ML20203D920

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Insp Repts 50-456/97-22 & 50-457/97-22 on 971216-980126. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20203D920
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 02/20/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20203D912 List:
References
50-456-97-22, 50-457-97-22, NUDOCS 9802260199
Download: ML20203D920 (22)


See also: IR 05000456/1997022

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION lil

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i Docket Nos: 50-456,50-457

License Nos: NPF 72, NPF 77

'- Report Nos: 50-456/97022(DRP); 50-457/97022(DRP)

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Licensee
Commonwealth Edison (Comed)

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Facility: Braidwood Nuclear Plant, Units 1 and 2

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Location: RR #1, Box 84

Braceville,IL 60407

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Dates: - December 16,1997, through January 26,1998

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Inspectors: C, Phillips, Senior Resident inspector

J. Adams, Residert inspector

'D Pelton, Resident inspector

T. Esper, Illinois Department of Nuclear Safety

Approved by: M. Jordan, Chief

Reactor Projects Branct. 3 -

9902260199 900220

PDR ADOCK 05000456

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EXECUTIVE SUMMARY

Braidwood Nuclear Plant, Units 1 & 2

NRC Inspection Report No. 50-456/97022(DRP); 50-457/97022(DRP)

This inspection included aspects of licensee operations, maintenance, engineering, and plant

support. The report covers a six week period of resident inspection from December 10,1997,

through January 26,1998.

Operations

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The inspectors concluded that the infrequently performed activity briefing of shift

personnel for removal of the *N" annunciator train was conducted and attended by the

appropriate personnel. The inspectors concluded that the licensee demonstrated an

excellent safety focus by providing additional Nuclear Station Operators (NSOs) in the

control room and additional non-licensed operators in the field to allow for continuous

monitoring of critical plant equipment normally monitored by the unavailable annunciators.

The inspectors concluded that the Unit Supervisor (US) demonstrated good surervisory

presence by remaining in or near the at-the-controls area and provided continuous

reminders to the NSOs to remain focused on the control board indicators. The inspectors

concluded that the licensee's restoration and testing of the "N" train of control room

annunciators was properly performed in accordance with established procedures.

(Section 01.1)

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On January 6 and 7, inspectors observed operators perform rounds of the auxiliary

building and turbine building. The inspectors reviewed the day shift equipment operator,

I auxiliary building, and turbine building logs and concluded that readings required by

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Technical Specification (TS) or other commitments were obtained. (Section 04,1)

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The inspectors observed licensed operator requalification training and determined that

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operators promptly identified all of the off-normal and casualty events included in the

training scenarios, properly used the correct procedures to place the plant in a stable

condition, and correctly used self checking and communication techniques. Inspectors

concluded that supervisory personnel provided directions to operators, conducted

periodic crew briefings, effectively supervised reactivity manipulations, correctly identified

and entered the applicable TS action statements, properly classified the Generating

Station Emergency Plan (GSEP) events, appropriately upgraded and downgraded GSEP

events, and simulated the required notifications. The inspectors concluded that the

simulator accurately represented the actual control boards in the control room.

Maintenance

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The inspectors concluded that the maintenance activities observed were performed in

accordance with the applicable procedures, that the procedures provided the requisita

information for the assigned work, that maintenance personnel demonstrated safe work

practices, and that maintenance personnel were knowledgeable of the associated TS

limiting condition for operations. (Section M1.1)

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  • The inspectors concluded that for observed surveillance activities acceptance criteria

were met, personnel correctly followed the test procedures, and that surveillance tests

verified the systems performed as required by the updated final safety analysis report and

TS. (Section M1.2)

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The licensee identified in 1989 that all four safety-related Unit 2 main feedwater check

valves (FWO79A, B, C, and D) had seized in an open position due to insufficient

clearances between critical components in the valve dampening mechanisms. The

inspectors identificd in December 1S97 that critical components in the Unit 1 FWO79A

and D check valve dampening mechanisms were replaced in May and April o.f 1997

respectively without being machined to the required clearances. The inspectors

concluded that the corrective actions taken for the seizing of the FWO79 check valve

piston rods in 1989 were not adequate to prevent recurrence. A violation was issued.

(Section M2.1)

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The inspectors concluded that the licensee accurately identified, quant;fied, tracked, and

reported the number of non-outage corrective work requests reported to the NRC as

committed to in the Braidwood Station March 28,1997, response to the NRC's request

for information pursuant to 10 CFR 50.54(f). (Section M7.2)

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The inspectors identified five examples where maintenance ar.d test equipment was not

stored in accordance with station procedures. The ir,spectors concluded that the

licensee was not appropriately controlling access to maintenance and test equipment. A

violation was issued. (Section M7.3)

Enaineerina

. The inspectors observed progress in reducing the total number of temporary alterations.

System and site engineering personnel were tracking open temporary alterations as listed

in the associated documentation. The inspectors concluded plant procedures related to

the temporary alteration process were followed for known plant alterations. However, the

inspectors identif!9d two unauthorized modifications that were in place for several years,

but were not identified in plant design documentation. A violation was issued.

