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Category:CORRESPONDENCE-LETTERS
MONTHYEARSVP-99-181, Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 9906301999-10-20020 October 1999 Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 990630 1CAN109906, Forwards Framatome Technologies,Inc non-proprietary TR BAW-10235P, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheet of Once-Through Sgs, Rev 11999-10-19019 October 1999 Forwards Framatome Technologies,Inc non-proprietary TR BAW-10235P, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheet of Once-Through Sgs, Rev 1 ML20217M1851999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Requal Pass Dates ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217J4971999-10-18018 October 1999 Requests Addl Info Re Results of Util Most Recent Steam Generator Insp at ANO-2 & Util Methodology Used to Predict Future Performance of SG Tubes ML20217J3601999-10-15015 October 1999 Informs That Topical Rept BAW-10235P, Management Program for Volumetric Outer Diameter Integranular Attack in Tubesheets of Once-Through SG, Rev 1 Marked as Proprietary Will Be Withheld from Public Disclosure ML20217J3871999-10-15015 October 1999 Informs That Topical Rept BAW-10235P, Management Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through SG, Rev 0 Marked as Proprietary Will Be Withheld from Public Disclosure JPN-99-035, Forwards Comments on Version 2 of Reactor Vessel Integrity Database for Plant.Table Listing Recommended Changes to Info in Rvid,Encl as Attachment 11999-10-15015 October 1999 Forwards Comments on Version 2 of Reactor Vessel Integrity Database for Plant.Table Listing Recommended Changes to Info in Rvid,Encl as Attachment 1 2CAN109902, Submits Withdrawal of Code Case N-593 for ANO-2 Replacement SGs1999-10-15015 October 1999 Submits Withdrawal of Code Case N-593 for ANO-2 Replacement SGs 2CAN109903, Forwards Response to RAI Re Proposed Tech Specs Change for Special SG Insp1999-10-14014 October 1999 Forwards Response to RAI Re Proposed Tech Specs Change for Special SG Insp ML20217K7011999-10-13013 October 1999 Provides Response to Questions Related to Request for License Amend,Per 10CFR50.90, Credit for Containment Overpressure. Supporting Calculations Encl JPN-99-034, Forwards Proposed risk-informed ISI Program,Provided from NRC Review & Approval as Alternative to Current ASME Section XI Insp Requirements for Class 1 & 2 Piping1999-10-13013 October 1999 Forwards Proposed risk-informed ISI Program,Provided from NRC Review & Approval as Alternative to Current ASME Section XI Insp Requirements for Class 1 & 2 Piping 05000254/LER-1999-004, Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action1999-10-12012 October 1999 Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action ML20217D1721999-10-0808 October 1999 Forwards RAI Re 990729 Request for Amend to TSs Allowing Special SG Insp for Plant,Unit 2.Questions Re Proposed Insp Scope for Axial Cracking Degradation in Eggcrate Support Region Submitted.Response Requested by 991015 JPN-99-033, Provides Response to Questions Contained in 990712,facsimile from NRC Re Ja FitzPatrick USI A-46 Program.Questions Were Also Discussed Between Members of Util & NRC Staff During Telcon1999-10-0808 October 1999 Provides Response to Questions Contained in 990712,facsimile from NRC Re Ja FitzPatrick USI A-46 Program.Questions Were Also Discussed Between Members of Util & NRC Staff During Telcon 05000254/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee1999-10-0707 October 1999 Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee ML20217F6321999-10-0707 October 1999 Forwards Insp Repts 50-254/99-01 & 50-265/99-01 on 990721- 0908.No Violations ML20212K9421999-10-0505 October 1999 Informs That NRC Accepts 990513 Inservice Inspection Relief Request CR-31 for Quad Cities Nuclear Power Station,Units 1 & 2 1CAN109905, Discusses Insp of Once Through SG Tubing Surveillance Performed During 1R15 Scheduled RFO on 990910.Category C-3 Results,Included1999-10-0404 October 1999 Discusses Insp of Once Through SG Tubing Surveillance Performed During 1R15 Scheduled RFO on 990910.Category C-3 Results,Included ML20212L0621999-10-0101 October 1999 Forwards Safety Evaluation & Exemption from Certain Requirements of 10CFR50,App R,Section III.G.2, Fire Protection of Safe Shutdown Capability ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr 1CAN099908, Withdraws 990919 Exigent TS Change Request to Allow Continued Installation of re-rolls for One Cycle of Operation Through End of Cycle 16 in Conjunction with Addl Insp Criteria1999-09-30030 September 