ML20199A578
ML20199A578 | |
Person / Time | |
---|---|
Site: | Braidwood |
Issue date: | 12/17/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
To: | |
Shared Package | |
ML20199A562 | List: |
References | |
50-456-97-16, 50-457-97-16, NUDOCS 9801280028 | |
Download: ML20199A578 (29) | |
See also: IR 05000456/1997016
Text
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U.S. NUCLEAR REGULATORY COMMISSION. l
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- R E G IO N lil
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50-456, 50-457.
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. Docket Nos:
, License Nos: NPF 72, NPF-77
Report No: - 50-456/97016(DRP): 50-457/97016(DRP)
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Licensee: Commonwealth Edison (Comed)- ,
Facility: Braldwood Nuclear Plant, Units 1 and 2 '
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Location: RR #1, Box 84
Braceville, IL 60407
Dates: September 23 through November 3,1997
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inspectors: C. Phillips, Senior _ Resident inspector
J. Adams, Resident inspector -
D. Pelton, Resident inspector
T. Esper, Illinois Department of Nuclear Safety
Approved by: Michael J. Jordan, Chief
Reactor Projects Branch 3
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' EXECUTIVE SUMMARY
Braidwood Nuclear Plant, Units 1 and 2
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NRC Inspection Report No. 50-456/97016(DRP); 50-457/97016(DRP)
This inspection included aspects of licensee operations, maintenance, engineering, and
plant support. The inspection report covers a 6-week period of resident inspection from
. September 23 through November 3,1997.
Operations
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The inspectors concluded that the Unit 2 shutdown for refueling outage A2R06,
conducted on September 26 and 27, was well planned and executed. The licensee
had a designated operator and supervisor to control reactivity changes. Senior plant
management was present to observe the shutdown and ensure the outage started
smoothly. Operators followed procedures and handled minor equipment problams
well, which prevented potential secondary plant transients (Section O1.1).
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The inspectors concluded that the corrective actions taken by the licensee to ensure
the correct positioning of equipment was not totally effective. The licensee identified
eleven mispositioned componens between September 2 and October 4,1997.
Problems with mispositioned components have been discussed in previous
inspection reports and this has been a recurring issue. The examples discussed in
this report were considered to be further examples of the violation issued in
Inspection Report No. 97015. It is too early to determine if the recent corrective
actions taken by licensee management have been effective in addressing this issue
(Section 01.2).
- The inspectors concluded that the licensee's "Reportability Manual" was incorrect for
reporting engineered safety feature actuations. The licensee failed to report a Unit 2
"A" train containment ventilation isolation. The inspectors informed the licensee that
the event was reportable and it took several days before the licensee agreed that the
event was reportable. A violation was issued (Section 03.1).
- The inspectors reviewed the licensee's tracking system for human performance
errors resulting in licensee evant reports (LERs) and problem identification forms
(PlFs) conceming out-of-services. The inspectors concluded the licensee accurately
identified and correctly tracked human performance errors described in LERs and
PIFs conceming out-of-services (Sections 01.3 and O1.4).
The inspectors reviewed the licensee's tracking system for entries into unplanned
limiting condition for operations (LCOs) and operator work arounds. The inspectors
concluded the licensee accurately identified and correctly tracked unplanned LCO
entries and operator work arounds (Sections 01.5 and O2.1).
Maintenance
The inspectors concluded that contractor personnel demonstrated poor human
performa.'. e on October 28,1997, by failing to follow the procedure to establish a
- freeze seal prior to maintenance. The inspectors observed two subsequent
maintenance
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cctiviti;s th t r;quir2d frc:ze s;als, conduct;d by both lic3nse2 end contractor j
personn;l, which r;vaal:d none of the previously not;d probi;ms. A violation was ;
- issu;d (S;ction M1.1).
The, inspectors concluded that the maintenance on valve 2CV-093A was performed
well by the maintenance crew. The inspectors observed that during the maintenance
work performed on 2CV-003A, the maintenance crew followed the procedure, noted
that the work would exceed the scope of the work packsge and had the package
changed, and used the proper materials for the job. However, the inspectors
observed a lack of concern demonstrated by mechanics after having dropped 2CV-
3121 and an associated test gauge on the floor (Section M1.2).
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The inspectors concluded that the construction, inspection, and tracking of
scaffolding was poor during the months of August and September 1997. The
inspectors and the licensee identified numerous examples (about 20) of the failure to
follow procedural requirements by maintenance personnel and operations
department supervisors regarding construction, inspection, and tracking of
scaffolding in areas affecting the operation of both units between August 24 and
September 17. The inspectors also concluded that the maintenance department
self assessment identified construction of scaffolding as an area that needed
improvement, but that future corrective actions were not made clear in the report. A
violation was issued (Section M2.1).
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The inspectors concluded that the six surveillance tests observed during this period
were performed in accordance with procedures and all acceptance criteria were met
or the proper actions were taken by the test directors when the acceptance criteria
were not met. Heightened level of awareness and pre-job briefings were thorough
and exceeded minimum briefing requirements. The surveillance test procedures
were well written and ensured Technical Specification and Updated Final Safety
Analysis Report requirements were tested (Section M4.1).
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The inspectors identified 17 examples where the licensee failed to take effective
corrective actions for the securing of movable carts in the auxiliary building. A
violation was previously issued for the licensee's failure to e, ' movable carts and
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equipment in NRC Inspection Report No. 50-456/96021(DR; ,, 50-457/96021(DRP).
A violation was issued (Section M8.1).
Ennineerina
- The inspectors concluded that the licensee accurately maintained, tracked and
controlled temporary alterations (Section E2.1).
- The inspectors conchded that the original revision of operability evaluation 97-015
for the 125 volt direct current battery charger was conducted poorly. After the
inspectors questioned the operability determination, the licensee reevaluated the
operability evaluation and determined that the sizing of the battery charger did meet
the design basis requirements. The inspectors concluded that the preparation and
superviscry review of the original operability evaluation 97-015 was poor, and that
the system engineer demonstrated a lack of knowledge of the 'esign basis
requirements of the 125 volt direct current battery chargers (Se.; tion E3.1).
- The inspectors concluded that the licensee failed to perform a modification to the
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o m:in turbine control software in accord nce with station procedures. - The licensee
l * _ h:d modiftd the runb:ck t:rmin: tion setpoint for both units in 1990, h:d not
ch:nged the simul: tor, cnd h:d not tr;ined oper;t:rs en the ch:nge. Tha inspectors
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concluded that the licensee conducted an accurate and thorough apparent cause
evaluation of the undocumented change of the turbine runback termination setpoint.
-This failure to perform a modification to the main turbine control software in
accordance with station procedures was a licensee identified non cited violation
(Section E4.1).
Plant Support
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The inspectors concluded that licensee management did not cleariy communicato
restrictions on use of skull caps as protective clothing to workers. The licensee had
a policy memorandum restricting the use of skull caps as protective clothing if hair =
could not be protected from contamination. However, this policy memorandum
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restriction on the use of skull caps was not in the procedure that govemed protective
clothing, nor was it in the radiation work pemlit (Section R3.1).
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- The inspectors concluded that between September 26 and October 15, there was an
unusually high number of improper radiological postings. A large portion of these
appeared to have been caused by contractor personnel failing to comply with
licensee procedures. A violation was issued.
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The inspectors concluded that licensee management had not effectively
communicated and/or had not enforced the requirements for the control of
combustible material. Corrective action for a previous violation of combustible
material control was ineffective to prevent recurrence. The inspectors identified that
between September 16 and Octo'o er 20,1997, there were at least ten examples of
the failure to adhere to procedures goveming combustible liquid control. A violation
was issued (Section F1.1).
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RODort Details
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Summarv of Plant Status
Unit 1 entered the period at 100 percent power and operated at that power level for the
entire period.
Unit 2 entered the period at 100 percent power and shut down for refueling outage A2R06
on September 26 and remained shut down for the remainder of the inspection period.
LO_pprations
01 Conduct of Operations
01.1 Unit 2 Shutdown For Refuelina Outaoo A280J}--
a. Incoection Scone (71707)
The inspectors reviewed the following procedures, 2BwGP 100-5, " Plant Shutdown
and Cooldown," Revision 12E2 and 2BwGP 100-6, " Refueling Outage," Revision 8.
