ML20236N094

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Insp Repts 50-456/98-08 & 50-457/98-08 on 980421-0608. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20236N094
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 07/06/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20236N089 List:
References
50-456-98-08, 50-456-98-8, 50-457-98-08, 50-457-98-8, NUDOCS 9807150005
Download: ML20236N094 (17)


See also: IR 05000456/1998008

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U.S. NUCLEAR REGULATORY COMMISSION

REGIONlli

Docket Nos: 50-456,50-457

License Nos: NPF-72, NPF-77

Report No: 50-456/98008(DRP); 50-457/98008(DRP)

Licensee: Commonwealth Edison Company

Facility: Braidwood Nuclear Plant, Units 1 and 2

Location: RR #1, Box 84

Braceville,IL 60407 j

Dates: April 21 through June 8,1998

Inspectors: C. Phillips, Senior Resident inspector

J. Adams, Resident inspector

D. Pelton, Resident inspector

- Z. Falevits, Lead Engineer

T. Esper, Illinois Department of Nuclear Safety

Approved by: M. Jordan, Chief

Reactor Projects Branch 3

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EXECUTIVE SUMMARY l

Braidwood Nuclear Plant, Units 1 & 2

NRC Inspection Repod 50-456/98008(DRP); 50-457/98008(DRP)

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This inspection included aspects of licensee operations, maintenance, engineering, and plant

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suppod. The report covers a 7-week period of resident inspection from April 21 through

June 8,1998.

Operations

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The inspectors concluded that the Unit 2 operators monitored pressurizer pressure poorly J

after securing backup heaters and did not re-energize the heaters in time to prevent

pressurizer pressure from going below the lower Technical Specification limit. The

operators secured the heaters to reduce the station electrical load to support electrical

grid needs during unseasonably hot weather. (Section O1.1)

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The inspectors were concemed about the frequency of mispositioned equipment events. '

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Six valves were mispositioned in the month of May. All of the valves were

non-safety-related and none of the mispositioning events resulted in a plant transient.

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The inspectors agreed with the licensee's conclusion that the number of equipment

mispositioning events that involved or affected safety-related equipment or that were

considered significant, declined from a year ago. However, the inspectors observed that

the number of equipment mispositioning events were increasing in 1998 which is

noteworthy and warrants consideration. (Section 01.2)

Maintenance

- The inspectors concluded that the replacement of the Unit 2 rod control negative 24 volt J

direct current power supplies in the shutdown Control Rod Banks B, C, and E cabinet was

planned and executed well. The instrument maintenance technicians demonstrated a

high level of proficiency as a result of excellent pre-job training and the careful validation

of the maintenance procedure. (Section M1.1)

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The inspectors concluded that the results obtained during four surveillance tests

observed during the inspection period met acceptance criteria. The inspectors also

concluded that the surveillance tests adequately tested the respective system to verify

that it would function per design. (Section M1.2)

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The ir'spectors concluded that the licensee was accurately counting and reporting the

number of Technical Specification surveillance pump and valve test failures in response

to commitments by Comed associated with the NRC's request for information pursuant to

10 CFR 50.54(f) regarding cyclical safety performance at Comed's nuclear stations.

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(Section M7.1)

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- The inspectors concluded that the licensee was accurately calcu!ating and reporting the

percent of corrective maintenance rework in response to commitments by Comed

associated with the NRC's request for information pursuant to 10 CFR 50.54(f) regarding

cyc!ical safety performance at Comed's nuclear stations. (Section M7.2) 1

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Enaineerina

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The inspectors concluded, following a review of three safety-related engineering

requests, that engineering personnel used appropriate technical evaluations and

engineering judgement to support their responses. The inspectors concluded that

engineering personnel documented their responses well and in accordance with

Braidwood Administrative Procedure 2320-2," Engineering Requests." (Section E2.1)

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The inspectors concluded that the licensee took inadequate corrective actions in

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response to a previous NRC violation regarding non-environmentally qualified safety-

related equipment subject to a harsh environment in the event of an accident. No actions