(Section E2.1)

Plant Support

. The inspectors concluded that the licensee accurately identified, quantified, tracked, and

reported the percent of contaminated square footage reported to the NRC as committed

to in the Braidwood Station March 28,1997, response to the NRC's request for

information pursuant to 10 CFR 50.54(f). (Section R7.1)

. The inspectors observed that the station response to a fire drill conducted on

December 31 was prompt and thorough and concluded fire brigade members performed

(or simulated) all tasks well. (Section F4.1)

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Report Details

Summary of Plant Status

Unit i entered the inspection period at full power and remained at or near full power for the entire

period. Unit 2 entered the inspection period at full power and remained at or near full power until

the reactor tripped at 9:53 p.m. on January 26. The cause of the kip was not identified by the

end of the inspection period.

,1, Operations

01 Conduct of Operations

01.1 Control Room Observations Durina a Planned Loss of Control Room "N" Train

Annunciators

a. Inspection Scope (71707)

The inspectors attended the infrequently performed activities (IPA) briefing and observed

Unit 2 control room operators during the performance of a maintencnce activity to repair

relay PNLA30J in panel 2PA30J. The inspectors reviewed the IPA briefing requirements

contained in Braidwood Administrative Procedure (BwAP) 100-12, " Human Performance

Awareness of Pre-Job Briefings / Meetings and Self Checking," Revision 5.

b. Observations and Findinas

On January 6, inspectors attended an IPA briefing for a maintenance activity that would

deenergize the Unit 2 power supplies for the "N" train of control room annunciators. The

"N" train annunciator power supplies provided power to all Unit 2 annunciators except for

the safety-related "A" and "B" trains and some of the Unit 0 annunciators. The inspectors

verified the IPA met the requirements of BwAP 100-12. The shift operations supervisor

led the IPA and stressed the importance of vigilance in monitoring equipment indicators

for the plant systems normally served by the "N" train annunciators. The system engineer

described the maintenance activity to be performed. The inspectors observed all

necessary personnel involved in the maintenance activity were in attendance at the

briefing.

The inspectors observed that the licensee augmented the shift with four additional non-

licensed operators and four additional Nuclear Station Operators (NSOs). The non-

licensed operstors were stationed appropriately in the turbine and auxiliary buildings to

monitor equipment. The additional NSOs were each assigned a specific section of the

control boards for the purpose of continuously monitoring the indicators of equipment

effected by the annunciator outage. The communication links between field personnel -

and the control room were tested and operable annunciator windows were identified prior

to the commencement of the maintenance activity.

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The inspectors observed the NSOs performing continuous monitoring of the control

boards prior to the deenergization of the *N" train annunciator power supplies. The

continuous monitoring of the control boards continued throughout the duration of the

maintenance activity until testing had verified that the "N" train annunciators were again

operable, inspectors observed direct supervision of the NSOs by the Unit Supervisor

(US) from within the at-the-controls area of the control room. The US provided the NSOs

frequent reminders to maintain their focus on the control board indicators.

c. Conclusions

The inspectors concluded that the infrequently performed activity briefing of shift

personnel for removal of the "N" annunciator train was conducted and attended by the

appropriate personnel. The inspectors concluded that the licensee demonstrated an

excellent safety focus by providing additional NSOs in the control room and additional

non-licensed operators in the field to allow for continuous monitoring of ci;tical plant

equipment normally monitored by the unavailable annunciators. The inspectors

concluded that the US demonstrated good supervisory presence by remaining in or near

the at-the controls area and provided continuous reminders to the NSOs to remain

focused on the control board indicators. The inspectors concluded that the licensee's

restoration and testing of the "N" train of control room annt.nciators was properly

performed in accordance with established procedures. (Section O1.1)

04 Operator Knowledge and Performance

04.1 Observation of Operator Rounds

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a. Inspection Scope (71707)

The inspectors observed non-licensed operators during the performance of their rounds

in the turbine building and auxiliary building. The inspectors performed a review of

" Equipment Operator Weekly Logs Logsheet," Revisions 10 and 11; " Auxiliary Building

U-1 (Unit 1) Weekly Logs Logsheet," Revisions 9 and 10; " Auxiliary Building U-2 (Unit 2]

Weekly Logs Logsheet," Revisions 8 and 9;" Turbine Building U-1 Weekly Logs

Logsheet," Revisions 14 and 15; and " Turbine Building U-2 Weekly Logs Logsheet,"

Revisions 14 and 15. Inspectors discussed recent changes to the equipment operator

logs with members of the operations staff, and discussed management expectations of

field operator performance with the Shift Operations Supervisor (SOS).

b. Observations and Findinas

On January 6, the inspectors accompanied an equipment operator performing rounds of

the 1E and non-1E high voltage switchgear,1E batteries, diesel generators, turbines,

transformers, and the switchyard; and on January 7, the inspectors accompanied the

Unit 1 auxiliary building operator while performing rounds of the auxiliary building. The

inspectors made the following observations:

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the operators observed radiation protection, housekeeping, and fire protection

requirements;

the operators inspected lesser traveled areas of the plant as part of their rounds;

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the operators checked all standby, running, and safety-related equipment during

their rounds; and

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the operators accurately measured equipment parameters and recorded the

associated readings in their logs.

The inspectors were told by auxiliary building operators that the number of readings taken

for the day shift logs had been reduced in September 1997. The inspectors reviewed

new and old revisions of the equipment operator, auxiliary building, and turbine building

logs. The companson revealed that readings taken to satisfy Technical Specification

(TS) requirements were obtained. The inspectors observed that the readings that were

removed were associated with equipment that rarely experienced any significant change,

provided little useful informatiori to operators, or were associated with annunciated

equipment. Many of the readings were moved from the day shift logs to either the

midnight or the afternoon logs.

