Letter Sequence Approval |
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EPID:L-2020-LLR-0050, 10 CFR 50.55a Request Number 2-TYP-4-RV-06, Hardship for Hot Leg Nozzle Inspections (Approved, Closed) |
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MONTHYEARML20093G6512020-04-0202 April 2020 Email Beaver Valley Unit 2 - Request for Additional Information - Snubber RR Project stage: RAI L-20-118, CFR 50.55a Request Number SRR-1, Revision 0, Snubber Testing2020-04-0303 April 2020 CFR 50.55a Request Number SRR-1, Revision 0, Snubber Testing Project stage: Request L-20-125, Response to Request for Additional Information Regarding 10 CFR 50.55a Request Number SRR-1, Rev. 0, Snubber Testing2020-04-0303 April 2020 Response to Request for Additional Information Regarding 10 CFR 50.55a Request Number SRR-1, Rev. 0, Snubber Testing Project stage: Response to RAI L-20-117, 10 CFR 50.55a Request Number 2-TYP-4-RV-06, Hardship for Hot Leg Nozzle Inspections2020-04-0303 April 2020 10 CFR 50.55a Request Number 2-TYP-4-RV-06, Hardship for Hot Leg Nozzle Inspections Project stage: Request ML20095J0992020-04-0404 April 2020 Email Beaver Valley Power Station, Unit 2 - Verbal Relief for Snubbers - Delivered 4/4/2020 at 4:00 P.M Project stage: Other ML20223A0142020-08-20020 August 2020 Issuance of Relief Request SSR-1, Revision 0, from the Requirements of the ASME Code (EPID L-2020-LLR-0050 (COVID-19)) Project stage: Approval 2020-04-03
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Category:Code Relief or Alternative
MONTHYEARML24226A3652024-05-13013 May 2024 Approval of Request for Alternative from Certain Requirements of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code ML23249A1842023-09-18018 September 2023 Authorization and Safety Evaluation for Alternative Request No. 2-TYP-4-RV-06 ML22082A2532022-03-29029 March 2022 Correction Letter - Issuance of Authorization of Proposed Alternative to Use ASME OM Code Case OMN-27 ML22012A2972022-01-21021 January 2022 Proposed Alternative to Use ASME OM Code Case OMN-27 L-20-256, Request to Use Provision in Later Edition of the ASME Boiler and Pressure Vessel Code, Section XI2020-09-28028 September 2020 Request to Use Provision in Later Edition of the ASME Boiler and Pressure Vessel Code, Section XI ML20223A0142020-08-20020 August 2020 Issuance of Relief Request SSR-1, Revision 0, from the Requirements of the ASME Code (EPID L-2020-LLR-0050 (COVID-19)) ML20206K8652020-08-0707 August 2020 Relief Requests 2-TYP-4-RV-06 and 2-TYP-4-RV-07 from the Requirements of the ASME Code (EPID L-2020-LLR-0053 and EPID L-2020-LLR-0054 (COVID-19)) ML20145A0002020-06-0303 June 2020 Relief from the Requirements of the ASME Code for Requests VRR6 and VRR5 (EPID L-2020-LLR-0049 and EPID L-2020-LLR-0051 (COVID-19)) ML20100N3222020-04-0909 April 2020 Verbal Relief for Penetration Evaluation and Hot Leg Nozzles - Delivered 4/9/2020 at 10:00 Am ML20099B2572020-04-0808 April 2020 Verbal Relief Unit 2 CIV ML20098F3012020-04-0707 April 2020 Verbal Relief for Appendix I Safety Relief Valves ML20095J2192020-04-0404 April 2020 Email Beaver Valley Power Station, Unit 2 - Verbal Relief for MOVs - Delivered 4/4/2020 at 4:00 Pm ML20095J0992020-04-0404 April 2020 Email Beaver Valley Power Station, Unit 2 - Verbal Relief for Snubbers - Delivered 4/4/2020 at 4:00 P.M L-20-117, 10 CFR 50.55a Request Number 2-TYP-4-RV-06, Hardship for Hot Leg Nozzle Inspections2020-04-0303 April 2020 10 CFR 50.55a Request Number 2-TYP-4-RV-06, Hardship for Hot Leg Nozzle Inspections L-20-118, CFR 50.55a Request Number SRR-1, Revision 0, Snubber Testing2020-04-0303 April 2020 CFR 50.55a Request Number SRR-1, Revision 0, Snubber Testing L-20-060, CFR 50.55a Request Number: VRR4, Revision 0, Containment Isolation Valve Test Frequency2020-04-0202 April 2020 CFR 50.55a Request Number: VRR4, Revision 0, Containment Isolation Valve Test Frequency L-20-116, CFR 50.55a Request Number VRR6, Revision 0, Motor-Operated Valve Test Frequency2020-04-0101 April 2020 CFR 50.55a Request Number VRR6, Revision 0, Motor-Operated Valve Test Frequency ML20079F8162020-03-26026 March 2020 Relief Requests 1-TYP-4-C2.21-1 and 1-TYP-4-RA-1 Regarding Weld Examination Coverage for the Fourth Inservice Inspection Interval ML19275E2942019-10-16016 October 2019 Issuance of Relief Request Proposed Alternative to Reactor Vessel Nozzle Weld Examination Frequency Requirements in Lieu of Specific ASME Code Requirements L-19-107, Impractical American Society of Mechanical Engineers Boiler and Pressure Vessel Code Section XI Examination Requirements2019-08-27027 August 2019 Impractical American Society of Mechanical Engineers Boiler and Pressure Vessel Code Section XI Examination Requirements ML19051A1082019-02-20020 February 2019 Request Alternative Examination Frequency for Reactor Vessel Nozzle to Safe-End Welds (Request 2-TYP-4-RV-05, Revision 0) ML18227A7332018-08-27027 August 2018 Request for Relief from the Requirements of the ASME Code ML18004A1222018-01-22022 January 2018 FENOC-Beaver Valley, Davis-Besse, and Perry - Alternative for the Use of ASME Code Case N-513-4 (CAC Nos. MG0120, MG0121, MG0122, and MG0123; EPID L-2017-LLR-0088) L-17-317, Request to Extend Certain Reactor Vessel Inspections from 10 to 20 Years (Request 1-TYP-4-BN-01)2017-11-15015 November 2017 Request to Extend Certain Reactor Vessel Inspections from 10 to 20 Years (Request 1-TYP-4-BN-01) L-17-308, 