! were taken to identify other non-environmentally qualified safety-related equipment

located in an area that could become a harsh environment until questioned by the j

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inspectors. The licensee later identified three more examples of non-environmentally ,

qualified safety-related equipment. A violation was issued. (Section E 8.1)

l Plant Support i

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The inspectors concluded that security personnel performed access control

responsibilities in an expeditious and professional manner in accordance with the i

requirements contained in applicable station procedures. The inspectors concluded that

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procedures.. (Section S1,1)

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' The inspectors concluded that contractor personnel performing work associated with the

Unit 1 steam generator replacement project failed to de-energize a welding machine and

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' failed to bleed off the pressure in the hoses of an oxygen-acetylene torch prior to leaving

' them unattended which was contrary to the requirements contained in Braidwood

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Administrative Procedure 1100-15, " Fire Prevention When Welding, Cutting, Grinding or

Performing Open Flame Work (Hot Work)." A violation was issued. (Section F4.1)

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Report Details

Summary of Plant Status

Unit 1 entered the period at full power and remained at or near full power for the entire period.

Unit 2 entered the period at full power and remained at or near full power for the entire period. I

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l. Operations

01 Conduct of Operations

O1.1 Unit 2 Pressurizer Pressure Reduction Below Technical Specification (TS) Limits

a. Inspection Scope (71707 )

The inspectors reviewed the shift manager's logbook for May 18 and Problem

Identification Form (PlF) A1998-01811.

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b. Observations and Findinas 1

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On May 18, Unit 2 operators secured the B group of pressurizer backup heaters. The

operators did not adequately monitor pressurizer pressure which dropped faster than

anticipated. Pressurizer pressure dropped from a nominal 2235 pounds per square inch

gauge (psig) to a minimum of 2219 psig before the group B pressurizer backup heaters

were re-energized. Both Units 1 and 2 normally operate with two of the three groups of

backup heaters energized and the pressurizer spray valves open. The operators entered

TS 3.2.5, which required that pressurizer pressure be restered to 2219 psig within

2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. Pressurizer pressure was restored to 2219 psig in 7 minutes. l

The heaters were secured because operators were looking for a way to reduce station

electrical load. Electrical grid conditions in northem lilinois were such that electrical

demand exceeded the supply. Operations management addressed the problem at

operations shift tumovers by stating that securing pressurizer heaters was acceptable. ]

The licensee was investigating why the pressurizer pressure decreased more rapidly than

anticipated with one group of pressurizer heaters secured. The licensee completed

preventive maintenance on the pressurizer heater breakers the previous week and

verified that the correct number of heaters were functioning. The licensee scheduled

maintenance activities to check that the heaters were operating at the rated capacity, to

check the set points for the variable pressurizer heater controller, and to check the spray

flow rate through the attemate spray valve.

c. Conclusions

The inspectors concluded that the Unit 2 operators monitored pressurizer pressure poorly

after securing L ackup heaters and did not re-energize the heaters in time to prevent

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pressurizer pre ssure frcm ;;oing relow the lower Technical Specification limit. The

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operators secured the heaters to reduce the station electricalload to support electrical

grid needs during unseasonably hot weather.

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01.2 ' Configuration Control Problems Continue

a. InsDeClion Scong (71707)

The inspectors reviewed the sections of the Operations Department First Quarter 1998

Self-Assessment and additional self-assessments that addressed out-of-service and

configuration controlissues. The inspectors reviewed the following PlFs: A1998-01777,

A1998-01793, A1998-01708, A1998-01812, A1998-01875, and A1998-01684. The

inspectors also discussed the topic of configuration control with senior operations

management.

b. - Observations and Findinas

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The inspectors reviewed the sections of the Operations Department First Quarter 1998

Self-Assessment information that acciressed configuration control and equipment

mispositionings. The inspectors agreed with the licensee's conclusion that the number of

mispositionings that have affected safety-related equipment or resulted in a significant

event declined from a year ago. However, the total number of equipment mispositionings

averaged between three and four per month in 1998, with an increasing trend. The

inspectors also noted that between May 1 and May 26 the licensee identified six

mispositioned valves. The licensee was unable to identify the root cause of any of these

mispositionings by the end of the inspection period.