The inspectors also observed portions of the shutdown.
b. Observations and Findinas
The inspectors observed that the licensee had a designated reactor operator and
senior reactor operator to perform and monitor all re- +< changes. The inspectors
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observed that communications between these oper m tne cognizant nuclear
engineer were clear and frequent
The inspectors observed that in addition to the shift manager there were two other
senior station managers present to observe the shutdown and ensure the outaga
started smoothly.
The inspectors observed that the procedures used appeared to be adequate and
that the operators followed the procedures. The inspectors also observed that the
operators handled several minor equipment problems well and minimized plant
transients. These included control of the feedwater regulating valves which operated
sluggishly and the recovery from steam dump failures.
c. Conclusion
The inspectors concluded that the Unit 2 shutdown for refueling outage A2R06,
conducted on September 26 and 27, was well planned and executed. The licensee
had a designated operator and supervisor to control reactivity changes. Senior plant
management was present to abserved the shutdown and ensure the outage started
smoothly.
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01'2_ Qontinued Problems With Mispositioned Eaulomenj,
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- a. ' ' Insoection Scope (71707)
The inspectors reviewed the following licensee problem identification forms (PlFs),
1997-03218, A1997-03221, A1997-03595, A1997-03620, A1997-03771, A1997-
04061, A1997-04121- A1997-04115 A1997-04179, A1997-04186, A1997-04187,
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A1997-04172, A1997-04166, and A1997-04160. The inspectors also interviewed
operations department managers,
b. Observations and Findinas
The inspectors identified through the review of licensee PIFs that mispositioned
equipment continued to be a problem area. The licensee identified eleven
mispositioned components b3 tween September 2 and October 4,1997.
The improper positioning of components has been a ret.ing problem. This issue
was discussed in Inspection Reports Nos. 96005,96008,96009,96012, and 97015.
A violation was issued in inspection Report No. 97015 (50-457/97015-01(DRP)) for
the failure to take effective corrective action regarding the proper positioning of
components. The licensee identified mispc,sitioned components were considered to
be more examples of the violation issued in inspection Report No. 97015.
The inspectors observed that the proper positioning of plant equipment was stresseo
at several operating shift turnovers by operations department management.
Licensee personnel stated that the number of OOS's that were issued to an
ind'vidual at one time were reduced to one or possibly two if there were radiation
dose concems. Operations management personnel stated that the number of
" Scorecard" appraisals of rmn licensed operator performance increased to about six
per shift An operations field supervisor was moved to the non-licensed operator
ready room during the Unit 2 refueling outage te monitor the amount of work
assigned to operators near the end of the shift.
c. Conclusion
The inspectors concluded that the corrective actions taken by the licensee to ensure
the correct positioning of equipment was not totally effective. New corrective actions
taken by licensee management has not yet had time to demonstrate effectiveness.
The licensee identified eleven mispositioned components between September 2,
1997, and October 4,1997. Problems with mispositioned components were
discussed in previous inspection reports and this has been a recurring issue. The
examples discussed in this report were considered to be further examples of the
violation issued in Inspection Report No. 97015.
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01.3 ligman Performance Error Licensee Event Reports (LER) Review
a. -Inspection Scoce (92901)
The inspectors reviewed all 199/ LERs for both Units 1 and 2; and QVL 20-97-065,
' *Braidwood Station Quality & Safety Assessment, Braidwood Integrated Performance '
Report - Third Quarter 1997."
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. b. Observations and Findinas.
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- Th3 inspect:rs revhwed Unit 1 cnd 2 LERs for 1997. The inspect:rs revtwed c:ch
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LER and found that the cause was accurately determined. The inspectors found '
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only one LER where the cause was attributed to a human performance error. The
inspectors findings were consis;ent with the number reported by the licensee in QVL ,
20-97-065, "Braidwood Station Quality & Safety Assessment. Braidwood Integrated
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Performance Report - Third Quarter 1997.*
c. Conclusions
The inspectors concluded that as of November 3, the licensee had accurately
tracked the number of human performance errors resulting in LERs, and has
accurately reported the number of human performance errors that resulted in LERs
in their self assessment reports.
01.4 Review of Out-Of-SeIyice (OOS) Errors
a. Inspection ScoDe (92901) -
The inspectors reviewed all PlF titles for the previous six months (April through
September 1997); NSWP-A-15, " Comed Nuclear Division Integrated Reporting
Provam," Revision 1; QVL 20-97-065, "Braidwood Station Quality & Safety
Assessment, Braidwood integrated Performance Report - Third Quarter 1997*; and
discussed the definition of an OOS error with operations management.
2 b.- Qkservations and Findjnal.
The inspectors conducted a review of PlF titles for the previous six months and
found 61'OOS related problems. Forty-three of the PlFs were due to errors in the
performance of the OOS process. The licensee screened the PIFs in accordance
with NSWP-A-15 and determined that none described a significant condition adverse
to quality and none of the PIFs were counted or tracked as an OOS error. The
inspectors found the licensee's definition of an OOS error to be subjective. The
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inspectors discussed the subjective definitions with licensee management. The
' licensee agreed with the inspectors that a more precise definition for an OOS error
was needed and has taken action within the operations peer group to develop a new
more precise definition for an OOS error. The inspectors observed that the licensee
has met their performance goals for the previous 6 months using the current
definitions for an OOS error and significant condition adverse to quality.
- c. Conclusions
The inspectors concluded that the licensee accurately identified OOS errors and
documented the errors in PIFs. The inspectors concluded that the licensee screened
the PlFs in accordance with NSWP-A-15, but were concemed with the degree of
subjectivity associated with the definition of significant condition adverse to quality. ,
The inspectors concluded that the licensee had met their performance goals for the
. previous 6 months using the current definitions for an OOS error.
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01.5 ' Review of Unolanned L%itino Condition for Operation (LCO) Entries
a. ' Insoection Scope (92901)
The inspectors reviewed a portion of the Limiting Condition for Operation Action
Requirements (LCOAR) database and QVL 20-97-065, 'Braidwood Station Quality &
Safety Assessment, Braldwood Integrated Performance Report - Third Quarter
1997." -
b. Observations and Findinos
The inspectors reviewed the method used for tracking unplanned LCO entries. The
inspectors found that the unit supervnors enter each LCO into the LCOAR database.
Each database entry is compared against the definition of an unplanned entry into a
LCO. If the LCO required a 7 day or less shutdown and was unplanned, then it was-
counted. Inspectors reviewed the LCOAR database input for the month of
September and found that the licensee has accurately counted unplanned LCO
entries. The inspectors findings were consistent with number reported by the
licensee in QVL 20 97-065, 'Braidwood Station Quality & Safety Assessment,
Braldwood integrated Performance Report - Third Quarter 1997.'
c. Conclusions
The inspectors concluded that the licensee has accuratel) identified, quantified,
tracked, and reported unplanned entries into LCOs.
O2 Operational Status of Facilities and Equipme. .
02.1 Operator Work Arounds Status Revievt
a. Inspection Scope (92901)
Tha inspectors reviewed the Operator Wnrk Around index; and QVL 20-97-065,
"Braidwood Station Quality & Safety Assessment, Braidwood Integrated Performance
Report - Third Quarter 1997." The inspectors also discussed efforts to eliminate
operator work arounds with a member of the operator work around committee.
b. Observations and Fi.n,dinas
lhe inspectors reviewed the onerator work around index and observed that there
were 53 operator work arounds identified. The inspectors performed control room
observations and panel walkdowns and found no operator work arounds that had not
been previously identified by the licensee. The inspectors findings were consistent
with number reported by the licensee in QVL 20-97 065, "Braidwood Station Quality
& Safety Assessment, Braidwood lntegrated Performance Report - Third Quarter
1997.'
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c. Conclusions
- The inspectors conclud:d that the licenses h s accuratlly id2ntifcu cnd quantifsd
the operator work arounds, has accurately tracked the status of the operator work
arounds, and has accurately reported the numbers and status of the operator work
arounds in their self assessment reports. The inspectors concluded that licensee
- has met their operator work around work down goals.
