IR 05000352/2007004: Difference between revisions

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{{Adams|number = ML073180045}}
{{Adams
| number = ML073180045
| issue date = 11/13/2007
| title = IR 05000352-07-004, 05000353-07-004; on 07/01/07-09/30/07; Limerick Generating Station, Units 1 and 2; Routine Integrated Report
| author name = Krohn P G
| author affiliation = NRC/RGN-I/DRP/PB4
| addressee name = Pardee C G
| addressee affiliation = Exelon Generation Co, LLC, Exelon Nuclear
| docket = 05000352, 05000353
| license number = NPF-039, NPF-085
| contact person = KROHN, PG
| document report number = IR-07-004
| document type = Inspection Report, Letter
| page count = 25
}}


{{IR-Nav| site = 05000352 | year = 2007 | report number = 004 }}
{{IR-Nav| site = 05000352 | year = 2007 | report number = 004 }}


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I475 ALLENDALE ROADKING OF PRUSSIA, PENNSYLVANIA 19406-1415 November 13, 2007Mr. Charles G. PardeePresident and CNO Exelon Nuclear Exelon Generation Company, LLC 200 Exelon Way Kennett Square, PA 19348
[[Issue date::November 13, 2007]]
 
Mr. Charles G. PardeePresident and CNO Exelon Nuclear Exelon Generation Company, LLC 200 Exelon Way Kennett Square, PA 19348


SUBJECT: LIMERICK GENERATING STATION - NRC INTEGRATED INSPECTIONREPORT 05000352/2007004 AND 05000353/2007004
SUBJECT: LIMERICK GENERATING STATION - NRC INTEGRATED INSPECTIONREPORT 05000352/2007004 AND 05000353/2007004
Line 27: Line 38:


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
......................................................iii
IR 05000352/2007-004, 05000353/2007-004; 07/01/2007 - 09/30/2007; Limerick GeneratingStation, Units 1 and 2; Routine Integrated Report.The report covered a three-month period of inspection by resident inspectors and announcedinspections by reactor inspectors. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight," Revision 4, dated December 2006.A.
 
===NRC-Identified and Self-Revealing Findings===
No findings of significance were identified.
 
===B. Licensee-Identified Violations===
 
None.


=REPORT DETAILS=
=REPORT DETAILS=
............................................................1
Summary of Plant StatusUnit 1 began this inspection period operating at full rated thermal power. On August 16, 2007,reactor power was reduced to 20 percent and the main generator was removed from service to repair the generator output number 11 disconnect switch. On August 17, 2007, the disconnect switch repairs were completed and the main generator was returned to service. Unit 1 returned to 100 percent power on August 18, 2007. With the exception of a planned end of summer load drop to 85 percent power on September 8, 2007, Unit 1 remained at full power for the remainder of the period.
 
Unit 2 began this inspection period operating at full rated thermal power. On August 6, 2007, reactor power decreased to 75 percent due to an unplanned speed reduction on the 2B reactor recirculation pump. The pump speed change was due to a recirculation motor generator electronic card failure. The card was replaced and Unit 2 was returned to 100 percent power later in the day. With the exception of a planned end of summer load drop to 60 percent power on September 15, 2007, Unit 2 remained at full power for the remainder of the period.


==REACTOR SAFETY==
==REACTOR SAFETY==
...........................................................11R01Adverse Weather Protection .........................................1
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weather Protection (71111.01 - 1 system sample)


====a. Inspection Scope====
The inspectors evaluated Exelon's preparations and protection for summer weather. OnJuly 10, 2007, the inspectors walked down Unit 1 and Unit 2 main generators and main transformers during hot weather and a grid heavy load voltage condition. The documents reviewed are listed in the Attachment.
====b. Findings====
No findings of significance were identified.
{{a|1R04}}
{{a|1R04}}
==1R04 Equipment Alignment ..............................................1==
==1R04 Equipment Alignment (71111.04)==


{{a|1R05}}
===.1 Partial Walkdown===
==1R05 Fire Protection....................................................2==
{{IP sample|IP=IP 71111.04Q|count=4}}


{{a|1R06}}
====a. Inspection Scope====
==1R06 Flood Protection Measures ..........................................31R11Licensed Operator Requalification Program .............................3==
The inspectors performed four partial walkdowns of plant systems to verify the operabilityof redundant or diverse trains and components when safety equipment in the opposite train was either inoperable, undergoing surveillance testing, or potentially degraded. The inspectors used plant Technical Specifications (TS), Exelon operating procedures, plantpiping and instrumentation drawings (P&IDs), and the Updated Final Safety Analysis Report (USFAR) as guidance for conducting partial system walkdowns. The inspectors reviewed the alignment of system valves and electrical breakers to ensure proper in-service or standby configurations as described in plant procedures and drawings.


{{a|1R12}}
2Enclosure During the walkdown, the inspectors evaluated material condition and generalhousekeeping of the system and adjacent spaces. The documents reviewed are listed in the Attachment. The inspectors performed walkdowns of the following systems:*Unit 1 High Pressure Coolant Injection (HPCI) system;*Unit 1 D-13 Emergency Diesel Generator (EDG);
==1R12 Maintenance Effectiveness ..........................................41R13Maintenance Risk Assessments and Emergent Work Control................41R15Operability Evaluations .............................................51R19Post-Maintenance Testing ..........................................51R22Surveillance Testing ...............................................6==
*Unit 1 Standby Liquid Control System; and
*Unit 1 Reactor Core Isolation Cooling (RCIC)..2Complete System Walkdown  (71111.04S - 1 sample)The inspectors conducted one complete walkdown of the Unit 1 and Unit 2 Control RodDrive (CRD) systems to verify functional capability of the system. The inspectors used plant TS, Exelon operating procedures, P&IDs, the UFSAR, and past surveillance tests as guidance for conducting the complete system walkdown. The inspectors reviewed the alignment of system valves, position of electrical breakers and settings of the system flow controller to ensure proper system configuration as described in plant procedures and drawings. During the walkdown, the inspectors evaluated the material condition and general housekeeping of the system and open issue reports associated with the system.


{{a|1R23}}
The walkdown also included an evaluation of system piping, supports, and component foundations to ensure they were not degraded. The documents reviewed are listed in the
==1R23 Temporary Plant Modifications .......................................6==
.


1EP6Drill Evaluation
====b. Findings====
 
No findings of significance were identified.
==OTHER ACTIVITIES==
{{a|1R05}}
..........................................................84OA1Performance Indicator (PI) Verification .................................8 4OA3Event Followup ...................................................9 4OA6Meetings, Including Exit............................................11ATTACHMENT: 
==1R05 Fire Protection.1Fire Protection - Tours==
 
  (71111.05Q - 8 samples)
=SUPPLEMENTAL INFORMATION=
 
==KEY POINTS OF CONTACT==
..................................................A-1
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
.............................A-1
==LIST OF DOCUMENTS REVIEWED==
.......................................................................................... A-2
==LIST OF ACRONYMS==
........................................................A-8
iiiSUMMARY
: [[OF]] [[]]
FINDINGSIR 05000352/2007-004, 05000353/2007-004; 07/01/2007 - 09/30/2007; Limerick GeneratingStation, Units 1 and 2; Routine Integrated Report.The report covered a three-month period of inspection by resident inspectors and announcedinspections by reactor inspectors. The NRC's program for overseeing the safe operation of
commercial nuclear power reactors is described in
: [[NUR]] [[]]
EG-1649, "Reactor Oversight," Revision
4, dated December
: [[2006.A.N]] [[]]
: [[RC]] [[-Identified and Self-Revealing FindingsNo findings of significance were identified.B. Licensee-Identified ViolationsNone.]]
: [[REPORT]] [[]]
DETAILSSummary of Plant StatusUnit 1 began this inspection period operating at full rated thermal power. On August 16, 2007,reactor power was reduced to 20 percent and the main generator was removed from service to
repair the generator output number 11 disconnect switch. On August 17, 2007, the disconnect
switch repairs were completed and the main generator was returned to service. Unit 1 returned
to 100 percent power on August 18, 2007. With the exception of a planned end of summer load
drop to 85 percent power on September 8, 2007, Unit 1 remained at full power for the remainder
of the period.


Unit 2 began this inspection period operating at full rated thermal power. On August 6, 2007,
====a. Inspection Scope====
reactor power decreased to 75 percent due to an unplanned speed reduction on the 2B reactor
The inspectors conducted a tour of the eight areas listed below to assess the materialcondition and operational status of fire protection features. The inspectors verified that combustibles and ignition sources were controlled in accordance with Exelon's administrative procedures, fire detection and suppression equipment was available for use, and that passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out-of-service, degraded, or inoperable fire protection equipment in accordance with Exelon's fire plan. The documents reviewed are listed in the Attachment. The inspectors performed the following samples:*Main Control Room and peripheral rooms;*Unit 1 Refuel Floor;
recirculation pump. The pump speed change was due to a recirculation motor generator
electronic card failure. The card was replaced and Unit 2 was returned to 100 percent power
later in the day. With the exception of a planned end of summer load drop to 60 percent power
on September 15, 2007, Unit 2 remained at full power for the remainder of the period. 1.
: [[REACTO]] [[R]]
SAFETYCornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weather Protection (71111.01 - 1 system sample)      a.Inspection ScopeThe inspectors evaluated Exelon's preparations and protection for summer weather. OnJuly 10, 2007, the inspectors walked down Unit 1 and Unit 2 main generators and main
transformers during hot weather and a grid heavy load voltage condition. The
documents reviewed are listed in the Attachment.      b.FindingsNo findings of significance were identified.1R04Equipment Alignment (71111.04) .1    Partial Walkdown (71111.04Q - 4 samples)      a.Inspection ScopeThe inspectors performed four partial walkdowns of plant systems to verify the operabilityof redundant or diverse trains and components when safety equipment in the opposite
train was either inoperable, undergoing surveillance testing, or potentially degraded. The
inspectors used plant Technical Specifications (TS), Exelon operating procedures, plantpiping and instrumentation drawings (P&IDs), and the Updated Final Safety Analysis
Report (USFAR) as guidance for conducting partial system walkdowns. The inspectors
reviewed the alignment of system valves and electrical breakers to ensure proper
in-service or standby configurations as described in plant procedures and drawings.
2Enclosure During the walkdown, the inspectors evaluated material condition and generalhousekeeping of the system and adjacent spaces. The documents reviewed are listed in
the Attachment. The inspectors performed walkdowns of the following systems:*Unit 1 High Pressure Coolant Injection (HPCI) system;*Unit 1 D-13 Emergency Diesel Generator (EDG);
*Unit 1 Standby Liquid Control System; and
*Unit 1 Reactor Core Isolation Cooling (RCIC)..2Complete System Walkdown  (71111.04S - 1 sample)The inspectors conducted one complete walkdown of the Unit 1 and Unit 2 Control RodDrive (CRD) systems to verify functional capability of the system. The inspectors used
plant
: [[TS]] [[, Exelon operating procedures, P&]]
: [[ID]] [[s, the]]
: [[UFS]] [[]]
AR, and past surveillance tests
as guidance for conducting the complete system walkdown. The inspectors reviewed the
alignment of system valves, position of electrical breakers and settings of the system flow
controller to ensure proper system configuration as described in plant procedures and
drawings. During the walkdown, the inspectors evaluated the material condition and
general housekeeping of the system and open issue reports associated with the system.
The walkdown also included an evaluation of system piping, supports, and component
foundations to ensure they were not degraded. The documents reviewed are listed in the
Attachment.      b.FindingsNo findings of significance were identified.1R05Fire Protection.1Fire Protection - Tours  (71111.05Q - 8 samples)      a.Inspection Scope The inspectors conducted a tour of the eight areas listed below to assess the materialcondition and operational status of fire protection features. The inspectors verified that
combustibles and ignition sources were controlled in accordance with Exelon's
administrative procedures, fire detection and suppression equipment was available for
use, and that passive fire barriers were maintained in good material condition. The
inspectors also verified that station personnel implemented compensatory measures for
out-of-service, degraded, or inoperable fire protection equipment in accordance with
Exelon's fire plan. The documents reviewed are listed in the Attachment. The inspectors
performed the following samples:*Main Control Room and peripheral rooms;*Unit 1 Refuel Floor;
*Unit 2 Refuel Floor;
*Unit 2 Refuel Floor;
*Unit 1 220 KV Switchyard;
*Unit 1 220 KV Switchyard;
*Unit 1 and Unit 2 Static Inverter compartments;
*Unit 1 and Unit 2 Static Inverter compartments;
*Unit 1 and Unit 2 Standby Gas Treatment system filter compartments and accessarea;
*Unit 1 and Unit 2 Standby Gas Treatment system filter compartments and accessarea; 3Enclosure *Control Room Structure fan room, Elevation 304; and*Unit 1 D14 Diesel Generator Room..2Fire Protection - Drill Observation (71111.05A - 1 sample)
3Enclosure *Control Room Structure fan room, Elevation 304; and*Unit 1 D14 Diesel Generator Room..2Fire Protection - Drill Observation (71111.05A - 1 sample)     a.Inspection ScopeThe inspectors observed one unannounced fire drill conducted in the Unit 1 aircompressor, electro-hydraulic control (EHC) power unit, and turbine lubricating oil
 
storage tank area on September 26, 2007. The inspectors observed the drill to evaluate
====a. Inspection Scope====
the readiness of the plant fire brigade to fight fires. The documents reviewed are listed in
The inspectors observed one unannounced fire drill conducted in the Unit 1 aircompressor, electro-hydraulic control (EHC) power unit, and turbine lubricating oil storage tank area on September 26, 2007. The inspectors observed the drill to evaluate the readiness of the plant fire brigade to fight fires. The documents reviewed are listed in the Attachment. Specific attributes evaluated were:*Proper donning of fire fighting turnout gear and self-contained breathingapparatus (SCBA); *Proper use and layout of fire hoses;  
the Attachment. Specific attributes evaluated were:*Proper donning of fire fighting turnout gear and self-contained breathingapparatus (SCBA); *Proper use and layout of fire hoses;  
*Employment of appropriate fire fighting techniques;  
*Employment of appropriate fire fighting techniques;  
*Sufficient fire fighting equipment brought to the scene;
*Sufficient fire fighting equipment brought to the scene;
Line 136: Line 98:
*Utilization of pre-planned strategies;
*Utilization of pre-planned strategies;
*Adherence to the pre-planned drill scenario; and  
*Adherence to the pre-planned drill scenario; and  
*Drill objectives.       b.FindingsNo findings of significance were identified.1R06Flood Protection Measures (71111.06 - 1 sample)Internal Flooding     a.Inspection Scope The inspectors reviewed documents and inspected structures, systems, and components(SSCs) relative to the adequacy of internal flood protection measures for the Unit
*Drill objectives.
: [[1 HP]] [[]]
 
CI
====b. Findings====
room. The inspectors performed walkdowns of the relevant areas to verify the adequacy
No findings of significance were identified.
of flood mitigation doors and barriers, drainage systems, and other flood protection
{{a|1R06}}
features. The documents reviewed are listed in the Attachment.     b.Findings No findings of significance were identified.1R11Licensed Operator Requalification Program (71111.11Q - 1 sample)Resident Inspector Quarterly Review (1 sample)     a.Inspection Scope
==1R06 Flood Protection Measures==
4Enclosure On August 28, 2007, the inspectors observed a licensed operator requalificationsimulator scenario. The scenario included a simulated spurious Division 1 Loss of
  (71111.06 - 1 sample)Internal Flooding
Coolant Accident (LOCA) signal with failure of the D11 EDG to start and an unisolablereactor water cleanup leak, which resulted in a manual scram and emergency blowdown.
 