' The following corrective actions have been taken or planned to improve configuration

control and equipment mispositioning performance. Operations management conducted

and planned to continue to hold event review boards with operators involved with

equipment configuration problems. The purpose was to increase personal accountability.

Specific training on equipment control, independent verification, and equipment line-ups

was completed for non-licensed operators, and training for licensed operators was

planned. Operations management distributed a plant equipment control memorandum to '

designate equipment that could be operated by plant personnel other than operators. For

example, radiation protection technicians would be responsible for and have operational

authority over the analysis / sampling segments of the process radiation system.

Continued training on human performance error reduction techniques and quarierly

human performance sessions was planned. The licensee also initiated a trend

investigation into mispositioned equipment.

c. Conclusions

The inspectors were concemed about the frequency of mispositioned equipment events.

Six valves we** mispositioned in the month of May. All of the valves were non-safety-

related and * one of the mispositioning events resulted in a plant transient. The

inspectors agreed with the licensee's conclusion that the number of equipment

mispositioning events that involved or affected safety-related equipment or that were

considered significant, declined from a year ago. However, the inspectors observed that

the number of equipment mispositioning events were increasing in 1998 which is

noteworthy and warrants consideration.

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08 Miscellaneous Operations issues (92901)

08.1 (Closed) Violation 50 456/97005-01(DRP): 50-457/97005-01(DRP): The inspectors

observed that Unit 1 Braidwood Functional Recovery Procedure (18wFR)-S.1, " Response

l- to Nuclear Power Generation / Anticipated Transient Without Scram Unit 1," Revision 1 A,

Step 4a, had not been maintained in that it diracted operators to start the chemical and

volume control system positive displacement charging pump if neither of the centrifugal

charging pumps could be started. The positive displacement charging pump was out-of-

service and had not run for about 10 years. Licensee management was trying to decide l

l whether to abandon the positive displacement pump in place or maintain it. The licensee

changed 1BwFR-S,1, Step 4a, to read, " Start a centrifugal charging pump. If neither

l pump will start, then start the positive displacement pump if available. If no charging

pump can be started then go to Step 5." The inspectors had no further concems. This

violation is closed.

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08.2 (Closed) Violation 50-457/97016-01(DRP): The inspectors identified that licensee

personnel failed to make a required notification in accordance with 10 CFR 50.72(b)(2)(ii)

after an automatic isolation of the containment ventilation system. Operations personnel

use the licensee's " Deportability Manual" to determine the deportability of any event. The

licensee's manual specifically stated that the containment ventilation isolation was not

reportable. However, this was in conflict with regulatory requirements for reporting. The

licensee changed the " Deportability Manual" to specifically state that a containment

ventilation isolation was a reportable event. The event was reported in Licensee Event

Report (LER) 50-457/97004-00. The inspectors had no further concems. This violation is

clost*d.

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11. Maintenance

M1 Conduct of Maintenance

M1.1 Replacement of Unit 2 Rod Control Shutdown Banks B. C. and E Cabinet Power Supolies

a. Inspection Scope (62707)

The inspectors reviewed Work Request 980038329 for the replacement of the Unit 2 rod

control system shutdown bank power supply. The inspectors attended a licensee

management meeting and an infrequently performed activity briefing regarding the

replacement of the Unit 2 rod control system power supply,

b. Observations and Findinas

On April 25, the licensee identified that one of the two negative 24 volt direct current

power supplies in the shutdown Control Rod Banks B, C, and E power supply cabinet had

failed. On April 27, the inspectors observed portions of the replacement of the two

negative 24 volt direct current power supplies. Only 30 percent of previous industry

attempts to replace these power supplies with the reactor at power were successful.

Mistakes at several stations during power supply replacements at power resulted in

reactor trips.

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The inspectors observed that licensee management clearly communicated the potential

operationalimpact of the maintenance activity to the maintenance technicians and to the

operators. Contingencies for a plant transient were also clearly communicated to the

maintenance technicians and to the operators.