1999 Withdraws 990919 Exigent TS Change Request to Allow Continued Installation of re-rolls for One Cycle of Operation Through End of Cycle 16 in Conjunction with Addl Insp Criteria 2CAN099902, Requests That NRC Assign CENPD-132,Suppl 4-P, Calculative Methods for Abb Cenp Large Break LOCA Evaluation Model, Review Priority So That Approval Will Be Granted No Later than Oct 31,20001999-09-29029 September 1999 Requests That NRC Assign CENPD-132,Suppl 4-P, Calculative Methods for Abb Cenp Large Break LOCA Evaluation Model, Review Priority So That Approval Will Be Granted No Later than Oct 31,2000 JPN-99-030, Forwards Application for Amend to License DPR-59,proposing Change to TS 3.5.B.3 & Associated Bases to Extend LCO Allowable Out of Service Time for RHRSW Sys from 7 Days to 11 Days1999-09-29029 September 1999 Forwards Application for Amend to License DPR-59,proposing Change to TS 3.5.B.3 & Associated Bases to Extend LCO Allowable Out of Service Time for RHRSW Sys from 7 Days to 11 Days JPN-99-032, Forwards Info Re Potential Environ Effects of Alternatives to Proposed Expansion of FitzPatrick Spent Fuel Pool,In Response to NRC Project Manager Request1999-09-29029 September 1999 Forwards Info Re Potential Environ Effects of Alternatives to Proposed Expansion of FitzPatrick Spent Fuel Pool,In Response to NRC Project Manager Request 1CAN099903, Forwards Rev 0 to COLR for ANO-1 Cycle 16, IAW TS 6.12.31999-09-27027 September 1999 Forwards Rev 0 to COLR for ANO-1 Cycle 16, IAW TS 6.12.3 1CAN099907, Requests That Alternative Be Allowed in Accordance with 10CFR50.55a(a)(3)(i) & (II) as Discussed in Encl 1.Encl 2 & 3 Stress Analysis & Flaw Evaluation Summaries Ref in Encl Alternative1999-09-26026 September 1999 Requests That Alternative Be Allowed in Accordance with 10CFR50.55a(a)(3)(i) & (II) as Discussed in Encl 1.Encl 2 & 3 Stress Analysis & Flaw Evaluation Summaries Ref in Encl Alternative 2CAN099901, Informs That G Kendrick,License SOP-43658,no Longer Has Need to Maintain Operating License on Ano,Unit 2.Entergy Requests That License for Individual Be Withdrawn,Due to Resignation, Effective 9908271999-09-24024 September 1999 Informs That G Kendrick,License SOP-43658,no Longer Has Need to Maintain Operating License on Ano,Unit 2.Entergy Requests That License for Individual Be Withdrawn,Due to Resignation, Effective 990827 1CAN099906, Forwards 1R15 Growth Data Obtained & Analyzed Through 990922 & Includes Plus Point Voltages,Axial Extent & Circumferential Extent Patches,As Well as Preliminary Growth Conclusions Based on Analysis of Data1999-09-24024 September 1999 Forwards 1R15 Growth Data Obtained & Analyzed Through 990922 & Includes Plus Point Voltages,Axial Extent & Circumferential Extent Patches,As Well as Preliminary Growth Conclusions Based on Analysis of Data 2CAN099904, Forwards Ano,Unit 2 10CFR50.59 Rept for Time Period Ending 990225.Rept Contains Brief Description of Changes in Procedures & in Facility as Described in Sar,Tests & Experiments Conducted & Other Changes to SAR1999-09-23023 September 1999 Forwards Ano,Unit 2 10CFR50.59 Rept for Time Period Ending 990225.Rept Contains Brief Description of Changes in Procedures & in Facility as Described in Sar,Tests & Experiments Conducted & Other Changes to SAR ML20212F8341999-09-22022 September 1999 Forwards Insp Rept 50-333/99-07 on 990718-0828.No Violations Noted ML20212F5031999-09-22022 September 1999 Forwards SER Granting Relief Requests 1-98-001 & 1-98-002 Which Would Require Design Mods to Comply with Code Requirements,Which Would Impose Significant Burden Pursuant to 10CFR50.55a(g)(6)(i) SVP-99-189, Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage1999-09-22022 September 1999 Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage ML20212J0451999-09-21021 September 1999 Forwards Safety Evaluation of Licensee USI A-46 Program at Quad Cities Nuclear Power Station,Units 1 & 2,established in Response to GL 87-02 Through 10CFR50.54(f) Ltr ML20212D8231999-09-20020 September 1999 Informs That Effectieve 991101,NRC Region III Will Be Conducting Safety System Design & Performance Capability Pilot Insp at Quad Cities Nuclear Power Station.Insp Will Be Performed IAW NRC Pilot Insp Procedure 71111-21 1CAN099905, Submits Supplemental Info in Support of SG Outer Diameter Intergranular Attack Alternate Repair Criteria.Proposed TS Rev & Info Related to Use of Alternate Repair Discussed in Attachments1999-09-17017 September 1999 Submits Supplemental Info in Support of SG Outer Diameter Intergranular Attack Alternate Repair Criteria.Proposed TS Rev & Info Related to Use of Alternate Repair