The inspectors observed the performance of two operating crews responding to the
====a. Inspection Scope====
same scenario. The inspectors assessed licensed operator performance, including
The inspectors reviewed documents and inspected structures, systems, and components(SSCs) relative to the adequacy of internal flood protection measures for the Unit 1 HPCI room. The inspectors performed walkdowns of the relevant areas to verify the adequacy of flood mitigation doors and barriers, drainage systems, and other flood protection features. The documents reviewed are listed in the Attachment.
operator critical tasks that measure operator actions required to ensure the safe
 
operation of the reactor and protection of the nuclear fuel and primary containment
====b. Findings====
barriers. The inspectors observed the training evaluators' critiques at the conclusion of
No findings of significance were identified.
each simulation. The documents reviewed are listed in the Attachment.     b.FindingsNo findings of significance were identified.1R12Maintenance Effectiveness (71111.12 - 3 samples)     a.Inspection Scope The inspectors evaluated Exelon's work practices and follow-up corrective actions forSSCs and identified issues to assess the effectiveness of Exelon's maintenance
{{a|1R11}}
activities. The inspectors reviewed the performance history of risk significant SSCs and
==1R11 Licensed Operator Requalification Program (71111.11Q - 1 sample)Resident Inspector Quarterly Review (1 sample)==
assessed Exelon's extent-of-condition determinations for those issues with potential
 
common cause or generic implications to evaluate the adequacy of the station's
====a. Inspection Scope====
corrective actions. The inspectors assessed Exelon's problem identification and
4Enclosure On August 28, 2007, the inspectors observed a licensed operator requalificationsimulator scenario. The scenario included a simulated spurious Division 1 Loss of Coolant Accident (LOCA) signal with failure of the D11 EDG to start and an unisolablereactor water cleanup leak, which resulted in a manual scram and emergency blowdown.
resolution actions for these issues to evaluate whether Exelon had appropriately
 
monitored, evaluated, and dispositioned the issues in accordance with Exelon
The inspectors observed the performance of two operating crews responding to the same scenario. The inspectors assessed licensed operator performance, including operator critical tasks that measure operator actions required to ensure the safe operation of the reactor and protection of the nuclear fuel and primary containment barriers. The inspectors observed the training evaluators' critiques at the conclusion of each simulation. The documents reviewed are listed in the Attachment.
procedures and the requirements of 10 CFR 50.65, "Requirements for Monitoring the
 
Effectiveness of Maintenance."  In addition, the inspectors reviewed selected SSC
====b. Findings====
classifications, performance criteria and goals, and Exelon's corrective actions that were
No findings of significance were identified.
taken or planned, to evaluate whether the actions were reasonable and appropriate. The
{{a|1R12}}
documents reviewed are listed in the Attachment. The inspectors performed the
==1R12 Maintenance Effectiveness==
following samples:*1A post
  (71111.12 - 3 samples)
: [[LO]] [[]]
 
CA recombiner maintenance rule (a)(1) determination;*2B Turbine Enclosure Cooling Water heat exchanger system outage window; and
====a. Inspection Scope====
*Unit 2 High Pressure Coolant Injection maintenance rule (a)(1) determination.1R13Maintenance Risk Assessments and Emergent Work Control (71111.13 - 8 samples)     a.Inspection Scope The inspectors evaluated the effectiveness of Exelon's maintenance risk assessmentsrequired by 10 CFR 50.65 (a)(4). This inspection included discussion with control room
The inspectors evaluated Exelon's work practices and follow-up corrective actions forSSCs and identified issues to assess the effectiveness of Exelon's maintenance activities. The inspectors reviewed the performance history of risk significant SSCs and assessed Exelon's extent-of-condition determinations for those issues with potential common cause or generic implications to evaluate the adequacy of the station's corrective actions. The inspectors assessed Exelon's problem identification and resolution actions for these issues to evaluate whether Exelon had appropriately monitored, evaluated, and dispositioned the issues in accordance with Exelon procedures and the requirements of 10 CFR 50.65, "Requirements for Monitoring the Effectiveness of Maintenance."  In addition, the inspectors reviewed selected SSC classifications, performance criteria and goals, and Exelon's corrective actions that were taken or planned, to evaluate whether the actions were reasonable and appropriate. The documents reviewed are listed in the Attachment. The inspectors performed the following samples:*1A post LOCA recombiner maintenance rule (a)(1) determination;*2B Turbine Enclosure Cooling Water heat exchanger system outage window; and
operators and risk analysis personnel regarding the use of Exelon's on-line risk
*Unit 2 High Pressure Coolant Injection maintenance rule (a)(1) determination.
monitoring software. The inspectors reviewed equipment tracking documentation, daily
{{a|1R13}}
work schedules, and performed plant tours to gain assurance that the actual plant
==1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 8 samples)==
configuration matched the assessed configuration. Additionally, the inspectors verified
 
that Exelon's risk management actions, for both planned and emergent work, were
====a. Inspection Scope====
5Enclosure consistent with those described in Exelon procedure,
The inspectors evaluated the effectiveness of Exelon's maintenance risk assessmentsrequired by 10 CFR 50.65 (a)(4). This inspection included discussion with control room operators and risk analysis personnel regarding the use of Exelon's on-line risk monitoring software. The inspectors reviewed equipment tracking documentation, daily work schedules, and performed plant tours to gain assurance that the actual plant configuration matched the assessed configuration. Additionally, the inspectors verified that Exelon's risk management actions, for both planned and emergent work, were 5Enclosure consistent with those described in Exelon procedure, ER-AA-600-1042, "On-Line RiskManagement."  The documents reviewed are listed in the Attachment. Inspectors reviewed risk assessments for the following issues:*Incorrect interpretation of ASME Code Case N-435-1;*Unit 1 HPCI room temperature high;
: [[ER]] [[-]]
AA-600-1042, "On-Line RiskManagement."  The documents reviewed are listed in the Attachment. Inspectors
reviewed risk assessments for the following issues:*Incorrect interpretation of
: [[ASME]] [[Code Case N-435-1;*Unit 1]]
HPCI room temperature high;
*Unit 2 Reactor Recirculation Motor Generator runback to minimum speed;
*Unit 2 Reactor Recirculation Motor Generator runback to minimum speed;
*Unit 1 Main Generator Disconnect high temperatures;
*Unit 1 Main Generator Disconnect high temperatures;
*Unit 1 Main Generator Disconnect phases A and C jumper installation;
*Unit 1 Main Generator Disconnect phases A and C jumper installation;
*Large
*Large VAR (Volt-Ampere Reactive) swings during EDG run;
: [[VAR]] [[(Volt-Ampere Reactive) swings during]]
EDG run;
*Unit 2 placing alternate steam jet air ejector in service; and
*Unit 2 placing alternate steam jet air ejector in service; and
*Unit 1 "D" Safety Relief Valve position indicator converter module replacement.     b.FindingsNo findings of significance were identified.1R15Operability Evaluations (71111.15 - 5 samples)     a.Inspection ScopeFor the five operability evaluations described below, the inspectors assessed thetechnical adequacy of the evaluations to ensure that Exelon properly justified TS
*Unit 1 "D" Safety Relief Valve position indicator converter module replacement.
operability and verified that the subject component or system remained available such
 
that no unrecognized increase in risk occurred. The inspectors reviewed the
====b. Findings====
: [[UFS]] [[]]
No findings of significance were identified.
AR to
{{a|1R15}}
verify that the system or component remained available to perform its intended safety
==1R15 Operability Evaluations==
function. In addition, the inspectors reviewed compensatory measures implemented to
  (71111.15 - 5 samples)
ensure that the measures worked and were adequately controlled. The inspectors also
 
reviewed a sample of issue reports (IRs) to verify that Exelon identified and corrected
====a. Inspection Scope====
deficiencies associated with operability evaluations. The documents reviewed are listed
For the five operability evaluations described below, the inspectors assessed thetechnical adequacy of the evaluations to ensure that Exelon properly justified TS operability and verified that the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors reviewed the UFSAR to verify that the system or component remained available to perform its intended safety function. In addition, the inspectors reviewed compensatory measures implemented to ensure that the measures worked and were adequately controlled. The inspectors also reviewed a sample of issue reports (IRs) to verify that Exelon identified and corrected deficiencies associated with operability evaluations. The documents reviewed are listed in the Attachment. The inspectors reviewed operability evaluations for the following components:*Unit 2 HPCI HV-055-2F006;*Unit 1 HPCI Room Cooler;
in the Attachment. The inspectors reviewed operability evaluations for the following
components:*Unit
: [[2 HPCI]] [[]]
: [[HV]] [[-055-2F006;*Unit]]
: [[1 HP]] [[]]
CI Room Cooler;
*Unit 2 Reactor Core Isolation Cooling Pump Suction High Pressure Alarm;
*Unit 2 Reactor Core Isolation Cooling Pump Suction High Pressure Alarm;
*Unit
*Unit 2 HPCI Oil Pressure; and
: [[2 HP]] [[]]
*Unit 2B Reactor Circulation Pump mechanical seal.
CI Oil Pressure; and
 
*Unit 2B Reactor Circulation Pump mechanical seal.     b.FindingsNo findings of significance were identified.1R19Post-Maintenance Testing (71111.19 - 8 samples)     a. Inspection ScopeThe inspectors reviewed the eight post-maintenance tests (PMTs) listed below to verifythat procedures and test activities ensured system operability and functional capability.
====b. Findings====
The inspectors reviewed Exelon's test procedures to verify that the procedures
No findings of significance were identified.
6Enclosure adequately tested the safety functions that may have been affected by the maintenanceactivity, and that the applicable criteria in the procedures were consistent with information
{{a|1R19}}
in the licensing and design basis documents. The inspectors also witnessed the test or
==1R19 Post-Maintenance Testing (71111.19 - 8 samples)==
reviewed test data to verify that the results adequately demonstrated restoration of the
 
affected safety functions. The documents reviewed are listed in the Attachment. The
====a. Inspection Scope====
inspectors reviewed post-maintenance tests for the following systems and components:*"C" Residual Heat Removal Service Water pump;*"2A" RHR Suppression Pool Cooling Valve;
The inspectors reviewed the eight post-maintenance tests (PMTs) listed below to verifythat procedures and test activities ensured system operability and functional capability.
 
The inspectors reviewed Exelon's test procedures to verify that the procedures 6Enclosure adequately tested the safety functions that may have been affected by the maintenanceactivity, and that the applicable criteria in the procedures were consistent with information in the licensing and design basis documents. The inspectors also witnessed the test or reviewed test data to verify that the results adequately demonstrated restoration of the affected safety functions. The documents reviewed are listed in the Attachment. The inspectors reviewed post-maintenance tests for the following systems and components:*"C" Residual Heat Removal Service Water pump;*"2A" RHR Suppression Pool Cooling Valve;
*"D" Emergency Diesel Generator;
*"D" Emergency Diesel Generator;
*D21 Diesel Generator;
*D21 Diesel Generator;
Line 215: Line 166:
*Unit 1 Reactor Core Isolation Cooling Flow Controller;
*Unit 1 Reactor Core Isolation Cooling Flow Controller;
*Unit 2 Reactor Core Isolation Cooling Outboard Steam Isolation Valve; and
*Unit 2 Reactor Core Isolation Cooling Outboard Steam Isolation Valve; and
*Unit 2 Redundant Reactivity Control System (RRCS).     b.FindingsNo findings of significance were identified.1R22Surveillance Testing (71111.22 - 5 samples)     a.Inspection ScopeThe inspectors witnessed the performance and reviewed test data for five surveillancetests that are associated with selected risk-significant SSCs. The review verified that
*Unit 2 Redundant Reactivity Control System (RRCS).
Exelon personnel followed TS requirements and that acceptance criteria were
 
appropriate. The inspectors also verified that the station established proper test
====b. Findings====
conditions, as specified in the procedures, that no equipment preconditioning activities
No findings of significance were identified.
occurred, and that acceptance criteria had been met. The documents reviewed are listed
{{a|1R22}}
in the Attachment. The inspectors reviewed the surveillance tests for the following
==1R22 Surveillance Testing (71111.22 - 5 samples)==
systems and components:*Unit 2 D24 EDG;*Unit 2 Division 2 Lower Pressure Coolant Injection;
 
====a. Inspection Scope====
The inspectors witnessed the performance and reviewed test data for five surveillancetests that are associated with selected risk-significant SSCs. The review verified that Exelon personnel followed TS requirements and that acceptance criteria were appropriate. The inspectors also verified that the station established proper test conditions, as specified in the procedures, that no equipment preconditioning activities occurred, and that acceptance criteria had been met. The documents reviewed are listed in the Attachment. The inspectors reviewed the surveillance tests for the following systems and components:*Unit 2 D24 EDG;*Unit 2 Division 2 Lower Pressure Coolant Injection;
*Unit 2 Control Rods;
*Unit 2 Control Rods;
*Unit 1 High Pressure Coolant Injection Pump; and
*Unit 1 High Pressure Coolant Injection Pump; and
*Unit 1 High Pressure Coolant Injection. b. FindingsNo findings of significance were identified.1R23Temporary Plant Modifications (71111.23 - 1 sample)     a.Inspection ScopeThe inspectors reviewed and compared the temporary modification listed below with theUFSAR and TS to verify that the modification did not affect operability or availability of
*Unit 1 High Pressure Coolant Injection.
the Unit 1 reactor recirculation motor generator. The inspectors ensured that station
 
7Enclosure personnel implemented the modification in accordance with the applicable temporaryconfiguration change process. The inspectors also reviewed the impact on existing
====b. Findings====
procedures to verify appropriate revisions were made to reflect the temporary
No findings of significance were identified.
configuration change. Additionally, the inspectors evaluated the adequacy of proposed
{{a|1R23}}
testing upon removal of the change. The documents reviewed are listed in the
==1R23 Temporary Plant Modifications==
Attachment. The inspectors performed the following sample:*TRT-D7-164, Install 1B Reactor Recirculation Pump Motor Generator TemporaryMechanical Stop. b. FindingsNo findings of significance were identified.
  (71111.23 - 1 sample)
Cornerstone: Emergency Preparedness (EP)1EP6Drill Evaluation (71114.06 - 2 samples).1General Emergency Classification due to Simulated Fuel Failure Coincident with FailedOpen Main Steam Line Isolation Valves       a.Inspection ScopeOn June 19, 2007, the inspectors observed an
 
: [[EP]] [[training drill in the control roomsimulator. The inspectors assessed Exelon's emergency response organization's (]]
====a. Inspection Scope====
ERO)
The inspectors reviewed and compared the temporary modification listed below with theUFSAR and TS to verify that the modification did not affect operability or availability of the Unit 1 reactor recirculation motor generator. The inspectors ensured that station 7Enclosure personnel implemented the modification in accordance with the applicable temporaryconfiguration change process. The inspectors also reviewed the impact on existing procedures to verify appropriate revisions were made to reflect the temporary configuration change. Additionally, the inspectors evaluated the adequacy of proposed testing upon removal of the change. The documents reviewed are listed in the
implementation of the Limerick emergency plan and implementing procedures, and the
. The inspectors performed the following sample:*TRT-D7-164, Install 1B Reactor Recirculation Pump Motor Generator TemporaryMechanical Stop.
ERO's response to simulated degraded plant conditions to identify weaknesses and
 
deficiencies in classification, notification, and protective action recommendation (PAR)
====b. Findings====
development activities. In addition, the inspectors assessed licensed operator
No findings of significance were identified.
performance required to ensure the safe operation of the reactor and the protection of
 
the nuclear fuel and primary containment barriers. The inspectors reviewed Exelon's
===Cornerstone:===
training evaluators' critiques and the formal critique report, dated July 31, 2007,
Emergency Preparedness (EP)1EP6Drill Evaluation (71114.06 - 2 samples).1General Emergency Classification due to Simulated Fuel Failure Coincident with FailedOpen Main Steam Line Isolation Valves
associated with the EP drill, to evaluate Exelon's identification of weaknesses and
 
deficiencies. The inspectors compared inspector observed weaknesses with those
====a. Inspection Scope====
identified in Exelon's formal drill critique to verify whether Exelon adequately identified
On June 19, 2007, the inspectors observed an EP training drill in the control roomsimulator. The inspectors assessed Exelon's emergency response organization's (ERO)implementation of the Limerick emergency plan and implementing procedures, and the ERO's response to simulated degraded plant conditions to identify weaknesses and deficiencies in classification, notification, and protective action recommendation (PAR)development activities. In addition, the inspectors assessed licensed operator performance required to ensure the safe operation of the reactor and the protection of the nuclear fuel and primary containment barriers. The inspectors reviewed Exelon's training evaluators' critiques and the formal critique report, dated July 31, 2007, associated with the EP drill, to evaluate Exelon's identification of weaknesses and deficiencies. The inspectors compared inspector observed weaknesses with those identified in Exelon's formal drill critique to verify whether Exelon adequately identified weaknesses and deficiencies at an appropriate threshold. The documents reviewed are listed in the Attachment.
weaknesses and deficiencies at an appropriate threshold. The documents reviewed are
 
listed in the Attachment.       b.FindingsNo findings of significance were identified..2Site Area Emergency Classification Due to a Simulated Reactor Coolant System Leak inthe Reactor Building     a.Inspection ScopeThe inspectors observed a licensed operator requalification simulator exercise evaluationto identify the timing and adequacy of classification, notification, and PAR development
====b. Findings====
activities. During the simulator evaluation, the inspectors reviewed checklists and forms
No findings of significance were identified..2Site Area Emergency Classification Due to a Simulated Reactor Coolant System Leak inthe Reactor Building
8Enclosure used for classification and notification activities, and compared them to the criteria inExelon's Emergency Plan,
 
: [[EP]] [[-]]
====a. Inspection Scope====
MA-114-100-F-01, "State/Local Event Notification Form,"
The inspectors observed a licensed operator requalification simulator exercise evaluationto identify the timing and adequacy of classification, notification, and PAR development activities. During the simulator evaluation, the inspectors reviewed checklists and forms 8Enclosure used for classification and notification activities, and compared them to the criteria inExelon's Emergency Plan, EP-MA-114-100-F-01, "State/Local Event Notification Form,"
and supporting procedures. The documents reviewed are listed in the Attachment.     b.FindingsNo findings of significance were identified.2.OTHER
and supporting procedures. The documents reviewed are listed in the Attachment.
: [[ACTIVI]] [[]]
 