10 CFR 50.55a Request for Alternate Reactor Vessel Nozzle Flaw Depth Sizing Criteria (Request 2-TYP-4-RVSE-2)2017-10-25025 October 2017 10 CFR 50.55a Request for Alternate Reactor Vessel Nozzle Flaw Depth Sizing Criteria (Request 2-TYP-4-RVSE-2) ML17167A0672017-06-26026 June 2017 Requests for Alternatives and Requests for Relief Fourth 10-Year Inservice Test Program Interval (CAC Nos. MF8333-MF8356). Note: Correction Safety Evaluation See ML17255A526 ML17159A4422017-06-26026 June 2017 Requests for Alternatives and Requests for Relief Fifth 10-Year Inservice Testing Program Interval (CAC Nos. MF8332 Through MF8357). Note: Correction Safety Evaluation See ML17255A508 ML17047A6102017-03-0202 March 2017 Relief from the Requirements of the American Society of Mechanical Engineers Code ML17041A1852017-03-0202 March 2017 Relief from the Requirements of the ASME Code ML17048A0042017-03-0202 March 2017 Relief from the Requirements of the ASME Code ML16328A1252017-01-23023 January 2017 Relief from the Requirements of the American Society of Mechanical Engineers (ASME) Code for Operation and Maintenance of Nuclear Power Plants (OM Code) (TAC No. MF7780 - MF7783) ML16190A1332016-12-27027 December 2016 Relief from the Requirements of the ASME Code ML16319A0572016-12-0101 December 2016 Acceptance of Requested Licensing Action Relief Request for Proposed Alternative to Perform As-Found Set-Pressure Test ML16257A6212016-11-21021 November 2016 Relief Request BV2-PZR-01, Regarding Alternative to Requirements for Components Connected to the Steam Side of the Pressurizer ML16228A4082016-10-21021 October 2016 Correction to Relief Request 2-TYP-3-RV-04, Revision 0, Regarding Repair Activities for Reactor Vessel Head Penetration Nozzles and Associated J-Groove Welds ML16147A3622016-06-17017 June 2016 Relief Request No. 2-TYP-3-RV-04, Revision 0, Regarding Repair Activities for Reactor Vessel Head Penetration Nozzles and Associated J-Groove Welds ML14363A4092015-01-28028 January 2015 Relief Request No. 1-TYP-4-RV-04 Regarding the Examination Requirements of Code Case N-729-1 ML1202702982012-02-0707 February 2012 Relief Request VRR3 Regarding Solenoid Operated Valve Remote Position Verification Frequency ML1131304282011-11-22022 November 2011 Relief Request VRR5 Regarding Turbine Driven Auxiliary Feedwater Valve Test Frequency for the 10-Year Inservice Testing Program Interval ML1126404122011-09-20020 September 2011 Acceptance Review Results for VC Summer Relief Request (ME6879) ML1107705512011-04-26026 April 2011 Relief Request VRR2 Regarding the 10-Year Inservice Testing Program Interval ML1104705572011-02-25025 February 2011 Relief Request Regarding an Alternative Weld Repair Method for Reactor Vessel Head Penetrations J-Groove Welds ML1006807812010-03-12012 March 2010 Third 10-Year ISI Interval Relief Request (ME2608) L-08-362, Beaver, Units 1 and 2, Proposed Alternative to American Society of Mechanical Engineers Boiler and Pressure Vessel Code Section XI, Paragraph IWA-5244 Examination Requirements2008-12-0202 December 2008 Beaver, Units 1 and 2, Proposed Alternative to American Society of Mechanical Engineers Boiler and Pressure Vessel Code Section XI, Paragraph IWA-5244 Examination Requirements L-08-207, Proposed Alternative to American Society of Mechanical Engineers Boiler and Pressure Vessel Code Section XI Inspection Period Extension Requirement2008-09-24024 September 2008 Proposed Alternative to American Society of Mechanical Engineers Boiler and Pressure Vessel Code Section XI Inspection Period Extension Requirement L-08-069, Impractical American Society of Mechanical Engineers Code Section XI Weld Examination Requirements (Request Nos. 1-TYP-3-RA-1, 1-TYP-3-RA-2, 1-TYP-3-RA-3)2008-04-0909 April 2008 Impractical American Society of Mechanical Engineers Code Section XI Weld Examination Requirements (Request Nos. 1-TYP-3-RA-1, 1-TYP-3-RA-2, 1-TYP-3-RA-3) ML0720504882007-09-17017 September 2007 Relief Request No. BV1-PZR-01 Regarding Weld Overlay Repairs on Pressurizer Nozzle Welds ML0705905552007-04-30030 April 2007 Relief, Relief Request No. BV2-PZR-01 Regarding Weld Overlay Repairs on Pressurizer Nozzle Welds L-07-056, Requests Approval of Proposed Alternatives and Relief for Inservice Testing Program Ten-Year Update2007-03-28028 March 2007 Requests Approval of Proposed Alternatives and Relief for Inservice Testing Program Ten-Year Update ML0625801202006-10-0202 October 2006 (BVPS-1 and 2), Inservice Inspection (ISI) Program, Alternative Examination of Reactor Coolant Pipe Welds, Request for Relief No. BV3-RV-2 2024-05-13
[Table view] Category:Letter