Discussed in Attachments JAFP-99-0262, Forwards Voluntary Response to Administrative Ltr 99-03, Re Preparation & Scheduling of Operator Licensing Exams. Completed NRC Form 536,containing Info Re Proposed Exam Preparation Schedule & Initial Operator License Exams,Encl1999-09-16016 September 1999 Forwards Voluntary Response to Administrative Ltr 99-03, Re Preparation & Scheduling of Operator Licensing Exams. Completed NRC Form 536,containing Info Re Proposed Exam Preparation Schedule & Initial Operator License Exams,Encl ML20212D9961999-09-16016 September 1999 Informs That on 990818,NRC Completed Midcycle PPR of Arkansas Nuclear One.Nrc Plan to Conduct Core Insps at Facility Over Next 7 Months.Details of Insp Plan Through March 2000 Encl 1CAN099902, Forwards Proprietary Rev 1 to Topical Rept BAW-10235P, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs, in Response to 990831 Rai.Proprietary Encl Withheld1999-09-15015 September 1999 Forwards Proprietary Rev 1 to Topical Rept BAW-10235P, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs, in Response to 990831 Rai.Proprietary Encl Withheld ML20212C6961999-09-15015 September 1999 Forwards Insp Repts 50-254/99-17 & 50-265/99-17 on 990823- 0827.No Violations Noted SVP-99-190, Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys1999-09-13013 September 1999 Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys ML20217H5661999-09-0909 September 1999 Discusses 990907 Pilot Plan Mgt Meeting Re Results to-date of Pilot Implementation of NRC Revised Reactor Oversight Process at Prairie Island & Quad Cities.Agenda & Handouts Provided by Utils Encl ML20211Q7961999-09-0909 September 1999 Forwards Correction to Administrative Error on Page 8 of NRC Insp Repts 50-254/99-16 & 50-265/99-16,transmitted by Ltr, 2CAN099905, Informs That Jk Caery,License OP-42589 & as Bates,License OP-42506,no Longer Need to Maintain Operating License at Ano,Unit 2.Withdrawal of Licenses Is Requested1999-09-0909 September 1999 Informs That Jk Caery,License OP-42589 & as Bates,License OP-42506,no Longer Need to Maintain Operating License at Ano,Unit 2.Withdrawal of Licenses Is Requested ML20212A6951999-09-0909 September 1999 Requests That Licensees Affected by Kaowool Fire Barriers Take Issue on Voluntary Initiative & Propose Approach for Resolving Subj Issues.Staff Plans to Meet with Licensees to Discuss Listed Topics ML20212A8341999-09-0909 September 1999 Requests That Licensees Affected by Kaowool Fire Barriers Take Issue on Voluntary Initiative & Propose Approach for Resolving Subj Issues.Staff Plans to Meet with Licensees to Discuss Listed Topics JAFP-99-0258, Forwards Operator License Restriction Change for Tj Pelton, License SOP-10090-3.License Is Requested to Be Reissued with Restriction for Corrective Lenses.Encl Withheld1999-09-0808 September 1999 Forwards Operator License Restriction Change for Tj Pelton, License SOP-10090-3.License Is Requested to Be Reissued with Restriction for Corrective Lenses.Encl Withheld ML20211N4301999-09-0808 September 1999 Discusses Proposed Meeting to Discuss Kaowool Fire Barriers. Staff Requesting That Affected Licensees Take Issue on Voluntary Initative & Propose Approach for Resolving Issues 05000333/LER-1998-015, Forwards LER 98-015-02 Re Logic Sys Functional Test Inadequacies,Per 10CFR50.73(A)(2)(i)(B).Rept Revised to Reflect Scheduled Completion Date for Corrective Action 3 of Jan 15, 2000 & Updates Status of Other C/As as Complete1999-09-0808 September 1999 Forwards LER 98-015-02 Re Logic Sys Functional Test Inadequacies,Per 10CFR50.73(A)(2)(i)(B).Rept Revised to Reflect Scheduled Completion Date for Corrective Action 3 of Jan 15, 2000 & Updates Status of Other C/As as Complete ML20211Q6511999-09-0808 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Quad Cities Operator License Applicants During Wk of 000327.Validation of Exam Will Occur at Station During Wk of 000306 1999-09-09
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217M1851999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Requal Pass Dates ML20217J4971999-10-18018 October 1999 Requests Addl Info Re Results of Util Most Recent Steam Generator Insp at ANO-2 & Util Methodology Used to Predict Future Performance of SG Tubes ML20217J3871999-10-15015 October 1999 Informs That Topical Rept BAW-10235P, Management Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through SG, Rev 0 Marked as Proprietary Will Be Withheld from Public Disclosure ML20217J3601999-10-15015 October 1999 Informs That Topical Rept BAW-10235P, Management Program for Volumetric Outer Diameter Integranular Attack in Tubesheets of