Maintenance department management obtained a procedure from another utility that was

recently successful in replacing the power supplies with the reactor at power.

Maintenance department management also sent two instrument maintenance

technicians, a foreman, and the system engineer, to a Westinghouse facility in Pittsburgh,

Pennsylvania, to practice the replacement using the work package procedure on similar

equipment. The inspectors reviewed the power supply replacement procedure and

determined that it was written well. The inspectors observed that the work progressed

quickly and smoothly. The instrument maintenance technicians demonstrated a high

level of proficiency during the replacement of the power supplies and detailed knowledge

b of the procedure.

c. Conclusions

The inspectors concluded that the replacement of the Unit 2 rod control negative 24 volt

direct current power supplies in the shutdown Control Rod Banks B, C, and E cabinet was

planned and executed well. The instrument maintenance technicians demonstrated a

) high level of proficiency as a result of excellent pre-job training and the careful validation

} of the maintenance procedure.

M1.2 Surveillance Observations

a. Inspection Scope (61726)

The inspectors reviewed the following procedures and observed portions of the

associated surveillance tests:

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Unit 1 Braidwood Engineering Surveillance Procedure (1BwVS) 3.1.3.2,

" Moderator Temperature Coefficient At Power," Revisions 0 and OE1;

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2BwVS 5.2.f.3-2, "ASME [American Society of Mechanical Engineers)

Surveillance Requirements For Residual Heat Removal Pump 2RH01PB,"

Revision SE1;

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2BwVS 0.5-3.DO.1, "ASME Requirement For Testing The Diesel Oil Transfer

System," Revision 1; and

- 18wVS 1.2.3.1-1, "ASME Surveillance Requirements For The 1A Centrifugal

Charging Pump and Check Valve 1CV8480 A Stroke Test," Revision 1.

b. Observations and Findinas

The inspectors compared the surveillance test requirements against the TS requirements

and the Updated Final Safety Analysis Report (UFSAR) design descriptions and found no

discrepancies. The test results met the acceptance criteria for the surveillance

observed.

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c. Conclusions

The inspectors concluded that the results obtained during four surveillance tests

observed during the inspection period met acceptance criteria. The inspectors also

concluded that the surveillance tests adequately tested the respective system to verify

that it would function per design.

M2 Maintenance and Material Condition of Facilities and Equipment

M2.1 Untested Safeauards Actuation Relav Contacts

a. Inspection Scope (92902)

The inspectors interviewed licensee system engineers. The inspectors also reviewed

Electrical Drawing 20E-1-4030EF01 and a licensee prepared position paper, " Position

Regarding Testing of Engineered Safety Feature Circuitry and Application to K608 Slave

Relay Circuitry," dated May 11,1998.

b. Observations and Findinas

On May 7, the licensee identified that contacts associated with the safeguards actuation

relays were not tested. The purpose of the relays was to simultaneously (block) start the

emergency core cooling pumps in the event of a safety injection signal if offsite power is

available. The block start contacts are in parallel with the sequencing contacts used to

start the emergency core cooling pumps if a safety injection signal occurs simultaneously

with a loss of off-site power. The sequencing contacts would also start the emergency

core cooling pumps if off-site power were available, (redundant to the function of the

block start contacts). The licensee's position paper stated that the sequencing of the

loads was credited for in the UFSAR and that the block start capability was redundant

and not required to be tested by TS 4.3.1,4.3.2, or 4.8.1.

The inspectors planned to review the licensee's position paper and discuss the

appropriateness of testing the safeguards actuation relay contacts with the office of

Nuclear Reactor Regulation management. Whether TS require the testing of the

safeguards actuation relay contacts is an unresolved item (50-456/98008-01(DRS);

50-457/98008-01(DRS)).