The inspectors discussed the abbreviation of the day shift logs with the operations staff

and were told the reason for the abbreviation was to increase the availability of field

operators for the support of plant activities and to respond to plant problems. The staff

told the inspectors that they conducted a review of the logs and determined that there

were many components with parameters that rcrely changed or were only measured

daily. The staff made the determination that these components could be adequately

monitored by recording the parameters on the other shift logs. The staff told the

inspectors that the changes to the logs were reviewed by all of the field supervisors prior

to implementation and no parameters that were required to be recorded to satisfy TS

requirements and othar commitments were removed from the logs.

The inspectors discussed management's expectations of operator performance of rounds

with the SOS, The SOS told the inspectors that the field operators were still expected to

visit all areas and to look at all the equipment on their rounds. The SOS told the

inspectors that several of the operators had expressed concerns with the abbreviation of

the day shift equipment operator, auxiliary building, and turbine building logs. A shift

manager was assigned to review the concerns raised by the operators but had not yet

completed the review.

The inspectors did not observe any behavior by operators that would indicate the

existence of operator workarounds. The inspectors noted that all areas visited as part of

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the rounds were accessible to operators and only a minimal number of contaminated

areas were encountered.

c. , Conclusion

'"5e inspectors observed operators while they performed their required rounds and

concluded that the operators properly checked the status of all the equipment; correctly

adhered to radiation protection, housekeeping, and fire protection requirements; and

accurately read and recorded the required equipment pcrameters. The inspectors

reviewed the abbreviated day shift logs and concluded that readings required by TS or

other commitments were obtained.

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05 Operator Training and Qualification

05.1 Observation of Licensed Operator Reaualification Simulator Trainina

a. Inspection Scope (71707)

The inspectors observed, in the plant simulator, the performance of licensed operators in

response to a loss of a condensate pump, a loss of a component cooling water pump,

steam generator tube rupture with a safety injection actuation, and a feedline break inside

containment.

b. Observations and Findinas

On January 14,1998, the inspectors observed licensed operators participating in the

licensee's licensed operator requalification program. The simulated scenarios observed

by the inspector included: a loss of a condensate pump, a loss of a component cooling

water pump, a steam generator tube rupture with a safety injection actuation, and a

feedline break inside containment. The inspectors observed that the operating crew q

promptly identified the problerns, properly used the correct procedures to stabilize the

plant, continuously self checked their actions prior to taking the actions, and effectively

used communication techniques. The US provided directions to operators, conducted

periodic crew briefings as permitted by plant conditions, and referred to TS and correctly

identified and entered the applicable action statements. The shift technical advisor

provided supervision over reactivity manipulations performed by the nuclear station

operators. The shift manager referred to the Generating Station Emergency Plan (GSEP)

and properly classified the events, upgraded and downgraded the events appropriately,

and made the required notifications.

The inspectors observed that the simulator accurately represented the actual control

boards in the control room. However, the inspectors observed that the existing problems

with the potential for some of the Unit 1 and 2 feedwater check valves (1/2FWO79A, B, C,

and D) to stick open were not included in the simulator's modeling. The instructors told

inspectors that they would discuss the issue at the next weekly operations training

meeting,

c. Conclusion

The inspectors observed licensed operator requalification training and determined that

operators promptly identified all of the off normal and casualty events included in the

training scenarios, properly used the correct procedures to place the plant in a stable

condition, and used proper self-checking and communication techniques, inspectors

concluded that supervisory personnel provided directions to operators, conducted

periodic crew briefings, effectively supervised reactivity manipulations, correctly identified

and entered the applicable TS action statements, property classified the GSEP events,

appropriately upgraded and lowngraded the GSEP events, and simulated the required

notifications. The inspectors concluded that the simulator accurately represented the

actual control boards in the control room.

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07 Quality Assurance in Operations

07.1 10 CFR 50.54m Letter Cormitment Review

a. Inspection Scope (92901)

The inspectors reviewed the status of commitments pertaining to the licensee's

March 28,1997, response to the NRC's request for information pursuant to

10 CFR 50.54(f). The commitment numbers correspond to those used by the licensee in

their March 28,1997, response.

b. Observations and Findinas

b.1 Commitment 1: "To reinforce these principles and ensure that per%fmance

results are achieved, the Chief Nuclear Operating Officer (CNOO) caiucts

Management Review Meetings (typically each month) at each site." ,m licensee

no longer has a management position entitled CNOO. This commitment was

fulfilled by the Vice President of Pressurized Water Reactors.

Commitment 75: "The CNOO conducts Management Review Meetings at each

site focused on safety performance and the effectiveness of improvement

initiatives. These meetings addcess trends of safety, performance, and cost

indicators; results of third party (NRC) inspections; results of site self-

assessments; status of material condition in the plant; outage planning and

performanco; and assessments of the quality of workforce product and training."

Commitment 100: "We have established the actions to be taken if the

performance criteria are not met. In order to assure that effective and timely

actions are taken, essessment of performance indicators and implementation of

actions based on this assessment will take place at the site, Nuclear Operating

Division and Board levels. Each of the perform?nce indicators described in

Sections 4.7.1 and 4.7.2 (of the Licensee's 10 CFR 50.54(f) response) above will

be monitored by the Site Vice Presidents, and will be reviewed during the periodic

Management Review Meeting for each station."