: [[TIES]] [[]]
====b. Findings====
: [[4OA]] [[1Performance Indicator (]]
No findings of significance were identified.2.OTHER ACTIVITIES
PI) Verification (71151- 8 samples)    1. Inspection ScopeThe inspector sampled Exelon's submittal of the performance indicators listed below toverify the accuracy of the data recorded from the third quarter of 2006 through the third
{{a|4OA1}}
quarter of 2007. The inspectors utilized performance indicator definitions and guidance
==4OA1 Performance Indicator (PI) Verification==
contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Performance
{{IP sample|IP=IP 71151|count=8}}
Indicator Guideline," Revision 5, to verify the basis in reporting for each data element.
1. Inspection ScopeThe inspector sampled Exelon's submittal of the performance indicators listed below toverify the accuracy of the data recorded from the third quarter of 2006 through the third quarter of 2007. The inspectors utilized performance indicator definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, to verify the basis in reporting for each data element.
The inspectors reviewed various documents, including portions of main control room
 
logs, issue reports, power history curves, work orders, and system derivation reports.
The inspectors reviewed various documents, including portions of main control room logs, issue reports, power history curves, work orders, and system derivation reports.
The inspectors also discussed the method for compiling and reporting performance
 
indicators with cognizant engineering personnel and compared graphical representations
The inspectors also discussed the method for compiling and reporting performance indicators with cognizant engineering personnel and compared graphical representations from the most recent PI report to the raw data to verify that the report correctly reflected the data. The documents reviewed are listed in the Attachment. Cornerstone: Initiating Events (2 samples)*Unit 1 Unplanned Power Changes per 7000 Critical Hours; and*Unit 2 Unplanned Power Changes per 7000 Critical Hours.Cornerstone: Mitigating Systems (6 samples)*Unit 1 High Pressure Coolant Injection system;*Unit 2 High Pressure Coolant Injection system;
from the most recent PI report to the raw data to verify that the report correctly reflected
the data. The documents reviewed are listed in the Attachment. Cornerstone: Initiating Events (2 samples)*Unit 1 Unplanned Power Changes per 7000 Critical Hours; and*Unit 2 Unplanned Power Changes per 7000 Critical Hours.Cornerstone: Mitigating Systems (6 samples)*Unit 1 High Pressure Coolant Injection system;*Unit 2 High Pressure Coolant Injection system;
*Unit 1 Reactor Core Isolation Cooling system;
*Unit 1 Reactor Core Isolation Cooling system;
*Unit 2 Reactor Core Isolation Cooling system;
*Unit 2 Reactor Core Isolation Cooling system;
*Unit 1 Emergency Diesel Generators; and
*Unit 1 Emergency Diesel Generators; and
*Unit 2 Emergency Diesel Generators.     b.FindingsNo findings of significance were identified.4OA2Identification and Resolution of Problems (71152)Review of Items Entered into the Corrective Action Program (CAP)
*Unit 2 Emergency Diesel Generators.
9Enclosure As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"and in order to help identify repetitive equipment failures or specific human performance
 
issues for follow-up, the inspectors performed a screening of all items entered into
====b. Findings====
Limerick's CAP. The inspectors accomplished this by reviewing the description of each
No findings of significance were identified.4OA2Identification and Resolution of Problems (71152)Review of Items Entered into the Corrective Action Program (CAP)9Enclosure As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of all items entered into Limerick's CAP. The inspectors accomplished this by reviewing the description of each new issue report and accessing Exelon's computerized database. The documents reviewed are listed in the Attachment.
new issue report and accessing Exelon's computerized database. The documents
 
reviewed are listed in the Attachment. b. FindingsNo findings of significance were identified. The inspectors observed that issues selectedfor review were appropriately categorized and prioritized in accordance with Exelon's
====b. Findings====
corrective action process.4OA3Event Followup (71153).1Unit 1 Main Generator Output Switchyard Disconnect Removal from Service due to HighTemperature   a.Inspection ScopeOn August 16, 2007, the inspectors responded to the plant due to a high temperature onthe Unit 1 main generator output disconnect. The inspectors discussed the switchyard
No findings of significance were identified. The inspectors observed that issues selectedfor review were appropriately categorized and prioritized in accordance with Exelon's corrective action process.4OA3Event Followup (71153).1Unit 1 Main Generator Output Switchyard Disconnect Removal from Service due to HighTemperature
disconnect problem with operations personnel, engineering personnel, and Exelon
 
management to gain an understanding of Exelon's response and follow-up actions. The
====a. Inspection Scope====
inspectors reviewed troubleshooting activities, the disconnect temperature surveillance
On August 16, 2007, the inspectors responded to the plant due to a high temperature onthe Unit 1 main generator output disconnect. The inspectors discussed the switchyard disconnect problem with operations personnel, engineering personnel, and Exelon management to gain an understanding of Exelon's response and follow-up actions. The inspectors reviewed troubleshooting activities, the disconnect temperature surveillance monitoring, and the planned actions to repair and correct the disconnect high temperature condition. The number 11 disconnect is located on the output of the Unit 1 main transformers and isphysically located in the Unit 1 220 kilovolt (kV) switchyard. The disconnect is comprised of three individual disconnects and associated bus bars. The disconnect "B" phase temperature reached a maximum value of 375 degrees Celsius and resulted in reactor power reductions to lower the temperature. The location of the elevated temperature was at the movable hinged section of the disconnect. The "A" and "C" phase temperatures were 95 to 100 degrees Celsius. The "B" phase high temperature was discovered during ongoing monthly temperature monitoring. In response to the high temperature, operators reduced reactor power from 100 percentdown to 25 percent to reduce the disconnect temperature and support removal of the main generator and disconnect from service to perform repairs. The inspectors observed "just-in-time training" in the simulator that was given to the operators prior to removing the main generator and disconnect from service. The inspectors also observed the operators' removal of the main generator and disconnect from service to support repairs.
monitoring, and the planned actions to repair and correct the disconnect high
 
temperature condition. The number 11 disconnect is located on the output of the Unit 1 main transformers and isphysically located in the Unit 1 220 kilovolt (kV) switchyard. The disconnect is comprised
After removal from service, the "B" phase disconnect was rebuilt and tested satisfactorily prior to being returned to service. The main generator was placed back in service and the plant was returned to 100 percent power. The documents reviewed are listed in the
of three individual disconnects and associated bus bars. The disconnect "B" phase
.
temperature reached a maximum value of 375 degrees Celsius and resulted in reactor
 
power reductions to lower the temperature. The location of the elevated temperature
====b. Findings====
was at the movable hinged section of the disconnect. The "A" and "C" phase
10Enclosure No findings of significance were identified..2(Closed) LER 05000353/02007-001, Scram Discharge Volume Vent and Drain Valves Failed Open Due to Clearance Tagging ErrorOn March 10, 2007, Limerick Unit 2 was in hot shutdown and depressurized toapproximately 25 psig for the 2R09 refueling outage. A full scram signal was present and the scram discharge volume (SDV) was isolated, as designed. Operators were in the process of applying a clearance in preparation for planned maintenance on the Reactor Protection System and the scram air header. As part of this clearance, operators removed the Reactor Protection System backup scram fuses which ultimately resulted in the SDV vent and drain valves opening unexpectedly. Water from the SDV began to vent through these open valves into the plant drain system. Station personnel discovered the condition and closed the SDV vent and drain valves, stopping the source of the water. Further investigation by the station determined that the inadvertent opening of the SDV vent and drain valves was due to an improperly written clearance. A non-cited violation (NCV) associated with this issue was documented in Section 1R20of NRC integrated inspection report 05000352/2007002 and 05000353/2007002. The inspectors reviewed this LER and did not identify any additional findings of significance.
temperatures were 95 to 100 degrees Celsius. The "B" phase high temperature was
 
discovered during ongoing monthly temperature monitoring. In response to the high temperature, operators reduced reactor power from 100 percentdown to 25 percent to reduce the disconnect temperature and support removal of the
Exelon documented this event and associated corrective actions in IR 602042. The documents reviewed are listed in the Attachment. This LER is closed..3(Closed) LER 05000353/02007-002, Valid Actuation of Main Condenser Low Vacuum Isolation Logic During OutageOn March 12, 2007, operators were in the process of lowering vacuum on Limerick Unit 2as part of refueling outage activities in accordance with procedure S07.2.A, "Shutdown of the Steam Jet Air Ejector and Breaking Main Condenser Vacuum."  During this evolution, the main condenser low vacuum main steam isolation valve (MSIV) isolation logic actuated unexpectedly. Further investigation revealed that due to a procedural execution error, station personnel had only bypassed two of the required four channels of the isolation logic. Even though this resulted in actuation of two channels of logic when vacuum was lowered, no valves actually repositioned since the MSIVs and other affected valves were closed earlier as required by procedure. This failure to comply with procedure S07.2.A constitutes a violation of minor significance that is not subject to enforcement action in accordance with Section IV of the NRC's enforcement policy. The inspectors reviewed this LER and did not identify any additional findings of significance.
main generator and disconnect from service to perform repairs. The inspectors observed
 
"just-in-time training" in the simulator that was given to the operators prior to removing
Exelon documented this event and associated corrective actions in IR 602921. This LER is closed.
the main generator and disconnect from service. The inspectors also observed the
 
operators' removal of the main generator and disconnect from service to support repairs.
===.4 (Closed) LER 05000353/02007-003, Automatic Actuation of the Reactor ProtectionSystem at PowerOn April 24, 2007, the Unit 2 Reactor Protection System automatically actuated whenreactor water level decreased from +35 inches to +12.5 inches.===
After removal from service, the "B" phase disconnect was rebuilt and tested satisfactorily
All control rods fullyinserted. When reactor level decreased to the low-low level setpoint of -38 inches, both HPCI and RCIC systems initiated and injected into the vessel. HPCI and RCIC were placed in manual mode when flow oscillations were observed on both systems. Both systems were automatically secured when reactor level increased to +54 inches.
prior to being returned to service. The main generator was placed back in service and
 
the plant was returned to 100 percent power. The documents reviewed are listed in the
11Enclosure Exelon's investigation determined that a circuit card in Redundant Reactivity ControlSystem (RRCS) Division 1, channel "B" spuriously actuated while channel "A" was in a tripped condition due to planned surveillance testing. This resulted in a feedwater runback. The feedwater runback reduced reactor level as expected.Exelon's investigation determined that HPCI and RCIC flow oscillations were due to flowcontrol loop tuning settings that did not properly account for differences in flow path testing conditions and vessel injection flow conditions. Station personnel replaced and successfully tested the affected RRCS circuit card. In addition the HPCI and RCIC flow controller gain and reset settings were adjusted to be consistent with Unit 1 settings, which are consistent with industry values and similar to previous Unit 2 settings when stable flow was demonstrated during Unit 2 initial startup testing. The procedure for tuning of HPCI and RCIC flow controls was revised to specify the required gain and reset settings.The inspectors reviewed Exelon's apparent cause investigation, Unit 2 TS, andnotification requirements. The apparent cause investigation determined that the HPCI and RCIC gain and reset settings were changed during system tuning in May 1999; therefore, this condition existed for approximately 8 years. This resulted in a condition that could have prevented the safety function of Unit 2 HPCI. A non-cited violation (NCV)associated with this issue was documented in Section IR19 of NRC integrated inspection report 05000352/2007003 and 05000353/2007003. Exelon documented this issue and its corrective actions in IR 620861. The review determined that Unit 1 was not affected.
Attachment.     b.Findings
 
10Enclosure No findings of significance were identified..2(Closed) LER 05000353/02007-001, Scram Discharge Volume Vent and Drain Valves Failed Open Due to Clearance Tagging ErrorOn March 10, 2007, Limerick Unit 2 was in hot shutdown and depressurized toapproximately 25 psig for the 2R09 refueling outage. A full scram signal was present
The inspectors reviewed the corrective actions, including revised procedures, and found no additional findings or unresolved issues. The documents reviewed are listed in the
and the scram discharge volume (SDV) was isolated, as designed. Operators were in
. This LER is closed.4OA6Meetings, Including ExitExit Meeting SummaryOn October 15, 2007, the resident inspectors presented the inspection results toMr. E. Callan and other members of his staff. The inspectors confirmed that proprietary information was not included in the inspection report. ATTACHMENT: 
the process of applying a clearance in preparation for planned maintenance on the
 
Reactor Protection System and the scram air header. As part of this clearance,
=SUPPLEMENTAL INFORMATION=
operators removed the Reactor Protection System backup scram fuses which ultimately
 
resulted in the
==KEY POINTS OF CONTACT==
: [[SDV]] [[vent and drain valves opening unexpectedly. Water from the]]
Exelon Generation Company
SDV
: [[contact::C. Mudrick]], Site Vice President
began to vent through these open valves into the plant drain system. Station personnel
: [[contact::E. Callan]], Plant Manager
discovered the condition and closed the SDV vent and drain valves, stopping the source
: [[contact::D. DiCello]], Radiation Protection Manager
of the water. Further investigation by the station determined that the inadvertent opening
: [[contact::R. Dickinson]], Director Engineering
of the
: [[contact::J. Berg]], System Manager, HPCI and RCIC
: [[SDV]] [[vent and drain valves was due to an improperly written clearance. A non-cited violation (]]
: [[contact::J. George]], System Manager, Remote Shutdown Panel
NCV) associated with this issue was documented in Section 1R20of NRC integrated inspection report 05000352/2007002 and 05000353/2007002. The
: [[contact::M. Gift]], System Manager, Radiation Monitoring Systems
inspectors reviewed this LER and did not identify any additional findings of significance.
: [[contact::R. Gosby]], Radiation Protection Technician, Instrumentation
Exelon documented this event and associated corrective actions in IR 602042. The
: [[contact::R. Harding]], Engineer, Regulatory Assurance
documents reviewed are listed in the Attachment. This
: [[contact::R. Kreider]], Manager, Regulatory Assurance
: [[LER]] [[is closed..3(Closed)]]
: [[contact::D. Malinowski]], Simulator Instructor
LER 05000353/02007-002, Valid Actuation of Main Condenser Low Vacuum Isolation Logic During OutageOn March 12, 2007, operators were in the process of lowering vacuum on Limerick Unit 2as part of refueling outage activities in accordance with procedure S07.2.A, "Shutdown of
: [[contact::B. Tracy]], System Manager
the Steam Jet Air Ejector and Breaking Main Condenser Vacuum."  During this evolution,
: [[contact::P. Tarpinian]], PRA Engineer
the main condenser low vacuum main steam isolation valve (MSIV) isolation logic
: [[contact::D. Boylan]], Summer Readiness Coordinator
actuated unexpectedly. Further investigation revealed that due to a procedural execution
: [[contact::R. Newmaster]], Manager - Emergency Preparedness, Limerick
error, station personnel had only bypassed two of the required four channels of the
: [[contact::J. Broillet]], Operations Shift Manager
isolation logic. Even though this resulted in actuation of two channels of logic when
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
vacuum was lowered, no valves actually repositioned since the
 