03 Operations Procedures and Documentation
03.1 Licensee Failed To Report Enoineered Safety Feature Actuation In Accordance With
a. In}pfction Scope (71707)
The inspectors reviewed PIF A1997-04424 on Ochber 15,10 CFR 50.72, NUREG
1022, Revision 1, Second Draft, and the licenue's *Reportability Manual," Revision
4. The inspectors attended the licensee's r., vent screening committee meeting on
October 15 and interviewed members of licensee "anagement.
b. Observations and Findinas
On October 14, a licensee instrument technician made an error when changing
setpoints on the Unit 2 containment area radiation monitor 2AR11J. The error
resulted in a high radiation alarm and an "A" train containment ventilation isolation.
The initial conclJsion during the licensee management review of the event was that it
was not reportable in accordance with 10 CFR 50.72 based on information provided
in the licensee's 'Reportabliity Manual.' The 'Reportability Manual" provides
guidance to operators on which events are reportable to the NRC and which are not.
The inspectors reviewed the repor1 ability criteria for a 4-hour non-emergency call
from the licensee to the NRC under 10 CFR 50.72 (b)(2)(ii) which states:
(ii) Any event or condition that results in a manual or automatic actuation
of any engineered safety feature (ESF), including the reactor
protection system, except when;
, (A) The actuation results from and is part of a pre-planned
sequence during testing or reactor operation;
(b) The actuation is invalid and;
(1) Occurs while the system is propctly removed from
service;
(2) Occurs after the safety function has been already
completed; or
(3) involves only the following specific ESFs or their
equivalent systems;
(i) Reactor water clean-up system;
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.(11) Control room smergrney vsntilation syst:m;
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(ill) Rsactor building vsntilation systsm;
(iv) Fuel building ventilation system; or
(v) Auxiliary building ventilation system.
The inspectors informed licensee management that the event was reportable since it
was an automatic actuation of an ESF and did not meet the exclusion criteria. The
actuation was not part of a preplanned evolution and although the actuation was
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invalid, the system was not removed from service, the safety feature had not already
been completed, and containment ventilation was not one of the listed ESF systems
for exclusion.
The licensee never made the required notification of the NRC as required by
10 CFR 50.72, but agreed several days later to write a licensee event report. The
failure to make a report of the ESF actuation within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> as required was a ,
violation of 10 CFR 50.72 (50-457/97016-01(DP,P)).
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c. Conclusion
The inspectors concluded that the licensee's "Reportability Manual" was incorrect for
reporting engineered safety feature actuations. The licensee failed to report a Unit 2
"A" train containment ventilation isolation that was due to an error made by a
mechanic while adjusting the setpoint on a radiation monitor. The inspectors
informed the licensee that the event was reportable and it took several days before
the licensee agreed that the event was reportable. A violation was issued.
II. Maintenance
M1 Conduct of Maintenance
M1.1 Repair of Essential Service Water (SX) Valve 2SX-2102.
. a. Inspection Scope (61726)
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On October 1, the inspectors observed maintenance on the 2A auxiliary feedwater
pump oil cooler SX isolation valve 2SX 2102. The inspectors monitored the
establishment of the required system isolation including the establishment of a freeze
seal in accordance with OwMP 3300-018, " Application of Liquid Nitrogen Freeze Seal
to all Piping," Revision SE1; monitored the performance of the valve repair in
accordance with BwMP 3305-024, " Disassembly - Reassembly of ITT Grinnel Ball
Valves," Revision 1; and interviewed both contractor and licensee personnel at the
job site,
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b. Observations and Findinas
- Th', work packrge css:ciat d with tha r: pair of valva 2SX-2102 r; quired tha
establishment of a freeze sealin accordance with BwMP 3300-018. Contractor
personnel were utilized to establish and monitor the freeze seal. The inspectors
observed several problems with the contractor personnel's use of BwMP 3300-018
during both the establishment and maintenance of the freeze seal. Problemc noted
included:
- Contractor personnel did not complete freeze seal status signatures in
BwMP 3300-018 prior to breaching the SX system. These signatures
included obtaining shift supervisory permission to start the freeze, evaluating
the freeze plug to determine integrity draining the isolated portion of the
piping to ensure the sealis holding, and acknowledgment of established
contingence plans for loss of the freeze seal.
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- Contractor personnel did not log 10 minute freeze seal temperature readings
in Attachment 2 of BwMP 3300-018 as required.
- BwMP 3300-018 requires oxygen readings to be taken at the work site once
the freeze is started. Subsequent to initial oxygen readings taken by licensee
plant Radiation Protection (RP) personnel, contractor personnel did not
coritinue take periodic oxygen readings as required.
The inspectors also observed the actions taken by contractor personnel when they
encountered problems with the establishment of the freeze seal. Contractor
personnel did not contact the operation's field supervisor as was discussed in the
heightened level of awareness discussion held prior to the start of the job.
The inspectors immediately discussed the above problems with the operation's field
supervisor who took action to ensure contractor personnel followed the procedure.
The inspectors monitored the repair of SX valve 2SX-2102 which was also
performed by contractor personnel in accordance with BwMP 3305-024. New
material was properly identified; the correct lubricant was used; during valve
reassembly, foreign material exclusion protection was provided for the open valve
body when not being worked on; radiation protection personnel took surveys to
determine potential removable radiological contamination (none was found); and
when a " Quality Control hold point" was reached in the maintenance procedure,
quality control personnel were contacted and present as required.
Subsequent to the above valve repair, the inspectors observed the establishment of
two additional freeze seals by both contractor and licensee personnel. None of the
problems with the uso of BwMP 3300-018, noted above, were observed.
Discussions held between the licensee and contractor supervisors conceming
following licensee procedures appear to have been effective.
The failure of contractor personnel to follow BwMP 3300-018 was an example of a
violation of TS 6.8.1.a (50-457/97016-02(DRP)).
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c. Conclusions
- Th] inspectors concluded that contr:ctor personn:l d:monstrat;d poor human
performance on October 28,1997, by failing to toilow the procedure to establish a
freeze seal prior to maintenance. The inspectors observed two subsequent
meintenance activities that required freeze seals, conducted by both licensee and
contractor personnel, which revealed none of the previously noted problems. A
violation was issued.
M1.2 Various Maintenance Activities Performed on Chemical and Volume Control (CV)
System Valves 2CV-093A and 2CV-8121
a. Irmoection Scoce (61726)
On October 28, the inspectors observed various maintenance activities on CV
system check valve 2CV-093A and relief valve 2CV-8121. The inspectors reviewed
the associated work packages; monitored the modification of 2CV-093A; monitored a
set point lift test of 2CV-8121 in accordance with BWMP 3305-028,
" Bench Testing / Setting of Safety / Relief Valves Used in Liquid Applications", Revision
6; monitored the removal of the defective 2CV-8121 from the CV system and
interviewed licensee personnel at thJ various job sites.
b. Observations and Findinas
The work package for valve 2CV-093A required the removal of an intemal spring
used to hold the valve clapper closed, inspectors monitored the cutting of the body-
to-bonnet seal weld, removal of the internal spring, performance of a contact surface
dye check of the seat, and re-welding of the body-to-bonnet joint. Once the. valve
was opened and the spring was removed, the mechanic noted an additional piece
with:n the valve, a spring seat, which appeared to also need to be removed but was
not addressed in the work package. This was reported to eng'aeering
, personnel
who performed a review and modified the work package to address the removal of
the spring seat. The inspectors verified that al1 materials used, including weld wire
a .d lubricant material was as specified in the work package. No problems were
noted.
Inspectors monitored the performance of the set-point test of relief valve 2CV-8121.
While en route to the auxiliary building, the inspectors noted that the cart used to
transport the valve and an associated calibrated test gauge tipped over and the relief
valve and test gauge fell to the floor. The mechanics picked up the equipment and
continued on to the hot room, they did not report h6ing dropped the valve and
gauge to their supervisor. Prior to testing, the inspectors looked over tne relief valve
i and test gauge. Although the valve appeared undamaged, the test gauge had its
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outer plastic casing broken. While the inspectors looked the gauge over, one of the
mechanics stated "the gauge was just calibrated four days ago; it should be okay."