Commitment 271: "The CNOO (typically monthly) conducts Management Review

Meetings at each site, focusing on safety performance and the effectiveness of

improvement initiatives."

Commitment 322: "Each month the CNOO conducts Management Review

Meetings at all sites."

The inspectors observed one of the monthly Management Review Meetings

conducted on January 12. Licensee management briefed the Vice President of

Pressurized Water Reactors on the current status of performance indicators

reported to the NRC, as a response to the March 28,199~,10 CFR 50.54(f) letter

to the utility. The Vice President made several commen.s regarding expectations

of excellence from station management. The inspectors concluded that the

com nitments: to conduct a monthly Management Review Meeting and to

reinforce management expectations; to discuss performance indicators, trends,

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and the results of self essessments by third party inspectors; and to discuss the

effectiveness of improvement initiatives at Braidwood were satisfied.

Commitments 1,75,100,271, and 322 are closed.

b.2 Commitment 54: "Our CNOO, during his periodic visits (typically monthly) to the

sites, conducts open discussions with groups of 15 - 20 employees regarding our

plans, and steps that can be taken to improve."

Commitment 316: "Our CNOO, during his monthly Management Review meetings

at the sites, has discussions with groups of 15 - 20 employees regarding our

plans, issues of concern, and steps for improvement."

The inspectors observed the Vice President of Pressurized Water Reactors

discuss current station concerns with a group of 20 - 30 workers on J.,nuary 12.

The inspectors concluded that the commitment to meet with small groups of

employees on a periodic basis at Braidwood was satisfied and Commitments 54

and 316 are closed.

c. Conclusion

The inspectors concluded that the licensee met Commitments 1,54,75,100,271,316,

and 322 regarding periodic management meetings.

11. Maintenance

M1 Conouct of Maintenance

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M1.1 Miscellaneous Maintenance Activities

a. Inspection Scope (62707)

Between December 31,1997, and January 15,1998, the inspectors observed all or

portions of the following maintenance activities:

+ Repair of relay PNLA30J within electrical cabinet 2PR30J in accordance with

Work Request 970134937-01,

Replacoment of the process radiation monitor 1PR11J pump motor in accordance

with BwHP 4006-011, " Electrical Maintenance Troubleshooting Work Sheet," _

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Revision 9.

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Replacement of a mechanical seal on 2A residual heat removal system pump in

accordance with BwMP 3110-015, " Residual Heat Removal Pump Disassembly,

inspection, and Reassembly," Revision 0.

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b. Observations and Findinos

The inspectors attended the heightened level of awareness and Infrequently Performed

Activities (IPA) meetings. All maintenance related topics weru discussed at the

heightened level of awareness and IPA meetings including responsibilities, safety

requirements, tooling required, communications, and contingency plans. The inspectors

noted that maintenance personnel were knowledgeable about the scope of the work, the

requi J system status, and electrical safety. The inspectors also reviewed the

applicable portions of the Updated Final Safety Analysis Report (UFSAR) and the TS

limiting condit;ons for operations and noted no conflicts with the planned work.

c. Conclusiong

The inspectors concluded that the maintenance activities observed were performed in

accordance with the applicable procedures, the procedures provided the requisite

information for the assigned work, that maintenance personnel demonstrated safe work

practices, and maintenance personnel were knowledgeable of the associated TS limiting a

condition for operations.

M1.2 MJscellaneous Surveillance Activities

a. Inspection Scope (61726)

The inspectors observed all or portions of the tollowing surveillance tests:

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2BwOS 6.2.3.a 1, *Reacto, Containment Fan Coolar Monthly Surveillance,"

Revision 4E1.

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BwVS 7.6.h 1," Control Room Recirculation Cnarcoal Adsorber Bank operability,"

Revision SE1.

b. Observations and Findinas

Between December 31 and January 9, the inspectors observed the performance of the

above listed surveillance tests, both locally and from the control room. The inspectors

observed operations personnel establish initial plant conditions for the surveillance tests,

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operate plant equipment, communicate between the control room and the auxi'iary and

containment buildings, and restore effected equipment to service. Operators correctly

followed the surveillance test procedures, used proper three way communications, and

properly performed independent verifications during oquipment rettoration. The

inspectors observed that the acceptance criteria specified in the surveillance test

procedures were met. The inspectors reviewed applicable sections of the UFSAR and

the TS and determined that the survei!!ance tests verified that the systems performed as

required.

c. Conclusions

The inspectors concluded that for observed surveillance activities acceptance criteria

were met, personnel correctly followed the test procedures, and surveillance tests verified

the systems performed as req'2: red by the USFAR and TS.

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M2 Maintenance and Material Condition of Facilities and Equipment

M2.1 Unit 1 and Unit 2 Main Feedwater Check Valve FWO79 Maintenance

a. inspection Scope (62707)

The inspectors reviewed Problem identification Form (PIF) A1997 05245," Unable To

Maintain U-2 Feedwater Pump Speed Controller in Auto"; completed work package

970008530-01, " steam generator 2C feedwater flow check valvo disassemble and inspect

during A2R06"; completed work package 37000853101, " steam generator 2D feedwater

flow check valve disassemble and inspect during A2R06"; BwMP 3305-087,"Borg-

Wamer FWO79 Check Valve Disassembly, inspection, and Reassembly," Revisions 4

and 5; Operability Determinations97-156,97-157, and 97-163; and completed

documentation for surveillance test 2BwVS 0.5-2.FW.2-2, " Main Feedwater Header

(2FWO79A, B, C, D) Check Valve Fuli-Close Operability Exercise Test During Refuel

Outages," Revision O.

b. Observations and Findinos

On November 26,1997, the licensee identified that main feedwater check valves

2FWO79C and D were not completely open with Unit 2 at 97 percent power. The

inspectors reviewed the most recent complete work package documentation on the four

feedwater check valves in both units.