M7 Quality Assurance in Maintenance Activities

M7.1 Failed TS Pump and Valve Surveillance Review

a. Inspection Scope (92702)

The inspectors interviewed the data steward for the failed TS pump and valve

surveillance performance indicator.

b. Observations and Findinas

The licensee committed in its March 28,1997, response to the NRC's request for

information pursuant to 10 CFR 50.54(f) regarding cyclical safety performance at Comed

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nuclear stations, to report to the NRC the number of failed pump and valve TS

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surveillance. In 1998, there were two failed surveillance. The inspectors verified that

I the two examples met the licensee's criteria for failed surveillance. The inspectors did

I not identify any other survei!!ance test results that should have been counted as a failure

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c. Conclusions

The inspectors concluded that the licensee was accurately counting and reporting the

number of TS surveillance pump and valve test failures in response to licensee

commitments by Comed associated with the NRC's request for information pursuant to

10 CFR 50.54(f) regarding cyclical safety performance at Comed's nuclear stations.

M7.2 Percent Rework Review

a. Inspection Scope (62707)

The inspectors interviewed the individual responsible for accumulating the data for the

percentage of maintenance rework.

b. Observations and Findinos

The licensee committed in its March 28,1997, response to the NRC's request for

information pursuant to 10 CFR 50.54(f) regarding cyclical safety performance at Comed

nuclear stations, to report to the NRC the percentage of reworked maintenance. The

inspectors verified that the licensee was reporting a 3-month rolling average of the

percent of reworked corrective maintenance. The licensee does not count a preventive

maintenance item that results in later rework in the percentage. The reason was that if

the number of preventive maintenance activities were added to the number of corrective

maintenance activities the percentage of rework would be very low and be a poor

indicator. The inspectors agreed with this conclusion.

c. Conclusions

The inspectors concluded that the licensee was accurately calculating and reporting the

percent of corrective maintenance rework in response to commitments associated with

the NRC's request for information pursuant to 10 CFR 50.54(f) regarding cyclical safety

performance at Comed's nuclear stations.

M8 Miscellaneous Maintenance issues (92902)

M8.1 ! Closed) Violation 50-456/96019-02fDRP): On November 7,1996, workers were

erecting scaffolding in front of the traveling screens in the lake screen house. The

workers dropped an 8-foot scaffold pole through a traveling screen opening into the bay.

The inspectors verified that there were no strainers or screens to prevent the introduction

of foreign materialinto the essential service water system pump suction. The licensee's

immediate corrective action was to install temporary covers over the traveling screen i

openings to prevent foreign materialintrusion into the bay. The licensee's long term

corrective action was to install permanent hinged covers over the openings of the

traveling screens. The inspectors have verified the installation of the permanent hinged

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covers on all but one of the traveling screens. The inspectors verified that the installation

of the remaining iraveling screen cover was in the maintenance schedule for June 1998.

This item is closed.

Ill. Enaineerina

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l E2 Engineering Support of Facilities and Equipment

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l E2.1 Review of Safetv-Related Enaineerina Reauests

a. Inspection Scope (37551)

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The inspectors reviewed safety-related Engineering Requests ER 9800743, " Evaluation

of the Use of the Spare Barton Gauges For Use as Residual Heat Removal Pump (

Minimum Flow Indicating Switch," ER 9800810, " Installation of North Battery

Rack 1DCO2EB Per M20-1-96-001," and ER9800800, " Erection of Barricade in Diesel

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Generator Exhaust Silencer and Rupture Disk Areas." The inspectors also reviewed

Braidwood Administrative Procedure (BwAP) 2320-2," Engineering Requests,"

Revision 5.

b. Observations and Findinas

The inspectors reviewed three safety-related engineering requests and concluded that

each provided a response that was based on appropriate technical evaluations and

engineering judgement. The inspectors noted that each of the engineering requests were

documented in accordance with BwAP 2320-2. The inspectors also noted that

BwAP 2320-2 clear 1y described the process by which engineering requests are submitted,

completed, and controlled.

c. Conclusions

The inspectors concluded, following a review of three safety-related engineering

requests, the engineering personnel used appropriate technical evaluations and

engineering judgement to support their responses. The inspectors concluded that

engineering personnel documented their responses well and in accordance with

Braidwood Administrative Procedure 2320-2," Engineering Requests."

