DOCKET NO.: 50-281 DATE: -1,...,0,.....,./.,,..,05,,.....,/""'"89=------
--,.,,(8'""'"0-=-4)...,,3-=57=--_-=3.,,..,18""""4-x_,4=7= OPERATING STATUS NOTES 1. Unit Name: Surry Unit 2 2. Reporting Period: Sept 1 -30, 1989 3. Licensed Thermal Power (MWt): 2441 4. Nameplate Rating (Gross MWe): 847.5 5. Design Electrical Rating (Net MWe): 788 6. Maximum Dependable Capacity (Gross MWe): 820 7. Maximum Dependable Capacity (Net MWe): .....,7=8=1--
COMPLETED BY: Linda A. Warren TELEPHONE: --,., (8'""'"0-=-4).. , 3-=57=--_-=3., . ,18""""4-x_,4=7= OPERATING STATUS                                 NOTES
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: -----------------------
: 1. Unit Name:         Surry Unit 2
: 9. Power Level To Which Restricted, If Any (Net MWe): 10. Reason For Restrictions, If Any: -----------
: 2. Reporting Period: Sept 1 - 30, 1989
------------------
: 3. Licensed Thermal Power (MWt): 2441
THIS MONTH YTD CUMULATIVE
: 4. Nameplate Rating (Gross MWe): 847.5
: 11. Hours In Reporting Period 720.0 6551.0 143927.0 12. Number of Hours Reactor Was Critical 327.1
: 5. Design Electrical Rating (Net MWe):       788
: 6. Maximum Dependable Capacity (Gross MWe): 820
: 7. Maximum Dependable Capacity (Net MWe): .....,7=8=1--
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
                          -----------------------
: 9. Power Level To Which Restricted, If Any (Net MWe):
: 10. Reason For Restrictions, If Any:                       -----------
                                      ------------------
THIS MONTH           YTD                     CUMULATIVE
: 11. Hours In Reporting Period                     720.0         6551.0                           143927.0
: 12. Number of Hours Reactor Was Critical           327.1
* 327.1
* 327.1
* 90021.4
* 90021.4 *
* 13. Reactor Reserve Shutdown Hours 0 0 328.1 14. Hours Generator On-Line 189.2
: 13. Reactor Reserve Shutdown Hours                       0                     0                           328.1
: 14. Hours Generator On-Line                       189.2
* 189. 2
* 189. 2
* 88482.2
* 88482.2 *
* 15. Unit Reserve Shutdown Hours 0 0 0 16. Gross Thermal Energy Generated (MWH) 187755.9 187755. 9 206928192.0
: 15. Unit Reserve Shutdown Hours                         0                     0                                     0
: 17. Gross Electrical Energy Generatecf"TMWH) 46725.0 46725. 0 67182969.0
: 16. Gross Thermal Energy Generated (MWH)       187755.9       187755. 9 206928192.0
: 18. Net Electrical Energy Generated (MWH) 40831. 0 40831. 0 63688209.0
: 17. Gross Electrical Energy Generatecf"TMWH)   46725.0         46725. 0                     67182969.0
: 19. Unit Service Factor 26.3% 2.9% 61. 5% 20. Unit Available Factor 26.3% 2.9% 61. 5% 21. Unit Capacity Factor (Using MDC Net) 7.3% .8% 56.5%* 22. Unit Capacity Factor (Using DER Net) 7.2% .8% 56.2% 23. Unit Forced Rate 34.2%* 34.2%* 15.0%* 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each): 25. If Shut Down at End of Report Period Estimated Date of Startup: ---~=--26. Unit In Test Status (Prior to Commercial Operation):
: 18. Net Electrical Energy Generated (MWH)       40831. 0       40831. 0                     63688209.0
FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION UNIT SHUTDOWN AND POWER REDUCTION REPORT MONTH: SEPTEMBER 1989 METHOD OF LICENSEE CORRECTED COPY 12/ 11/89* , DOCKET NO.: 50-281 UNIT NAME: -s=-u-r-ry___,..U__,ni....,.t-2=----
: 19. Unit Service Factor                             26.3%                 2.9%                                 61. 5%
DATE: 10/05/89 COMPLETED BY: Christle Arney TELEPHONE:
: 20. Unit Available Factor                           26.3%                 2.9%                               61. 5%
804-357-3184 x477 DURATION SHUTTING EVENT SYSTEM COMPONENT CAUSE & CORRECTIVE ACTION TO PREVENT RECURRENT NO. DATE TYPE(l) (HOURS) REASON(2)
: 21. Unit Capacity Factor (Using MDC Net)             7.3%                     .8%                             56.5%*
DOWN REACTOR{3)
: 22. Unit Capacity Factor (Using DER Net)             7.2%                     .8%                             56.2%
REPORT# CODE(4) CODE(5) ~6 09-01-89 S 432.6 C 1,3 *C-10-2 09-19-89 F 20.5 G 3
: 23. Unit Forced Rate                               34.2%*             34.2%*                                 15.0%*
* 09-22-89 F 19.8 B 4
: 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
* 09-28-89 F 57.9 B 4 (1) F: Forced S: Scheduled (2) REASON: A -Equipment Failure (Explain)
: 25. If Shut Down at End of Report Period Estimated Date of Startup:
B -Maintenance or Test C -Refueling D -Regulatory Restriction E -Operator Training & License Examination F -Administrative G -Operational Error (Explain)
: 26. Unit In Test Status (Prior to Commercial Operation):       FORECAST             ---~=--  ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
H -Other (Explain) 281/88-22 281/89-10 J~ N/A N/A (3) METHOD: Manual TA TA 2 -Manual Scram. 3 -Automatic Scram. 4 -Other (Explain)
 