The mechanics continued on with the lift set-point testing. The inspectors reported
these observations to the mechanics supervisor and discussed the potential for
having invalidated the calibration of the test gauge by dropping it. The supervisor
stated that a " post-calibration" check of the gauge would be required to be performed
prior to the valve being installed in the CV system. The inspectors reviewed the
completed work package. The valve passed the set-point test and the test gauge
passed the post-calibration check.
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Tha inspectors discussid the dropping of tha cquipmint with a s2nior m: Int;n:nce
m:nig2r, including ths fact that tha m;chanics did not qu3stion ths validity of tha l
' calibration of ths 12st gauga aftsr having dropped it on the floor. The maintsnance
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manager agreed with the inspectors concems and subsequently discussed his
expectations with the mechanics and the mechanics supervisor,
c. Conclusions
The inspectors concluded that the maintenance on valve 2CV093A was performed
well by the maintenance crew. The inspectors observed that during the maintenance
work performed on 2CV-093A the maintenance crew followed the procedure, noted
that the work would exceed the scope of the work package, had the package
changed, and used the proper materials for the job. However, the inspectors
observed a lack of concern on the validity of the test gauge calibration demonstrated
by mechanics after having dropped 2V-8121 and an associated test gauge on the
floor.
M2 Maintenance and Material Condition of Facilities and Equipment
M2.1 Failure to Follow Scaffold Procedure Results in Numerous Scaffold Deficiencies and
a TS Violation
a. Inspection Scope (62707)
The inspectors monitored the status of scaffolding erected in safety-related areas of
the plant. The inspectors interviewed site engineering, operations, and maintenance
personnel. The inspectors reviewed procedure BwMP 3300-025, " Erection,
,
inspection, use, and Dismantling of Scaffolding, Ladders and Temporary Barriers,"
Revision 3 and LER 50-457/97001 00. The inspectors also reviewed quality and
safety assessment field monitoring reports for July, August, and September 1997,
and the "Draidwood Integrated Performance Assessment Report - Third Quarter
1997,* dated October 24.
b. Observations and Findinas
Procedure BwMP 3300-025A2 lists requirements for scaffolding placed in safety-
related areas of the plant. This procedure requires that scaffolds in safety-related
structures (i.e., containment, auxiliary building, fuel handling building) be constructed
to catisfy seismic requirements. Completion of form BwAP 3300-025A1 documents
the engineering review for seismic scaffolding.
,
Step E.13 of BwMP ?300-025A2 requires that all scaffolds erected in seismic areas
have a Scaffold Request Form (BwMP 3300-025A1) posted on the scaffold prict to
placing the scaffold in use. Additionally, Step F.7 of BwMP 3300-025A2 requires all
seismic scaffolds to be logged in the scaffold tracking program. The inspectors
~ found several scaffolds in seismic areas of the plant, and close to safety-related
t
components, which did not satisfy the requirements of procedure BwMP 3300-
l 025A2. These scaffolds included:
!
-
A scaffold was erected at auxiliary building elevation 364 at curved wall area
coordinates R-24 next to the Unit 2 containment spray additive tank
l
(2CS01T). Licensee personnel noted on August 8,1997, that this scaffold did
13
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n:t h:va the required BwMP 3300-025A1 f:rm cnd was not logged in th>
, ,
scaff:Id tracking progr:m. This was document:d on action requ:st tag
302006. On August 25,1997, th] inspectors n:t:d th] missing paperwork
and determined that no corrective actions were performed to address action
request tag 302006 in the 17 days since the action request tag was
generated.
-
On August 28,1997, the inspectors found three scaffolds erected in the
1A/C diesel oil storage tank room over the 1A diesel oil storage tank transfer
pump and next to the riiesel oil storage tanks. None of the scaffolds had the
required BwMP 3300-025A1 form and the scaffolds were not logged into the
tracking program. Initial investigation by the licensee indicated that the
scaffolds had been in place since March 1997.
-
On September 8,1997, the inspectors found that a scaffold was erected in
Unit 2 main steam pipe tunnel at elevation 367, column P-28. The scaffold
did not have the required liwMP 3300-025A1 form and was not logged into
the. tracking program.
On Septamber 16, the inspectors found a scaffold erected in the auxiliary
building at elev.ation 401, column S-24 and over the 28 containment chiller.
The scaffold did not have the required BwMP 330n-025A1 form attached.
During the period, the licensee also identified 17 additional scaffold-related problems.
One of the licensee identified p oblems resulted in LER 50-457/97001-00.
The LER also stated that on September 17, scaffolding appeared to be blocking the
travel of extraction steam non-return check valve 2ES0178 and the action statement
for TS 3.3.4 was entered until the scaffold was removed. The LER stated that the
scaffolding had been constructed long enough such that the 6 hour6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> limiting condition
for operation for TS 3.3.4 was exceeded. The licensee stated in the LER that one of
the causes for this problem was failure of operations supervisors to follow procedure
BwMP 3300-025A1. Step 1.c.1 of the procedure required the shift
manager / designee to review the scaffold for impact on plant operations and
equipment and to note any concerns or special instructions The LER stated that
discussions with operations supervisors revealed that it was not normal practice to
perform a physical inspection of the scaffold erection area if the supervisor was
familiar with the area.
The LER stated that the noperability of the extraction steam non-retum check valve
.
had no safety significance because no credit is taken for operability of these valves
in any safety analysis. The inspectors reviewed the Updated Final Safety Analysis
Report (UFSAR) Chapters 10 and 15. The inepectors agreed that the Chapter 15
safety analyses did not take crodit for operation of the extraction steam non-retum
check valves and Chapter 10, Section 10.2.2.5 specifically stated that the failure of
the extraction steam valves does not affect the safe shutdown capability of the plant.
This was a le'ss significant failure to comply with an actbn statement for a technical
specification limiting condition for operation where the appropriate action was not
taken within the time allowed
The licensee performed a separate root cause analysis (457-230-97-CAQS00001)
for the scaffolding deficiencies not discussed in LER 50-457/97001-00. The only
additional corrective action not already addressed in the LER was that the site
scaffold coordinator would develop a consistent process to track scaffolding to
l 14
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- -- . _- _ -. -- _ _ - . . _. . _ - . _ -. _- -
r2moval. This corr:ctiva action was due Ftbruary 18,1998.
,_
, Tha inspectors r:vi;wed qurlity and safsty cssissm:nt fi;ld monitoririg raports for
July, August, cnd Sgpt2mber 1997, and tha *Braidwood inttgratrd Pmform:nce
Assessment Report Third Quarter 1997," dated October 24. Quality and safety
assessment field monitoring reports indicated that licensee inspectors made several
observations of scaffold construction in the field. Deficiencies identified were
characterized as minor. The third quarter assessment did not indicate that there was
a problem with scaffold construction.
.
The inspectors reviewed the Maintenance department, "Self-Assessment Summary,"
for the Third Quarter of 1997. This assessment did identify the construction of
scaffolding as a problem area end that training sessio' Md continue to be held to
focus attention on the impact of the piant operations stason of the scaffold
procedure. However, the assessment did not say who would be trained or by when.
The failure to follow the scaffold construction procedure BwMP 3300-025, " Erection,
inspection, Use, and Dismantling of Scaffolding, Ladders and Temporary Barriers,"
4 Revision 3, was a violation of 10 CFR Part 50, Appendix B, Criterion V
(50-456/97016-03(DRP); 50-457/97016-03(DRP)).
c. Conclusion
The inspectors concluded that the construction, inspection, and tracking of
'
scaffolding was poor during the months of August and September 1997. The
inspectors and the licensee identified numerous examples (about 20) of the failure to
follow procedural requirements by maintenance personnel and operations
department supervisors regarding construction, inspection, and tracking of
scaffolding in areas affecting the operation of both units between August 24 and
September 17. The inspectors also concluded that the maintenance department
self assessment identified construction of scaffolding as an area that needed
improvement, but that future corrective actions were not made clear in the report. A
Notice of Violation was issued.