E8 Miscellaneous Engineering issues (92903)

E8.1 (Closed) Violation 50-456/97012-(.5(DRS): The licensee failed to prevent the installation

of a non-environmentally qualified breaker subject to a harsh environment. Following

NRC questioning, the licensee identified that on February 18,1997, a

non-environmentally qualified circuit breaker was erroneously installed in the 1 A residual

heat removal pump minimum flow valve circuit breaker cubicle, which was subject to a

harsh environment in the event of an accident. The breaker was changed out under

Setpoint/ Scaling Change Request 95-049. An incorrect store item number (767C26) was

specified by the engineer for the replacement breaker. This store item number was for a

non-environmentally qualified breaker. This error was not identified by the work analyst

and the quality controlinspectors.

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To address this problem, the licensee generated Operability Determination 97-098, dated

i August 11,1997, to evaluate operability of the breaker. The licensee concluded that the

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installed breaker would be able to perform its safety function. In addition, the

non-environmentally qualified breaker was replaced on August 26,1997. Design

engineering personnel, work analysts, and maintenance personnel were informed of this

event and provided appropriate training.

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l prevent recurrence. On April 7,1998, the inspectors questioned the licensee as to

whether a generic review of work history records had been conducted to determine if

l other non-environmentally qualified breakers or components were potentially installed in

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any motor control center located in an area that could be subject to a harsh environment.

l Subsequently, on April 9,1998, the licensee issued PlF A1998-01350 to document the

discovery in Motor Control Centers 1/2AP21E of non-environmentally qualified

safety-related components including a breaker, some thermal overloads and a meter.

The licensee performed a preliminary review of the safety-related, non-environmentally

qualified items and determined that they were still operable. The licensee completed

Operability Determination 98-029 in which it was concluded that the safety-related

components were operable.

This violation is considered closed since the original non-qualified breaker was replaced.

However, the licensee's failure to implement comprehensive and effective corrective

action to prevent recurrence is considered a violation of 10 CFR Part 50, Appendix B,

Criterion XVI (50-456/98008-02(DRS); 50-457/98008-02(DRS)).

E8.2 (Closed) LER 50-456/96004-00: On March 21,1996, the licensee identified that

surveillance procedure BwVS 6.2.2.d-1 " Containment Spray Additive Flow Rate

Verification," failed to incorporate a density adjustment for water flowing through a flow

cell calibrated for a sodium hydroxide solution. During the design basis reconstitution of

the containment spray system and the spray additive system, the licensee identified that

the UFSAR description vras incorrect and contained conflicting information. The licensee

also determined proper f,ow set'ings for spray additive flow and eductor motive flow. The

licensee made changes tc., the UFSAR to remove incorrect and/or conflicting information

and changed the TS surveillance test procedures to reflect the proper spray additive tank

level, spray additive flow rate, and eductor motive flow rate. The inspectors observed the

performance of the surveillance test in accordance with BwVS 6.2.2.d-1 and verified that

all acceptance criteria, TS requirements and UFSAR commitments / conditions were met.

The licensee determined that during e.t early segment of the injection phase of a

containment spray actuation, the pH of the spray additive solution injected into the

containment atmosphere could exceed the environmental qualification pH limits of certain

equipment inside the containment for about 31 minutes. The licensee performed an

operability determination and an evaluation of equipment environmental qualification at

increased pH and concluded that there would be no adverse effect. An analysis

performed by the NRC staff also arrived at a similar conclusion. A non-cited violation was

issued in Inspection Report 50-456/98005 for exceeding the TS limit for spray additive

flow. The licensee's immediate and long-term corrective actions have been completed

and were considered appropriate. This item is closed.

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IV. PLANT SUPPORT

So Conduct of Security and Safeguards Activities

S1,1 Access Control to Site Protected Areas

a. Inspection Scope (71750)

The inspectors observed security personnel controlling access to site protected areas.