Once-Through SG, Rev 1 Marked as Proprietary Will Be Withheld from Public Disclosure ML20217D1721999-10-0808 October 1999 Forwards RAI Re 990729 Request for Amend to TSs Allowing Special SG Insp for Plant,Unit 2.Questions Re Proposed Insp Scope for Axial Cracking Degradation in Eggcrate Support Region Submitted.Response Requested by 991015 ML20217F6321999-10-0707 October 1999 Forwards Insp Repts 50-254/99-01 & 50-265/99-01 on 990721- 0908.No Violations ML20212K9421999-10-0505 October 1999 Informs That NRC Accepts 990513 Inservice Inspection Relief Request CR-31 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20212L0621999-10-0101 October 1999 Forwards Safety Evaluation & Exemption from Certain Requirements of 10CFR50,App R,Section III.G.2, Fire Protection of Safe Shutdown Capability ML20212F5031999-09-22022 September 1999 Forwards SER Granting Relief Requests 1-98-001 & 1-98-002 Which Would Require Design Mods to Comply with Code Requirements,Which Would Impose Significant Burden Pursuant to 10CFR50.55a(g)(6)(i) ML20212F8341999-09-22022 September 1999 Forwards Insp Rept 50-333/99-07 on 990718-0828.No Violations Noted ML20212J0451999-09-21021 September 1999 Forwards Safety Evaluation of Licensee USI A-46 Program at Quad Cities Nuclear Power Station,Units 1 & 2,established in Response to GL 87-02 Through 10CFR50.54(f) Ltr ML20212D8231999-09-20020 September 1999 Informs That Effectieve 991101,NRC Region III Will Be Conducting Safety System Design & Performance Capability Pilot Insp at Quad Cities Nuclear Power Station.Insp Will Be Performed IAW NRC Pilot Insp Procedure 71111-21 ML20212D9961999-09-16016 September 1999 Informs That on 990818,NRC Completed Midcycle PPR of Arkansas Nuclear One.Nrc Plan to Conduct Core Insps at Facility Over Next 7 Months.Details of Insp Plan Through March 2000 Encl ML20212C6961999-09-15015 September 1999 Forwards Insp Repts 50-254/99-17 & 50-265/99-17 on 990823- 0827.No Violations Noted ML20211Q7961999-09-0909 September 1999 Forwards Correction to Administrative Error on Page 8 of NRC Insp Repts 50-254/99-16 & 50-265/99-16,transmitted by Ltr, ML20212A6951999-09-0909 September 1999 Requests That Licensees Affected by Kaowool Fire Barriers Take Issue on Voluntary Initiative & Propose Approach for Resolving Subj Issues.Staff Plans to Meet with Licensees to Discuss Listed Topics ML20212A8341999-09-0909 September 1999 Requests That Licensees Affected by Kaowool Fire Barriers Take Issue on Voluntary Initiative & Propose Approach for Resolving Subj Issues.Staff Plans to Meet with Licensees to Discuss Listed Topics ML20217H5661999-09-0909 September 1999 Discusses 990907 Pilot Plan Mgt Meeting Re Results to-date of Pilot Implementation of NRC Revised Reactor Oversight Process at Prairie Island & Quad Cities.Agenda & Handouts Provided by Utils Encl ML20211Q6511999-09-0808 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Quad Cities Operator License Applicants During Wk of 000327.Validation of Exam Will Occur at Station During Wk of 000306 ML20211N4301999-09-0808 September 1999 Discusses Proposed Meeting to Discuss Kaowool Fire Barriers. Staff Requesting That Affected Licensees Take Issue on Voluntary Initative & Propose Approach for Resolving Issues ML20211L4901999-09-0101 September 1999 Forwards Insp Repts 50-313/99-12 & 50-368/99-12 on 990711- 0821.No Violations Noted ML20211J2351999-08-31031 August 1999 Forwards Request for Addl Info Re SG Outer Diameter Intergranular Attack Alternate Repair Criteria for Plant, Unit 1 ML20211F8251999-08-25025 August 1999 Forwards Insp Repts 50-254/99-15 & 50-265/99-15 on 990816-20.No Violations Noted.Insp Evaluated Effectiveness of Maint Rule Program & Review Periodic Evaluation Specifically Required for 10CFR50.65 ML20211F4181999-08-25025 August 1999 Forwards SE Accepting Licensee 980603 & 990517 Requests for Approval of risk-informed Alternative to 1992 Edition of ASME BPV Code Section Xi,Insp Requirements for Class 1, Category B-J Piping Welds ML20211B8691999-08-20020 August 1999 Forwards Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Action Plans Developed to Address Configuration Control Weaknesses Not Totally Effective as Listed ML20211D1491999-08-19019 August 1999 Forwards Insp Repts 50-254/99-16 & 50-265/99-16 on 990719-22.Staff Identified Major Discrepancy Re Accuracy of Data Submitted to NRC for Protected Area Security Equipment Performance ML20211C7601999-08-19019 August 1999 Confirms NRC Intent to Meet with NSP & Ceco on 990807 in Lisle,Il to Discuss with Region III Pilot Plants,Any Observations,Feedback,Lessons Learned & Recommendations Relative to