M4.1 Surveillance Test Performance Observations
a. Inspection Scope (61726)
,
The inspectors attended Heightened Level of Awareness (HLA) briefings and
observed the performance of all or a portion of the following surveillance tests:
-
18wOS 7.1.2.1.a.1-2, " Unit One Diesel Driven Auxiliary Feedwater Pump
Monthly Surveillance," Revision 4;
18wVS 0.5-3.AF.1-2, " Unit One Diesel Driven Auxiliary Feedwater Pump
American Society of Mechanical Engineers Quarterly Surveillance," Revision
5;
2BwVS _8.1.1.2.f-21, " Unit 2 2A Diesel Generator 24 Hour Endurance Run
And Hot Restart Test 18 IAonth," Revision 2;
-
2BwVS 800-14," Unit 2 Full Flow Testing And Equipment Response Time Of
Auxiliary Feedwater Pumps," Revision 1;
15
- -
_ __ . -_. . -- - , . -. -. - . - - . _ . -
2BwVS 0.5-2.SI.2, 'Saf1ty injection Systtro Chick Valva Stroks Tost,'
, ,
R : vision 16E2; and
-
BwHS 4009-058, "Uriit 2A Diesel Generator Room And Day Tank Room Low
Pressure Carbon Dioxide Actuation Surveillance," Revision 5.
b. Observations and Findinas
The inspectors observed pre-job or HLA briefings for each of the sunteillances listed
4
above. The inspectors found that the briefings exceeded the requirements of
BwAP 100-12, " Human Performance Awareness." Briefingt, stressed the sequence
of tasks for the activity to be pc, formed, direction of the activity, potential problems,
and contingency plans in the event that a problem arises.
The iesctors observed and verified that all surveillance tests were performed in
accordance with their applicable orocedures, that proper communications between
the control room and personnel in the field occurred, and that all instruments were in
calibration inspectors verified that equ!pment operation and performance
parameters met acceptance criteria or that the test directors took the proper actions
when the acceptance criteria was not met. For example, during the performance of
SwHS 4009-058, a predischarge timer, a discharge timer, and a fire damper failed to
meet their acceptance criteria. The test director immediately informed the shift
engineer as required by procedure. The inspectcrs also observed the lest director
for 2EswVS 8.1.1.23-21 take the proper actions when the 2A diesel generator failed to
reach a stable voltage in the required time during the hot restart test of the 2A diesel
generator.
The inspectors reviewed applicable TSs and applicable sections of the UFSAR and
found that the surveillance tests ensured TS and UFSAR requirements were met.
c. Conclusions
The inspectors concluded that the six surveillance tests observed during this period
were performed in accordance with procedures and all acceptance criteria were met
or the proper actions were taken by the test directors when the acceptance criteria
were not met. HLA and pre-job briefings were thorough and exceeded minimum
briefing requirements. The surveillance test procedures were well written and
ensured TS and UFSAR requirements were tested.
M8 Miscellaneous Maintenance issues
M8.1 Unattended Rollina Carts in Safetv-Related Areas
a. Inspection Scoce (62707)
NRC violation 50-456/96021-01f; 50-457/96021-01f was issued to document a
violation of station procedures and policies used for controlling unattended rolling
carts and equipment in safety-related areas. As a response to the violation, the
licensee performed corrective actions, including a revision to Braidwood Policy
Memo #65, removing rolling carts from the auxiliary building, painting carts remaining
in the auxiliary building, and attaching brakes or anchoring devices to carts
remaining in the auxiliary building. The inspectors performed routine inspections of
L 16
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_. _ _ _ _ . _ _ --
_ _ . _ - _ _ . . _._ _._ _. _ _ _ __ __ _ _
plant ara:s to vsrify complianco with requirem3nts for rolling certs cnd to dst 2rmina
if corrcctiva cetions w2re sffsetive. The inspectors revi;wed BwAP 100-10,
'
' Conduct of Station Psrsonnsi," Rcvision 3 and
, BwAP 1100-18, " Station Housekeeping / Material
Condition Program," Revision 6.
b. Observations and Findjngt
BwAP 10010, steps c.4.d and c.4.e list the requirements for securing moveable '
-
carts ano equipment. During the period, the inspectors found several instances
c where carts and equipment were not secured in accordance with BwAP 100-10.
- Some examples of unsecured or improperly secured carts and equipment found
close to safety-related components or systems included:
- Auxiliary building elevation 426, column S-18, on September 15,1997,a
large gang oox on wheels was found tied to conduit for the junction box for
'
1RT-AR012, " Fuel Handling Building Incident Monitor." Additionally, the cart
was not adequately restrained to prevent contact with the junction box for
1RT-AR014, " Containment and Containment and Auxiliary Building Radiation
Monitor."
3
. ESF switchgear room division 21, elevation 426, column L-27, on
September 22,1997, a cart with electrical maintenance department tools and
instrumentation was found within 1 foot of ESF Bus 241, Cubicle 21, "SX
i Pump 2A." The rolling cart was not secured and was unattended.
Auxiliary building elevation 330, column M-16, on September 29, a rolling cart
'
with a large quantity of flanges, pipes and tools was found approximately 4
feet from the 2A essential service water pump motor. The cart was not
secured and the area was unattended.
.
- Auxiliary building elevation 401, column V.9-19, on October 14, a rolling cart
was found tied to the instrument rack for 2F1-SX094, " Containment Spray
(CS) Pump 2B Cubicle Cooler SX Outlet Flow"
- Auxiliary building elevation 346, column V.9-19, on October 20, a rolling cart
with instruments and tools was found tied to residual heat removal (dH)
ir.strument panel. The cart was not adequately restrained to prevent contact
with 2FIS-0611, "RH Pump 28 Miniflow Line Flow Control," and 2FIS-CS-14,
"CS Eductor 2B Suction Flow."
- - Auxiliary building elevation 426, column Q 28, on October 21 a rolling cart
was found tied to 2JB1808A, " Source Range N32 Preamplifier."
- Auxiliary building elevation 364, column P-18, on October 22 a large canister
vacuum c!eaner was found unsecured and within two feet of
Motor Control ': enter 132X1.
The inspectors also found 10 additional examples of unsecured or improperly
secured carts in the auxiliary and fuel handling buildings that were within the scope
of procedure BwAP 100-10 but were not in close proximity to safety-related
components or systems.
17
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- -.
_ _. ___ _ _ _ _ _ _ _ __ _ _ . _ _ _
Tha inspectors report:d the unsecur:d c:rts to operations or maint: nance personn:l l
.
, s,J tha carts w:ro discov:r:d. Tha carts were s: cur:d or r:mov:d by licenso I
personntl in ord:r to comply with proc dure r:quirements.
! The inspectors interviewed numerous plant personnel to determine geners'
knowledge of requirements regarding rolling carts. Parsonne' were generally aware
of a requirement to restrain rolling equipment. However, the number of carts found
secured to safety related equipment indicates that personnel may not fully
understand why carts ata restrained.
Corrective actions implemented by the licensee for NRC violation
50-456/9602101f(DRP); 50 457/95021-01f(DRP) have not been effective in
prevt. ting recurrence of rolling cart deficiencies. Failure to implement effective
- corrective actions to preclude repetition is a violation of 10 CFR 50, Appendix B,
Criterion XVI, (50 456/97016-04(DRP); 50-457/97016 04(DRP)).
c. Conclusions
The inspectors identif;ed 17 examples where 'he licensee faued to take effective i
corrective actions for the securing of movable carts in the auxiliary building. A
I
violation was previously issued for the licensee's failure to control movable carts and
equipment in NRC Inspetton Report No. 50 456/96021(DRP); 50-457/96021(DRP). ;
t'
M8.2 (Closed) LER 50-457/970014Q Two Extraction Steam Non Return Check Valve
Made Inoperable By Installed Scaffolding As A Result Of Knowledge Detelencies,
Improper Assumptions and Not Adhering To Procedures. Tne details of this LER are ;
discussed in Section M2.1 of this report. The inspectors reviewed the report and l
'
had no additional concema. A violation was issued in this report (50-456/97016
03(DRP); 50-457/97016 03(DRP)) for the failure to follow procedures. The corrective
actions for this event will be tracked through the violation mentioned above. This
item is closed.