The 2FWO79A, B, C, ano O valves were 16 inch tilting disc, anti-slam check valves in the

main feedwater lines to all twr steam generators. Hydraulic pistons provided resistance

to prevent check valve slam. Testing of the check valves to verify closure was required

by American Society of Mechanical Engineers Code,Section XI, Article IWV-3520 and by
TS 4.0.S. Relief request VR-31 was granted by the NRC on August 18,1995, to allow

periodic inspection of the valves instead of quarterly flow checks.

The inspectors identified in the vendor manual a letter from Berg-Warner to Comed dated

June 26,1992, that stated valve sticking could occur if there was not enough clearance

(greater than .003 inches) between the outer diameter of the piston rod bushing and the

inner diameter of the valve bonnet bore due to thermal expansion of the bronze piston rod

bushing. The coefficient of thermal expansion for the bronze rod bushing w. : twice that -

of the steel of the valve bonnet. The bronze bushing would expand untilit twJe contact

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with the valve bonnet and then stress relieve. When the bushing cooled down to about

250 to 300 degrees Fahrenheit during plant shutdown, the bronze bushing would contract

to a diameter smaller than original. This would cause the piston rod bushing to collapse

onto the piston rod causing the valve to stick open. The letter recommended that the

licensee machine the bronze bushing outer diameter to a dimension of 3.992/3.993

inches. When questioned by the_ inspectors, the licensee provided documentation that

stated that all four Unit 2 FWO79 check valves were found stuck 100 percent open in

November of 1989. Operability Evaluation 89-128 documented that the root cause of the

sticking valves was insu'ficient clearance between the piston rod bushing outer diameter

and the valve bonnet bore.

The inspectors reviewed the most recent work package and identified that the piston rod

bushings for check valves 1FWO79A and D were replaced in April and May of 1997 with

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neither the inside nor the outside diameter of the bushing machined. The documentation

lacked sufficient data to determine the clearance between the piston rod bushing and the

piston rod. The licensee stated that check valves 1FWO79A and D would most probably

stick below 40 percent power based on predicted feedwater temperatures. The FWO79

check valves were relied upon in UFSAR, Chapter 15.2.8 *Feedwater System Pipe

Break," to provide immediate isolation of the steam generators to reduce the amount of

inventory loss prior to the closure of tha feedwater isolation valves. The licensee initiated

an Operability Evaluation 97163, which evaluated the three check valves sticking below

40 percent power. The licensee concluded that the feedwater sstem for both units was

operable based on the isolation capability of the feed isolation valve.

The inspectors reviewM BwMP 3305 087, Revision 5. The licensee included acceptance

criteria for the as found valve position but did not include steps to measure and record

the clearance between the piston rod bushing and the valve bonnet bore, and the

clsatance between the piston rod and the piston rod bushing.

DwAP 1250 2,' Deviation Reporting," Revision 2, Step C.1, defined a deviation as "a

departure from accepted equipment performance...which results in, or could, if

uncorrected, result in a failure of an item to perform as required by TS or approved

procedures." S%p C3.a.4 required that a person identifying a deviation initiate a deviation

report. Step C.3.d.1 b e equired that any additional corrective action required to

investigate, correct the condition, or to prevent the recurrence be determined and

specified. The licensee did not prepare a deviation report nor initiate corrective actions

thH would preclude recurrence of the condition wnere the Unit 2 main feed water check

v& *i stuck open.

As mentioned above, all four feedwater check val 9 on Unit 2 stuck open in 1989 due to

a valve design problem. The failure to take corrective actions to prevent recurrence of a

significant condition adverse to quality was a violat,on of 10 CFR Part 50, Appendix B,

Criterion XVi(50-456/97022 01(DRP); 50-457/97022 01(DRP)).

c. Conclugiqa

Ths licensee identified in 1989 that all four Unit 2 main feedwater check valves (FWO79A.

B, C, and D) had stized in an open position due to insufficient cleasances between critical

compnnents in the valve dampening mechanisms. The licensee did not change the

Maign of the valve, did not include work package instructions to machine the rod piston

bushing to the proper dimensions if replaced, did not include steps in the work package to

measure and record critical clearance parameters, and did not include as found

acceptance criteria in the work package instructions thct would identify a problem. The

inspectors identified in December 1997 that entical components in the Unit 1 FWO79A

and D check valve dampening mechanisms were replaced in May and April of 1997

respectively without being machined to th:, required clearances. The inspectors

concluded that the corrective actions taken because of the seizing of the FWO79 check

valve piston rods in 1989 were not adequate to prevent recurrence. A violation was

issued.

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M7 Quality Assurance in Malntenance Activities

M7.1 10 CFR 50.54ff) Letter Commitment Review

a. Inspection Scope (92902)

The inspectors reviewed the status of commitments pertaining to the Brr'1 wood Station

March 28,1997, response to the NRC's request for information purst a'. O

10 CFR 50.54(f). The following commitments related to work control were i aviewed by

the inspectors. The commitment numbers correspond to those used by the licensee in its

March 28,1997, response,

b. Observations and Findinal

b.1 Com_mitment 48: "A standard screening process has been put in place at all six

sitet w ensure maintenance *.vork is properly classified and prioritized."