MONTHYEARIR 05000334/20240112024-10-17017 October 2024 License Renewal Phase IV Inspection Report 05000334/2024011 L-24-038, License Amendment Request to Remove the Expired One-Time Action for Valve Leak Repair in Technical Specification (TS) 3.5.2 and to Correct Core Operating Limits Rep Ort (COLR) References2024-09-17017 September 2024 License Amendment Request to Remove the Expired One-Time Action for Valve Leak Repair in Technical Specification (TS) 3.5.2 and to Correct Core Operating Limits Rep Ort (COLR) References L-24-015, Twenty-Ninth Refueling Outage Inservice Inspection Summary Report2024-09-17017 September 2024 Twenty-Ninth Refueling Outage Inservice Inspection Summary Report ML24134A1522024-09-17017 September 2024 Exemption from the Requirements of 10 CFR 50.71(e)(4) Final Safety Analysis Report Update Schedule (EPID L-2024-LLE-0005) - Letter ML24260A1912024-09-16016 September 2024 Operator Licensing Examination Approval IR 05000334/20240052024-08-29029 August 2024 Updated Inspection Plan for Beaver Valley Power Station, Units 1 and 2 (Reports 05000334/2024005 and 05000412/2024005) L-24-188, Submittal of Quality Assurance Program Manual, Revision 302024-08-27027 August 2024 Submittal of Quality Assurance Program Manual, Revision 30 L-24-199, Discharge Monitoring Report (NPDES) Permit No. PA00256152024-08-22022 August 2024 Discharge Monitoring Report (NPDES) Permit No. PA0025615 IR 05000334/20244022024-08-22022 August 2024 Security Baseline Inspection Report 05000334/2024402 and 05000412/2024402 (Cover Letter Only) L-24-186, Response to RAI for Exemption Request from 10 CFR 50.71(e)(4) Final Safety Analysis Update Schedule2024-08-15015 August 2024 Response to RAI for Exemption Request from 10 CFR 50.71(e)(4) Final Safety Analysis Update Schedule IR 05000334/20240022024-08-0505 August 2024 Integrated Inspection Report 05000334/2024002 and 05000412/2024002 ML24208A0462024-07-26026 July 2024 NRC Office of Investigations Case No. 1-2023-005 L-24-182, Discharge Monitoring Report (NPDES) Permit No. PA00256152024-07-23023 July 2024 Discharge Monitoring Report (NPDES) Permit No. PA0025615 L-24-161, Discharge Monitoring Report (NPDES) Permit No. PA00256152024-07-19019 July 2024 Discharge Monitoring Report (NPDES) Permit No. PA0025615 05000334/LER-2024-004, Reactor Trip Due to Bypass Feedwater Regulating Valve Failure to Control2024-07-17017 July 2024 Reactor Trip Due to Bypass Feedwater Regulating Valve Failure to Control L-24-014, Annual 10 CFR 50.46 Report of Changes to or Errors in Emergency Core Cooling Svstem Evaluation Models2024-07-16016 July 2024 Annual 10 CFR 50.46 Report of Changes to or Errors in Emergency Core Cooling Svstem Evaluation Models ML24193A2912024-07-16016 July 2024 Revision to Reactor Vessel Surveillance Capsule Withdrawal Schedule IR 05000334/20245012024-07-0808 July 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000334/2024501 and 05000412/2024501 05000334/LER-2024-003, Unanalyzed Containment Bypass Condition Due to Degraded River Water Piping2024-07-0202 July 2024 Unanalyzed Containment Bypass Condition Due to Degraded River Water Piping L-24-164, BV-2, Post Accident Monitor Report2024-06-27027 June 2024 BV-2, Post Accident Monitor Report IR 05000334/20244012024-06-26026 June 2024 Material Control and Accounting Program Inspection Report 05000334/2024401 and 05000412/2024401 (Cover Letter Only) L-24-094, Reactor Vessel Surveillance Capsule Withdrawal Schedule2024-06-24024 June 2024 Reactor Vessel Surveillance Capsule Withdrawal Schedule L-24-152, Response to NRC Regulatory Issue Summary 2024-01 Preparation and Scheduling of Operator Licensing Examinations2024-06-17017 June 2024 Response to NRC Regulatory Issue Summary 2024-01 Preparation and Scheduling of Operator Licensing Examinations 05000334/LER-2024-002, Automatic Reactor Trip Due to Low Reactor Coolant Flow Caused by Transformer Overexcitation Protection Relay Actuation2024-06-11011 June 2024 Automatic Reactor Trip Due to Low Reactor Coolant Flow Caused by Transformer Overexcitation Protection Relay Actuation 05000334/LER-2024-001, Offsite AC Power Source Inoperable Due to Breaker Failure Resulting in Condition Prohibited by Technical Specification2024-06-0606 June 2024 Offsite AC Power Source Inoperable Due to Breaker Failure Resulting in Condition Prohibited by Technical Specification ML24135A2282024-05-29029 May 2024 Review of the Spring 2023 Outage Generic Letter 95-05 Voltage-Based Alternate Repair Criteria and Steam Generator F Star Reports ML24135A1702024-05-29029 May 2024 – Steam Generator Tube Inspection - Review of the Spring 2023 Tube Inspection Reports L-24-021, Cycle 30 Core Operating Limits Report2024-05-23023 May 2024 Cycle 30 Core Operating Limits Report L-24-121, Discharge Monitoring Report (NPDES) Permit No. PA00256152024-05-23023 May 2024 Discharge Monitoring Report (NPDES) Permit No. PA0025615 ML24141A1052024-05-20020 May 2024 Senior Reactor and Reactor Operator Initial License Examinations IR 05000334/20240102024-05-15015 May 2024 Information Request for Quadrennial Baseline Comprehensive Engineering Team Inspection; Notification to Perform Inspection 05000334/2024010 and 05000412/2024010 L-24-107, CFR 50.55a Request 1-TYP-5-RRP-l, for Alternative Method of Nondestructive Examination for River Water Outlet Piping Weld Repair2024-05-13013 May 2024 CFR 50.55a Request 1-TYP-5-RRP-l, for Alternative Method of Nondestructive Examination for River Water Outlet Piping Weld Repair IR 05000334/20240012024-05-0808 May 2024 Integrated Inspection Report 05000334/2024001 and 05000412/2024001 L-23-269, Application to Revise Technical Specifications to Adopt TSTF-569, Revision of Response Time Testing Definitions2024-05-0707 May 2024 Application to Revise Technical Specifications to Adopt TSTF-569, Revision of Response Time Testing Definitions L-24-054, Submittal of 2023 Annual Radioactive Effluent Release Report 2023 Annual Radiological Environmental Operating Report and 2023 Annual Environmental Operating Report (Non-Radiological)2024-04-29029 April 2024 Submittal of 2023 Annual Radioactive Effluent Release Report 2023 Annual Radiological Environmental Operating Report and 2023 Annual