Implementation of Pilot Program ML20210T9941999-08-13013 August 1999 Forwards Insp Repts 50-254/99-12 & 50-265/99-12 on 990628-0716.Violations Noted ML20210R7451999-08-13013 August 1999 Forwards Insp Repts 50-254/99-11 & 50-265/99-11 on 990601-0720.NRC Identified Several Issues Which Were Categorized as Being of Low Risk Significance.Two Issues Involved NCVs of Regulatory Requirements ML20211A9501999-08-12012 August 1999 Discusses 990720-21 Workshop Conducted in Region IV Ofc,Re Exchange of Info in Area of Use of Risk Insights in Regulatory Activities.List of Attendees,Summary of Topic & Issues,Agenda & Copies of Handouts Encl IR 05000368/19990111999-08-12012 August 1999 Forwards Insp Repts 50-313//99-11 & 50-368/99-11 on 990719-23.No Violations Noted.Insp Focused on Review of Licensed Operator Requalification Program & Observation of Requalification Exam Activities at Unit 1 ML20210U2621999-08-12012 August 1999 Forwards Insp Rept 50-333/99-06 on 990601-0717.No Violations Noted ML20210R9541999-08-10010 August 1999 Informs That During 990804 Telcon Between J Bartlet & M Bielby,Arrangements Were Made for NRC to Insp License Operator Requalification Program at Plant.Insp Planned for Wks of 991018 & 25 ML20210M5461999-08-0606 August 1999 Discusses 990804 Telcon Between J Bartlet & M Bielby,Where Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wks of 991018 & 25 ML20210L1461999-08-0303 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Requests Submittal of Ltr Identifying Individuals Taking Exam,Personnel Allowed Access to Exams & Mailing Address for Exams ML20210L8371999-08-0202 August 1999 Forwards SE Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety Related Motor-Operated Valves ML20210M4691999-07-30030 July 1999 Forwards Insp Repts 50-254/99-14 & 50-265/99-14 on 990713-15.One NCV Was Identified & Discussed in Encl Insp ML20210L3581999-07-29029 July 1999 Ltr Contract,Task Order 43, Arkansas Nuclear One Safety System Engineering Insp (Ssei), Under Contract NRC-03-98-021 ML20210H4661999-07-29029 July 1999 Forwards Insp Repts 50-254/99-13 & 50-265/99-13 on 990628-0702.No Violations Noted.Insp Consisted of Selective Examination of Procedures & Representative Records, Observations of Activities & Interviews with Personnel ML20216D8131999-07-28028 July 1999 Forwards Request for Addl Info Re SG Tube End Cracking Alternate Repair Criteria for Plant,Unit 1 ML20216D9421999-07-28028 July 1999 Forwards Safety Evaluation Granting Requests for Relief from Requirements of ASME Code,Section XI for Second 10-year ISI Interval for James a FitzPatrick NPP ML20210C2191999-07-21021 July 1999 Forwards Insp Repts 50-313/99-08 & 50-368/99-08 on 990530-0710 at Arkansas Nuclear One,Units 1 & 2,reactor Facility.No Violations Noted.Conduct of Activities at Plant Generally Characterized by safety-conscious Operations ML20210A7001999-07-16016 July 1999 Forwards Request for Addl Info to Supplement Response Provided for GL 97-05, Steam Generator Tube Insp Techniques ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) ML20209H5251999-07-15015 July 1999 Informs That as Result of NRC Review of Licensee 980701 & 990311 Responses to GL 92-01,rev 1 & Suppl 1 & Suppl 1 RAI, Staff Revised Info in Reactor Vessel Integrity Database & Releasing Database as Rvid Version 2 ML20209E5551999-07-0808 July 1999 Informs That as Result of NRC Review of Util Responses to GL 92-01,rev 1,suppl 1,staff Revised Info in Rv Integrity Database & Releasing Database as Rvid Version 2 ML20209D8521999-07-0707 July 1999 Responds to Util 990706 Request That NRC Exercise Discretion Not to Enforce Compliance with Actions Required by TS 3.7.2, Auxiliary Electrical Sys. NOED Warranted & Approval Granted for Extension of Allowed Outage Time to 14 Days ML20209D5511999-07-0606 July 1999 Informs That as Result of NRC Review of Licensee Response to GL 92-01,rev 1,suppl 1,staff Revised Info in Reactor Vessel Integrity Database & Releasing Database as Rvid Version 2 ML20209B2081999-06-29029 June 1999 Discusses Closure of Response to RAI Re GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity. Rvid,Version 2 Issued as Result of Review of Responses.Info Should Be Reviewed & Comments Submitted by 990901 ML20209A8561999-06-25025 June 1999 Refers to Investigation Rept A4-1998-042 Re Potential Falsification of Training Record by Senior Licensed Operator at Arkansas Nuclear One Facility.Nrc Concluded That Training Attendance Record Falsified 1999-09-09
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April 2,-1999 t.
Mr. C. Rdndy Hutchinson
' Vice President, Operations ANO Entergy Operations, Inc.