: [[MS]] [[]]
===Closed===
IVs and other affected
: [[Closes LER::05000353/LER-2007-001]]-0LERScram Discharge Volume Vent and DrainValves Failed Open due to Clearance
valves were closed earlier as required by procedure. This failure to comply with
: Tagging Error (Section 40A3.2)
procedure S07.2.A constitutes a violation of minor significance that is not subject to
: [[Closes LER::05000353/LER-2007-002]]-0LERValid Actuation of Main Condenser LowVacuum Isolation Logic During Outage
enforcement action in accordance with Section
(Section 40A3.3)
: [[IV]] [[of the]]
: [[Closes LER::05000353/LER-2007-003]]LERAutomatic Actuation of the ReactorProtection System at Power (Section
NRC's enforcement policy. The
: 40A3.4)
inspectors reviewed this LER and did not identify any additional findings of significance.
===Discussed===
Exelon documented this event and associated corrective actions in
None
: [[IR]] [[602921. This]]
A-2Attachment
: [[LER]] [[is closed.         .4(Closed) LER 05000353/02007-003, Automatic Actuation of the Reactor ProtectionSystem at PowerOn April 24, 2007, the Unit 2 Reactor Protection System automatically actuated whenreactor water level decreased from +35 inches to +12.5 inches. All control rods fullyinserted. When reactor level decreased to the low-low level setpoint of -38 inches, both]]
==LIST OF DOCUMENTS REVIEWED==
: [[HPCI]] [[and]]
==Section 1R01: ==
: [[RCIC]] [[systems initiated and injected into the vessel.]]
: Adverse Weather ProtectionProceduresOP-AA-108-107-1001, "Station Response to Grid Capacity Conditions," Revision 2S32.3.A, "Main Generator Inspection During Heavy Grid Load," Revision 7Section 1R04: Equipment AlignmentProceduresTechnical Specification 3/4 8.1, "A.C. Sources"S92.9.N, "Routine Inspection of the Diesel Generators," Revision 53
: [[HPCI]] [[and]]
: 1S46.1.A (COL), "Valve and Breaker Alignment for Start-up of the Control Rod Drive Hydraulic Supply System for Service"
RCIC were
: ST-6-048-230-1, "SLC Pump, Valve, and Flow Test"
placed in manual mode when flow oscillations were observed on both systems. Both
: S49.3.A, "RCIC Fill and Vent," Revision 17
systems were automatically secured when reactor level increased to +54 inches.
: Troubleshooting, Rework, and Testing Control Form, TRT No. 07-174, RCIC Fill and Vent
11Enclosure Exelon's investigation determined that a circuit card in Redundant Reactivity ControlSystem (RRCS) Division 1, channel "B" spuriously actuated while channel "A" was in a
 
tripped condition due to planned surveillance testing. This resulted in a feedwater
==Section 1R05: Fire ProtectionProceduresARC-MCR-006 B1L, Fire Alarm Response Card, Revision 2F-A-452, "Unit 1 Static Inverter Room, Fire Area 20," Revision 7==
runback. The feedwater runback reduced reactor level as expected.Exelon's investigation determined that
: F-A-453, "Unit 2 Static Inverter Room, Fire Area 20," Revision 4
: [[HPCI]] [[and]]
: F-A-533, "Control Room 533 and Peripheral Rooms 530 to 535 (EL. 269) Fire Area 24," Revision 10F-A-619, "Control Structure Fan Room (EL. 304) Fire Area 27," Revision 6
RCIC flow oscillations were due to flowcontrol loop tuning settings that did not properly account for differences in flow path
: F-A-624, "Standby Gas Treatment Area Rooms 624 & 625, Fire Area 28," Revision 6
testing conditions and vessel injection flow conditions. Station personnel replaced and
: F-D-311D, "D14 Diesel Generator Room and Fuel Oil and Lube Oil Tank Room Rooms 311Dand 312D (EL. 217) Fire Area 82," Revision 5F-T-328, "Unit 1 Air Compressor, EHC Power Unit, and Turbine Lube Oil Storage Tank AreasRooms 328, 330, and 331 (EL. 217) Fire Area 93," Revision 5OP-AA-201-003, "Fire Drill Performance," Revision 8
successfully tested the affected
: SE-8, "Fire," Revision 31
: [[RRCS]] [[circuit card. In addition the]]
: ST-6-022-551-0, "Fire Drill," Revision 8, conducted on 9/26/07Issue Reports and Action Requests (ARs)IR
: [[HPCI]] [[and]]
: 676038, "Fire Brigade Member EO Key Ring"A1261436, "Evaluate Propping Open of Doors"MiscellaneousUFSAR Appendix 9A
: [[RC]] [[]]
 
IC flow
==Section 1R06: Flood Protection MeasuresProceduresSE-4, "Flood," Revision 5SE-4-1, "Reactor Enclosure Flooding," Revision 8==
controller gain and reset settings were adjusted to be consistent with Unit 1 settings,
: A-3AttachmentIssue Reports and Action RequestsIR
which are consistent with industry values and similar to previous Unit 2 settings when
: 634795, "Floor Drain Clogged in U/1 HPCI Room"MiscellaneousBLP-31981, "Moderate Energy Pipe Break (MEPB) Analysis," dated February 1984NPB-14, "Moderate Energy Line Break," Revision 4
stable flow was demonstrated during Unit 2 initial startup testing. The procedure for
: NPB-32, "Flooding of ECCS Compartments from the Suppression Pool," Revision 3NPB-33, "Moderate Energy Pipe Break Report," Revision 3
tuning of
 
: [[HPCI]] [[and]]
==Section 1R11: Licensed Operator Requalification ProgramProceduresEOP==
RCIC flow controls was revised to specify the required gain and reset
: T-101, "RPV Control," Revision 20 EOP T-103, "Secondary Containment Control," Revision 17
settings.The inspectors reviewed Exelon's apparent cause investigation, Unit
: EOP T-112, "Emergency Blowdown," Revision 12
: [[2 TS]] [[, andnotification requirements. The apparent cause investigation determined that the]]
: EOP T-270, "Terminate and Prevent injection into RPV," Revision 12
: [[HPCI]] [[and]]
 
: [[RC]] [[]]
==Section 1R12: Maintenance EffectivenessProceduresER-AA-310, "Implementation of the Maintenance Rule," Revision 6ER-AA-310-1004, "Maintenance Rule - Performance Monitoring," Revision 5==
IC gain and reset settings were changed during system tuning in May 1999;
: ER-AA-310-1003, "Maintenance Rule - Performance Criteria Selection," Revision 3
therefore, this condition existed for approximately 8 years. This resulted in a condition
: ER-AA-310-1005, "Maintenance Rule - Dispositioning Between (a)(1) and (a)(2)," Revision 5
that could have prevented the safety function of Unit
: ER-LG-310-1010, "Maintenance Rule Implementation," Revision 7
: [[2 HPCI.]] [[A non-cited violation (]]
: ER-AA-310, "Implementation of the Maintenance Rule," Revision 6Issue Reports and Action RequestsIR
NCV)
: 483496, "TECW Unavailability Issues"IR
associated with this issue was documented in Section
: 637270, "Possible Maintenance Rule (a)(1) for Excessive TECW System Outage Window"
: [[IR]] [[19 of]]
: IR 642006, "2B TECW Heat Exchanger Unavailability Hours Exceeded"
NRC integrated inspection
: IR 667927, "Document Unit 2 HPCI Maintenance Rule (a)(1) Determination"
report 05000352/2007003 and 05000353/2007003. Exelon documented this issue and
: IR 506692, "Points 3 & 5 Failing"
its corrective actions in IR 620861. The review determined that Unit 1 was not affected.
: IR 546231, "1A Recombiner Valve
The inspectors reviewed the corrective actions, including revised procedures, and found
: FV-DO-101A Failed to Open"
no additional findings or unresolved issues. The documents reviewed are listed in the
: IR 551504, "1A Post LOCA Recombiner MRule FF (A)(1) Determination"MiscellaneousMaintenance Rule Expert Panel Meeting Minutes, dated 11/01/2006, 11/30/2006Maintenance Rule Expert Panel Meeting Minutes, dated 09/14/2000, 02/15/2001, 04/20/2006,
Attachment. This
: 06/19/2007
: [[LER]] [[is closed.4]]
 
OA6Meetings, Including ExitExit Meeting SummaryOn October 15, 2007, the resident inspectors presented the inspection results toMr. E. Callan and other members of his staff. The inspectors confirmed that proprietary
==Section 1R13: Maintenance Risk Assessments and Emergent Work ControlProceduresER-AA-600-1045, "Risk Assessments of Missed or Deficient Surveillances," Revision 0S07.6.A, "Placing Alternate Steam Jet Air Ejector In Service," Revision 27==
information was not included in the inspection report.
: ST-2-041-661-1, "Safety Relief Valves - Safety Relief Valve Position Indicators Functional Test,"Revision 12Issue Reports and Action RequestsIR
: [[ATTACH]] [[]]
: 598489, "D11 - Adjust Voltage Regulator Droop to 3% - 5%"  
: [[MENT]] [[:]]
: A-4AttachmentIR
: [[SUPPLE]] [[]]
: 601471, "ISI Inspection Volume for Code Case N-435"IR
: [[MENTAL]] [[]]
: 649698, "Incorrect Interpretation of ASME Code Case N-435-1"
: [[INFORM]] [[]]
: IR 657596, "2B Reactor Recirculation MG Set Runback to Min Speed"
: [[ATION]] [[A-1AttachmentSUPPLEMENTAL]]
: IR 668047, "Large VAR Swings During D12 D/G/ Run"IR
: [[INFORM]] [[]]
: 674591, "SRV 'D' Position Indicator Functional Test Failed"
: [[ATIONK]] [[EY]]
: A1456726, "Excursion in KVAR and KW"
: [[POINTS]] [[]]
: A1600437, "D12 Voltage Regulator VAR Swings When Paralleled to Offsite"
: [[OF]] [[]]
: A1628762, "IR for Generation of Activity to Swap Unit 2 SJAE"
: [[CONTAC]] [[]]
: A1631597, "Repair/Replace/Recal Loop Component," Dated 09/24/2007MiscellaneousOperator Logs dated 07/13/2007Limerick Generating Station On-Line Work Schedule, 09/14/2007-09/16/2007
TExelon Generation CompanyC. Mudrick, Site Vice PresidentE. Callan, Plant Manager
 
D. DiCello, Radiation Protection Manager
==Section 1R15: OperabilityIssue Reports and Action RequestsIR
: [[R.]] [[Dickinson, Director Engineering]]
: 060981, "HPCI Turbine Steam Supply Valve Position Relay Contacts Failed"IR
: [[J.]] [[Berg, System Manager,]]
: 101384, "Inappropriate Conclusions in Disp==
: [[HPCI]] [[and]]
: PEP I0012531/CR 00060981"
: [[RC]] [[]]
: IR 641784, "HPCI Aux Oil Pump Did Not Stop per PV&F"
IC
: IR 642617, "HV-055-2F006 Failed to Stroke Open"
J. George, System Manager, Remote Shutdown Panel
: IR 658690, "Unit 2 RCIC OOS/Gross Fail Alarm"
M. Gift, System Manager, Radiation Monitoring Systems
: IR 658931, "RCIC Pump Suction HI Press Alarm Came in While Swapping Suction Valves"
R. Gosby, Radiation Protection Technician, Instrumentation
: IR 658950, "HPCI Oil Pressure Lower Than Desired Band"
R. Harding, Engineer, Regulatory Assurance
: A1626638, "HPCI Oil Pressure Lower Than Desired Band"
R. Kreider, Manager, Regulatory Assurance
: IR 651187, "HPCI Higher than Normal Unit 1 HPCI Pump Room Temperature"
D. Malinowski, Simulator Instructor
: IR 664065, "Unit 2 Recirculation Pump #2 Seal Pressure Drop"MiscellaneousLimerick Generating Station UFSAR Section 6.3LEAM-0008, "HPCI Flow to RPV w/Single Discharge Path Open," Revision 0
: [[B.]] [[Tracy, System Manager]]
: M-48-12, "SLCS Boron Injection Delay Time," Revision 4
: [[P.]] [[Tarpinian,]]
: M-55-10, "HPCI Line Sizing Check," Revision 4
PRA Engineer
: M-55-26, "ATWS 3A HPCI Flow Split Calculation to Size a Flow Orifice for Branch to CoreSpray," Revision 6ECR
D. Boylan, Summer Readiness Coordinator
: LG 01-01152, "HPCI Failed Injection Valve - Provide Quality Docs"
: [[R.]] [[Newmaster, Manager - Emergency Preparedness, Limerick]]
 
: [[J.]] [[Broillet, Operations Shift Manager]]
==Section 1R19: Post Maintenance TestingProceduresST-2-042-638-2, "ATWS - Reactor Vessel Water Level - Low Low, Functional Test," Revision 12ST-6-051-231-2, "A==
: [[LIST]] [[]]
: RHR Pump, Valve and Flow Test," Revision 52
: [[OF]] [[]]
: ST-6-012-231-0, "A Loop RHRSW Pump, Valve and Flow Test", Revision 54
: [[ITEMS]] [[]]
: ST-6-048-230-1, "SLC Pump, Valve and Flow Test", Revision 32
: [[OPENED]] [[,]]
: ST-6-107-201-0,"IST Valve Stroke for New Baseline," Revision 4
: [[CLOSED]] [[,]]
: M-C-792-001, "Fairbanks Morse Opposed Piston Diesel Engine Examination and GeneralMaintenance," Revision 4Issue Reports and Action RequestsIR
: [[AND]] [[]]
: 338368, "Unit 2 RCIC Small Packing Leak from
DISCUSSEDClosed05000353/2007-001-0LERScram Discharge Volume Vent and DrainValves Failed Open due to Clearance
: HV-049-2F008 OUTBD PCIV"IR
Tagging Error (Section 40A3.2)05000353/2007-002-0LERValid Actuation of Main Condenser LowVacuum Isolation Logic During Outage
: 381319, "Unit 2 RCIC
(Section 40A3.3) 05000353/2007-003LERAutomatic Actuation of the ReactorProtection System at Power (Section
: HV-049-2F008 Packing Leak"  
40A3.4) DiscussedNone
: A-5AttachmentIR
A-2AttachmentLIST
: 654021,"D22 Diesel Lube Oil Circ Pump Making Excess Noise"IR
: [[OF]] [[]]
: 654041, "Dual Indication for
: [[DOCUME]] [[NTS]]
: HV-51-2F024A During Stroke Close"
: [[REVIEW]] [[]]
: IR 663431, "D21: Brush Holder Cable Replacement Not Identical to Original"
EDSection 1R01:  Adverse Weather ProtectionProceduresOP-AA-108-107-1001, "Station Response to Grid Capacity Conditions," Revision 2S32.3.A, "Main Generator Inspection During Heavy Grid Load," Revision 7Section 1R04: Equipment AlignmentProceduresTechnical Specification 3/4 8.1, "A.C. Sources"S92.9.N, "Routine Inspection of the Diesel Generators," Revision 53
: IR 664060, "D21 Diesel Rapid Shutdown Due to Cylinder Leak"
1S46.1.A (COL), "Valve and Breaker Alignment for Start-up of the Control Rod Drive Hydraulic
: IR 664291, "D21 Emergency Stop Alarm Failed to Annunciate"
Supply System for Service"
: IR 676024, "Indicating Lights did not Illuminate"
: [[ST]] [[-6-048-230-1, "]]
: A1178453, "Disassemble and Inspection 20" Manual Check Valve, 012-0001C"
SLC Pump, Valve, and Flow Test"
: A1624433, "Replace RRCS
S49.3.A, "RCIC Fill and Vent," Revision 17
: HPII/HPOI Cards"A1628140, "D21 Over Excitation During Break-In Run"
Troubleshooting, Rework, and Testing Control Form,
: A1628023, "Alarms on D21 Still Annunciated and Will Not Clear"
: [[TRT]] [[No. 07-174,]]
: A1628302, "D21 Diesel Rapid Shutdown Due to Cylinder Leak"
RCIC Fill and VentSection 1R05: Fire ProtectionProceduresARC-MCR-006 B1L, Fire Alarm Response Card, Revision 2F-A-452, "Unit 1 Static Inverter Room, Fire Area 20," Revision 7
: A1630245, "Unit 2 RCIC Steam Line Outboard PCIV"Work OrdersR1005988, "D21 24 Month Diesel Inspection Per M-C-792-001" MiscellaneousLimerick Generating Station On-Line Work Schedule 08/23/2007-08/26/2007Operator Logs dated 08/23/2007
F-A-453, "Unit 2 Static Inverter Room, Fire Area 20," Revision 4
: Safety Relief Valve Technical Specification Accident Monitoring Instrumentation Table 3.3.7.5-1
F-A-533, "Control Room 533 and Peripheral Rooms 530 to 535 (EL. 269) Fire Area 24," Revision 10F-A-619, "Control Structure Fan Room (EL. 304) Fire Area 27," Revision 6
 
F-A-624, "Standby Gas Treatment Area Rooms 624 & 625, Fire Area 28," Revision 6
==Section 1R22: Surveillance TestingProceduresST-2-051-802-2, "Division 2==
F-D-311D, "D14 Diesel Generator Room and Fuel Oil and Lube Oil Tank Room Rooms 311Dand 312D (EL. 217) Fire Area 82," Revision 5F-T-328, "Unit 1 Air Compressor,
: LPCI System Response Time Testing," Revision 8ST-2-055-810-1, "HPCI System Response Time Testing," Revision 11, completed 09/18/2007
: [[EHC]] [[Power Unit, and Turbine Lube Oil Storage Tank AreasRooms 328, 330, and 331 (]]
: ST-6-055-230-1, "HPCI Pump, Valve, and Flow Test," Revision 65, completed 09/18/2007
: [[EL.]] [[217) Fire Area 93," Revision]]
: ST-6-092-314-2, "D24 Diesel Generator Slow Start Operability Test Run," Revision 61,completed 07/16/07ST-6-107-790-2, "Control Rod Scram Timing," Revision 11, completed 09/20/2007Issue Reports and Action RequestsA1614302, "U2
: [[5OP]] [[-]]
: HCU 46-47 Has No Full Out Position Indication on Full Core Display"IR
AA-201-003, "Fire Drill Performance," Revision 8
: 671836, "Blue Scram Light Failed to Light During ST-6-107-790-2"
: [[SE]] [[-8, "Fire," Revision 31]]
 