Ill. Enoineerina
E2 Engineering Support of Facilities and Equipment
E2.1 Temocrary Plant Alteration Proaram Revkg
a. Inspection Scone (92903)
The inspectors reviewed listings of existing temporary alterations, conducted in plant
inspections for unauthorized temporary plant alterations, and reviewed the following
documents: Braidwood Temporary Pla1t Alterations Log; BwAP 2321,' Temporary
Alterations," Revision 3E1; BwAP 232118T11, ' Determination of Temporary
Alterations," Revision 3E1; and OVL 20 97 065 *Braidwood Station Quality & Safety
Assessment, Braidwood integrated Performance Report - Third Quarter 1997.*
.
18
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. _ _ _ _ _ _ _ . - . _ . _ _ _ _ _ _ _ _ _ _ __ _ ___ _
b. Observations and Findinal
- Tha inspectors revi:w ^1 the Braidwood Tcmporary Alt:rctions Log and found that
the log was maintained as required by procedure BwAP 2321," Temporary
Alteration? The inspectors ah,o found agreement with the number of tempurary plant
alterations and the number reported in the Braidwood integrated Performance Report
, - Third Quarter 1997.* On several occasions during the inspection period, inspectors
performed in-plant observations for the purpose of identi/ ing unauthorized
temporary plant alterations and none were found.
The inspectors reviewed the monthly activity in the temporary alteration program and
the program's goals for the last 6 months, inspectors observed peak activity during
refueling outages. Non-outage periods were characterized by the opening and
closing of only a few temporary plant alterations.
c. fandosions
inspectors concluded that the licensee has ma'.ntained the temporary alteration
program in accordance with the procedure, has accurately tracked the opening and
closing of temporary plant alterations, has accurately reported program activity, and
has monitored program activity against established workdown goals.
E3 Engineering Procedures and Documentation
E3.1 Onorability Evaluation For 125 Volt Direct Current BJtterv Charag[g
a. [nipfctior Scope (37551)
The inspectors reviewed operability evaluation 97 015, dated February 18,1997,and
interviewed the system engineer and members of engineerin9 management.
b. Observations and Findinal
The inspectors questioned statements in the operability evaluation that said the 125
volt direct current battery chargers could not meet the requirements of design basis
documents (IEEE S.d. 308 1974 and Regulatory Guide 1.32) but remained operable.
The design basis stated that the sizing of the battery charger must be able to supply
steady stato direct current loads and recharge the battery at the same time under all
plant conditions. The inspectors questioned why, if the battery chargers could not
meet design basis requirements they were still considered operable, and after 8
months, a 10 CFR 50.59 safety evaluation had not been performed. The inspectors
also questioned who this condition had not been reported under 10 CFR 50.72 or
The licensee reviewed operability evaluation 97-015 and determined tb .t the system
engineer used design basis battery loads and did not take into account that the
direct current inverter would supply some of the direct current loads if the alternating
current power sJpply was reestablished. The reevaluation determined that the sizing
of the battery charger did meet the design basis requirements. The inspectors
reviewed the now operability determination and had no further concerns.
Licensee management had no response to the questions as to why the evaluation
19
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_- . _ _ _ _ _. _ _ - -
had gon] so long without a 10 CFR 50.59 cvaluation or why the problem h:d not
, be:r. r: port:d und:r 10 CFR 50.72 or 10 CFR 50.73.
c. Qpnclusion
The inspectors concluded that the original revision of operability evaluation 97-015
for the 125 voit direct current battery chargers was conducted poorly. After the
inspectors questioned the operability determination, the licensee reevaluated tha
operability evaluation and determined that the sizing of the battery charger did meet
the design basis requirements. The inspectors concluded that the preparation and
supeNisory review of the original operability evaluation 97-015 was poor, and that
the system engineer demonstrated a lack of knowledge of the design basis
requirements of the 125 volt direct current battery chargers.
E4 Engineering Staff Knowledge and Performance
E4.1 Unit 2 Diaital Electro-Hydraulic Controller (DEHC) Runback Pronram Confiauration
!moroDerIV Chanced
a. Inspection Scope (37551)
The inspectors independently inspected the circumstances surrounding a runback of
the Unit 2 main turbine beyond the expected setpoint of 700 megawatts electric
during a loss of a feedwater pump. The inspectors reviewed the followir.g
documentation: PIF #A1997-03581; Apparent Cause Evaluation #A1997-03581; and
BwAP 50011, * Plant Computer Configuration Control," Revision 3E1. The
inspectors discussed the event with the operatioas manager and the systems
engineering supervisor,
b. Observations and Findinas
On August 26,1997, the 2B feedwater pump speed controller failed resulting in a
loss of flow from the 2B feedwater pump (Inspection Report No. 97015, Section
01.2). In response to the event, operators initiated a main turbine runback.
Operators observed that the turbine ran back further than expected. The operators
expected and had been trained that the turbine runback would terminate at 700
megawatts, bt* observed the turbine load below 700 megawatts. The operators
manually terminated the turbine ran back at 530 megawatts.
The inspectors reviewed the licensee performed investigation and agreed with the
,
licensee's findings. The runback termination set point had been changed to
500 megawetts by station operations analysis department (SOAD) in response to a
request t,y the system engineer. The system engineer requested the reduction in
the setpoint to address feedwater pump cavitation concems observed following a
previous feedwater pump trip. The licensee determinea that the turbine runback
setpoint change was performed following the installation of the runback push button
modification that was performed on both units in 1990. Procedure BwAP 50011,
' Plant Computer Configuration Control," provides instructions for the documentation
and control changes to various statinn computer systems including the DEHC
system. The setpoint change to the DEHC system and necessary approva's should
have been documented on request form BwAP 50011T1. The licensee conducted a
review of completed BwAP 50011T1 request famis for 1990 and 1991 and did not
20
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find a complet;d BwAP 50011T1 form for th]'urbine runback s:tpoint change. Th]
, licensco att:rrpt:d to r;vi;w B;!AP 50011T1 forms from 1992, through 1995, but
could not find the forms and conclud:d that they had cith:r be:n lost or misplaced.
The licensee concluded that it was highly unlikely that a request form was used to
perform the turbine runback setpoint change.
The licensee identified a failure to follow procedure BwAP 50011, a lack of
awareness of BwAP 50011 and its requirements by personnelinvolved in the
, change process, and a failure to specify and perform the appropriate departmental
reviews as deficiencies that caused or contributed to the event. In response to the
identified deficiencies, the licensee identificd the following corrective actions:
- engineering planned to reevaluate the runback termination setpoint under
ER 9702313;
e site angineering planned to review and revise as necessary BwAP 50011 to
ensure adequate controls are in place, including appropriate departmental
reviews and 10 CFR 50.59 screenings for applicable changes;
- BwOP EH 11, ' Displaying / Changing Digital Electro Hydraulic Controi .1 ware
Parameters / will be changed to include a completed BwAP 50011 review as
a prerequisite for any CEHC change;
e engineering, with assistance from SOAD and nuclear information services
(NIS), planned to evaluate the processes currently used to document and
wtrol computer software to ensure adequate controir, are in place for
software that affects the design of the plant (this evaluation will ensure
simulator fidelity and will include verification that adequate documentetion
curruntly exists for required software products); and
- training requirements for configuration change procedures will be identified for
operations, engineering, SOAD, and NIS.
The failure to perform the required actions of procedure BwAP 50011 was an
example of a violation of TS 6.8.1.a which requires that written procedures be
adhered to. This non repetitive, licensee identified and corrected violation is being
treated as a Non Cited Violation, consistent with Section Vll.B.1 of the NRC
Enforcement Policy (50-456/97016-05(DRP); 50-457/97016-05(DRP)).
c. Conclusions
The inspectors concluded that the licensee failed to perform a modification to the
main turbine control software in accordance with station procedures. The licensee
had modified the runback termination setpoint for both units in 1990, had not
changed the simulator, and had not trained nperators on the change. The inspectors
concluded that the licensee conducted an accurate and thorough apparent cause
evaluation of the undocumented change of15,3 turbine runback termination setpoint.
The inspectors concluded that the licensee's proposed corrective actions appeared
adequate to address the causes and contributing factors of the event and should
prevent recurrence. This failure to perform a modification to the main turbine control
software in accordance with station procedures was a licensee identified
non-cited violation.