SG TB TB (4) Unit shutdown for ing Outage, automatic reactor trip. 1 B 1 Steam Generator Lo-Lo Level while attempting to place Main Feed Regulator Valves inservice.
CORRECTED COPY 12/ 11/89* ,
Unit taken off line for Turbine Overspeed Test and Balancing of Main Turbine. Reactor remained Critical.
DOCKET NO.: 50-281 UNIT SHUTDOWN AND POWER REDUCTION                              UNIT NAME: -s=-u-r-ry___,..U__,ni....,.t-2=----
Ulnit taken off line for Turbine Balancing.
DATE: 10/05/89 COMPLETED BY: Christle Arney REPORT MONTH:  SEPTEMBER 1989                                TELEPHONE: 804-357-3184 x477 METHOD OF        LICENSEE                            CAUSE & CORRECTIVE DURATION             SHUTTING         EVENT     SYSTEM   COMPONENT       ACTION TO PREVENT NO. DATE     TYPE(l)   (HOURS) REASON(2) DOWN REACTOR{3) REPORT# CODE(4)         CODE(5)         RECURRENT
Reactor remained critical.
~6     09-01-89 S         432.6     C         1,3             281/88-22                            Unit shutdown for Refuel-ing Outage,            automatic reactor trip.
Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG 0161) (5) Exhibit 1 -Same Source}}
*C-10-2 09-19-89 F         20.5       G         3               281/89-10 J~       SG             1 B1 Steam Generator Lo-Lo Level while attempting to place Main Feed Regulator Valves inservice.
* 09-22-89 F        19.8      B        4              N/A        TA        TB              Unit taken off line for Turbine Overspeed Test and Balancing of Main Turbine.
Reactor remained Critical.
* 09-28-89 F        57.9      B        4              N/A        TA        TB              Ulnit taken off line for Turbine Balancing. Reactor remained critical.
(1)              (2)                                            (3)                            (4)
F: Forced        REASON:                                        METHOD:
S: Scheduled    A - Equipment Failure (Explain)              Manual                Exhibit G - Instructions for B - Maintenance or Test                        2 - Manual Scram.        Preparation of Data Entry Sheets C - Refueling                                  3 - Automatic Scram.      for Licensee Event Report (LER)
D - Regulatory Restriction                    4 - Other (Explain)      File (NUREG 0161)
E - Operator Training &License Examination F - Administrative                                                                    (5)
G - Operational Error (Explain)
H - Other (Explain)                                                      Exhibit 1 - Same Source}}