: [[ST]] [[-6-022-551-0, "Fire Drill," Revision 8, conducted on 9/26/07Issue Reports and Action Requests (]]
==Section 1R23: Temporary Plant ModificationsProceduresCC-AA-112, "Temporary Configuration Changes," Revision 12S43.0.C, "Clearing an Electrical or Mechanical Stop," Revision 18MiscellaneousTRT-D7-164, "Install 1B Reactor Recirculation Pump Motor Generator Temporary Mechanical Stop"C0221920, "Install Temporary Mechanical High Speed Stop in==
: [[AR]] [[s)IR 676038, "Fire Brigade Member]]
: XY-M1-1S001B" Limerick Generating Station UFSAR Section 5.4
: [[EO]] [[Key Ring"A1261436, "Evaluate Propping Open of Doors"Miscellaneous]]
: Limerick Generating Station Technical Specifications 3/4.4.1Issue Reports and Action RequestsIR
: [[UFSAR]] [[Appendix]]
: 631119, "1B Recirc Pump Speed Changes"IR
: [[9AS]] [[ection 1R06: Flood Protection MeasuresProcedures]]
: 654530, "Emergent PRA - Need New AR Created to Install Travel Limiter"
SE-4, "Flood," Revision 5SE-4-1, "Reactor Enclosure Flooding," Revision 8
: A1616738, "1B Recirc Pump Speed Changes"  
A-3AttachmentIssue Reports and Action RequestsIR 634795, "Floor Drain Clogged in U/1
: A-6AttachmentA1625008, "Need New AR Created to Install Travel Limiter"
: [[HPCI]] [[Room"Miscellaneous]]
 
: [[BLP]] [[-31981, "Moderate Energy Pipe Break (MEPB) Analysis," dated February 1984NPB-14, "Moderate Energy Line Break," Revision 4]]
==Section 1EP6: Drill EvaluationProceduresEOP==
: [[NPB]] [[-32, "Flooding of]]
: T-117, "Level/Power Control," Revision 15EOP T-104, "Radioactivity Release Control," Revision 12
: [[ECCS]] [[Compartments from the Suppression Pool," Revision]]
: EOP T-103, "Secondary Containment Control," Revision 17
: [[3NPB]] [[-33, "Moderate Energy Pipe Break Report," Revision 3Section 1R11: Licensed Operator Requalification ProgramProcedures]]
: EOP T-270, "Terminate and Prevent Injection Into RPV," Revision 12
EOP T-101, "RPV Control," Revision 20 EOP T-103, "Secondary Containment Control," Revision 17
: EP-AA-122, "Drills and Exercises," Revision 7
: [[EOP]] [[T-112, "Emergency Blowdown," Revision 12]]
: EP-AA-122-F-01, "Drill and Exercise Evaluation Criteria," Revision B
: [[EOP]] [[T-270, "Terminate and Prevent injection into]]
: EP-AA-122-1001, "Drill and Exercise Scheduling, Development, and Conduct," Revision 8
: [[RPV]] [[," Revision 12Section 1R12: Maintenance EffectivenessProceduresER-AA-310, "Implementation of the Maintenance Rule," Revision]]
: EP-AA-122-1002-F-02, "Drill and Exercise Objective Evaluation Data Tables," Revision B
: [[6ER]] [[-]]
: LS-AA-120, "Issue Identification and Screening Process," Revision 7
: [[AA]] [[-310-1004, "Maintenance Rule - Performance Monitoring," Revision 5]]
: T-103, "Secondary Containment Control," Revision 17MiscellaneousIR 437320IR 670538
: [[ER]] [[-]]
: Limerick [EP] Training Drill Series Evaluation Report, dated 07-31-2007
: [[AA]] [[-310-1003, "Maintenance Rule - Performance Criteria Selection," Revision 3]]
: LSES-8020, "Licensed Operator Training Simulator Evaluation Scenario," Revision 0
: [[ER]] [[-]]
: NRC IR 50-352&353/2005009
: [[AA]] [[-310-1005, "Maintenance Rule - Dispositioning Between (a)(1) and (a)(2)," Revision 5]]
 
: [[ER]] [[-]]
==Section 4OA1: Performance Indicator (PI) VerificationProceduresS92.6.N, "Diesel Oil Storage Tank Lineup to Fill Other than its Associated Day Tank," Revision 10Issue Reports and Action RequestsIR
: [[LG]] [[-310-1010, "Maintenance Rule Implementation," Revision 7]]
: 556902, "Minor Leakby of 049-2F014 Discovered During==
: [[ER]] [[-]]
: ST-2-049-601-2"IR
: [[AA]] [[-310, "Implementation of the Maintenance Rule," Revision 6Issue Reports and Action RequestsIR 483496, "TECW Unavailability Issues"IR 637270, "Possible Maintenance Rule (a)(1) for Excessive]]
: 565800, "HV-049-1F019 RCIC Min Flow Shows Dual Indication at 600 GPM"
: [[TE]] [[]]
: IR 620861, "GP-18 Review HPCI/RCIC Oscillations"
: [[CW]] [[System Outage Window"]]
: IR 628573, "RCIC MOV Overload or Power Loss DS14"
: [[IR]] [[642006, "2B]]
: IR 628579, "Inadvertent RCIC OOS Annunciator"
: [[TECW]] [[Heat Exchanger Unavailability Hours Exceeded"]]
: IR 628600, "2DA-09 Tripped on Thermals"
: [[IR]] [[667927, "Document Unit 2]]
: IR 642618, "Valve Stroke Time Outside Acceptable Range"
HPCI Maintenance Rule (a)(1) Determination"
: IR 652846, "RCIC Overspeed Test Potentiometers Possibly Not Locked"
: [[IR]] [[506692, "Points 3 & 5 Failing"]]
: A1238085, "Determine if HPCI is Operable With Temperature Instrumentation Installed"
: [[IR]] [[546231, "1A Recombiner Valve]]
: A1295250, "FI-49-1R600-1 Spiking"
: [[FV]] [[-DO-101A Failed to Open"]]
: A1304397, "Revise the
: [[IR]] [[551504, "1A Post]]
: ML-008 Spec to Correctly Reflect the Safety Classification of the RCICMin Flow Line"MiscellaneousNEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5Reactor Oversight Program MSPI Bases Document, Limerick Generating Station, Revision 1
: [[LOCA]] [[Recombiner]]
: MSPI Derivation Reports for HPCI, RCIC, and EDGs Operator Logs dated 07/01/2007 through 07/31/2007
: [[MR]] [[ule]]
: Maintenance Rule Failure Reports for HPCI, RCIC, and EDGs
FF (A)(1) Determination"MiscellaneousMaintenance Rule Expert Panel Meeting Minutes, dated 11/01/2006, 11/30/2006Maintenance Rule Expert Panel Meeting Minutes, dated 09/14/2000, 02/15/2001, 04/20/2006,
: LG 01-00170, "Classification of the RCIC Min Flow Line"
06/19/2007Section 1R13: Maintenance Risk Assessments and Emergent Work ControlProceduresER-AA-600-1045, "Risk Assessments of Missed or Deficient Surveillances," Revision 0S07.6.A, "Placing Alternate Steam Jet Air Ejector In Service," Revision 27
 
: [[ST]] [[-2-041-661-1, "Safety Relief Valves - Safety Relief Valve Position Indicators Functional Test,"Revision 12Issue Reports and Action Requests]]
==Section 4OA2: Other==
IR 598489, "D11 - Adjust Voltage Regulator Droop to 3% - 5%"
: A-7AttachmentIssue Reports and Action RequestsA16106882C-P501 Packing Leakoff Excessive (Complete)A16159402C Circ Pump Step Change in Vibration
A-4AttachmentIR 601471, "ISI Inspection Volume for Code Case N-435"IR 649698, "Incorrect Interpretation of
: A1620985Spray Pond Level/Temp Alarming Before Setpoints Reached
: [[AS]] [[]]
: A16219922C-P501 Excessive Packing Leakage (Complete)
: [[ME]] [[Code Case N-435-1"]]
: A1622672Control Rod 22-35 Temp at 305 Deg F
: [[IR]] [[657596, "2B Reactor Recirculation]]
: A1628676Spray Pond Hi Temp Alarms Early
: [[MG]] [[Set Runback to Min Speed"]]
: C02212742C-P501-DR Inspect or Replace Motor Bearings
: [[IR]] [[668047, "Large]]
: IR 6120832C-P501 Packing Leakoff Excessive
VAR Swings During D12 D/G/ Run"IR 674591, "SRV 'D' Position Indicator Functional Test Failed"
: IR 612647Drive Mechanism Temperature for
A1456726, "Excursion in
: HCU 30-35 is @429 Degrees F
: [[KVAR]] [[and]]
: IR 6275952C Circ Pump Surge Capacitor Damaged
KW"
: IR 6289652C Circ Pump Step Change in Vibration
A1600437, "D12 Voltage Regulator VAR Swings When Paralleled to Offsite"
: IR 639934"Spray Pond Lo Level/Hi Temp" Alarm Locked In
A1628762, "IR for Generation of Activity to Swap Unit
: IR 643596Spray Pond Level/Temp Alarming Before Setpoints Reached
: [[2 SJ]] [[]]
: IR 6454662C-P501 Excessive Packing Leakage
AE"
: IR 648107Control Rod 22-35 Temp at 305 Deg F (Completed)
A1631597, "Repair/Replace/Recal Loop Component," Dated 09/24/2007MiscellaneousOperator Logs dated 07/13/2007Limerick Generating Station On-Line Work Schedule, 09/14/2007-09/16/2007Section 1R15: OperabilityIssue Reports and Action RequestsIR 060981, "HPCI Turbine Steam Supply Valve Position Relay Contacts Failed"IR 101384, "Inappropriate Conclusions in Disp
: IR 649388Hairline Crack Identified on Yoke
: [[PEP]] [[I0012531/]]
: IR 6498062C-P501-DR Temp Cooling
: [[CR]] [[00060981"]]
: IR 654068Hairline Crack Identified on Yoke
: [[IR]] [[641784, "]]
: IR 654070Hairline Crack Identified on Yoke
: [[HPCI]] [[Aux Oil Pump Did Not Stop per PV&F"]]
: IR 665262Spray Pond Hi Temp Alarms Early
: [[IR]] [[642617, "]]
: IR 6723152C-P501 High Packing Leak OffOther DocumentsPlant Health Committee System Presentation: Circ Water, June, 2007Plant Health Committee System Presentation: Control Rod Drive Supply, June, 2007
: [[HV]] [[-055-2F006 Failed to Stroke Open"]]
: Plant Health Committee System Presentation: EDG, June, 2007
: [[IR]] [[658690, "Unit 2]]
: Plant Health Committee System Presentation: RHRSW, June, 2007
: [[RCIC]] [[OOS/Gross Fail Alarm"]]
: SHIP Chronic Problem Report: Circ Water, June, 2007
: [[IR]] [[658931, "]]
: SHIP Chronic Problem Report: EDG, June, 2007
: [[RCIC]] [[Pump Suction HI Press Alarm Came in While Swapping Suction Valves"]]
: System Health Overview Report: Circ Water, June, 2007
: [[IR]] [[658950, "]]
: System Health Overview Report: Control Rod Drive Supply, June, 2007
HPCI Oil Pressure Lower Than Desired Band"
: System Health Overview Report: EDG, June, 2007
A1626638, "HPCI Oil Pressure Lower Than Desired Band"
: System Health Overview Report: RHRSW, June, 2007
: [[IR]] [[651187, "]]
: System Health Overview Report: Circ Water, Sept, 2007
: [[HPCI]] [[Higher than Normal Unit]]
: System Health Overview Report: Control Rod Drive Supply, Sept, 2007
: [[1 HP]] [[]]
: System Health Overview Report: EDG, Sept, 2007
: [[CI]] [[Pump Room Temperature"]]
: System Health Overview Report: RHRSW, Sept, 2007
: [[IR]] [[664065, "Unit 2 Recirculation Pump #2 Seal Pressure Drop"MiscellaneousLimerick Generating Station]]
 