21
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. ,
IV. Plant Support
R3 RP8C Procedures and Documentation
R3.1 Protective Clothina Reovirements Were Not ,,iad?,Qlear
a. [nspection Scope (71750)
On October 27, the inspectors made a routine tour of the Unit 2 containment to
monitor refueling outage activities. The inspectors observed the removal of
scaffolding from inside the missile barrier. The inspectors interviewed radiation
protection technicians and radiation protection management personnel. The
inspectors also reviewed, Radiation Work Permit 976115, * Radiation Protection
Policy Memo CCP5,* on the use of skull caps as anti-contamination clothing as an
alternative to a cloth hood, DwRP 5270 5, * Protective Clothing," Revision 1; and
DwRP 6200 5, " Writing Radiation Work Permits," Revision 5.
b. Obsgrvations and Findinag
On October 27, the inspectors observed that some personnel removing scaffolding
from inside of the containment had long hair that was not contained inside their skull
cap and in some cases was hanging dow.. to their shoulders or onto their back. The
inspectore found that * Radiation Protection Policy Memo CCP-05,* stated that, *at no
time will the use of a ' skull cap' be allowed if the hair of the head is not appropriately
protected from the potential of contamination from radioactive material." The
inspectors could not find this restriction in the procedure that governed the use of
protective clothing (BwRP 5270 5) or in Radiation Work Permit 976115 for scaffold
removal from the containment.
Radiation protection department management stated that the policy memo on the
use of skull caps would be eliminated and that in the future any restrictions on the
use of skull caps would be placed in the radiation work permit. Management
personnel then stated that the station may go to a policy of only wearing hard hats in
contaminated areas.
c. Conclusion
The inspectors concluded that licensee management did not clearly communicate
restrictions on use of skull caps as protective clothing to workers. The licensee had
a policy memorandum restricting the use of skull caps as protective clothing if hair
could not be protected from contamination. However, this policy memorandum
restriction on the t,se of skull caps was not in the procedure that govemed protective
clothing nor was it in the radiation work permit.
22
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<
R4 Staff Knowledg3 cnd P:rf;rmanco in RP&C
' ~
R4.1 Radiotoaical Postinas
a. Inspection Scooft (71750)
t
The inspectors routinely intpected the status and posting of radiologically controlled
areas e.g., radiologically posted areas. The inspectors reviewed licensee
,
procedures BwRP 5010, * Radiological Posting and Labeling Requirements", Revision
7 and BwRP 5310 2, "Contr)! of Access to High Radiation Areas and Very High
Radiation Areas *, Revision 4. The inspectors also reviewed Licensee identified
radiological problems documented in PIFs A1997 03864, A1997-03989, A1997
03993, A1997-04038, A1997 04064, A1997 04458, A1997-04459, A1997-04518, and
A1997-04530.
b. Observations and Findinas
During an inspection in the auxiliary building on September 26, the inspectors noted
a posted radiation area adjacent to the door to the Unit 1 containment spray pump i
'
room on elevation 346 (" cubby hole" to the right of the door with several pipes
running through it). Review of posted radiation surveys indicated no ,. milar posting
adjacent to the donr to the Unit 2 containment spray pump room although a similar
" cubby hole" area exists. This was discussed with radiation protection personnel
who then performed radiation surveys within the " cubby hole" area and discovered
radiation levels to be 12 millirem per hour (mr/hr) at 30 centimeters from the source.
l
This exceeds both the licent,ees and the 10 CFR 20 limit for posting an area as a
radiation area which is 5 mr/hr at 30 centimeters from the source. The area was
immediately posted as a radiation area. The failure to recognize and post this
, radiation area is a violation of BwRP 5010-1, * Radiological Post ngt and Labeling
Requirements," and is an example of a violation (50-457/97016-06 (DRP) of TS 6.11
which requires procedures for personnel radiation protection to be adhered to.
During an inspection in the Unit 1 curved wall area at elevation 364 on September
24, the inspectors noted a contamination area posting that wea inconsistent with
other similar postings. Specifically, at either end of the curved wall areas there are
large diameter pipes that must be crawled under to access the safety injection and
centrifugal charging pump rooms. Contamination area signs and rope barriers
typically run under these pipes parallel to the walkway and clearly identify the area
beneath the pipes that is considered a contamination area. The posting in question
hsJ the boundary rope running over the top of the pipe such that when crawling
beneath it, the contamination area boundary could not be determined. This poor
radiological posting practice was discussed with radiation protection personnel who
reposted the pipe.
During a tour of the fuel handling building on September 26, uie inspectors
discovered a swing gate used to control access to a posted radiation area had been
> moved without proper authority. The inspector notified radiatbn protection personnel
of the moved swing gate. RP personnel responded to the area and placed the swing
gate h the correct position. At the request of the inspector, the RP technician also
.
'
performed a survey of the area. Dose rates in the area at the time of the survey
were from 0.1 mr/hr to
23
. _ .
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r=W*wW5"M-**v-""-
_ _ __ . _ __ _ _ ._ -. _. __ . _ _ __ _ _ __ _
0.3 mr/hr which are below the lev:1 f:r which 10 CFR 20 requires radicti:n crea _f
, , postings. The licensee could not det:rmine h:w cr why the g:11 w:s moved. .
The licensee documen'ed on PlFs six additional problems with radiological postings
between September 17 and October 19,1997. Corrective action had been initiated ;
on allidentified problems. The majority of the documes.ted problems appear to have ;
been the result of contractor personnel nonoompliance with licensee procedures. An
insufficient amount of time has passed to dete,mine how effective the licensee's
acticas were in preventing recurrence,
c. Conclusions
<
The inspectors concluded that between September 26 and October 15, there was an :
unusually high number of improper radiological postings. A large portion of these i
appeared to have been caused by contractor personnel failing to comply with ;
licensee procedures.
F1 Control of Mrs Protectirin Activities
F1,1 Combustible Materials in Safety Related Structureg
,
s. Inspection Scope (71707)
NRC violation 50 456/97007 03c; 50-457/97007-03c was issued to document a
violation of station procedures used for controlling unattended combustible materials
in safety-related areas, in iesponse to the violation, the licensee implemented
corrective actions, including publishing articles in the daily station newsletter, making
presentatione to first line supervisors to heighten awareness of fire protection issues,
and committing to routinely monitor the plant during outage periods.
The inspectors performed routine inspections of plant areas to verify compliance with
requirements for unattended combustible materials and to determine if corrective
actions were effective. The inspectors reviewed procedures BwAP 550-15,
"Braldwood Station Chemical Control Program," Revision 8; BwAP 110010, " Control
and Use of Flammable and Combustible Liquids and Aerosols," Revision 1; BwAP
,
110011. " Fire Prevention for Use of Lumber and Other Combustibles," Revision 7;
and BwAP 110018," Station Housekeeping / Material Condition Program," Revision 6.
The inspectors also interviewed fire protection, system engineering, site engineering
and operations personnel.
b. Observations and Findinas
Step F.5 of procedure BwAP 110010 states that " flammable and combustible
materials shall not be stored in, near or adjaceret to safety related buildings or
systems without approval of the fire marshall." Step F.4 of procedure BwAP 1100-10-
states that certain liquids such as paints, epoxy, and adhesives may be used
provided they are not left unattended in safety related areas. Additionally, Stop
C.1.m of procedure BwAP 1100-11 and Step F.1 of procedure BwAP 1100 10
require that flamrnble and combustible liquids shall be in approved safety cans at all
times. Discussion with licensee management indicated that the above procedures
applied to all areas of the auxiliary building.
Contrary to the procedure requirements, the inspectors found flammable and
24
.
_
y- 'v g 'P 'r -
y w e- T*---vmvv+er" p e- v- c"* :-
. -
combustible liquids left unatt:nded in the auxill:ry building on sev;ral occasions.
, ,
N:ne cf the it:ms found h:d tr ns':nt fire load tags. Additi:nally, n:ne of the it:ms
found wer] in cpproved saf;ty cans. The it:ms found include:
- Auxiliary building elevation 401, column M 23, on September 16,1997, the
inspectors found a full 1 gallon glass jar (the original container) of kerosene at
the radiation protection desk. The area was unattended.