1448 S. R. 333 Russellville, AR 72801
SUBJECT:
REQUEST FOR A TECHNICAL REVIEW OF A DRAFT INFORMATION NOTICE DESCRIBING THE UNANTICIPATED REACTOR WATER-DRAINDOWN AT QUAD CITIES NUCLEAR POWER STATION, UNIT 2, ARKANSAS NUCLEAR ONE, UNIT 2, AND THE JAMES A. FITZPATRICK NUCLEAR POWER PLANT
Dear Mr. Hutchinson:
The U.S. Nuclear Regulatory Commission is planning to issue an information Notice (lN) that describes the unanticipated reactor water draindown at Quad Cities Nuclear Power Station, Unit 2, Arkansas Nuclear One, Unit 2, and the James A. FitzPatrick Nuclear Power Plant. This
. IN is being issued to alert other licensees as to the potential for such an event happening at their facilities.
We request that you review the enclosed draft IN to ensure that the technical information regarding the event at your plant is accurate. If we do not receive written comments within 1 week of the date of issuance for this letter, we will assume that you have no comments. Your cooperation in this matter is appreciated.
Sincerely, ;
ORIGINAL SIGNED BY l
M. Christopher Nolan, Project Manager, Section 1 Project Directorate IV & Decommissioning Division of Licensing Project Management i Office of Nuclear Reactor Regulation i Docket Nos. 50-265, 50-368, and 50-333 DISTRIBUTION:
[DocketFiled PUBLIC K. Brockman, RIV
Enclosure:
As stated PDIV-1 r/f S.Richards J. Zwolinski/S. Black 1 OGC M. C. Nolan ACRS
\
cc: See next page R. Gramm C.' Petrone R. Pulsifer >
R. Denning J. Williams S.Richards QO
\
DOCUMENT NAME: G:\ANO2FINA\LTRA2729.WPD Tm receive a copy of this document, Indicate in the box: "C" = Copy without enclosures "E* = Copy'with encionres "N" = No copy OFFICE PM:PDIV-1 E LA:PDIV-i3f' N PECB v BC:PECB: DRIP SC:PDIV-1, NAME- CNolan M LBerry W\l CPetrone tf,W RDennig M4 RGramm (L(O DATE 04/o/ /99 04/ W /99-- \ 04/ % /99 ~ ~ 04/ % /99' V 04/ 1 /99'
\ OFFICIAL RECDRD COPY r
.s33,1.
'. L 9904070026 990402 PDft ADOCK 05000265 G PDR
O g Mr. C. Randy Hutchinson i Entergy Operations, Inc. Arkansas Nuclear One, Unit 2 cc:
Executive Vice President Vice President. Operations Support
& Chief Operating Officer Entergy Operations, Inc.
Entergy Operations, Inc. P. O. Box 31995 P. O. Box 31995 Jackson, MS 39286-1995 l Jackson, MS 39286-199 Wise, Carter, Child & Caraway Director, Division of Radiation P. O. Box 651 Control and Emergency Management Jackson, MS 39205 Arkansas Department of Health 4815 West Markham Street, Slot 30 Little Rock, AR 72205-3867 Winston & Strawn 1400 L Street, N.W.
Washington, DC 20005-3502 l
Manager, Rockville Nuclear Licensing I Framatone Technologies 1700 Rockville Pike, Suite 525 Rockville, MD 20852 Senior Resident inspector U.S. Nuclear Regulatory Commission P. O. Box 310 London, AR 72847 Regional Administrator, Region IV U.S. Nuclear Regulatory Commission 611 Ryan Plaza Drive, Suite 400 Arlington, TX 76011-8064 County Judge of Pope County Pope County Courthouse Russellville, AR 72801 i
1 l
I i
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DRAFT-DRAFT-DRAFTUNITED STATESDRAFT-DRAFT-DRAFT NUCLEAR REGULATORY COMMISSION OFFICE OF NUCLEAR REACTOR REGULATION WASHINGTON, D.C. 20555-0001 March XX,1999 NRC INFORMATION NOTICE 99-XX: UNANTICIPATED REACTOR WATER DRAINDOWN AT QUAD CITIES NUCLEAR POWER STATION, UNIT 2, ARKANSAS NUCLEAR ONE, UNIT 2, AND THE JAMES A.
FITZPATRICK NUCLEAR POWER PLANT Addressees All holders of licenses for nuclear power, test, and research reactors.
Purpose The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice to alert addressees to the potential for personnel errors during infrequently performed evolutions that result in, or contribute to, events such as the inadvertent draining of water from the reactor .
vessel during shutdown operations. It is expected that recipients will review the information for applicability to their facilities and consider actions, as appropriate, to prevent a similar occurrence. However, suggestions contained in this information notice are not NRC requirements; therefore, no specific action or written rPFponse to this notice is required.