UFSAR Section 6.3LEAM-0008, "HPCI Flow to RPV w/Single Discharge Path Open," Revision 0
==Section 4OA3: Event FollowupProceduresOP-LG-109-101-1001, "Limerick System Specific Tagging Guides," Revision 15Issue Reports and Action RequestsIR
M-48-12, "SLCS Boron Injection Delay Time," Revision 4
: 601910, "Drainage System Clogged"IR
M-55-10, "HPCI Line Sizing Check," Revision 4
: 602042, "Unit 2==
M-55-26, "ATWS 3A
: SDV Vent/Drain Valves Open With Scram Signal Present"
: [[HPCI]] [[Flow Split Calculation to Size a Flow Orifice for Branch to CoreSpray," Revision 6]]
: IR 602921, "Division 1 and 4 MSIV Isolation Logic Alarms"  
: [[ECR]] [[]]
: A-8AttachmentMiscellaneousLER 2007-001, "Scram Discharge Volume Vent and Drain Valves Failed Open Due to ClearanceTagging Error"LER 2007-002, "Valid Actuation of Main Condenser Low Vacuum Isolation Logic During Outage"
: [[LG]] [[01-01152, "]]
: LER 2007-003, "Automatic Actuation Of The Reactor Protection System at Power"
: [[HPCI]] [[Failed Injection Valve - Provide Quality Docs"Section 1R19: Post Maintenance TestingProceduresST-2-042-638-2, "ATWS - Reactor Vessel Water Level - Low Low, Functional Test," Revision]]
==LIST OF ACRONYMS==
: [[12ST]] [[-6-051-231-2, "A]]
ADAMSAgencywide Documents Access Management SystemARaction request
: [[RHR]] [[Pump, Valve and Flow Test," Revision 52]]
ASMEAmerican Society of Mechanical Engineers
: [[ST]] [[-6-012-231-0, "A Loop]]
CAPCorrective Action Program
: [[RHRSW]] [[Pump, Valve and Flow Test", Revision 54]]
CFRCode of Federal Regulations
: [[ST]] [[-6-048-230-1, "]]
: [[SLC]] [[Pump, Valve and Flow Test", Revision 32]]
: [[ST]] [[-6-107-201-0,"]]
IST Valve Stroke for New Baseline," Revision 4
M-C-792-001, "Fairbanks Morse Opposed Piston Diesel Engine Examination and GeneralMaintenance," Revision 4Issue Reports and Action RequestsIR 338368, "Unit
: [[2 RCIC]] [[Small Packing Leak from]]
: [[HV]] [[-049-2F008]]
: [[OUTBD]] [[]]
: [[PCIV]] [["IR 381319, "Unit]]
: [[2 RCIC]] [[]]
HV-049-2F008 Packing Leak"
A-5AttachmentIR 654021,"D22 Diesel Lube Oil Circ Pump Making Excess Noise"IR 654041, "Dual Indication for HV-51-2F024A During Stroke Close"
IR 663431, "D21: Brush Holder Cable Replacement Not Identical to Original"
IR 664060, "D21 Diesel Rapid Shutdown Due to Cylinder Leak"
IR 664291, "D21 Emergency Stop Alarm Failed to Annunciate"
IR 676024, "Indicating Lights did not Illuminate"
A1178453, "Disassemble and Inspection 20" Manual Check Valve, 012-0001C"
A1624433, "Replace
: [[RRCS]] [[]]
HPII/HPOI Cards"A1628140, "D21 Over Excitation During Break-In Run"
A1628023, "Alarms on D21 Still Annunciated and Will Not Clear"
A1628302, "D21 Diesel Rapid Shutdown Due to Cylinder Leak"
A1630245, "Unit
: [[2 RCIC]] [[Steam Line Outboard]]
PCIV"Work OrdersR1005988, "D21 24 Month Diesel Inspection Per M-C-792-001"
MiscellaneousLimerick Generating Station On-Line Work Schedule 08/23/2007-08/26/2007Operator Logs dated 08/23/2007
Safety Relief Valve Technical Specification Accident Monitoring Instrumentation Table 3.3.7.5-1Section 1R22: Surveillance TestingProceduresST-2-051-802-2, "Division
: [[2 LPCI]] [[System Response Time Testing," Revision 8]]
: [[ST]] [[-2-055-810-1, "HPCI System Response Time Testing," Revision 11, completed 09/18/2007]]
: [[ST]] [[-6-055-230-1, "]]
: [[HPCI]] [[Pump, Valve, and Flow Test," Revision 65, completed 09/18/2007]]
: [[ST]] [[-6-092-314-2, "D24 Diesel Generator Slow Start Operability Test Run," Revision 61,completed 07/16/07]]
: [[ST]] [[-6-107-790-2, "Control Rod Scram Timing," Revision 11, completed 09/20/2007Issue Reports and Action RequestsA1614302, "U2]]
: [[HCU]] [[46-47 Has No Full Out Position Indication on Full Core Display"]]
: [[IR]] [[671836, "Blue Scram Light Failed to Light During]]
: [[ST]] [[-6-107-790-2"Section 1R23: Temporary Plant ModificationsProcedures]]
CC-AA-112, "Temporary Configuration Changes," Revision 12S43.0.C, "Clearing an Electrical or Mechanical Stop," Revision 18MiscellaneousTRT-D7-164, "Install 1B Reactor Recirculation Pump Motor Generator Temporary Mechanical Stop"C0221920, "Install Temporary Mechanical High Speed Stop in XY-M1-1S001B"
Limerick Generating Station
: [[UFS]] [[]]
AR Section 5.4
Limerick Generating Station Technical Specifications 3/4.4.1Issue Reports and Action RequestsIR 631119, "1B Recirc Pump Speed Changes"IR 654530, "Emergent
: [[PRA]] [[- Need New]]
AR Created to Install Travel Limiter"
A1616738, "1B Recirc Pump Speed Changes"
A-6AttachmentA1625008, "Need New
: [[AR]] [[Created to Install Travel Limiter"Section 1]]
EP6: Drill EvaluationProceduresEOP T-117, "Level/Power Control," Revision 15EOP T-104, "Radioactivity Release Control," Revision 12
: [[EOP]] [[T-103, "Secondary Containment Control," Revision 17]]
: [[EOP]] [[T-270, "Terminate and Prevent Injection Into]]
: [[RPV]] [[," Revision 12]]
: [[EP]] [[-]]
: [[AA]] [[-122, "Drills and Exercises," Revision 7]]
: [[EP]] [[-]]
: [[AA]] [[-122-F-01, "Drill and Exercise Evaluation Criteria," Revision B]]
: [[EP]] [[-]]
: [[AA]] [[-122-1001, "Drill and Exercise Scheduling, Development, and Conduct," Revision 8]]
: [[EP]] [[-]]
: [[AA]] [[-122-1002-F-02, "Drill and Exercise Objective Evaluation Data Tables," Revision B]]
: [[LS]] [[-]]
AA-120, "Issue Identification and Screening Process," Revision 7
T-103, "Secondary Containment Control," Revision 17MiscellaneousIR 437320IR 670538
Limerick [EP] Training Drill Series Evaluation Report, dated 07-31-2007
: [[LS]] [[]]
: [[ES]] [[-8020, "Licensed Operator Training Simulator Evaluation Scenario," Revision 0]]
: [[NRC]] [[]]
: [[IR]] [[50-352&353/2005009Section]]
: [[4OA]] [[1: Performance Indicator (]]
: [[PI]] [[) VerificationProceduresS92.6.N, "Diesel Oil Storage Tank Lineup to Fill Other than its Associated Day Tank," Revision 10Issue Reports and Action RequestsIR 556902, "Minor Leakby of 049-2F014 Discovered During]]
: [[ST]] [[-2-049-601-2"]]
: [[IR]] [[565800, "HV-049-1F019]]
: [[RCIC]] [[Min Flow Shows Dual Indication at 600]]
: [[GPM]] [["]]
: [[IR]] [[620861, "]]
: [[GP]] [[-18 Review]]
: [[HPCI]] [[/]]
: [[RCIC]] [[Oscillations"]]
: [[IR]] [[628573, "]]
: [[RCIC]] [[]]
: [[MOV]] [[Overload or Power Loss]]
: [[DS]] [[14"]]
: [[IR]] [[628579, "Inadvertent]]
: [[RCIC]] [[OOS Annunciator"]]
: [[IR]] [[628600, "2]]
DA-09 Tripped on Thermals"
: [[IR]] [[642618, "Valve Stroke Time Outside Acceptable Range"]]
: [[IR]] [[652846, "]]
RCIC Overspeed Test Potentiometers Possibly Not Locked"
A1238085, "Determine if
: [[HP]] [[]]
CI is Operable With Temperature Instrumentation Installed"
A1295250, "FI-49-1R600-1 Spiking"
A1304397, "Revise the
: [[ML]] [[-008 Spec to Correctly Reflect the Safety Classification of the]]
: [[RCICM]] [[in Flow Line"MiscellaneousNEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5Reactor Oversight Program]]
: [[MS]] [[]]
: [[PI]] [[Bases Document, Limerick Generating Station, Revision 1]]
: [[MSPI]] [[Derivation Reports for]]
: [[HPCI]] [[,]]
: [[RCIC]] [[, and]]
EDGs
Operator Logs dated 07/01/2007 through 07/31/2007
Maintenance Rule Failure Reports for
: [[HPCI]] [[,]]
: [[RCIC]] [[, and EDGs]]
: [[LG]] [[01-00170, "Classification of the]]
RCIC Min Flow Line"Section 4OA2: Other
A-7AttachmentIssue Reports and Action RequestsA16106882C-P501 Packing Leakoff Excessive (Complete)A16159402C Circ Pump Step Change in Vibration
A1620985Spray Pond Level/Temp Alarming Before Setpoints Reached
A16219922C-P501 Excessive Packing Leakage (Complete)
A1622672Control Rod 22-35 Temp at 305 Deg F
A1628676Spray Pond Hi Temp Alarms Early
C02212742C-P501-DR Inspect or Replace Motor Bearings
: [[IR]] [[6120832C-P501 Packing Leakoff Excessive]]
: [[IR]] [[612647Drive Mechanism Temperature for]]
HCU 30-35 is @429 Degrees F
IR 6275952C Circ Pump Surge Capacitor Damaged
IR 6289652C Circ Pump Step Change in Vibration
IR 639934"Spray Pond Lo Level/Hi Temp" Alarm Locked In
IR 643596Spray Pond Level/Temp Alarming Before Setpoints Reached
IR 6454662C-P501 Excessive Packing Leakage
IR 648107Control Rod 22-35 Temp at 305 Deg F (Completed)
: [[IR]] [[649388Hairline Crack Identified on Yoke]]
: [[IR]] [[6498062C-P501-]]
DR Temp Cooling
IR 654068Hairline Crack Identified on Yoke
IR 654070Hairline Crack Identified on Yoke
IR 665262Spray Pond Hi Temp Alarms Early
IR 6723152C-P501 High Packing Leak OffOther DocumentsPlant Health Committee System Presentation: Circ Water, June, 2007Plant Health Committee System Presentation: Control Rod Drive Supply, June, 2007
Plant Health Committee System Presentation: EDG, June, 2007
Plant Health Committee System Presentation:
: [[RHR]] [[]]
: [[SW]] [[, June, 2007]]
: [[SH]] [[]]
: [[IP]] [[Chronic Problem Report: Circ Water, June, 2007]]
: [[SHIP]] [[Chronic Problem Report:]]
EDG, June, 2007
System Health Overview Report: Circ Water, June, 2007
System Health Overview Report: Control Rod Drive Supply, June, 2007
System Health Overview Report: EDG, June, 2007
System Health Overview Report:
: [[RHR]] [[]]
SW, June, 2007
System Health Overview Report: Circ Water, Sept, 2007
System Health Overview Report: Control Rod Drive Supply, Sept, 2007
System Health Overview Report: EDG, Sept, 2007
System Health Overview Report:
: [[RHRSW]] [[, Sept, 2007Section 4]]
: [[OA]] [[3: Event FollowupProceduresOP-LG-109-101-1001, "Limerick System Specific Tagging Guides," Revision 15Issue Reports and Action RequestsIR 601910, "Drainage System Clogged"IR 602042, "Unit 2 SDV Vent/Drain Valves Open With Scram Signal Present"]]
: [[IR]] [[602921, "Division 1 and 4]]
MSIV Isolation Logic Alarms"
A-8AttachmentMiscellaneousLER 2007-001, "Scram Discharge Volume Vent and Drain Valves Failed Open Due to ClearanceTagging Error"LER 2007-002, "Valid Actuation of Main Condenser Low Vacuum Isolation Logic During Outage"
: [[LER]] [[2007-003, "Automatic Actuation Of The Reactor Protection System at Power"]]
: [[LIST]] [[]]
: [[OF]] [[]]
: [[ACRONY]] [[MSADAMSAgencywide Documents Access Management SystemARaction request]]
: [[ASM]] [[]]
: [[EA]] [[merican Society of Mechanical Engineers]]
: [[CA]] [[]]
: [[PC]] [[orrective Action Program]]
: [[CF]] [[]]
RCode of Federal Regulations
CRDcontrol rod drive
CRDcontrol rod drive
EDGemergency diesel generator
EDGemergency diesel generator
EHCelectro-hydraulic control
EHCelectro-hydraulic control
: [[EP]] [[emergency preparedness]]
EPemergency preparedness
: [[ER]] [[]]
EROEmergency Response Organization
: [[OE]] [[mergency Response Organization]]
HPCIhigh pressure coolant injection
: [[HP]] [[]]
CIhigh pressure coolant injection
IRissue report
IRissue report
kVkilo volt
kVkilo volt
: [[LE]] [[]]
LERLicensee Event Report
: [[RL]] [[icensee Event Report]]
LOCAloss of coolant accident
: [[LO]] [[]]
MSIVmain steam isolation valve
: [[CA]] [[loss of coolant accident]]
NCVnon-cited violation
: [[MS]] [[]]
NEINuclear Energy Institute
IVmain steam isolation valve
NRCNuclear Regulatory Commission
: [[NCV]] [[non-cited violation]]
: [[NE]] [[]]
: [[IN]] [[uclear Energy Institute]]
: [[NR]] [[]]
CNuclear Regulatory Commission
OAother activities
OAother activities
: [[PAR]] [[protective action recommendation]]
PARprotective action recommendation
: [[PAR]] [[]]
PARSPublicly Available Records
SPublicly Available Records
PIperformance indicator
: [[PI]] [[performance indicator]]
P&IDpiping and instrumentation drawing
: [[P&]] [[]]
PMTpost-maintenance test
IDpiping and instrumentation drawing
RCICreactor core isolation cooling
: [[PMT]] [[post-maintenance test]]
RHRresidual heat removal
: [[RC]] [[]]
RRCSredundant reactivity control system
ICreactor core isolation cooling
SCBAself-contained breathing apparatus
: [[RHR]] [[residual heat removal]]
SDVscram discharge volume
: [[RR]] [[]]
: [[SHIP]] [[ystem health indicator program]]
: [[CS]] [[redundant reactivity control system]]
: [[SSC]] [[structure, system, component]]
: [[SC]] [[]]
TStechnic al specification
BAself-contained breathing apparatus
: [[UFSAR]] [[updated final safety analysis report]]
: [[SDV]] [[scram discharge volume]]
: [[SH]] [[]]
IPsystem health indicator program
SSC structure, system, component
: [[TS]] [[technic al specification]]
: [[UFS]] [[]]
: [[AR]] [[updated final safety analysis report]]
}}
}}

Revision as of 21:32, 21 October 2018

IR 05000352-07-004, 05000353-07-004; on 07/01/07-09/30/07; Limerick Generating Station, Units 1 and 2; Routine Integrated Report
ML073180045
Person / Time
Site: Limerick  Constellation icon.png
Issue date: 11/13/2007
From: Krohn P G
Reactor Projects Region 1 Branch 4
To: Pardee C G
Exelon Generation Co, Exelon Nuclear
KROHN, PG
References
IR-07-004
Download: ML073180045 (25)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I475 ALLENDALE ROADKING OF PRUSSIA, PENNSYLVANIA 19406-1415 November 13, 2007Mr. Charles G. PardeePresident and CNO Exelon Nuclear Exelon Generation Company, LLC 200 Exelon Way Kennett Square, PA 19348

SUBJECT: LIMERICK GENERATING STATION - NRC INTEGRATED INSPECTIONREPORT 05000352/2007004 AND 05000353/2007004

Dear Mr. Pardee:

On September 30, 2007, the U. S. Nuclear Regulatory Commission (NRC) completed aninspection at your Limerick Generating Station Units 1 and 2. The enclosed integrated inspection report documents the inspection results which were discussed on October 15, 2007, with Mr. E. Callan and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.Based on the results of this inspection, no findings of significance were identified.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/Paul G. Krohn, ChiefProjects Branch 4 Division of Reactor ProjectsDocket Nos: 50-352, 50-353License Nos: NPF-39, NPF-85

Enclosure:

Inspection Report 05000352/2007004 and 05000353/2007004

w/Attachment:

Supplemental Information

SUMMARY OF FINDINGS

IR 05000352/2007-004, 05000353/2007-004; 07/01/2007 - 09/30/2007; Limerick GeneratingStation, Units 1 and 2; Routine Integrated Report.The report covered a three-month period of inspection by resident inspectors and announcedinspections by reactor inspectors. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight," Revision 4, dated December 2006.A.

NRC-Identified and Self-Revealing Findings

No findings of significance were identified.

B. Licensee-Identified Violations

None.

REPORT DETAILS

Summary of Plant StatusUnit 1 began this inspection period operating at full rated thermal power. On August 16, 2007,reactor power was reduced to 20 percent and the main generator was removed from service to repair the generator output number 11 disconnect switch. On August 17, 2007, the disconnect switch repairs were completed and the main generator was returned to service. Unit 1 returned to 100 percent power on August 18, 2007. With the exception of a planned end of summer load drop to 85 percent power on September 8, 2007, Unit 1 remained at full power for the remainder of the period.

Unit 2 began this inspection period operating at full rated thermal power. On August 6, 2007, reactor power decreased to 75 percent due to an unplanned speed reduction on the 2B reactor recirculation pump. The pump speed change was due to a recirculation motor generator electronic card failure. The card was replaced and Unit 2 was returned to 100 percent power later in the day. With the exception of a planned end of summer load drop to 60 percent power on September 15, 2007, Unit 2 remained at full power for the remainder of the period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weather Protection (71111.01 - 1 system sample)

a. Inspection Scope

The inspectors evaluated Exelon's preparations and protection for summer weather. OnJuly 10, 2007, the inspectors walked down Unit 1 and Unit 2 main generators and main transformers during hot weather and a grid heavy load voltage condition. The documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed four partial walkdowns of plant systems to verify the operabilityof redundant or diverse trains and components when safety equipment in the opposite train was either inoperable, undergoing surveillance testing, or potentially degraded. The inspectors used plant Technical Specifications (TS), Exelon operating procedures, plantpiping and instrumentation drawings (P&IDs), and the Updated Final Safety Analysis Report (USFAR) as guidance for conducting partial system walkdowns. The inspectors reviewed the alignment of system valves and electrical breakers to ensure proper in-service or standby configurations as described in plant procedures and drawings.

2Enclosure During the walkdown, the inspectors evaluated material condition and generalhousekeeping of the system and adjacent spaces. The documents reviewed are listed in the Attachment. The inspectors performed walkdowns of the following systems:*Unit 1 High Pressure Coolant Injection (HPCI) system;*Unit 1 D-13 Emergency Diesel Generator (EDG);

  • Unit 1 Reactor Core Isolation Cooling (RCIC)..2Complete System Walkdown (71111.04S - 1 sample)The inspectors conducted one complete walkdown of the Unit 1 and Unit 2 Control RodDrive (CRD) systems to verify functional capability of the system. The inspectors used plant TS, Exelon operating procedures, P&IDs, the UFSAR, and past surveillance tests as guidance for conducting the complete system walkdown. The inspectors reviewed the alignment of system valves, position of electrical breakers and settings of the system flow controller to ensure proper system configuration as described in plant procedures and drawings. During the walkdown, the inspectors evaluated the material condition and general housekeeping of the system and open issue reports associated with the system.

The walkdown also included an evaluation of system piping, supports, and component foundations to ensure they were not degraded. The documents reviewed are listed in the

.

b. Findings

No findings of significance were identified.

1R05 Fire Protection.1Fire Protection - Tours

(71111.05Q - 8 samples)

a. Inspection Scope

The inspectors conducted a tour of the eight areas listed below to assess the materialcondition and operational status of fire protection features. The inspectors verified that combustibles and ignition sources were controlled in accordance with Exelon's administrative procedures, fire detection and suppression equipment was available for use, and that passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out-of-service, degraded, or inoperable fire protection equipment in accordance with Exelon's fire plan. The documents reviewed are listed in the Attachment. The inspectors performed the following samples:*Main Control Room and peripheral rooms;*Unit 1 Refuel Floor;

  • Unit 2 Refuel Floor;
  • Unit 1 and Unit 2 Static Inverter compartments;
  • Unit 1 and Unit 2 Standby Gas Treatment system filter compartments and accessarea; 3Enclosure *Control Room Structure fan room, Elevation 304; and*Unit 1 D14 Diesel Generator Room..2Fire Protection - Drill Observation (71111.05A - 1 sample)

a. Inspection Scope

The inspectors observed one unannounced fire drill conducted in the Unit 1 aircompressor, electro-hydraulic control (EHC) power unit, and turbine lubricating oil storage tank area on September 26, 2007. The inspectors observed the drill to evaluate the readiness of the plant fire brigade to fight fires. The documents reviewed are listed in the Attachment. Specific attributes evaluated were:*Proper donning of fire fighting turnout gear and self-contained breathingapparatus (SCBA); *Proper use and layout of fire hoses;

  • Employment of appropriate fire fighting techniques;
  • Sufficient fire fighting equipment brought to the scene;
  • Effectiveness of fire brigade leader communications, command, and control;
  • Search for victims and propagation of fire into other plant areas;
  • Smoke removal operations;
  • Utilization of pre-planned strategies;
  • Adherence to the pre-planned drill scenario; and
  • Drill objectives.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

(71111.06 - 1 sample)Internal Flooding

a. Inspection Scope

The inspectors reviewed documents and inspected structures, systems, and components(SSCs) relative to the adequacy of internal flood protection measures for the Unit 1 HPCI room. The inspectors performed walkdowns of the relevant areas to verify the adequacy of flood mitigation doors and barriers, drainage systems, and other flood protection features. The documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11Q - 1 sample)Resident Inspector Quarterly Review (1 sample)

a. Inspection Scope

4Enclosure On August 28, 2007, the inspectors observed a licensed operator requalificationsimulator scenario. The scenario included a simulated spurious Division 1 Loss of Coolant Accident (LOCA) signal with failure of the D11 EDG to start and an unisolablereactor water cleanup leak, which resulted in a manual scram and emergency blowdown.