- Auxiliary building elevation 346, column M 19, on September 29, the
inspectors found two containers labeled " Mineral Spirits - SI Number 857130"
unattended. Mineral Spirits hold a National Fire Proterdion Association
(NFPA) rating of 2, indicating the material is combustible. The two containers
were a i gallon jug and a i quart spray bottle.
- Auxiliary building elevation 401, colunin M 23, on October 1, the inspectors
found a full 1 gallon container (original container) of denatured alcohol at the
radiation protection decon area. The area was unattended.
- Auxiliary building elevation 330, column M 20, on October 14, the inspectors
found a i quart spray bottle labeled "KROIL" The fire label indicated that the
liquid was combustible (NFPA fire ra6ng of 2). The area was unattended.
- Auxiliary building elevation 364, column P 17, on October 14 the inspectors
found three containers contelning flammable and combustible liquids. They
were a i quart spray bottle with no product label but with a fire label stating
the liquid was flammable (NFPA fire rating of 4 maximum fire rating), a i
quart spray bottle of" Grease B Gone" (NFPA rating of 2), and a 1 quart spray
bottle of " mineral spirits" (NFPA rating of 2).
- Auxiliary building elevation 330, column M 23, on October 17, the inspectors
found two containers containing combustible liquids unattended. They were a
1 auart spray bottle labeled *KROIL" (NFPA rating of 2), and a i quart spray
bottle of " Grease B-Gone" (NFPA rating of 2).
- Auxiliary building elevation 364, column P 17, on October 17, toe inspectors
found s 1 quart spray bottle of mineral spirits (NFPA rating of 2) unattended.
- Auxiliary building elevation 346, column S 24, on October 20, the inspectors
found three containers of liquids in the hot machine shop that were
unattended. They were a i quart bottle labeled " Laboratory Cleaner SI
858181", a 1 gallon container of " Grease B-Gone" (NFPA rating of 2), and a 1
gallon container of what appeared to be lubricating oil and was labeled "Si 732786."
The inspectors reported unattended combustibles to plant personnel as the items
were discovered. Plant personnel promptly removed the items. The inspectors
checked for PIFs for the items. No PIFs were generated for the items listed above,
t he inspectors found other problems with the control of combustible materials in
safety-related structures. The licensee placed two high efficiency particulate air
(HEPA) filters in the auxiliary building on elevation 451 at column S 19 on
September 9,1997. These filters were labeled as "VQ Mini-Purge Exhaust HEPA
Filters." Step 2.b of procedure BwAP 1100 11 defines HEPA filters as a major
25
s
- transtnt combustible. Howevsr, no transtnt fire load permit was obtein:d for ths
, , filt:rs, as r:quir:d by St2p 3.a of procedura BwAP 1100 11. Additionan y, th3 filtgrs
remain:d in the auxiliary building for great 3r than fiva w::ks until tha inspe@rs
notified plant personnel of the condition.
On October 16, the inspectors found three 55 gallon drums of waste oilin the
auxiliary building elevation 401 general area (Fire Zone 11.5 0). The three drums
had transient fire load permit tags; however, there were problems with the condition.
Two of the drums were located adjacent to an open hatchway in the floor to another
fire zone at column P.19. Step F.20 of procedure BwAP 110010 prohibits storing
combustibles in the proximity of hatchways.
The licensee had not completed E.n established set of corrective actions for this
problem by the close of the inspection period.
Corrective actions implemented by the licensee for NRC violation
50 456/97007-03c(DRP); 50-457/97007-03c(DRP) have not been effective in
preventing recurrence of unattended ccmbustible deficiencies. Failure to implement
effective corrective actions to preclude repetition is a violation of 10 CFR 50,
Appendix B, Criterion XVI (50 456/97016 07(DRP); 50 457/97016-07(DRP)).
c. Conclusions
The inspectors concluded that licensee management had not effectively
communicated and/or have not enforced the requirements for the control of
combustible material. Corrective action for a previous violation of combustible
material control was ineffective to prevent recurrence. The inspectors identified that
betwon September 16,1997, and October 20,1997, there were at least ten
examples of the failure to adhere to procedures goveming combustible liquid control.
A violation was issued.
V. Management Meetinas
X1 Exit Meeting Summary
The inspectors presented the inspection results to members of licensee management
'
at the conclusion of the inspection on November 3,1997. The licensee
acknowledged the findings presented. The inspectors asked the licensee whether
any materials examined during the inspection should be considered proprietary. No
proprietary information was identified.
26
_ - _. . -- . - _
. _ . -__ _______. _ _. _ _ _ _ _ _ ..
_
PARTIAL LIST OF PERSONS CONTACTED
- *
Licensse
'T. Tulon, Site Vice President
A. Haeger, Health Physics and Chemistry Supervisor
R. Byers, Maintenance Superintendent
- R. Graham, Work Control Superintendent
'T. Simpkin, Regulatory Assurance Superv!sor
'C. Dunn. System Engineering Supervisor
J. Meister,- Engineering Manager
'R. Wegner, Operations Manager
'M. Riegel, Quality Assurance Manager
'M. DiPonzio, Nuclear Licensing
- B. Boyle, Fire Marshal
'M. Pack, Assistant Fire Marshal
'R. Thacker, Lead Health Physics
- D. Radice, Engineering
- J. Stone, Maintenance
- M. Cassidy, Regula'ory Assurance . NRC Coordinator
NEG
R. Lanksbury, Chief, Reactor Projects Branch 3
- C, Phillips, Senior Resident inspector
- J. Adams, Resident inspector
- D. Pelton, Resident inspector
ID.d1
T. Espr,r
- Denotes those who attended the exit interview conducted on November 3,1997.
.
c 27
__
. . . _ _ . _ _ . . _ _ _ _ _ . _ - - _ _ _ _ . _ . _ . . _ _ _ . _ . _ _ . _ _ _ . - _ - . - . _ _ . . . _ _._
INSPECTl0N PROCEDURES USED
IP 37551: Onsita Engineering
IP 61726: Gurveillance Observations ,
if' 62707: Maintenance Observation !
IP 71707: Plant Operations l
- IP 71750: Plant Support Activities
IP 92901: Followup Plant Operations l
!
IP 92903: Followup - Enginaering
ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
'
50-457/97016-01 VIO failure to report ESF actuation
50 457/97016-02 VIO failure to follow procedurs
50-456/97016-03; 50-457/97016-03 VIO failure to follow procedure i
50-456/97016-04; 50-457/97016-04 VIO failure to take corrective actions i
50-456/97016-05; 50-457/97016 05 NCV failure to follow procedure
'
50 457/97016 06 VIO failure to post radiation area '
50-456/97016-07; 50-457/97016-07 - VIO failure to take corrective actions
Closed
50-457/97001-00 LER extraction steam non return check valves
inoperable due to scaffold construction
Discussed
50-456/96021; 50-457/96021-01f failure to control movaole carts and equipment
50-456/97007; 50-457/97007-03c failure to follow procedure for combustible
materials
50-456/97015; 50-457/97015-01 failure to take proper corrective action for
positioning components
Qitcussed Reports
50 4 56/96005; 50-457/96005
50 456/96008; 50-457/96008
-50-456/96009; 50-457/96009
50-456/96012; 50-457/96012
i
28
!
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__ . _ _ _ _ . _ _ .._ _. ___
LIST OF ACRONYC8 USED
'
CFR Code of Fsd:ral R:gul:tions
CV Chemical and Volume Control l
l
DEHC - Digital Electro Hydraulic Controller
ESF Engineered Safety Feature !
HEPA High Efficiency Particulate Air i
I
HLA Heightened Level of Awareness
LCO ~ Limiting Condition for Operation i
LCOAR Limiting Condition for Operation Action Requirements '
LER Licensee Event Report
mR/Hr Millirem per hour i
NFPA National Fire Protection Association
NIS Nuclear Information System i
NRC Nuclear Regulatory Cornmission
OOS Oui .Sf Service -
PlF Problem Identification Form :
RP Radiation Protection ,
RP&C Radiological Protection & Chemistry ' '
SOAD Station Operations Analysis Department
SX Essentia' Service Water
TS Technical Specification
'
UFSAR - Updated Final Safety Analysis Report
VIO Violation j
,
I
%
i
'
29
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