Descriotion of Circumstances Quad Cities, Unit 2 On February 24,1999, Quad Cities Unit 2 was in cold shutdown with reactor water temperature at about 144 'F and reactor water level in a band of 90 to 94 inches indicated level (normal level during operations is 30 inches indicated or about 173 inches above the top of active fuel (TAF]). Core cooling was being maintained in a band of 120 *F to 170 *F by the "A" loop of the residual heat removal (RHR) mode of shutdown cooling, after being switched from the "B" loop at about 12:32 a.m. Sometime later operators noted a decreasing reactor water level and at about 1:02 a.m. secured the "2A" RHR pump and isolated shutdown cooling. At 1:55 a.m.
operators restored the "2A" loop of shutdown cooling to the proper lineup and started the "2A" RHR pump. Water level had decreased to a minimum of about 45 inches indicated, and reactor water temperature had risen to a maximum of about 163 *F. Forced circulation of reactor vessel water using a reactor recirculation pump remained in effect throughout the event.
On the basis of post event reviews, it appears that the minimum flow valve was left open because the nuclear station operator failed to ensure that the tasks were performed in the sequence specified in the operating procedures. The nuclear station operator who was directing the evolution from the control room gave the non-licensed operator permission to de-energize the breaker for the "A" RHR minimum flow valve operator before the valve was taken to the required closed position. De-energizing the breaker also removed power to the valve INIGURE
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DRAFT-DRAFT-DRAFT IN 99-xx g March xx,1999 Page 2 of 5 position indicator lights in the control room. Thus, when the nuclear station operator tried to verify that the valve was closed, there was no position indication in the control room to make that verification. The nuclear station operator made the incorrect assumption that f ne valve was already closed and moved to the next step in the procedure. This failure to close the "A" RHR minimum flow valve opened a drain path from the reactor to the suppression pool. To further complicate the event, the operating crew did not recognize that there was any problem until the water level had decreased about 13 inches. After detecting the decrease, the operating crew was slow to react, which allowed the level to decrease another 20 inches before the operators isolated shutdown cooling which terminated the draindown. The licensee estimated that a total of 6000 to 7000 gallons was drained from the reactor to the suppression pool. j Poor practices in operations including poor communications, poor activity briefings for high-risk activities, lack of pre-shift briefings, inadequate supervision of important control room activities, inadequate monitoring of control room panels, and slow event response may have contributed to the event. However, although the unintended less of inventory to the suppression p, al was significant and highlighted significant weaknesses in plant operations, the safety signifi ance was minimized by two features. First, a reactor recirculation pump remained in service throughout the event which served to distribute decay heat. Additionally, an automatic isolation of shutdown cooling would have occurred at 8 inches indicated level which would have stopped the draining event. An indicated water level of 8 inches corresponds to approximately 151 inches of water level above the TAF in the reactor core.
Arkansas Nuclear One, Unit 2 On February 2,1999, at Arkansas Nuclear One, Unit 2, the operators were draining the refueling canal in preparation for installing the reactor vessel head. Refueling was complete and steam generator nozzle dams were installed. The operators were using the two low pressure safety injection (LPSI) pumps to drain the canal to the refueling water storage tank; one pump also served as the shutdown cooling pump. The rate of draindown was approximately 3.3 Inches per minute. When the water level reached 105 inches, the reactor operator noted that level started to lower rapidly. Operators stopped one of the LPSI pumps and instructed a local operator to close the isolation valve to the refueling water tank. This manually operated valve required 55 turns of the handwheel to fully close. Within approximately 1.5 minutes, the reactor vessel level had dropped below the 65 inch level (where reduced inventory begins) and continued down to 56 inches before the valve could be fully closed.
(Reference zero on these level instruments is the bottom of the hot leg, with mid-loop being defined at approximately 24 inches.) The average rate of level decrease between 105 inches and 56 inches was 33 inches per minute. At its lowest level,56 inches indicated, there were still 93 inches of water above the TAF. Using the high pressure safety injection (HPSI) pump the operators brought the level back up to 90 inches. The olant was in reduced inventory operations (below 65 inches) for approximately 7 minutes. During the event the level remained well above the point where LPSI pump cavitation would be expected.
On the basis of post event reviews, it was determined that the procedure used for draining l down the refueling canal was inadequate in that it provided the wrong level at which operators l were to secure the draining. The procedure incorrectly stated that the draindown should be I
secured at the 90-inch level. The procedure should have directed that the rate of draining be secured at the 106-inch level so that appropriate precautions could be taken before resuming f
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the draindown. These precautions should have included reminders to the operating crew that below the 106-inch level the level will drop much more quickly because most of the water has been drained from the refueling canal. Therefore, in order the maintain control of the water level, the draindown rate should be decreased and an operator should be stationed to directly l monitor the level. l Additional factors that contributed to this event include: the operators received little specific training on this evolution, and the crew was inexperienced in performing this task; the task should have been classified as an infrequent task, recuiring a more thorough briefing; and, operators failed to follow the procedure that required that an operator be stationed to monitor the refueling canal level and relied instead on a camera that did not provide a cicer picture of the water level in the refueling canal.