The inspectors observed the performance of two operating crews responding to the same scenario. The inspectors assessed licensed operator performance, including operator critical tasks that measure operator actions required to ensure the safe operation of the reactor and protection of the nuclear fuel and primary containment barriers. The inspectors observed the training evaluators' critiques at the conclusion of each simulation. The documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

(71111.12 - 3 samples)

a. Inspection Scope

The inspectors evaluated Exelon's work practices and follow-up corrective actions forSSCs and identified issues to assess the effectiveness of Exelon's maintenance activities. The inspectors reviewed the performance history of risk significant SSCs and assessed Exelon's extent-of-condition determinations for those issues with potential common cause or generic implications to evaluate the adequacy of the station's corrective actions. The inspectors assessed Exelon's problem identification and resolution actions for these issues to evaluate whether Exelon had appropriately monitored, evaluated, and dispositioned the issues in accordance with Exelon procedures and the requirements of 10 CFR 50.65, "Requirements for Monitoring the Effectiveness of Maintenance." In addition, the inspectors reviewed selected SSC classifications, performance criteria and goals, and Exelon's corrective actions that were taken or planned, to evaluate whether the actions were reasonable and appropriate. The documents reviewed are listed in the Attachment. The inspectors performed the following samples:*1A post LOCA recombiner maintenance rule (a)(1) determination;*2B Turbine Enclosure Cooling Water heat exchanger system outage window; and

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 8 samples)

a. Inspection Scope

The inspectors evaluated the effectiveness of Exelon's maintenance risk assessmentsrequired by 10 CFR 50.65 (a)(4). This inspection included discussion with control room operators and risk analysis personnel regarding the use of Exelon's on-line risk monitoring software. The inspectors reviewed equipment tracking documentation, daily work schedules, and performed plant tours to gain assurance that the actual plant configuration matched the assessed configuration. Additionally, the inspectors verified that Exelon's risk management actions, for both planned and emergent work, were 5Enclosure consistent with those described in Exelon procedure, ER-AA-600-1042, "On-Line RiskManagement." The documents reviewed are listed in the Attachment. Inspectors reviewed risk assessments for the following issues:*Incorrect interpretation of ASME Code Case N-435-1;*Unit 1 HPCI room temperature high;

  • Unit 2 Reactor Recirculation Motor Generator runback to minimum speed;
  • Unit 1 Main Generator Disconnect high temperatures;
  • Unit 1 Main Generator Disconnect phases A and C jumper installation;
  • Large VAR (Volt-Ampere Reactive) swings during EDG run;

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

(71111.15 - 5 samples)

a. Inspection Scope

For the five operability evaluations described below, the inspectors assessed thetechnical adequacy of the evaluations to ensure that Exelon properly justified TS operability and verified that the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors reviewed the UFSAR to verify that the system or component remained available to perform its intended safety function. In addition, the inspectors reviewed compensatory measures implemented to ensure that the measures worked and were adequately controlled. The inspectors also reviewed a sample of issue reports (IRs) to verify that Exelon identified and corrected deficiencies associated with operability evaluations. The documents reviewed are listed in the Attachment. The inspectors reviewed operability evaluations for the following components:*Unit 2 HPCI HV-055-2F006;*Unit 1 HPCI Room Cooler;

  • Unit 2 HPCI Oil Pressure; and
  • Unit 2B Reactor Circulation Pump mechanical seal.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19 - 8 samples)

a. Inspection Scope

The inspectors reviewed the eight post-maintenance tests (PMTs) listed below to verifythat procedures and test activities ensured system operability and functional capability.

The inspectors reviewed Exelon's test procedures to verify that the procedures 6Enclosure adequately tested the safety functions that may have been affected by the maintenanceactivity, and that the applicable criteria in the procedures were consistent with information in the licensing and design basis documents. The inspectors also witnessed the test or reviewed test data to verify that the results adequately demonstrated restoration of the affected safety functions. The documents reviewed are listed in the Attachment. The inspectors reviewed post-maintenance tests for the following systems and components:*"C" Residual Heat Removal Service Water pump;*"2A" RHR Suppression Pool Cooling Valve;

  • D21 Diesel Generator;
  • Unit 2 Redundant Reactivity Control System (RRCS).

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22 - 5 samples)

a. Inspection Scope

The inspectors witnessed the performance and reviewed test data for five surveillancetests that are associated with selected risk-significant SSCs. The review verified that Exelon personnel followed TS requirements and that acceptance criteria were appropriate. The inspectors also verified that the station established proper test conditions, as specified in the procedures, that no equipment preconditioning activities occurred, and that acceptance criteria had been met. The documents reviewed are listed in the Attachment. The inspectors reviewed the surveillance tests for the following systems and components:*Unit 2 D24 EDG;*Unit 2 Division 2 Lower Pressure Coolant Injection;

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

(71111.23 - 1 sample)

a. Inspection Scope

The inspectors reviewed and compared the temporary modification listed below with theUFSAR and TS to verify that the modification did not affect operability or availability of the Unit 1 reactor recirculation motor generator. The inspectors ensured that station 7Enclosure personnel implemented the modification in accordance with the applicable temporaryconfiguration change process. The inspectors also reviewed the impact on existing procedures to verify appropriate revisions were made to reflect the temporary configuration change. Additionally, the inspectors evaluated the adequacy of proposed testing upon removal of the change. The documents reviewed are listed in the

. The inspectors performed the following sample:*TRT-D7-164, Install 1B Reactor Recirculation Pump Motor Generator TemporaryMechanical Stop.

b. Findings

No findings of significance were identified.

Cornerstone:

Emergency Preparedness (EP)1EP6Drill Evaluation (71114.06 - 2 samples).1General Emergency Classification due to Simulated Fuel Failure Coincident with FailedOpen Main Steam Line Isolation Valves

a. Inspection Scope

On June 19, 2007, the inspectors observed an EP training drill in the control roomsimulator. The inspectors assessed Exelon's emergency response organization's (ERO)implementation of the Limerick emergency plan and implementing procedures, and the ERO's response to simulated degraded plant conditions to identify weaknesses and deficiencies in classification, notification, and protective action recommendation (PAR)development activities. In addition, the inspectors assessed licensed operator performance required to ensure the safe operation of the reactor and the protection of the nuclear fuel and primary containment barriers. The inspectors reviewed Exelon's training evaluators' critiques and the formal critique report, dated July 31, 2007, associated with the EP drill, to evaluate Exelon's identification of weaknesses and deficiencies. The inspectors compared inspector observed weaknesses with those identified in Exelon's formal drill critique to verify whether Exelon adequately identified weaknesses and deficiencies at an appropriate threshold. The documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified..2Site Area Emergency Classification Due to a Simulated Reactor Coolant System Leak inthe Reactor Building

a. Inspection Scope

The inspectors observed a licensed operator requalification simulator exercise evaluationto identify the timing and adequacy of classification, notification, and PAR development activities. During the simulator evaluation, the inspectors reviewed checklists and forms 8Enclosure used for classification and notification activities, and compared them to the criteria inExelon's Emergency Plan, EP-MA-114-100-F-01, "State/Local Event Notification Form,"

and supporting procedures. The documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.2.OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

1. Inspection ScopeThe inspector sampled Exelon's submittal of the performance indicators listed below toverify the accuracy of the data recorded from the third quarter of 2006 through the third quarter of 2007. The inspectors utilized performance indicator definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, to verify the basis in reporting for each data element.

The inspectors reviewed various documents, including portions of main control room logs, issue reports, power history curves, work orders, and system derivation reports.

The inspectors also discussed the method for compiling and reporting performance indicators with cognizant engineering personnel and compared graphical representations from the most recent PI report to the raw data to verify that the report correctly reflected the data. The documents reviewed are listed in the Attachment. Cornerstone: Initiating Events (2 samples)*Unit 1 Unplanned Power Changes per 7000 Critical Hours; and*Unit 2 Unplanned Power Changes per 7000 Critical Hours.Cornerstone: Mitigating Systems (6 samples)*Unit 1 High Pressure Coolant Injection system;*Unit 2 High Pressure Coolant Injection system;

b. Findings

No findings of significance were identified.4OA2Identification and Resolution of Problems (71152)Review of Items Entered into the Corrective Action Program (CAP)9Enclosure As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of all items entered into Limerick's CAP. The inspectors accomplished this by reviewing the description of each new issue report and accessing Exelon's computerized database. The documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified. The inspectors observed that issues selectedfor review were appropriately categorized and prioritized in accordance with Exelon's corrective action process.4OA3Event Followup (71153).1Unit 1 Main Generator Output Switchyard Disconnect Removal from Service due to HighTemperature

a. Inspection Scope

On August 16, 2007, the inspectors responded to the plant due to a high temperature onthe Unit 1 main generator output disconnect. The inspectors discussed the switchyard disconnect problem with operations personnel, engineering personnel, and Exelon management to gain an understanding of Exelon's response and follow-up actions. The inspectors reviewed troubleshooting activities, the disconnect temperature surveillance monitoring, and the planned actions to repair and correct the disconnect high temperature condition. The number 11 disconnect is located on the output of the Unit 1 main transformers and isphysically located in the Unit 1 220 kilovolt (kV) switchyard. The disconnect is comprised of three individual disconnects and associated bus bars. The disconnect "B" phase temperature reached a maximum value of 375 degrees Celsius and resulted in reactor power reductions to lower the temperature. The location of the elevated temperature was at the movable hinged section of the disconnect. The "A" and "C" phase temperatures were 95 to 100 degrees Celsius. The "B" phase high temperature was discovered during ongoing monthly temperature monitoring. In response to the high temperature, operators reduced reactor power from 100 percentdown to 25 percent to reduce the disconnect temperature and support removal of the main generator and disconnect from service to perform repairs. The inspectors observed "just-in-time training" in the simulator that was given to the operators prior to removing the main generator and disconnect from service. The inspectors also observed the operators' removal of the main generator and disconnect from service to support repairs.

After removal from service, the "B" phase disconnect was rebuilt and tested satisfactorily prior to being returned to service. The main generator was placed back in service and the plant was returned to 100 percent power. The documents reviewed are listed in the

.

b. Findings

10Enclosure No findings of significance were identified..2(Closed) LER 05000353/02007-001, Scram Discharge Volume Vent and Drain Valves Failed Open Due to Clearance Tagging ErrorOn March 10, 2007, Limerick Unit 2 was in hot shutdown and depressurized toapproximately 25 psig for the 2R09 refueling outage. A full scram signal was present and the scram discharge volume (SDV) was isolated, as designed. Operators were in the process of applying a clearance in preparation for planned maintenance on the Reactor Protection System and the scram air header. As part of this clearance, operators removed the Reactor Protection System backup scram fuses which ultimately resulted in the SDV vent and drain valves opening unexpectedly. Water from the SDV began to vent through these open valves into the plant drain system. Station personnel discovered the condition and closed the SDV vent and drain valves, stopping the source of the water. Further investigation by the station determined that the inadvertent opening of the SDV vent and drain valves was due to an improperly written clearance. A non-cited violation (NCV) associated with this issue was documented in Section 1R20of NRC integrated inspection report 05000352/2007002 and 05000353/2007002. The inspectors reviewed this LER and did not identify any additional findings of significance.

Exelon documented this event and associated corrective actions in IR 602042. The documents reviewed are listed in the Attachment. This LER is closed..3(Closed) LER 05000353/02007-002, Valid Actuation of Main Condenser Low Vacuum Isolation Logic During OutageOn March 12, 2007, operators were in the process of lowering vacuum on Limerick Unit 2as part of refueling outage activities in accordance with procedure S07.2.A, "Shutdown of the Steam Jet Air Ejector and Breaking Main Condenser Vacuum." During this evolution, the main condenser low vacuum main steam isolation valve (MSIV) isolation logic actuated unexpectedly. Further investigation revealed that due to a procedural execution error, station personnel had only bypassed two of the required four channels of the isolation logic. Even though this resulted in actuation of two channels of logic when vacuum was lowered, no valves actually repositioned since the MSIVs and other affected valves were closed earlier as required by procedure. This failure to comply with procedure S07.2.A constitutes a violation of minor significance that is not subject to enforcement action in accordance with Section IV of the NRC's enforcement policy. The inspectors reviewed this LER and did not identify any additional findings of significance.

Exelon documented this event and associated corrective actions in IR 602921. This LER is closed.

.4 (Closed) LER 05000353/02007-003, Automatic Actuation of the Reactor ProtectionSystem at PowerOn April 24, 2007, the Unit 2 Reactor Protection System automatically actuated whenreactor water level decreased from +35 inches to +12.5 inches.

All control rods fullyinserted. When reactor level decreased to the low-low level setpoint of -38 inches, both HPCI and RCIC systems initiated and injected into the vessel. HPCI and RCIC were placed in manual mode when flow oscillations were observed on both systems. Both systems were automatically secured when reactor level increased to +54 inches.

11Enclosure Exelon's investigation determined that a circuit card in Redundant Reactivity ControlSystem (RRCS) Division 1, channel "B" spuriously actuated while channel "A" was in a tripped condition due to planned surveillance testing. This resulted in a feedwater runback. The feedwater runback reduced reactor level as expected.Exelon's investigation determined that HPCI and RCIC flow oscillations were due to flowcontrol loop tuning settings that did not properly account for differences in flow path testing conditions and vessel injection flow conditions. Station personnel replaced and successfully tested the affected RRCS circuit card. In addition the HPCI and RCIC flow controller gain and reset settings were adjusted to be consistent with Unit 1 settings, which are consistent with industry values and similar to previous Unit 2 settings when stable flow was demonstrated during Unit 2 initial startup testing. The procedure for tuning of HPCI and RCIC flow controls was revised to specify the required gain and reset settings.The inspectors reviewed Exelon's apparent cause investigation, Unit 2 TS, andnotification requirements. The apparent cause investigation determined that the HPCI and RCIC gain and reset settings were changed during system tuning in May 1999; therefore, this condition existed for approximately 8 years. This resulted in a condition that could have prevented the safety function of Unit 2 HPCI. A non-cited violation (NCV)associated with this issue was documented in Section IR19 of NRC integrated inspection report 05000352/2007003 and 05000353/2007003. Exelon documented this issue and its corrective actions in IR 620861. The review determined that Unit 1 was not affected.