Environmental Operating Report (Non-Radiological) L-24-089, Emergency Preparedness Plan2024-04-23023 April 2024 Emergency Preparedness Plan L-24-088, Discharge Monitoring Report (NPDES) Permit No. PA0025615 for March 20242024-04-22022 April 2024 Discharge Monitoring Report (NPDES) Permit No. PA0025615 for March 2024 ML24101A2752024-04-10010 April 2024 Response to Request for Additional Information Regarding Spring 2023 180-Day Steam Generator Tube Inspection Report L-24-082, Withdrawal of Exemption Request2024-04-0303 April 2024 Withdrawal of Exemption Request L-24-013, Annual Notification of Property Insurance Coverage2024-03-26026 March 2024 Annual Notification of Property Insurance Coverage L-24-064, Submittal of Discharge Monitoring Report (NPDES) Permit No. PA00256152024-03-13013 March 2024 Submittal of Discharge Monitoring Report (NPDES) Permit No. PA0025615 ML24044A0662024-03-0404 March 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0083 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting ML24057A0752024-03-0101 March 2024 The Associated Independent Spent Fuel Storage Installations IR 05000334/20230062024-02-28028 February 2024 Annual Assessment Letter for Beaver Valley Power Station, Units 1 and 2 (Reports 05000334/2023006 and 05000412/2023006) L-23-264, Request for Exemption from 10 CFR 50.71(e)(4) Final Safety Analysis Report Update Schedule2024-02-23023 February 2024 Request for Exemption from 10 CFR 50.71(e)(4) Final Safety Analysis Report Update Schedule CP-202300502, Notice of Planned Closing of Transaction and Provision of Documents to Satisfy Order Conditions2024-02-23023 February 2024 Notice of Planned Closing of Transaction and Provision of Documents to Satisfy Order Conditions L-24-050, Retrospective Premium Guarantee2024-02-22022 February 2024 Retrospective Premium Guarantee 05000412/LER-2023-003-01, Missile Barrier Door Left Open Resulting in a Loss of Safety Function2024-02-20020 February 2024 Missile Barrier Door Left Open Resulting in a Loss of Safety Function IR 05000334/20230042024-02-12012 February 2024 Integrated Inspection Report 05000334/2023004 and 05000412/2023004 ML24025A0922024-01-25025 January 2024 Requalification Program Inspection 2024-09-17
[Table view] Category:Safety Evaluation
MONTHYEARML24193A2912024-07-16016 July 2024 Revision to Reactor Vessel Surveillance Capsule Withdrawal Schedule ML23198A3592023-10-0202 October 2023 Issuance of Amendment Nos. 322 and 212 Analytical Methodology to the Core Operating Limits Report for a Full Spectrum Loss of Coolant Accident (EPID L-2022-LLA-0129) - Nonproprietary ML23237B4282023-09-28028 September 2023 Energy Harbor Nuclear Corp. - Vistra Operations Company LLC - Enclosure 2, Draft Conforming License Amendments ML23237B4302023-09-28028 September 2023 Energy Harbor Nuclear Corp. - Vistra Operations Company LLC - Enclosure 4, Safety Evaluation for Transfer of Licenses and Draft Conforming License Amendments (EPID L-2023-LLM-0000) (Public) ML23249A1842023-09-18018 September 2023 Authorization and Safety Evaluation for Alternative Request No. 2-TYP-4-RV-06 ML23188A0982023-07-17017 July 2023 – Correction to the Safety Evaluation Issued Related to Amendment Nos. 321 and 211 Consolidate Fuel Decay Time Technical Specifications in a New Limiting Condition for Operation Titled Decay Time ML23102A1472023-05-22022 May 2023 Issuance of Amendment Nos. 321 and 211 Consolidate Fuel Decay Time Technical Specifications in a New Limiting Condition for Operation Titled Decay Time ML23019A0032023-03-16016 March 2023 – Issuance of Amendment Nos. 320 and 210 Adoption of Technical Specifications Task Force (Tstf) Traveler Tstf-501, Revision 1, Relocate Stored Fuel Oil and Lube Oil Volume Values to Licensee Control ML23062A5212023-03-0606 March 2023 – Issuance of Amendment No. 319 Revise Technical Specification (TS) 3.5.2, ECCS – Operating, Limiting Condition for Operation (LCO) 3.5.2, ML22277A8142022-10-0707 October 2022 Correction of Errors in Safety Evaluation Associated with License Amendment Nos. 315 and 205 Regarding Changes to the Emergency Preparedness Plan ML22210A0102022-09-16016 September 2022 Energy Harbor Fleet- Issuance of Amendments Regarding Adoption of TSTF 554, Revise Reactor Coolant Leakage Requirements ML22235A7672022-09-0101 September 2022 Correction of Errors in Safety Evaluation Associated with License Amendment Nos. 315 and 205 Regarding Changes to the Emergency Preparedness Plan ML22222A0862022-09-0101 September 2022 Issuance of Amendment Nos. 317 and 208 Revise Technical Specification 3.3.5, Loss of Power (LOP) Diesel Generator (DG) Start and Bus Separation Instrumentation ML22202A4642022-06-29029 June 2022 Emergency Plan Safety Evaluation ML22140A2092022-06-28028 June 2022 Issuance of Amendment No. 207 Correct TS 3.1.7 Change Made by TSTF-547 ML22095A2352022-05-10010 May 2022 Issuance of Amendment Nos. 316 and 206 Revise Technical Specification 5.6.3, Core Operating Limits Report (COLR) ML21286A7822022-05-0606 May 2022 Issuance of Amendment Nos. 315 and 205 Regarding Changes to the Emergency Plan ML22077A1342022-05-0202 May 2022 Issuance of Amendment Nos. 314 and 204 Revise Technical Specifications to Adopt TSTF-577, Revision 1, Revised Frequencies for Steam Generator Tube Inspections ML22082A2532022-03-29029 March 2022 Correction Letter - Issuance of Authorization of Proposed Alternative to Use ASME OM Code Case OMN-27 