The inspectors reviewed Braidwood Administrative Procedure 900-4," Access Control,"

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Revision 15; Braidwood Security Procedure 03, " Personnel and Package Entry / Exit

Procedure," Revision 10; Corporate Nuclear Security Guideline Number 100, "X-Ray

Search," Revision 3; Corporate Nuclear Security Guideline Number 101,

" Package / Material Search," Revision 1; and Corporate Nuclear Security Guideline

Number 10, " Personnel Search / Ingress," Revision 3.

b. Observations and Findinas

On May 5, the inspectors observed security personnel conducting searches of individuals

authorized unescorted access to the main plant site and the lake screen house protected

areas. The inspectors observed security personnel monitor plant personnel as they

passed through metal and explosive detectors, perform x-ray inspection of hand carried

items, perform occasional pat-down searches of personnel entering the site, escort

individuals from the main plant site to the lake screen house, and admit personnel to the

lake screen house protected area. The inspectors discussed access control

requirements with security personnel and determined that they were knowledgeable of l

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c. Conclusions

The inspectors concluded that security personnel performed access control

responsibilities in an expeditious and professional manner in accordance with the

. requirements contained in applicable station procedures. The inspectors concluded that '

security personnel were knowledgeable of the requirements contained in those

procedures.

F. Fire Protection Staff Knowledge and Performance

F4.1 Failure to Follow Fire Protection Proaram Requirements

a. - Inspection Scope (71750)

The inspectors routinely monitored maintenance work areas. The inspectors reviewed

Procedures BwAP 1100-10," Control and Use of Flammable and Combustible Liquids and

Aerosols," Revision 2; BwAP 1100-11, " Fire Prevention for Use of Lumber and Other

Combustibles," Revision 7; and BwAP 1100-15, " Fire Prevention When Welding, Cutting,

Grinding or Performing Open Flame Work (Hot Work)," Revision 8. The inspectors also

interviewed operations, fire protection, and maintenance personnel.

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b. Observations and Findinas l

On April 24, the inspectors observed an unattended welding machine on the 411 foot

elevation of the fuel handling building that was energized. The inspectors reported the

energized welder to operations and fire protection personnel and the welding machine

was immediately de-energized by plant personnel.

Step C.2.8 of Procedure BwAP 1100-15 stetes, " Ensure welding machines are

de-energized, cylinder valves are isolated, and hoses are depressurized when the

assigned workers are not in the immediate area, or when these items are not in use

(i.e., during breaks, lunch, end of day, etc.)." Contrary to this step, the welding machine

was left energized and unattended. The failure to follow Plant Fire Protection Procedure )

BwAP 1100-15 was an example of a violation of TS 6.8.1.g, " Fire Protection Program

implementation," (50-456/98008-03a(DRP); 50-457/98008-03a(DRP)) as described in the

attached NOV.

On May 1, the inspectors observed a maintenance work area that was unattended while ,

the workers were on a scheduled break. The inspectors checked an oxygen-acetylene j

torch and observed that the cylinders'stop values were shut, however, the pressure  !

regulator gauges indicated that the oxygen and acetylene hoses were pressurized. The

inspectors reported the conditions to operations and fire protection personnel and the

hoses were immediately de-pressurized by plant personnel. When the worker using the

oxygen-acetylene torch retumed to the work site, the inspectors questioned the worker on

the requirements for leaving the items unattended. The worker stated that he did not

know of any requirements for bleeding pressure off of gas lines.

Step C.2.8 of Procedure BwAP 1100-15 states, " Ensure welding machines are

de-energized, cylinder valves are isolated, and hoses are depressurized when the

assigned workers are not in the immediate area, or when these items are not in use

(i.e., during breaks, lunch, end of day, etc.)." Contrary to this step, the hoses of the

oxygen-acetylene torch were pressurized with oxygen and acetylene gas and left

unattended. The failure to follow Plant Fire Protection Procedure BwAP 1100-15 was an i

example of a violation of TS 6.8.1.g," Fire Protection Program implementation" j

(50-456/98008-03b(DRP); 50 457/98008-03b(DRP)) as described in the attached NOV. {

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c. Conclusions

The inspectors concluded that contractor personnel performing work associated with the  !

!

