ML20216B076

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Insp Repts 50-456/98-02 & 50-457/98-02 on 980127-0309. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support
ML20216B076
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 04/08/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20216B037 List:
References
50-456-98-02, 50-456-98-2, 50-457-98-02, 50-457-98-2, NUDOCS 9804130362
Download: ML20216B076 (24)


See also: IR 05000456/1998002

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U.S. NUCLEAR REGULATORY COMMISSION

REGION lil

Docket Nos: 50-456; 50-457

Licence Nes: NPF-72; NPF-77

Report No: 50-456/98002(DRP); 50-457/98002(DRP)

Licensee: Commonwealth Edison (Comed)

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Facility: Braidwood Nuclear Plant, Units 1 and 2

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Location: RR #1, Box 84

Braceville,IL 60407

Dates: January 27,1997, through March 9,1998

Inspectors: C. Phillips, Senior Resident inspector l

J. Adams, Resident inspector i

D. Pelton, Resident inspector

T. Esper, Illinois Department of Nuclear Safety

Approved by: Michael Jordan, Chief

Reactor Projects Branch 3

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PDR ADOCK 05000456

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EXECUTIVE SUMMARY

Braidwood Nuclear Plant, Units 1 & 2

NRC Inspection Report No. 50-456/98002(DRP); 50-457/98002(DRP) -

This inspection included aspects of licensee operations, maintenance, engineering, and plant

support. The report covers a six-week period of resident inspection.

Operations

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The inspectors concluded that the quality of supervision declined during the Unit 2 startup

from observed performance during previous reactor startups. This conclusion was based

on operations supervision not identifying an error made by an operator during the review .

of a shutdown margin calculation; supervision's failure to direct the retum to service of

the boron dilution prevention system after shutting down the reactor which is required by

Technical Specification; and supervision not verifying the proper steam supply to the

gland seal steam system. However, the inspectors did recognize the attempt by licensee

management to improve operational performance by dedicating an operator and

supervisor to monitor reactivity changes, and by developing a well prepared pre-evolution

briefing. The problems with supervisory oversight were identified and corrected by the

licensee and therefore, a non-cited violation was issued. (Section 01.1)

  • The inspectors concluded that licensee management demonstrated a good safety focus

during the paralleling of the steam-driven feedwater pumps during the Unit 2 reactor

startup. The 28 steam-driven main feedwater pump would not respond to automatic or

manual controls due to a failed low pressure govemor. The shift manager ensured

procedural compliance and maintained excellent control of the troubleshooting evolution

until the problem was resolved. (Section 01.2)

- The inspectors concluded that the as-found configuration of the Essential Service Water

(SX) system was consistent with system drawings, Updated Final Safety Analysis Report '

system description, Technical Specifications, mechanical lineups, and electrical imoups

with a few minor exceptions. The inspectors determined that the exceptions did not

affect the operability of the Unit 2 SX system. The inspectors concluded that the SX .

- system procedures were well-written and contained sufficient guidance for personnel to

complete the activity covered by the procedure. The material condition of the system was

good. The heat exchanger inspections, heat exchanger performance tests, and blocide

' injection into the essential service water system were being scheduled, performed, and ,

documented to meet Generic Letter 89-13 commitments. (Section 02.1)

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Maintenance

- During surveillance testing, operations personnel and the involved system engineer were

knowledgeable of system operation, testing setup, and testing methods. Operators

identified and resolved potential problems between plant configuration and procedural l

guidance prior to starting the test. Surveillance tests were performed in accordance with

plant procedures and all acceptance criteria were met. (Section M1.1)

. Technical Specification and American Society of Mechanical Engineers surveillance

requirements for the essential service water system were being met by the performance

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of surveillance tests. However, the inspectors identified that safety-related valves were

manipulated during the performance of Unit 1 and Unit 2 Technical Staff Surveillance

tests and independent verifications of proper system alignment were not subsequently

conducted as required by Braidwood Administrative Procedure 100-18. A violation was

issued. (Section M3.1)

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The inspectors concluded that licensee management demonstrated a good safety focus

in addressing problems with the maintenance and test equipment program, originally

identified by the inspectors in inspection Report No. g7022. The licensee established a

team of station employees to address these problems, and the team took a broad look at

the problem and was able to identify additional concems that needed to be resolved.

(Section M 8.1)

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The inspectors concluded that operability determinations regarding the reactor coolant

system leakage calculations and the automatic operation of the pressurizer power

operated relief valves reflected good engineering judgement and safety focus.