Revision as of 00:22, 21 October 2019

Corrected Operating Data Rept for Sept 1989 for Surry Unit 2
ML18153C070
Person / Time
Site: Surry  Dominion icon.png
Issue date: 09/30/1989
From: Warren L
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
Shared Package
ML18152A486 List:
References
NUDOCS 9001230020
Download: ML18153C070 (2)


Text

  • CORRECTED COPY*

01/05/90 OPERATING DATA REPORT DOCKET NO.: 50-281 DATE: -1,...,0,.....,./.,,..,05,,.....,/""'"89=------

COMPLETED BY: Linda A. Warren TELEPHONE: --,., (8'""'"0-=-4).. , 3-=57=--_-=3., . ,18""""4-x_,4=7= OPERATING STATUS NOTES

1. Unit Name: Surry Unit 2
2. Reporting Period: Sept 1 - 30, 1989
3. Licensed Thermal Power (MWt): 2441
4. Nameplate Rating (Gross MWe): 847.5
5. Design Electrical Rating (Net MWe): 788
6. Maximum Dependable Capacity (Gross MWe): 820
7. Maximum Dependable Capacity (Net MWe): .....,7=8=1--
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:

9. Power Level To Which Restricted, If Any (Net MWe):
10. Reason For Restrictions, If Any: -----------

THIS MONTH YTD CUMULATIVE

11. Hours In Reporting Period 720.0 6551.0 143927.0
12. Number of Hours Reactor Was Critical 327.1
  • 327.1
  • 90021.4 *
13. Reactor Reserve Shutdown Hours 0 0 328.1
14. Hours Generator On-Line 189.2
  • 189. 2
  • 88482.2 *
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 187755.9 187755. 9 206928192.0
17. Gross Electrical Energy Generatecf"TMWH) 46725.0 46725. 0 67182969.0
18. Net Electrical Energy Generated (MWH) 40831. 0 40831. 0 63688209.0
19. Unit Service Factor 26.3% 2.9% 61. 5%
20. Unit Available Factor 26.3% 2.9% 61. 5%
21. Unit Capacity Factor (Using MDC Net) 7.3% .8% 56.5%*
22. Unit Capacity Factor (Using DER Net) 7.2% .8% 56.2%
23. Unit Forced Rate 34.2%* 34.2%* 15.0%*
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
25. If Shut Down at End of Report Period Estimated Date of Startup:
26. Unit In Test Status (Prior to Commercial Operation): FORECAST ---~=-- ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

CORRECTED COPY 12/ 11/89* ,

DOCKET NO.: 50-281 UNIT SHUTDOWN AND POWER REDUCTION UNIT NAME: -s=-u-r-ry___,..U__,ni....,.t-2=----

DATE: 10/05/89 COMPLETED BY: Christle Arney REPORT MONTH: SEPTEMBER 1989 TELEPHONE: 804-357-3184 x477 METHOD OF LICENSEE CAUSE & CORRECTIVE DURATION SHUTTING EVENT SYSTEM COMPONENT ACTION TO PREVENT NO. DATE TYPE(l) (HOURS) REASON(2) DOWN REACTOR{3) REPORT# CODE(4) CODE(5) RECURRENT

~6 09-01-89 S 432.6 C 1,3 281/88-22 Unit shutdown for Refuel-ing Outage, automatic reactor trip.

  • C-10-2 09-19-89 F 20.5 G 3 281/89-10 J~ SG 1 B1 Steam Generator Lo-Lo Level while attempting to place Main Feed Regulator Valves inservice.

Reactor remained Critical.

  • 09-28-89 F 57.9 B 4 N/A TA TB Ulnit taken off line for Turbine Balancing. Reactor remained critical.

(1) (2) (3) (4)

F: Forced REASON: METHOD:

S: Scheduled A - Equipment Failure (Explain) Manual Exhibit G - Instructions for B - Maintenance or Test 2 - Manual Scram. Preparation of Data Entry Sheets C - Refueling 3 - Automatic Scram. for Licensee Event Report (LER)

D - Regulatory Restriction 4 - Other (Explain) File (NUREG 0161)

E - Operator Training &License Examination F - Administrative (5)

G - Operational Error (Explain)

H - Other (Explain) Exhibit 1 - Same Source