The inspectors reviewed the corrective actions, including revised procedures, and found no additional findings or unresolved issues. The documents reviewed are listed in the

. This LER is closed.4OA6Meetings, Including ExitExit Meeting SummaryOn October 15, 2007, the resident inspectors presented the inspection results toMr. E. Callan and other members of his staff. The inspectors confirmed that proprietary information was not included in the inspection report. ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Exelon Generation Company

C. Mudrick, Site Vice President
E. Callan, Plant Manager
D. DiCello, Radiation Protection Manager
R. Dickinson, Director Engineering
J. Berg, System Manager, HPCI and RCIC
J. George, System Manager, Remote Shutdown Panel
M. Gift, System Manager, Radiation Monitoring Systems
R. Gosby, Radiation Protection Technician, Instrumentation
R. Harding, Engineer, Regulatory Assurance
R. Kreider, Manager, Regulatory Assurance
D. Malinowski, Simulator Instructor
B. Tracy, System Manager
P. Tarpinian, PRA Engineer
D. Boylan, Summer Readiness Coordinator
R. Newmaster, Manager - Emergency Preparedness, Limerick
J. Broillet, Operations Shift Manager

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Closed

05000353/LER-2007-001-0LERScram Discharge Volume Vent and DrainValves Failed Open due to Clearance
Tagging Error (Section 40A3.2)
05000353/LER-2007-002-0LERValid Actuation of Main Condenser LowVacuum Isolation Logic During Outage

(Section 40A3.3)

05000353/LER-2007-003LERAutomatic Actuation of the ReactorProtection System at Power (Section
40A3.4)

Discussed

None

A-2Attachment

LIST OF DOCUMENTS REVIEWED

Section 1R01:

Adverse Weather ProtectionProceduresOP-AA-108-107-1001, "Station Response to Grid Capacity Conditions," Revision 2S32.3.A, "Main Generator Inspection During Heavy Grid Load," Revision 7Section 1R04: Equipment AlignmentProceduresTechnical Specification 3/4 8.1, "A.C. Sources"S92.9.N, "Routine Inspection of the Diesel Generators," Revision 53
1S46.1.A (COL), "Valve and Breaker Alignment for Start-up of the Control Rod Drive Hydraulic Supply System for Service"
ST-6-048-230-1, "SLC Pump, Valve, and Flow Test"
S49.3.A, "RCIC Fill and Vent," Revision 17
Troubleshooting, Rework, and Testing Control Form, TRT No.07-174, RCIC Fill and Vent

Section 1R05: Fire ProtectionProceduresARC-MCR-006 B1L, Fire Alarm Response Card, Revision 2F-A-452, "Unit 1 Static Inverter Room, Fire Area 20," Revision 7

F-A-453, "Unit 2 Static Inverter Room, Fire Area 20," Revision 4
F-A-533, "Control Room 533 and Peripheral Rooms 530 to 535 (EL. 269) Fire Area 24," Revision 10F-A-619, "Control Structure Fan Room (EL. 304) Fire Area 27," Revision 6
F-A-624, "Standby Gas Treatment Area Rooms 624 & 625, Fire Area 28," Revision 6
F-D-311D, "D14 Diesel Generator Room and Fuel Oil and Lube Oil Tank Room Rooms 311Dand 312D (EL. 217) Fire Area 82," Revision 5F-T-328, "Unit 1 Air Compressor, EHC Power Unit, and Turbine Lube Oil Storage Tank AreasRooms 328, 330, and 331 (EL. 217) Fire Area 93," Revision 5OP-AA-201-003, "Fire Drill Performance," Revision 8
SE-8, "Fire," Revision 31
ST-6-022-551-0, "Fire Drill," Revision 8, conducted on 9/26/07Issue Reports and Action Requests (ARs)IR
676038, "Fire Brigade Member EO Key Ring"A1261436, "Evaluate Propping Open of Doors"MiscellaneousUFSAR Appendix 9A

Section 1R06: Flood Protection MeasuresProceduresSE-4, "Flood," Revision 5SE-4-1, "Reactor Enclosure Flooding," Revision 8

A-3AttachmentIssue Reports and Action RequestsIR
634795, "Floor Drain Clogged in U/1 HPCI Room"MiscellaneousBLP-31981, "Moderate Energy Pipe Break (MEPB) Analysis," dated February 1984NPB-14, "Moderate Energy Line Break," Revision 4
NPB-32, "Flooding of ECCS Compartments from the Suppression Pool," Revision 3NPB-33, "Moderate Energy Pipe Break Report," Revision 3

Section 1R11: Licensed Operator Requalification ProgramProceduresEOP

T-101, "RPV Control," Revision 20 EOP T-103, "Secondary Containment Control," Revision 17
EOP T-112, "Emergency Blowdown," Revision 12
EOP T-270, "Terminate and Prevent injection into RPV," Revision 12

Section 1R12: Maintenance EffectivenessProceduresER-AA-310, "Implementation of the Maintenance Rule," Revision 6ER-AA-310-1004, "Maintenance Rule - Performance Monitoring," Revision 5

ER-AA-310-1003, "Maintenance Rule - Performance Criteria Selection," Revision 3
ER-AA-310-1005, "Maintenance Rule - Dispositioning Between (a)(1) and (a)(2)," Revision 5
ER-LG-310-1010, "Maintenance Rule Implementation," Revision 7
ER-AA-310, "Implementation of the Maintenance Rule," Revision 6Issue Reports and Action RequestsIR
483496, "TECW Unavailability Issues"IR
637270, "Possible Maintenance Rule (a)(1) for Excessive TECW System Outage Window"
IR 642006, "2B TECW Heat Exchanger Unavailability Hours Exceeded"
IR 667927, "Document Unit 2 HPCI Maintenance Rule (a)(1) Determination"
IR 506692, "Points 3 & 5 Failing"
IR 546231, "1A Recombiner Valve
FV-DO-101A Failed to Open"
IR 551504, "1A Post LOCA Recombiner MRule FF (A)(1) Determination"MiscellaneousMaintenance Rule Expert Panel Meeting Minutes, dated 11/01/2006, 11/30/2006Maintenance Rule Expert Panel Meeting Minutes, dated 09/14/2000, 02/15/2001, 04/20/2006,
06/19/2007

Section 1R13: Maintenance Risk Assessments and Emergent Work ControlProceduresER-AA-600-1045, "Risk Assessments of Missed or Deficient Surveillances," Revision 0S07.6.A, "Placing Alternate Steam Jet Air Ejector In Service," Revision 27

ST-2-041-661-1, "Safety Relief Valves - Safety Relief Valve Position Indicators Functional Test,"Revision 12Issue Reports and Action RequestsIR
598489, "D11 - Adjust Voltage Regulator Droop to 3% - 5%"
A-4AttachmentIR
601471, "ISI Inspection Volume for Code Case N-435"IR
649698, "Incorrect Interpretation of ASME Code Case N-435-1"
IR 657596, "2B Reactor Recirculation MG Set Runback to Min Speed"
IR 668047, "Large VAR Swings During D12 D/G/ Run"IR
674591, "SRV 'D' Position Indicator Functional Test Failed"
A1456726, "Excursion in KVAR and KW"
A1600437, "D12 Voltage Regulator VAR Swings When Paralleled to Offsite"
A1628762, "IR for Generation of Activity to Swap Unit 2 SJAE"
A1631597, "Repair/Replace/Recal Loop Component," Dated 09/24/2007MiscellaneousOperator Logs dated 07/13/2007Limerick Generating Station On-Line Work Schedule, 09/14/2007-09/16/2007

==Section 1R15: OperabilityIssue Reports and Action RequestsIR

060981, "HPCI Turbine Steam Supply Valve Position Relay Contacts Failed"IR
101384, "Inappropriate Conclusions in Disp==
PEP I0012531/CR 00060981"
IR 641784, "HPCI Aux Oil Pump Did Not Stop per PV&F"
IR 642617, "HV-055-2F006 Failed to Stroke Open"
IR 658690, "Unit 2 RCIC OOS/Gross Fail Alarm"
IR 658931, "RCIC Pump Suction HI Press Alarm Came in While Swapping Suction Valves"
IR 658950, "HPCI Oil Pressure Lower Than Desired Band"
A1626638, "HPCI Oil Pressure Lower Than Desired Band"
IR 651187, "HPCI Higher than Normal Unit 1 HPCI Pump Room Temperature"
IR 664065, "Unit 2 Recirculation Pump #2 Seal Pressure Drop"MiscellaneousLimerick Generating Station UFSAR Section 6.3LEAM-0008, "HPCI Flow to RPV w/Single Discharge Path Open," Revision 0
M-48-12, "SLCS Boron Injection Delay Time," Revision 4
M-55-10, "HPCI Line Sizing Check," Revision 4
M-55-26, "ATWS 3A HPCI Flow Split Calculation to Size a Flow Orifice for Branch to CoreSpray," Revision 6ECR
LG 01-01152, "HPCI Failed Injection Valve - Provide Quality Docs"

Section 1R19: Post Maintenance TestingProceduresST-2-042-638-2, "ATWS - Reactor Vessel Water Level - Low Low, Functional Test," Revision 12ST-6-051-231-2, "A

RHR Pump, Valve and Flow Test," Revision 52
ST-6-012-231-0, "A Loop RHRSW Pump, Valve and Flow Test", Revision 54
ST-6-048-230-1, "SLC Pump, Valve and Flow Test", Revision 32
ST-6-107-201-0,"IST Valve Stroke for New Baseline," Revision 4
M-C-792-001, "Fairbanks Morse Opposed Piston Diesel Engine Examination and GeneralMaintenance," Revision 4Issue Reports and Action RequestsIR
338368, "Unit 2 RCIC Small Packing Leak from
HV-049-2F008 OUTBD PCIV"IR
381319, "Unit 2 RCIC
HV-049-2F008 Packing Leak"
A-5AttachmentIR
654021,"D22 Diesel Lube Oil Circ Pump Making Excess Noise"IR
654041, "Dual Indication for
HV-51-2F024A During Stroke Close"
IR 663431, "D21: Brush Holder Cable Replacement Not Identical to Original"
IR 664060, "D21 Diesel Rapid Shutdown Due to Cylinder Leak"
IR 664291, "D21 Emergency Stop Alarm Failed to Annunciate"
IR 676024, "Indicating Lights did not Illuminate"
A1178453, "Disassemble and Inspection 20" Manual Check Valve, 012-0001C"
A1624433, "Replace RRCS
HPII/HPOI Cards"A1628140, "D21 Over Excitation During Break-In Run"
A1628023, "Alarms on D21 Still Annunciated and Will Not Clear"
A1628302, "D21 Diesel Rapid Shutdown Due to Cylinder Leak"
A1630245, "Unit 2 RCIC Steam Line Outboard PCIV"Work OrdersR1005988, "D21 24 Month Diesel Inspection Per M-C-792-001" MiscellaneousLimerick Generating Station On-Line Work Schedule 08/23/2007-08/26/2007Operator Logs dated 08/23/2007
Safety Relief Valve Technical Specification Accident Monitoring Instrumentation Table 3.3.7.5-1

Section 1R22: Surveillance TestingProceduresST-2-051-802-2, "Division 2

LPCI System Response Time Testing," Revision 8ST-2-055-810-1, "HPCI System Response Time Testing," Revision 11, completed 09/18/2007
ST-6-055-230-1, "HPCI Pump, Valve, and Flow Test," Revision 65, completed 09/18/2007
ST-6-092-314-2, "D24 Diesel Generator Slow Start Operability Test Run," Revision 61,completed 07/16/07ST-6-107-790-2, "Control Rod Scram Timing," Revision 11, completed 09/20/2007Issue Reports and Action RequestsA1614302, "U2
HCU 46-47 Has No Full Out Position Indication on Full Core Display"IR
671836, "Blue Scram Light Failed to Light During ST-6-107-790-2"

Section 1R23: Temporary Plant ModificationsProceduresCC-AA-112, "Temporary Configuration Changes," Revision 12S43.0.C, "Clearing an Electrical or Mechanical Stop," Revision 18MiscellaneousTRT-D7-164, "Install 1B Reactor Recirculation Pump Motor Generator Temporary Mechanical Stop"C0221920, "Install Temporary Mechanical High Speed Stop in

XY-M1-1S001B" Limerick Generating Station UFSAR Section 5.4
Limerick Generating Station Technical Specifications 3/4.4.1Issue Reports and Action RequestsIR
631119, "1B Recirc Pump Speed Changes"IR
654530, "Emergent PRA - Need New AR Created to Install Travel Limiter"
A1616738, "1B Recirc Pump Speed Changes"
A-6AttachmentA1625008, "Need New AR Created to Install Travel Limiter"

Section 1EP6: Drill EvaluationProceduresEOP

T-117, "Level/Power Control," Revision 15EOP T-104, "Radioactivity Release Control," Revision 12
EOP T-103, "Secondary Containment Control," Revision 17
EOP T-270, "Terminate and Prevent Injection Into RPV," Revision 12
EP-AA-122, "Drills and Exercises," Revision 7
EP-AA-122-F-01, "Drill and Exercise Evaluation Criteria," Revision B
EP-AA-122-1001, "Drill and Exercise Scheduling, Development, and Conduct," Revision 8
EP-AA-122-1002-F-02, "Drill and Exercise Objective Evaluation Data Tables," Revision B
LS-AA-120, "Issue Identification and Screening Process," Revision 7
T-103, "Secondary Containment Control," Revision 17MiscellaneousIR 437320IR 670538
Limerick [EP] Training Drill Series Evaluation Report, dated 07-31-2007
LSES-8020, "Licensed Operator Training Simulator Evaluation Scenario," Revision 0
NRC IR 50-352&353/2005009

==Section 4OA1: Performance Indicator (PI) VerificationProceduresS92.6.N, "Diesel Oil Storage Tank Lineup to Fill Other than its Associated Day Tank," Revision 10Issue Reports and Action RequestsIR

556902, "Minor Leakby of 049-2F014 Discovered During==
ST-2-049-601-2"IR
565800, "HV-049-1F019 RCIC Min Flow Shows Dual Indication at 600 GPM"
IR 620861, "GP-18 Review HPCI/RCIC Oscillations"
IR 628573, "RCIC MOV Overload or Power Loss DS14"
IR 628579, "Inadvertent RCIC OOS Annunciator"
IR 628600, "2DA-09 Tripped on Thermals"
IR 642618, "Valve Stroke Time Outside Acceptable Range"
IR 652846, "RCIC Overspeed Test Potentiometers Possibly Not Locked"
A1238085, "Determine if HPCI is Operable With Temperature Instrumentation Installed"
A1295250, "FI-49-1R600-1 Spiking"
A1304397, "Revise the
ML-008 Spec to Correctly Reflect the Safety Classification of the RCICMin Flow Line"MiscellaneousNEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5Reactor Oversight Program MSPI Bases Document, Limerick Generating Station, Revision 1
MSPI Derivation Reports for HPCI, RCIC, and EDGs Operator Logs dated 07/01/2007 through 07/31/2007
Maintenance Rule Failure Reports for HPCI, RCIC, and EDGs
LG 01-00170, "Classification of the RCIC Min Flow Line"

Section 4OA2: Other

A-7AttachmentIssue Reports and Action RequestsA16106882C-P501 Packing Leakoff Excessive (Complete)A16159402C Circ Pump Step Change in Vibration
A1620985Spray Pond Level/Temp Alarming Before Setpoints Reached
A16219922C-P501 Excessive Packing Leakage (Complete)
A1622672Control Rod 22-35 Temp at 305 Deg F
A1628676Spray Pond Hi Temp Alarms Early
C02212742C-P501-DR Inspect or Replace Motor Bearings
IR 6120832C-P501 Packing Leakoff Excessive
IR 612647Drive Mechanism Temperature for
HCU 30-35 is @429 Degrees F
IR 6275952C Circ Pump Surge Capacitor Damaged
IR 6289652C Circ Pump Step Change in Vibration
IR 639934"Spray Pond Lo Level/Hi Temp" Alarm Locked In
IR 643596Spray Pond Level/Temp Alarming Before Setpoints Reached
IR 6454662C-P501 Excessive Packing Leakage
IR 648107Control Rod 22-35 Temp at 305 Deg F (Completed)
IR 649388Hairline Crack Identified on Yoke
IR 6498062C-P501-DR Temp Cooling
IR 654068Hairline Crack Identified on Yoke
IR 654070Hairline Crack Identified on Yoke
IR 665262Spray Pond Hi Temp Alarms Early
IR 6723152C-P501 High Packing Leak OffOther DocumentsPlant Health Committee System Presentation: Circ Water, June, 2007Plant Health Committee System Presentation: Control Rod Drive Supply, June, 2007
Plant Health Committee System Presentation: EDG, June, 2007
Plant Health Committee System Presentation: RHRSW, June, 2007
SHIP Chronic Problem Report: Circ Water, June, 2007
SHIP Chronic Problem Report: EDG, June, 2007
System Health Overview Report: Circ Water, June, 2007
System Health Overview Report: Control Rod Drive Supply, June, 2007
System Health Overview Report: EDG, June, 2007
System Health Overview Report: RHRSW, June, 2007
System Health Overview Report: Circ Water, Sept, 2007
System Health Overview Report: Control Rod Drive Supply, Sept, 2007
System Health Overview Report: EDG, Sept, 2007
System Health Overview Report: RHRSW, Sept, 2007

==Section 4OA3: Event FollowupProceduresOP-LG-109-101-1001, "Limerick System Specific Tagging Guides," Revision 15Issue Reports and Action RequestsIR

601910, "Drainage System Clogged"IR
602042, "Unit 2==
SDV Vent/Drain Valves Open With Scram Signal Present"
IR 602921, "Division 1 and 4 MSIV Isolation Logic Alarms"
A-8AttachmentMiscellaneousLER 2007-001, "Scram Discharge Volume Vent and Drain Valves Failed Open Due to ClearanceTagging Error"LER 2007-002, "Valid Actuation of Main Condenser Low Vacuum Isolation Logic During Outage"
LER 2007-003, "Automatic Actuation Of The Reactor Protection System at Power"

LIST OF ACRONYMS

ADAMSAgencywide Documents Access Management SystemARaction request

ASMEAmerican Society of Mechanical Engineers

CAPCorrective Action Program

CFRCode of Federal Regulations

CRDcontrol rod drive

EDGemergency diesel generator

EHCelectro-hydraulic control

EPemergency preparedness

EROEmergency Response Organization

HPCIhigh pressure coolant injection

IRissue report

kVkilo volt

LERLicensee Event Report

LOCAloss of coolant accident

MSIVmain steam isolation valve

NCVnon-cited violation

NEINuclear Energy Institute

NRCNuclear Regulatory Commission

OAother activities

PARprotective action recommendation

PARSPublicly Available Records

PIperformance indicator

P&IDpiping and instrumentation drawing

PMTpost-maintenance test

RCICreactor core isolation cooling

RHRresidual heat removal

RRCSredundant reactivity control system

SCBAself-contained breathing apparatus

SDVscram discharge volume

SHIP ystem health indicator program
SSC structure, system, component

TStechnic al specification

UFSAR updated final safety analysis report