FitzPatrick l On December 2,1998, at the James A. FitzPatrick Nuclear Power Plant, the operators'were in the process of reassembling the reactor following refueling. Operators were controlling the reactor vessel water level at approximately 350 inches above TAF by adjusting the water discharge rate to compensate for the constant input from the control rod drive cooling water system. As required by their risk analysis, they were relying on two independent reactor level instruments. One was the wide-range level indicator (which provided indication up to the top of the reactor vessel) and the other was a narrow range indicator which was off-scale high.
In order for the wide-range level indicator to remain operable with the reactor head removed, a temporary standpipe and fill funnel were used to replace a portion of the reference leg. At the ,
time of the event, the licensee was in the process of removing this temporary standpipe and i reinstalling the original reference leg components. As the water drained from the standpipe, it caused the wide-range level indicator to erroneously show an increasing water level. For a period of approximately one hour, the operators in the control room, unaware that the ongoing maintenance would cause an error in the indicated water level, compensated for the apparent increasing level by increasing the discharge rate. This action had the effect of reducing the actual water level from 350 inches to 250 inches. During the same time period, the operators were also in the process of filling and venting the reactor feedwater piping, which also affected the reactor water level. Once the normal reference leg piping had been reinstalled and the reference leg began to refill, the indicated level decreased from 350 inches to the actual level of 250 inches. The second level instrument (the narrow-range level indicator) which does not come on-scale until the level goes below 224 inches, remained off-scale high.
When operators discovered the level discrepancy, they used a temporary pressure gauge connected to the reactor vessel low-point tap to confirm the actual water level. After confirming the accuracy of the wide-range indicator, they restored the level to 350 inches. The 100-inch error represented approximately 15,000 gallons of water. The licensee determined that the safety significance of this event was low since the reactor was in cold shutdown and the reactor water level remained well above the TAF. In addition, the drain-down would have been limited by an automatic isolation of the draindown path, which would have occurred at 177 inches above the TAF.
DRAFT-DRAFT-DRAFT IN 99-xx l March xx,1999 Page 4 of 5 The licensee's review of the event identified weaknesses in the operator's knowledge of the reactor assembly process and weaknesses in the plant risk assessment process. Contrary to the assumption in the plant risk analysir ' hat two reactor water level indicators were available, l only one, the wide range indicator, was awe to provide level indication above 224 inches. l When the reference leg on the wide-range instrument was disassembled and drained, it was l rendered inoperable. The second instrument, the narrow-range indicator, was pegged off-scale ,
high and remained that way throughout the event because the level never dropped below l 224 inches. Proposed corrective actions included procedural enhancements to address the loss of level indication during reactor disassembly and reassembly and providing for an alternate means of level indication.
Discussion Personnel errors appear to have caused, or contributed to, these three inadvertent reactor l vessel draindown events. The likelihood of personnel errors is dependent upon the operator's knowledge of the task gained through previous experience and training. It is also dependent l upon the quality of the procedures used to perform the task, the level of supervision, the l adequacy of pre-job briefings, fatigue, and distractions resulting from multiple tasks. In each of the events, the plant staff made errors during a seldom-performed evolution. Because it was a seldom-performed evolution, more training, better pre-job briefings, closer supervision, and procedures that contain more details than those for frequently performed activities might have prevented the event. l l
The current trend in the Nuclear Power Industry is to reduce cost by reducing plant staff and minimizing outage time. These reductions in plant staff may have led to an overalllowering of l plant staff knowledge due to the loss of some of the most experienced personnel, including supervisors and managers, at many plants. It is possible that decreases in plant staff experience levels would show up first in infrequently performed tasks such as outage activities, rather than in routine tasks perforrr ed during power operation. In addition, the decrease in plant staff and shorter outage times could have the combined effect of increasing the workload of the remaining staff. Increases in work load also leads to longer shifts, fatigue and an ,
increase in the likelihood of personnel errors.
The extent to which these factors may have contributed to the events described in this information notice is unknown. However, these events should serve as a reminder to all licensees that reductions in staff and decreases in outage times can lead to an increased number of personnel errors if they are not carefully controlled.
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i This information notice requires no specific action or written response. If you have any j questions about the information in this notice, please contact the technical contact listed below, ;
,. the appropriate regional office, or the appropriate office of Nuclear Reactor Regulation (NRR) i Project Manager, j l
David B. Matthews, Director Division of Regulatory Improvement Programs ,
l Office of Nuclear Reactor Regulation Technical contact: Chuck Petrone, NRR 301-415-1027' E-mail: cdo@nrc.aov
REFERENCES:
NRC Integrated inspection Report No. 50-333/98 08, issued February 10,1999 (Accession No.
9902170348) for the James A. FitzPatrick Nuclear Power Plant for the period November 22, 1998, through January 10,1999.
4 Attachments:
- 1. List of Recently issued NMSS Information Notices l 2. List of Recently issued NRC Information Notices I
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