ML22012A2972022-01-21021 January 2022 Proposed Alternative to Use ASME OM Code Case OMN-27 ML21197A0092021-11-0101 November 2021 Issuance of Amendment Nos. 313 and 203 Reactor Coolant System, Pressure and Temperature Limits Report ML21214A2752021-10-15015 October 2021 Issuance of Amendment Nos. 312 and 202 Atmospheric Dump Valves ML21153A1762021-06-30030 June 2021 Issuance of Amendment No. 201 Revision of Technical Specifications Related to Steam Generator Tube Inspection, and Repair Methods ML21075A1132021-04-16016 April 2021 Issuance of Amendment Nos. 311, 200, and 302 to Incorporate the Applicable Standard Technical Specification 5.2.2, Unit Staff, Into the Technical Specifications ML21070A0002021-03-22022 March 2021 Issuance of Amendment 310, Revise Technical Specification 5.5.5.1, Unit 1 SG Program, to Defer Spring 2021 Refueling Outage Steam Generator Inspections to Fall 2022 Refueling Outage ML20346A0222021-03-10010 March 2021 Issuance of Amendment Nos. 309 and 199 to Change Technical Specifications to Implement New Surveillance Methods for the Heat Flux Hot Channel Factor ML20335A0522021-02-18018 February 2021 Issuance of Amendment Nos. 308 and 198 to Modify Certified Fuel Handler Related Technical Specifications for Permanently Defueled Condition ML20345A2362021-01-28028 January 2021 Issuance of Amendment Nos. 307 and 197 to Add Containment Sump Technical Specifications to Address GSI-191 Issues ML20335A0232020-12-28028 December 2020 Issuance of Amendment Nos. 306 and 196 to Remove License Conditions B and C Related to the Irradiated Fuel Management Plans ML20285A2662020-10-21021 October 2020 Correction to Safety Evaluation for Amendment Nos. 305 and 195 Issued September 23, 2020, Modify Primary and Secondary Coolant Activity Technical Specifications ML20279A4402020-10-0808 October 2020 Energy Harbor Fleet-Beaver Valley Power Station; Davis-Besse Nuclear Power Station, and Perry Nuclear Power Plant - Request to Use a Provision of a Later Edition of the ASME Engineers Boiler and Pressure Vessel Code, Section XI ML20213A7312020-09-23023 September 2020 Issuance of Amendment Nos. 305 and 195 to Modify Primary and Secondary Coolant Activity Technical Specifications ML20223A0142020-08-20020 August 2020 Issuance of Relief Request SSR-1, Revision 0, from the Requirements of the ASME Code (EPID L-2020-LLR-0050 (COVID-19)) ML20206K8652020-08-0707 August 2020 Relief Requests 2-TYP-4-RV-06 and 2-TYP-4-RV-07 from the Requirements of the ASME Code (EPID L-2020-LLR-0053 and EPID L-2020-LLR-0054 (COVID-19)) ML20153A0142020-07-16016 July 2020 Relief from the Requirements of the American Society of Mechanical Engineers Code Regarding Request VRR4 (EPID L-2020-LLR-0052 (COVID-19)) ML20145A0002020-06-0303 June 2020 Relief from the Requirements of the ASME Code for Requests VRR6 and VRR5 (EPID L-2020-LLR-0049 and EPID L-2020-LLR-0051 (COVID-19)) ML20080J7892020-04-28028 April 2020 Relief Requests 2 TYP-3-B3.110-1, 2-TYP-3-C2.21-1, 2-TYP-3-C1.30-1, and 2-TYP-3-RA-1 Regarding Weld Examination Coverage for the Third Inservice Inspection Interval ML20079F8162020-03-26026 March 2020 Relief Requests 1-TYP-4-C2.21-1 and 1-TYP-4-RA-1 Regarding Weld Examination Coverage for the Fourth Inservice Inspection Interval ML19336A0282019-12-18018 December 2019 Safety Evaluation Irradiated Fuel Management Plans ML19305B1312019-12-0202 December 2019 Firstenergy Nuclear Operating Company - Enclosure 6, Non-Proprietary Safety Evaluation, Direct and Indirect Transfer of Licenses and Draft Conforming Amendments for Beaver Valley Units 1 and 2, Davis-Besse Unit 1, and Perry Unit 1 ML19275E2942019-10-16016 October 2019 Issuance of Relief Request Proposed Alternative to Reactor Vessel Nozzle Weld Examination Frequency Requirements in Lieu of Specific ASME Code Requirements ML19028A0302019-04-11011 April 2019 FENOC - Beaver Valley Power Station, Unit 1 & 2; Davis-Besse Nuclear Power Station Unit 1; and Perry Nuclear Power Plant Unit 1 - Approval of Certified Fuel Handler Training and Retraining Program ML18348B2062019-02-25025 February 2019 Issuance of Amendment No. 193 Revise Steam Generator Technical Specifications ML18249A1692018-09-0707 September 2018 Seismic Hazard Mitigation Strategies Assessment (CAC Nos. MF7800 and MF7801; EPID L-2016-JLD-0006) ML18227A7332018-08-27027 August 2018 Request for Relief from the Requirements of the ASME Code ML18205A2922018-08-10010 August 2018 Correction of Errors in Safety Evaluation Associated with Relief Request 2-TYP-4-RV-02 ML18179A4672018-07-30030 July 2018 FENOC-Beaver Valley Power Station, Unit No. 1 and 2; Davis-Besse Nuclear Power Station, Unit 1, and Perry Nuclear Power Plant, Unit 1 - Issuance of Amendments Request to Adopt TSTF-529, Clarify Use and Application Rules ML18178A1122018-07-0202 July 2018 Relief Request No. 2-TYP-4-RV-02 Regarding the American Society of Mechanical Engineers Boiler and Pressure Vessel Code Case N-729-4 Examination Requirements ML18065A4032018-04-0505 April 2018 Correction of Errors in Safety Evaluation Associated with License Amendment Nos. 301 and 190 ML18073A1062018-03-28028 March 2018 Safety Evaluation of Proposed Alternatives 1-TYP-4-BA-01 and TYP-4-BN-01 Regarding the Fourth 10- Year Interval of the Inservice Inspection Program 2024-07-16
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August 20, 2020 Mr. Rod L. Penfield Site Vice President Energy Harbor Nuclear Corp.