The inspectors verified that a standard screening process was put in place at

Braidwood by interviewing the work control center supervisor, reviewing

NSWP.WM 08, " Action Request Screening Process," Revision 1, and attending a

daily screening meeting. The inspectors concluded that the commitment to

implement a standard screening process at Braidwood was satisfied and this item

is closed,

b.2 Commitment 49: " Work Planning n, being evaluated to identify inefficiencies in the

planning process that prevent work from being performed."

The inspectors verified that the evaluation of the work planning process was a

continuous process through an interview with the work control superintendent and

the work control center superviror. Braidwood station has a full time

representative assigned to the company's corporate office to evaluate the work

control process. The inspectors concluded that the commitment to evaluate the

work planning process at Braidwood was satisfied and this item is closed.

b.3 Commitment 50: *All sites are currently implemming a minimal work request

process which enhances job planning for minor work."

The inspectors venfied that a minimal work request process was implemented by

interviewing the work control superintendent and the work control center

supervisor, and by reviewing nuclear station work procedure NSWP WM-06,

" Minor Maintenance Process," Revision 1. The nuclear station work procedure

defined and established criteria for categorizing tool pouch and minor

maintenance. The inspectors concluded that the commitment to implement a

minimal work request process at Braldwood was satisfied and this item is closed,

b.4 Commitment 52: "The amount of emergent work completed by the Fix-It Now

(FIN) teams is measured to determine the effectiveness of the initiatives."

The inspectors reviewed the weekly report that compared emergent work tasks

performed by the FIN team versus the emergent work taska performed by the

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maintenance shops. The licensee used the information to determine the proper

size of the FIN team and also was able to determine that the amount of resource

loading for the regular maintenance crews was too high based on the amount of

amergent work that was performed by the shops. The inspectors concluded tb it

the commitment to measure the amount of emergent work completed by the Fl.

team to evaluate the effectiveness of work planning initiatives at Braidwood was

satisfied and this item is closed.

b.5 Commitment 225: "The Getting Work Done Plan used dedicated work teams (FIN

team and a work analyst team) to reduce the backlogs and improve sche %Ie

adherence on work tasks. The FIN team is estilized to protect execution of the

weekly schedule by assuming responsibility for all emergent work requirements

inat arise during the week."

The residents verified that a FIN team was implemented at Braidwood and work

request backlogs were significantly reduced. The percent completion of the

weekly schedule increased. However, the FIN team did not assume the

responsibility for all emergent work. The FIN team works the day shift only and

primarily performed jobs that could be completed in a single shift. Emergent work

that required multiple shifts to complete was performed by maintenance shop

personnel. The inspectoio concluded that the commitment to use dedicated work

teams to reduce work backlogs at Braidwood was satisfied and this item is closed.

c. Qpnclusion

The inspectors concluded that the licensee met Commitments 48,49,50,52, and 225

regarding work control initiatives.

M7.2 Non-Outaae Corrective Work Reauest Status Review

a. jntpection Scope (92902)

The inspectors reviewed the licensee's infermation on the non-outage corrective work

requect backlog and interviewed the work control superintendent and the work control

center supervisor.

b. Observations and Findinos

The number of non-outage corrective work requests was developed from the licensee's

electronic work control system, The licensee screened all action requests and assigned

each to a specific category. If the category data field was left blank, the computer

automatically assumed that the work was non outage corrective maintenance. Action

requests were not hand wr'. ten but entered into the computer by operations,

maintenance, or engineering personnel.

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, c. Conclusions

The inspectors concluded that the licensee accurately identified, quantified, tracked, and

reported the number of non outage corrective work requests reported to the NRC as

committed to in the Braidwood Station March 28,1997, response to the NRC's request

for information pursuant to 10 CFR 50.54(f).

M7.3 Mt.ejurement and Test Eouipment (M&TE)

a. Inspection Scope (62707)

The inspectors monitored the licensee's controls of M&TE. The inspectors reviewed

BwAP 400-4, * Control of Portable Measurement and Test Equipment," Revision 10E1.

, The inspectors monitored M&TE in use in the plant, as well as M&TE storage facilities.

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The inspectors also interviewed maintenance staff, system engineering, site engineering,

and operations personnel.

b. Observations and Findinal

BwAP 400 4, Step F.6.a.1.b stated that "The M&TE storage facility will be locked when

unmanned." The inspectors identified five occasions when this requirement was not

satisfied, including:

  • On November 26,1997, the inspectors entered the hot tool room in the auxiliar;

building. The inspectors identified numerous calibrated torque wrenches.

pressure gages and alignment tools that were left unlocked and unattended,

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con ary to the requirement of BwAP 400-4.

  • On Cecen,oer 1,2, and 3, ih6 inspectors entered the hot tool room and observed

additional examples of M&TE left unlocked and unattended, contrary to the

requirements of BwAP 400-4

  • On December 12, the inspector t.ntered the instrument maintenance department

tool room located in the turbine building. M&TE stored in this room was left

unlocked and unattended, contrary to regt'irements of BwAP 400-4.

The failure to follow Frocedure BwAP 400-4 is a violation of TS 6.8.1.a.