(Section E3.1)

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The inspectors performed a review of post-modification and surveillance testing

procedures for a modification that installed a pressure control and fire damper assembly

between the auxiliary and turbine buildings and concluded that all acceptance criteria

associated with those procedures were met. The post-modification test procedure was

well-written and verified that the modification performed as designed. The inspectors

concluded that the pressure control and fire damper assembly properiy controlled the

differential pressure between the auxiliary and turbine buildings. (Section E3.2)

  • The inspectors concluded that the licensee was not aware of 134 engineering requests in

its database that had not been prioritized. The inspectors also concluded that 253 high

priority engineering requests had no due dates assigned. The 253 high prionty

engineering requests without due dates assigned made up about 54 percent of the high

pflority backlogs. With this high percentage, the inspectors concluded that the number of

high priority overtiue engineering requests was not a good performance indicator of

backlog reduction which was a performance indicator committed to in the licensee's

March 28, igg 7 response to the NRC request for information pursuant to

10 CFR 50.54(f). (section E7.1)

Plant Support

- The inspectors concluded that the As-Low-As Reasonably-Achievable and Heightened

Level of Awareness briefings for the transfer of resin were pr'speriy performed and

documented. The inspectors concluded that the auxiliary building 383 foot elevation

access points to the radwaste tunnel were properly posted and access was prohibited by

locked doors. Post-transfer radiation surveys were completed and posted.

(Section R1.1)

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The radiation preiedien department's control of radiation monitoring devices and postings

was good, instruments and postings were controlled in accordance with plant

procedures. (Sections R2.1 and R2.2)

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The inspectors concluded that the continuous fire watch requirament for the Unit i lower

cable spreading room was not met at least three times on January 29. The inspectors

concluded that the fire watch was not adequately supervised because the instructions to

the individual assigned to the fire watch were unclear, the stated post-order requirements

were not enforced, and supervisory review of the watch documentation as well as

observation of the fire watch did not identify these problems. A violation was issued.

(Section F1.1)

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Report Details

Summary of Plant Status

Unit 1 entered the inspection period at full power and remained at or near full power for the entire

period Unit 2 entered the inspection period in a hot standby condition. While shut down, repairs

were made to feedwater check valves and relief valves. Unit 2 was synchronized to the grid on

February 4. Unit 2 remained at or near full power for the remainder of the period.

I. Operations

01 Conduct of Operations

01.1 Unit 2 Restart From Forced Outane 4

a. Inspechon Scope (71707)

The i t:,pectors reviewed Unit 2 Braidwood General Operating Procedure (2BwGP) 100-2,

" Plant Startup," Revisions 10 and 10E1; Unit 2 Braidwood Operating Surveillance

Procedure (2BwOS) 1.1.1.1.e-1, " Unit Two Shutdown Margin Daily Verification During

Shutdown" Revision 11E1; and 2BwGP 100-3, " Power Ascension," Revision 13E1. The

inspectors reviewed Onsite Review item 98-015, on the aborted startup at Unit 2 entitled,

"Startup of Unit 2 following forced outage A2F30 was aborted due to exceeding 500

percent millitho (pcm) difference between the estimated cntical condition and the entical

condition predicted by the eight-fold methodology." The inspectors observed portions of

the startup.

b. Observations and Findinas

The inspectors observed that the communications between operators, nuclear engineers, .

and supervisors were clear both during the pre-evolution briefings and during the conduct d

of the startup. A nuclear station operator and a senior reactor operator were assigned

exclusively to monitor plant reactivity changes. In addition to the shift manager and the

unit supervisor, senior operstm's department management was present for all portions

of the startup observed by the inspectors. The inspectors observed portes of pro-

evolution briefings given by licensee management prior to the startup. The quality of the

briefings was excellent. Procedural steps and contingencies for potential problems with

the startup were covered in detail. All necessary personnel were in attendance.

During an attempt to pull control rods to achieve criticality on February 3, the nuclear

engineers predicted that the unit would reach criticality greater than 500 pcm below the

estimated condition for criticality. The withdrawal of control bank rods was stopped and

control bank rods were reinserted as required by BwGP 100 2, Step F.24. The insertion

of control rods resulted in the change of Unit 2 operational modes from Mode 2 (startup)

to Mode 3 (hot standby). During Mode 2, both trains of the boron dilution prevention

systems were bypassed as required by plant procedure rendering them inoperable.

Technical Specificate (TS) 3.1.2.7 stated that with the unit in Mode 3 and both boron

dilution prevention subsystems inoperable, within one hour, and at least once every 12

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hours thereafter, verify the boron dilution prevente system valves are closed and

secured in position and verify compliance with the shutdown margin requirements of

TS 3.1.1.1 or 3.1.1.2 as applicable. The licensee identified that the unit was retumed to

Mode 3 at 12:00 p.m., but the boron dilution prevention system was not retumed to

service until 2:4g p .m., nor were the boron dilution prevention system isolation valves

verified to be in the correct position The licensee reported the event in Licensee Event

Report 50-457/98002. The inspectors reviewed the report and noted that the licensee

identified personrMI error and an inadequate procedure as the causes of the event. The

licensee identified the following corrective actions to prevent recurrence:

Operating personnel were briefed on this event, which included management

expectations regarding conservative decision making, TS compliance, delayed

startups, and the operation of the boron dilution prevention system; and

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Procedures 1/2BwGP 100-2 will be revised to clarify the requirements for the

boron dilution prevention system when a delay in startup is encountered, to

ensure the requirements are met before startup resumption following a delay, and

to address restoration of the boron dilution prevention system when proceeding to

shutdown per 1/2BwGP 100 5, " Plant Shutdown and Cooldown", due to a

termination in the startup.