Beaver Valley Power Station Mail Stop P-BV-SSEB P.O. Box 4, Route 168 Shippingport, PA 15077
SUBJECT:
BEAVER VALLEY POWER STATION, UNIT 2 - ISSUANCE OF RELIEF REQUEST SRR-1, REVISION 0, FROM THE REQUIREMENTS OF THE ASME CODE (EPID L-2020-LLR-0050 [COVID-19])
Dear Mr. Penfield:
By letter dated April 3, 2020 (Agencywide Documents Access and Management System (ADAMS) Accession Nos. ML20092K031), as supplemented by a letter also dated April 3, 2020 (ADAMS Accession No. ML20094K449), Energy Harbor Nuclear Corp. (the licensee) proposed an alternative to specific requirements in the 2004 Edition through 2006 Addenda of the American Society of Mechanical Engineers (ASME) Code for Operation and Maintenance of Nuclear Power Plants (OM Code) at Beaver Valley Power Station (Beaver Valley), Unit 2.
Specifically, pursuant to Title 10 of the Code of Federal Regulations (10 CFR) 50.55a(z)(2), the licensee requested to use the proposed alternative in request SRR-1, Revision 0 (titled as SSR-1 in the original request dated April 3, 2020), on the basis that complying with the requirements of the OM Code would result in hardship without a compensating increase in the level of quality and safety.
The U.S. Nuclear Regulatory Commission (NRC) staff concludes that request SRR-1, Revision 0, will provide reasonable assurance that the snubbers at Beaver Valley, Unit 2, listed in the licensees request are operationally ready to perform their safety functions until refueling outage 2R22 currently scheduled for the fall of 2021. The NRC staff finds that complying with the requirements of the OM Code would result in hardship without a compensating increase in the level of quality and safety. Accordingly, the NRC staff concludes that the licensee has adequately addressed all the regulatory requirements set forth in 10 CFR 50.55a(z)(2).
Therefore, the NRC authorizes the use of request SRR-1 at Beaver Valley, Unit 2, until the next scheduled refueling outage (2R22) in fall 2021.
The enclosed safety evaluation documents the technical basis for the NRCs verbal authorization of April 9, 2020 (ADAMS Accession No. ML20100N322).
All other requirements in the ASME OM Code for which relief was not specifically requested and approved in this request remains applicable.
R. Penfield If you have any questions, please contact Jennifer Tobin, the Beaver Valley Project Manager, at 301-415-2328 or by e-mail to Jennifer.Tobin@nrc.gov.
Sincerely, Digitally signed by James James G. G. Danna Date: 2020.08.20 Danna 13:27:00 -04'00' James G. Danna, Chief Plant Licensing Branch I Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-412
Enclosure:
Safety Evaluation cc: Listserv
SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELIEF REQUEST SRR-1, REVISION 0 REGARDING ALTERNATE SNUBBER TESTING ENERGY HARBOR NUCLEAR CORP.
BEAVER VALLEY POWER STATION, UNIT 2 DOCKET NO. 50-412
1.0 INTRODUCTION
By letter dated April 3, 2020 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML20092K031) as supplemented by a letter also dated April 3, 2020 (ADAMS Accession No. ML20094K449), Energy Harbor Nuclear Corp. (the licensee) proposed an alternative to specific requirements in the 2004 Edition through 2006 Addenda of the American Society of Mechanical Engineers (ASME) Code for Operation and Maintenance of Nuclear Power Plants (OM Code) for Beaver Valley Power Station (Beaver Valley), Unit 2, pursuant to Title 10 of the Code of Federal Regulations (10 CFR) Section 55a, Codes and Standards.
Specifically, the licensees proposed alternative, 10 CFR 50.55a Request Number SRR-1, Revision 0 (titled as SSR-1 in the original request dated April 3, 2020), requests the U.S. Nuclear Regulatory Commission (NRC) to authorize a one-time extension of the operational readiness testing to the next refueling outage (RFO) (2R22) for 24 specific snubbers in the inservice testing (IST) program at Beaver Valley Power Station (Beaver Valley), Unit 2. The licensee provided justification that compliance with certain requirements in the ASME OM Code, Subsection ISTD, Preservice and Inservice Examination and Testing of Dynamic Restraints (Snubbers) in Light-Water Reactor Nuclear Power Plants, paragraph ISTD-5200, Inservice Operational Readiness Testing, to perform functional testing of the specific snubbers during RFO 2R21 in the spring of 2020 would result in a hardship without a compensating increase in the level of quality and safety in accordance with 10 CFR 50.55a(z)(2).
The NRC verbally authorized the licensees request on April 9, 2020 (ADAMS Accession No. ML20100N322).
2.0 REGULATORY EVALUATION
Adherence to the ASME OM Code is mandated by 10 CFR 50.55a(g)(4), which states, in part, that ASME Code Class 1, 2, and 3 components will meet the requirements, except the design and access provisions and the preservice examination requirements, set forth in the ASME OM Code for snubber examination and testing that become effective subsequent to editions and Enclosure
addenda specified in 10 CFR 50.55a(g)(2) and (3) and that are incorporated by reference in 10 CFR 50.55a(a), to the extent practical, within the limitations of design, geometry, and materials of construction of the components.
Pursuant to 10 CFR 50.55a(b)(3)(v)(B), Snubbers: Second provision, the licensee must comply with the provisions for examining and testing snubbers in Subsection ISTD of the ASME OM Code and make appropriate changes to its technical specifications or licensee-controlled documents when using the 2006 Addenda and later editions and addenda of Section XI of the ASME Boiler and Pressure Vessel Code.
Paragraph 50.55a(z) of 10 CFR states, in part, that alternatives to the requirements of paragraphs (b) through (h) of 10 CFR 50.55a, or portions thereof, may be used when authorized by the Director, Office of Nuclear Reactor Regulation. A proposed alternative must be submitted and authorized prior to implementation. The applicant or licensee must demonstrate that: (1) the proposed alternative would provide an acceptable level of quality and safety; or (2) compliance with the specified requirements of this section would result in hardship without a compensating increase in the level of quality and safety.
Based on the above, and subject to the following technical evaluation, the NRC staff finds that regulatory authority exists for the licensee to request the use of an alternative and the NRC to grant relief and the use of the proposed alternative.