(50 456/97022 02(DRP); 50 457/07 22 02(DRP)) as described in the attached NOV.

c, Conclusions

The inspectors concluded that access to M&TE was not consistently controlled based on

finding M&TE storage locations unlocked and unattended, on five separate occasions,

which violated licensee M&l E storage control procedural requirements. A violation wcs

issued,

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111. Enalneerina

E2 Engineering Support of Facilities and Equipment

E2.1 Temporary Alterations

a. In1pection Scooe (37550)

The inspectors reviewed temporary alteration processes. The inspectors reviewed

documentation for several temporary alterations and performed plant walkdowns of

several temporary alterations. Temporary alterations were reviewed for compliance

with the UFSAR and TS requirements. The inspectors also reviewed Procedure

BwAP 2321 18. " Temporary Alterations," Revision 3E1.

b. Observations and Findinan

Review of the niorithly temporary altJration report issued on December 29,1997,

revealed that there were 19 documented temporary alterations in the plant. Eight

alterations had been in place for greater than 18 months. The report also showed that

plans were in place to remove all temporary alterations or to take necessary actions in

order to make the alteration a permanent modification. ('

The inspectors reviewed 10 CFR 50.59 safety evaluations for a sample of temporary

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alterations. The evaluations were performed correctly and referenced required licensing

and design documents. The inspectors performed a walkdown of temporary alterations

931010 and 93 2 019. The physicalinstallation of the alterations was in agreement with

the installation documentation.

The inspectors also looked for undocumented modifications to the plant while performing

routine plant walkdowns. Two unauthorized plant modifications were identified. Steel

buildings had been erected in the electrical penetration rooms for each unit. These

structures were called " Local Leak Rate Test shacks" because they were used to store

localleak rate test equipment. Although an exact date the steel buildings were installed

could not be determined, plant personnel stated they were built in the late 1980s.

Upon discovering the two steel buildings, the inspectors checked to see if the structures

were identified in plant documentation. UFSAR Section 1.2, Braidwood Fire Protection

Report Section 2.3.11.49, and Plant Drawings M 6, M 7, A 256, A 258, S 1298, and

S 1296 were reviewed. None of the documents included the structures. The inspectors

reported this to the licensee. Site engineering personnel determined that the structures

should not be in place. Since the buildings were installed close to numerous scfety-

related components, site engineering completed Operability Evaluation 98-002. The

inspectors reviewed the evaluation for both buildings and considered it acceptable.

Both buildin9s were removed as of January 22. Site engineering management stated that

site engineers were performing a review of plant facilities in order to identify any other

unauthorized modifications. The failure to perform design analysis and to document the

installation of the structures in the electrical penetration rooms for each unit is a violation

of 10 CFR Part 50, Appendix B, Criterion 111, Design Control (50-456/9702203(DRP);

- 50-45767022-03(DRP)).

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c. Conclusions

The inspectors concluded that the licensee made progress toward reducing the total

number of temporary alterations. System and site engineering personnel were tracking

open temporary alterations as listed in the associated documentation. The inspectors

conc!uded that plant procedures related to the temporary alteration process were followed

for known plant alterations. However, the inspectors identified two unauthorized

modification: that were in place for several years but were not identified in plant design

documentation. A violation was issued.

E7 Quality Assurance in Engineering Activities

E7.1 10 CFR 50.54fD t.etter Commitmed RdY.itW

a. Inspection Scope (9290.3_)

The inspectors reviewed the status of vommitments pertaining to the Braidwood Station

March 28,1997, response to the NRC's reqvsst for information pursuant to

10 CFR 50.54(f). The following commitments related to advanced engineering and

configuration management training were reviewed by the inspectors. The commitment

number corresponds to those used by the licensee in their March 28,1997, response.

b. Observations and Findinal

Commitment 24: ' Additional training will be conducted to address identified areas for

improvement such as design basis adherence, configuration management

implementation, operability determinations, and safety evaluation preparation."

The inspectors interviewed the supervisor of the corporate design basis programs

department to determine the scope of the training on safety evaluation preparation and

who would be trained. The supervisor stated that advance training in 10 CFR 50.59

safety evaluation preparation would be conducted. This training will be completed in the

summer of 1998 and will inciude information on design basis definition and adherence,

and operability determination preparation. The primary target group for the training would

be engineers with at least two years experience. The strategy for the training was to

increase the knowledge level of about 30 to 40 engineers at each station and upgrade

( procedures at each station to include elements of the training. In mid 1998, the training

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for the rest of the engineering staff would include the 10 CFR 50.59 pret. aration

procedural changes. The inspectors reviewed a course book for the training.

The inspectors also interviewed the supervisor of the corporate configuration

management department to determine the scope of the training on configuration

management and who would be trained. The supervisor stated that the training was

targeted primarily for operators and maintenance workers that had the opportunity to

make plant changes through their normal course of work. The training was designed to

define what a plant change was, the importance of writing problem identification forms

when changes were identified, and what the roles of operators and maintenance workers

were in maintaining plant configuration control. The training was completed at Braidwood

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in September 1997 for about 133 operators and 247 maintenance workers. The

inspectors reviewed the training material and determined that the training given met the

commitment.

c. Conclusion

The inspectors concluded that Commitment 24 to conduct additional training on identified

areas for improvement such as design basis adherence, configuration management

implementation, operability determinations, and safety evaluation preparation at

Braidwood was satisfied and this item is closed.