The inspectors noted that the licensee's corrective actions addressed the causes of the

event. The inspectors had no further concoms.

The licensee's nuclear fuel services organization performed a root cause analysis of why

the estimated critical position was off by such a large margin. The inspectors reviewed

the onsite review document and had no concems. The inspectors observed that the

subsequent startup actual critical condition was within the 500 pcm band of the estimated

critical condition.

The licensee identified that shutdown margin calculation Surveillance 2BwoS 1.1.1.1.e-1,

performed prior to withdrawal of the shutdown rod banks on February 3, was conducted

incorrectly. The nuclear station operator made a sign convention error in the calculation.

The senior reactor operator performed an independent verification of the calculation The

senior reactor operator stated to the inspectors that he made the same error as the

nuclear station operator. The licensee determined that adequate shutdown margin did

axist at the time of the original error. The licensee also identified that the steam supply to

the gland seal had not been transferred from the auxiliary boiler to the operating unit as

required by 2BwGP 100-3, Step 31. The operations field supervisor had erroneously

stated that the step was completed and the nuclear station operator had signed off the

step in the startup procedure.

' The failure to restore the boron dilution prevention system to service within an hour of

retuming Unit 2 to Mode 3 was a violation of TS 3.1.2.7. This non-repetitive, licensee-

identified and corrected violation is being treated as a Non-Cited Violation, consistent with

Section Vll.B.1 of the NRC Enforcement Policy (50-457/98002-01(DRP)).

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c. Conclusion

The inspectors concluded that the quality of supervision declined during the Unit 2 startup

from observed performance during previous reactor startups. This conclusion was based

on supervision not identifying an error made by an operator during the review of a

shutdown margin calculation; supervision's failure to direct the retum to service of the

boron dilution prevention system which is required by Technical Specification, after

shutting down the reactor and supervision not verifying the proper steam supply to the

gland seal steam system. However, the inspectors did recognize the attempt by licensee

management to improve operational performance by dedicating an operator and

supervisor to monitor reactivity changes, and by developing a well prepared pre-evolution

briefing. The problems with supervisory oversight were identified and corrected by the

licensee and therefore, a non-cited violation was issued.

01.2 2B Feedwater Pump Control Failure

a. Inspection Scope (71707)

The inspectors observed portions of the evolution involving the changing of main

feedwater pumps during the Unit 2 reactor startup. The inspectors reviewed Temporary

Procedure Change 7536 to Braidwood Operating Procedure (BwOP) FW-02, " Shutdown

of A Turbine Driven Main Feedwater Pump," Revision gE1.

b. Observations and Findinos

The 2B main feedwater pump had a failed low pressure govemor that prevented load

sharing between the 28 and 2C foodwater pumps, this in tum prevented power limreases

above 60 percent. The inspectors observed that the shift manager maintained excellent

step-by-:teo rt,ntrol of the trouble shooting and held several crew briefings discussing the

status of efforts to identify the problem and to ensure all members of he crew were

aware of their responsibilities. The operators identified the problem with the 2B

feedwater pump. The procedure to secure a foodwater pump, SWOP FW-02, was

changed appropriately to allow for a manual isolation of steam to the low pressure

govemor,

c. Conclusion

The inspectors concluded that licensee management demonstrated good safety focus

during the paralleling of the steam-driven feedwater pumps during the Unit 2 reactor

startup. The shift manager ensured procedural compliance and maintained excellent

control over the trouble shooting in the identification and resolution of a failed low

pressure govemor for the 2B steam-driven feedwater pump.

01.3 Out-of-Service Review

a. Inspection Scope (71707)

The inspectors reviewed two safety-related out-of-services (OOSs) in effect and an OOS

recently cleared. The inspectors also interviewed operations personnel in the work

control conter about the administration of the OOS program.

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~ b. Observations and Findinas )i

The inspectors reviewnd safety-related OOSs 970000723 and 970000741 that were in

effect. The OOSs woro ,Moperty prepared and authorized. All components listed on the

OOSs were in positions required by the OOSs and OOS cards were affixed to the

components.