3.0 TECHNICAL EVALUATION
3.1 ASME Code Components Affected
Request SRR-1, Revision 0 In its submittal, the licensee requests a one-time extension of the operational readiness testing interval for the following 24 snubbers at Beaver Valley, Unit 2:
Table 1 Snubber Component Snubber Model Defined Test Component Service Life Number Plan Group Classification Expiration (DTPG) 2CCP-PSSP301 PSA-10 AB Safety-Related 10/5/2030 2EDG-PSSP042A PSA-3 DG Safety-Related 9/25/2030 2FWS-PSSP002A 30 72 56 RC1-SP FW Safety-Related 10/1/2038 2FWS-PSSP002B 30 72 56 RC1-SP FW Safety-Related 10/1/2038 2MSS-PSSP108A 30 72 16 RC1-S5 MS-H Safety-Significant 9/28/2038 2MSS-PSSP108B 30 72 16 RC1-S5 MS-H Safety-Significant 9/30/2038 2MSS-PSSP103 PSA-100 MS-P10Y Safety-Significant 10/15/2022 2MSS-PSSP456 PSA-1 MS-P10Y Safety-Related 10/28/2027 2MSS-PSSP151B PSA-10 MS-P6Y Safety-Significant 11/30/2021 2CHS-PSSP024 30 18 56 RF1 RBX-L Safety-Related 3/22/2034
Snubber Component Snubber Model Defined Test Component Service Life Number Plan Group Classification Expiration (DTPG) 2CHS-PSSP025 30 18 56 RF1 RBX-L Safety-Related 3/9/2034 2BDG-PSSP947 30 18 56 RF1 RBX-L Safety-Related 3/19/2034 2RCS-PSSP012A PSA-10 RBX-P Safety-Significant 4/12/2022*
2RCS-PSSP019X PSA-10 RBX-P Safety-Significant 10/21/2024 2RCS-PSSP891A PSA-3 RBX-P Safety-Significant 10/21/2024 2RCS-PSSP892A PSA-10 RBX-P Safety-Significant 10/1/2024 2SIS-PSSP208X PSA-1 RBX-P Safety-Related 2/18/2023*
2SIS-PSSP209A PSA-1 RBX-P Safety-Related 2/18/2023*
2RCS-SN21C12 12 X 6.25 S/G Safety-Related 8/14/2027 2RSS-PSSP579A 30 18 56 RF1 SFGD-H Safety-Related 9/28/2035 2RSS-PSSP579B 30 18 56 RF1 SFGD-H Safety-Related 9/28/2035 2SIS-PSSP449A PSA-1 SFGD-M Safety-Related 9/26/2027 2SIS-PSSP449B PSA-1 SFGD-M Safety-Related 9/26/2027 2SWS-PSSP754Y PSA-10 SFGD-M Safety-Related 10/11/2023*
- Section 5 of the licensees request dated April 3, 2020, contains additional detail regarding the service life for these snubbers.
3.2 Applicable Code Edition and Addenda The applicable Code edition and addition is the ASME Code,Section XI, 2013 Edition.
3.3 Applicable Code Requirement The IST requirements of the ASME OM Code, as incorporated by reference in 10 CFR 50.55a related to this alternative request are as follows:
ASME OM Code, Subsection ISTD, paragraph ISTD-5200, states, in part, that Snubbers shall be tested for operational readiness during each fuel cycle [every 2 years].
Paragraph ISTD-5300, The 10% Testing Sample, and paragraph ISTD-6000, Service Life Monitoring, in the ASME OM Code, Subsection ISTD, specify sampling and service life monitoring (SLM) requirements for snubbers, respectively.
3.4 Reason for Request The licensee planned to start the 21st RFO (2R21) at Beaver Valley 2 on April 12, 2020. The licensee reported that the snubbers listed in its request are functionally tested in accordance with the frequency specified in ASME OM Code (2004 Edition through 2006 Addenda),
Subsection ISTD, paragraph ISTD-5200, every 2 years. Therefore, these snubbers were scheduled to be functionally tested during the RFO in the spring of 2020.
The licensee stated that on March 13, 2020, the President of the United States declared a national emergency due to the spread and infectious nature of the Coronavirus-2019 (COVID-19) virus and resulting pandemic. The most recent guidance from the Centers for Disease Control and Prevention includes recommendations for social distancing by maintaining approximately 6 feet from other personnel to limit the spread of the virus. On March 28, 2020, the Governor of Pennsylvania issued a stay-at-home order for Beaver County and the surrounding counties of Allegheny and Butler. Furthermore, on March 28, 2020, the Department of Homeland Security identified workers in the nuclear energy sector as essential critical infrastructure workers.
To prevent the spread of COVID-19 and to protect the health and safety of plant personnel while maintaining responsibilities to support critical infrastructure, the licensee intends to reduce the amount of personnel on site, which will pose a hardship for completing the currently planned 2R21 RFO work scope. The licensee has a contingency plan in case some of its workforce becomes unavailable due to the COVID-19 outbreak. The licensee stated that with the current work scope and potential loss of personnel, it may not be able to complete the RFO in a timely manner, which could affect critical infrastructure that is needed during this time.
The licensee submitted the relief request considering the expected hardship of obtaining and maintaining onsite staff sufficient to prepare, perform, and recover from the examination. The licensee stated that the functional testing of the snubbers listed in its request during the spring 2020 refueling outage at Beaver Valley, Unit 2, would represent a hardship during the COVID-19 outbreak. For example, the licensee intended to reduce the amount of personnel on site to prevent the spread of COVID-19 at Beaver Valley, Unit 2. The licensee was also contingency planning in case some of its workforce became unavailable due to the COVID-19 outbreak.
Therefore, the licensee asserted that the testing of the specified snubbers at Beaver Valley, Unit 2, during the spring 2020 refueling outage would result in a hardship without a compensating increase in the level of quality and safety in accordance with 10 CFR 50.55a(z)(2).
3.5 Proposed Alternative The licensee proposed an extension of the IST program testing intervals for the snubbers listed in its request to the next RFO for Beaver Valley, Unit 2, currently scheduled for the fall of 2021.
In its request for a one-time extension of the operational readiness testing for the specified snubbers, the licensee provided information indicating that the service life of those snubbers extends to at least RFO 2R22 in the fall of 2021. The licensee stated that the snubbers with service life expiration dates in the years shortly following RFO 2R22 would receive service life maintenance or visual examinations during RFO 2R21 in the spring of 2020. If maintenance was unsuccessful, the licensee reported that corrective actions would be performed for those snubbers. Further, the licensee stated that based on the Beaver Valley, Unit 2, snubber test history, since 2009, there have been approximately 211 tests of program snubbers with only one snubber not meeting its test criteria, but it was determined to be fully functional in the as-found condition.