Unit 1 steam generator replacement project failed to de-energize a welding machine and

failed to bleed off the pressure in the hoses of an oxygen-acetylene torch prior to leaving

them unattended which was contrary to the requirements contained in Braidwood

Administrative Procedure 1100-15, " Fire Prevention When Welding, Cutting, Grinding or

Performing Open Flame Work (Hot Work)."

F8 Miscellaneous Fire Protection issues (92904)

F8.1 (Closed) Inspection Followup ltem 50-456/96012-05fDRP): On August 14,1996, the

master selector valve (OCOO36) for the auxiliary building carbon dioxide system failed.

The licensee replaced the valve and sent the failed valve back to the manufacturer for

analysis. The manufacturer determined that the numerous opening and closing cycles

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experienced by the master selector valve during the performance of carbon dioxide fire

suppression system puff tests resulted in premature failure of the valve. The

manufacturer determined that the valve intemal materials were not adequate for the

number of times the valve was cycled and recommended installing valve intemal parts

made of upgraded materials. The valve failed again on April 3,1998, and was replaced

on April 4,1998, with a valve that had the upgraded parts installed (Work

Request 980034810). The inspectors had no further concems. This item is closed.

V. Manaaement Meetinas

X1 Exit Meeting Summary

.The inspectors presented the inspection results to members of licensee management and

staff at the conclusion of the inspection on June 8,1998. The licensee acknowledged the

findings presented. The inspectors asked the licensee whether any materials examined

during the inspection should be considered proprietary. No proprietary information was

identified.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

T. Tulon, Site Vice President

K. Schwartz, Station Manager

  • R. Wegner, Operations Manager
  • R. Byers, Maintenance Superintendent

A. Haeger, Health Ph/sics and Chemistry Supervisor

  • R. Graham, Work Control Superintendent
  • T. Simpkin, Regulatory Assurance Supervisor

C. Dunn, System Engineering Supervisor

J. Meister, Engineering Manager

  • M. Cassidy, Regulatory Assurance - NRC Coordinator

NRC

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- M. Jordan, Chief, Reactor Projects Branch 3

C. Phillips, Senior Resident inspector

  • J. Adams, Resident inspector
  • D. Pelton, Resident inspector

T. Tongue, Project Engineer

IDNS

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T. Esper

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l * Denotes those who attended the exit interview conducted on June 8,1998.

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INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

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p IP 61726: Surveillance Observations

l IP 62707: Maintenance Observation

l- IP 71707: Plant Operations

IP 71750: Plant Support Activities

IP 92702: Followup on Corrective Actions For Violations and Deviations

- iP 92901: Followup - Plant Operations

IP 92902: Followup - Plant Maintenance

IP 92903: Followup - Engineering

l.

i IP 92904: Followup _- Plant Support

ITEMS OPENED AND CLOSED

Opened

! 50-456/98008-01; 50-457/98008-01 URI untested actuation relay contacts

50-456/98008-02; 50-457/98008-02 VIO failure to implement corrective action

50-456/98008-03; 50-457/98008-03 VIO failure to follow fire protection procedures

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50-456/96004-00 LER failure to density adjust CS flow rate

,

50-456/96012-05 IFl- failure of CO2 master selector valve

50-456/96019-02 VIO failure to maintain adequate procedures

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50-456/97005-01; 50-457/97005-01 VIO failure to maintain procedure

50-456/97012-06 VIO failure to prevent use of non-EQ breaker

failure to report ESF actuation )

50-457/97016-01 VIO

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LIST OF ACRONYMS USED

ASME American Society of Mechanical Engineers

BwAP Braidwood Administrative Procedure

BwFR Braldwood Functional Recovery Procedure

BwVS Braidwood Engineering Surveillance Procedure

CENT Centrifugal

CFR Code of Federal Regulations

DRP Division of Reactor Projects

DRS Division of Reactor Safety

IFl inspection Followup Item

LER Licensee Event Report

NRC Nuclear Regulatory Commission

NRR Nuclear Reactor Regulations

PlF Problem Identification Form

psig pounds per square inch

TS Technical Specification

UFSAR Updated Final Safety Analysis Report

URI Unresolved Item

VIO Violation

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