IV. Plant Support

R7 Miscellaneous Radiation Protection and ControlIssuos

R7.1 Percent Contaminated Souare Footajle Review

a. Ingection Sggne f71750)

The inspectors reviewed the licensee's information on the percent contaminated square

footage and interviewed radiation protection personnel,

b. Observations and Findinal

The percent of contaminated square footage was calculated from a list of all auxiliary

building and fuel handling building rooms and the square footage of each room. The

contaminated areas in the plant were estimated and compared to the total amount of

square footage. Some areas, such as the containment, were exempted from the

computation. The inspectors reviewed the exempt areas and the basis for why they were

considered exempt and had no concerns. The inspectors also inspected the plant and

had no concerns with the amount of square footage the licensee considered

contaminated.

c. Conclusions

The inspectors concluded that the licensee accurately identified, quantified, trackad, and

reported the percent of contaminated square footage reported to the NRC as committed

to in the Braidwood Station March 28,1997, response to the NRC's request for

information pursuant to 10 CFR 50.54(f).

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F4 Fire Protection Staff Knowledge and Performance

F4.1 Fire Drill

a. Inspection Scope f71750)

The inspectors observed a fire dril! at the plant. The inspectors also attended the fire drill

critique session.

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b. Qt?servations and Findinas

At 11:05 a.m. on December 31, the licensee staged a fire drillin the turbine building

trackway. The drill scenario was a simulated forklift fire and an assumed out of service

fire sprinkler system for the affechd area.

The drill was announced on the plant page system at 11:06 a.m. The fire chief arrived on

the scene at 11:08 a.m. and the full fire brigade was on the scene at 11:12 a.m. All fire

brigade members reported to the scene wearing fire turn out gear. One fire brigade

member also reported with a self contained breathing apparatus (SCBA). Several

additional operators also reported to the scene in order to provide support for the fire

brigade members. Security personnel were at the scene to p ovide access control.

.

Actions simulated were appropriate in order to control the fire and to limit the effects of

the fire on plant equipment. The fire chief and operations supervisors assessed possible

problem areas. All equipment brought to the fire was observed to be in good condition

and all inspections (when required) were up to date. Fire personnel brought additional

hoses, SCBAs, fire extinguishers, and a foam unit to the scene. Following the drill, all

equipment was returned to storage.

Following the drill, the fire marshail presented a critique session for all personnel that

responded. Potential areas for improvement and the drill scenario were discussed. Fire

brigade members and operating personnel actively participated in the meeting.

c. Conclusioni

Plant personnel response to the fire drill was prompt and thorough. Fire brigade

members performed (or simulated) all tasks well with a positive attitude.

V. Manaaement Mettinas

X1 Exit Meetinry Summary

The inspectors presented the inspection results to members of licensee management at

the conclusion of the inspection on January 26,1998. The licensee acknowledged the

findings presented. The inspectors asked the licensee whether any materials examined

during the inspection should be considered proprietary. No proprietary information was

identified.

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PART.AL LIST OF PERSONS CONTACTED

Licensee

T. Tulon, Site Vice President

  • K. Schwartz, Station Manager
  • R. Wegner, Operations Manager
  • R. Byers, Maintenance Superintendent

A. Haeger, Health Physics and Chemistry Supervisor

  • R. Graham, Work Control Superintendent
  • T. Simpkin, Regulatory Assurance Supervisor
  • C, Dunn, System Engineering Supervisor

l - 'J. Meister, Engineering Manager

j *B. Boyle, Fire Marshal .

'J. Nalewajka, Integrated Safety Engineering Group 1

  • J. Neyhart, Shift Manager ,
  • C. Herzog, Executive Assistant
  • M. Cassidy, Regulatory Assurance . NRC Coordinator

NRC

  • M. Jordan, Chief, Reactor Projects Branch 3
  • C. Phillips, Senior Resident inspector
  • J. Adams, Resident inspector

D. Pelton, Resident inspector

IDNS

  • T. Esper
  • Denotes those who attended the exit interview conducted on January 26,1998.

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INSPECTION PROCEDURES USED

IP 37550: Onsite Engineering

i IP 61726: Surveillance Observations

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IP 62707: Maintenance Observation

IP 71707: Plant Operations ,

l lP 71750: Plant Support Activities

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IP 92901: Followup Plant Operations

IP 92902: Followup Plant Maintenance ,

IP 92903: Followup Engineering

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i ITEMS OPENED, CLOSED, AND DISCUSSED

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Opened  ;

50-456/97022 01; 50 457/97022 01 VIO failure to take corrective actions

50-456/97022 02; 50 457/97022 02 VIO failure to follow procedure

50 456/97022 03; 50-457/97022 03 VIO failure to perform design analysis

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LIST OF ACRONYMS USED  !

CNOO Chief Nuclear Operating Officer

CFR- Code of Federal Regulations

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FIN Flx It Now

GSEP Generating Station Emergency Plan  !

IPA Infrequently Performed Activity - *

M&TE Measuring and Test Equipment

NRC Nuclear Regulatory Commission i

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NRR Nuclear Reactor Regulations

NSO Nuclear Station Operator .

PDR Public Document Room

PlF Problem Identification Form

RP&C Radiological Protection & Chemistry

SCBA Self contained Breathing Apparatus

SOS Shift Operations Supervisor

TS Technical Specification

UFSAR Updated Final Safety Analysis Report .  ;

US Unit Supervisor

VIO Violation

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