3.6 Basis for Use The licensee stated that there have been no dynamic events or transients during plant operation since the previous RFO that might affect snubber performance. The licensee reported that there was a recent internal operating experience that applied to one large bore steam generator snubber listed in the request that the licensee had addressed in its corrective action program.
Overall, the licensee stated that the snubber population at Beaver Valley, Unit 2, has been operating at a high level of performance for the past 10 years. The licensee asserted that the performance of these snubbers supports extending the one-time operational readiness test interval and provides reasonable assurance that the snubbers are operationally ready to perform their safety functions.
Further, the licensee indicated that SLM activities would be performed during RFO 2R21 in the spring of 2020 to ensure the snubber service life will not be exceeded. The licensee stated that inservice testing of the Beaver Valley, Unit 2, snubbers will resume in alignment with paragraph ISTD-5200 of the ASME OM Code, Subsection ISTD, with sampling performed in accordance with the 10 percent plan contained in ASME OM Code, Subsection ISTD, paragraph ISTD-5300, and the SLM program at Beaver Valley, Unit 2, during RFO 2R22 in the fall of 2021.
3.7 Duration of Proposed Alternative For request SRR-1, Revision 0, the licensee requested relief to allow a one-time extension of the operational readiness testing interval for the 24 snubbers listed in Table 1 of this safety evaluation at Beaver Valley, Unit 2, during the 2R21 RFO. The licensee stated that it will resume the normal outage examination frequency at the next opportunity, currently expected to be the next RFO (2R22) in fall 2021.
3.8 NRC Staff Evaluation As incorporated by reference in 10 CFR 50.55a, ASME OM Code (2004 Edition through 2006 Addenda), Subsection ISTD, requires that snubbers shall meet (1) the inservice visual examination requirements in paragraph ISTD-4000, Specific Examination Requirements; (2) the inservice operational readiness testing requirements in paragraph ISTD-5000, Specific Testing Requirements; and (3) the SLM requirements in paragraph ISTD-6000. Paragraph ISTD-5200 requires that snubbers within the scope of the ASME OM Code that have specific inservice operational readiness requirements are required to be functionally tested at least once every 2 years. As a result, the Beaver Valley, Unit 2, snubbers listed in Table 1 of this safety evaluation were required to be functionally tested during RFO 2R21 in the spring of 2020.
In its request, the licensee provided justification that compliance with the requirements in the ASME OM Code, Subsection ISTD, paragraph ISTD-5200, as incorporated by reference in 10 CFR 50.55a to conduct functional testing of specific snubbers at Beaver Valley, Unit 2, during the spring 2020 RFO would result in a hardship without a compensating increase in the level of quality and safety in accordance with 10 CFR 50.55a(z)(2). For example, the licensee indicated that the functional testing of snubbers during the spring 2020 RFO would represent a hardship during this COVID-19 outbreak because the licensee intended to reduce the amount of personnel on site to prevent the spread of COVID-19 at Beaver Valley. The licensee was also contingency planning in case some of its workforce became unavailable due to the COVID-19 outbreak.
In its request, the licensee reported that the snubbers with service life expiration dates in the years shortly following RFO 2R22 would receive service life maintenance or visual examinations during RFO 2R21 in the spring of 2020. If maintenance was unsuccessful, the licensee stated that corrective actions would be performed for those snubbers. Further, the licensee stated that based on the Beaver Valley, Unit 2, snubber test history, since 2009, there have been approximately 211 tests of program snubbers with only one snubber not meeting its test criteria
but was determined to be fully functional in the as-found condition. The licensee stated that there have been no dynamic events or transients during plant operation since the previous RFO that might affect snubber performance. Overall, the licensee demonstrated that the snubber population at Beaver Valley, Unit 2, has been operating at a high level of performance for the past 10 years.
Based on the information described above for the specific snubbers at Beaver Valley, Unit 2, listed in the licensees request, the NRC staff finds that: (1) snubber population testing during the past 10 years indicates their acceptable historical performance; (2) ongoing inservice visual examination and testing activities have not identified snubber performance concerns, except an operating experience item related to steam generator snubbers that was addressed by the licensees corrective action program; (3) SLM activities of all snubbers are performed every RFO, and service life maintenance activities will continue as needed; and (4) a hardship existed for certain IST program activities related to these snubbers during RFO 2R21 in the spring of 2020 that would be contrary to the health and safety of plant personnel.
Therefore, the NRC staff finds that the licensees proposed alternative for a one-time extension of operational readiness testing for the 24 specified snubbers at Beaver Valley, Unit 2, in accordance with 10 CFR 50.55a(z)(2) will provide reasonable assurance that the snubbers will be operationally ready to perform their safety functions until RFO 2R22 in the fall of 2021.
4.0 CONCLUSION
The NRC staff concludes that proposed alternative SRR-1, Revision 0, will provide reasonable assurance that the snubbers at Beaver Valley, Unit 2, listed in the licensees request are operationally ready to perform their safety functions until RFO 2R22 currently scheduled for the fall of 2021. The NRC staff finds that complying with certain requirements of the ASME OM Code would result in hardship without a compensating increase in the level of quality and safety.
Accordingly, the NRC staff concludes that the licensee has adequately addressed all the regulatory requirements set forth in 10 CFR 50.55a(z)(2). Therefore, the NRC authorizes the use of proposed alternative SRR-1, Revision 0, at Beaver Valley, Unit 2, until the next scheduled RFO (2R22) in fall 2021.
All other requirements in the ASME OM Code for which relief was not specifically requested and approved in this request remain applicable.
Principal Contributor: G. Bedi Date: August 20, 2020
ML20223A014 OFFICE NRR/DORL/LPL1/PM NRR/DORL/LPL1/LA NRR/DEX/EMIB/BC NAME JTobin LRonewicz ABuford DATE 08/12/2020 08/11/2020 08/04/2020 OFFICE NRR/DORL/LPL1/BC NRR/DORL/LPL1/PM NAME JDanna JTobin DATE 08/20/2020 08/20/2020