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The inspectors reviewed recently cleared safety-related OOS 980001103. All l

components were retumed to the required position listed or the 008. AM OOS tags were

removed from components,

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- c. Conclusion

The OOss on safety-related components were property placed and removed.

Documentation for the reviewed OOSs was complete.

.O2 Operational Status of Faollities and Equipment

O2.1 Unit 2 Essential Service Water (SX) System Welkdown

a. hsDedion scope (71707)

The inspectors performed a detailed walkdown of the accessable portions of the

Unit 2 SX system. As part of the walkdown, the inspectors reviewed the following

documents:

Piping and Instrumentation Diagrams (P&lD) M-42, M-126, and M152;

BwOP SX-E2, " Electrical Lineup - Unit 2 Essential Service Water System,"

Revision SE2;

BwoP SX-M2, " Operating Mechanical Lineup - Unit 2 Essential Service Water

System," Revision 13E2;

  • BwoP SX-M2, " Operating Mechanical Lineup - Unit 2 Essential Service Water

System," Revision 12 (Completed 12/19/97);

  • Braidwood TS, Section 3/4.7.4
  • BwOP SX-3, " Essential Service Water System Fill and Verd," Revision 4;
  • BwoP SX-3, " Essential Service Water System Drain," Revision 3; and

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BwAP 340-2, "Use of Mechanical and Electrical Lineups," Revision 15E1.

b. Observations and Findmos i

The inspectors performed a detailed walkdown of the accessable portions of the

UnN 2 SX system. As part of this detailed inspection, the inspectors compared the as-

found system configuration to the system drawings, UFSAR system description, TSs, and

mechanical and electrical lineups. The inspectors determined that the system was

' aligned in accordance with the mechanical lineup of BwoP SX-M2, with a few minor

exceptions. The inspectors evaluated the identified exceptions and determined that they

had no affect on the operability of the Unit 2 essential service water system. The

inspectors discussed each exception with operations personnel and were told that each  ;

problem would be corrected. i

The inspectors performed a review of operating procedures for the startup, shutdown,

system fill and vent, and system drain of the Unit 2 SX system. The inspectors

determined that the procedures were well written and contained sufficient guidance for

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e personnel to complete the activity addressed by the procedures.

The inspectors examined the material condition of SX system components and reviewed

a list of Unit 2 SX problems identified by the licensee. The material condition problems

observed by the inspectors were few in number, minor, identified by the licensee, and

entered in the licensee's corrective action program.

The inspectors evaluated housekeeping and environmental condihons to assess their

' impact on Unit 2 SX system performance. The inspectors determined that the

housekeeping efforts were effective since no accumulation of trash, debris, or

combustibles was found during the walkdown. The SX system components were clean

with no accumulation of dirt, grease, or oil. Motor cooling vents were clean and free from

obstruction. The inspectors observed very little scaffolding in the vicinity of SX system

components. The scaffolding that was present was property documented and did not

interfere with the SX system operation.

The inspectors reviewed the licensee's commitments to Genenc Letter 89-13, " Service

Water Problems Affecting Safety-related Equipment," and the licensee's program to

monitor the condition and performance of heat exchangers served by the SX system.

The inspectors discussed the operation of the blocide injection system with the system

engineer, examined documentation of safety-related heat exchanger inspections, and j

verified that the Unit "0" component cooling water heat exchanger was aligned to biocide

treated SX flow on a periodic basis. The inspectors did not find any heat exchanger

inspection documentation that identified a significant amount of heat exchanger fouling.

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c. Conclusion

The inspectors concluded that the as-found configuration of the Essential Service Water

(SX) system was consistent with system drawings, Updated Final Safety Analysis Report

system description, Technical Specifications, mechanical lineups, and electrical lineups

with a few minor exceptions. The inspectors determined that the exceptions did not

affect the operability of the Unit 2 SX system. The inspectors concluded that the SX

system procedures were well-written and contained sufficient guidance for personnel to

complete the activity covered by the procedure. The matetial condition of the system was

good. The heat exchanger inspections, heat exchanger performance tests, and blocide

injection into the essential service water system were being scheduled, performed, and -

documented to meet Generic Letter 8g-13 commitments.

07 Follow up Plant Operations (92901)

07.1 10 CFR 50.54m Letter Commitment Review

a. Inspection Scope

The inspectors reviewed the status of commitments pertaining to the Braidwood Station

March 28,1997, response to the NRC's request for information pursuant to

10 CFR 50.54(f). The following commitments related to periodic management review

meetings were reviewed by the inspectors. The commitment numbers correspond to ,

those used by the licensee in their March 28, igg 7, response.

' b. Observations and Findinos

b.1 Commitment 68 and 69 These commitments discussed the use of peer groups

to address common problems between sites and to ensure a uniform method of

addressing activities at the Comed stations.

The inspectors interviewed the station manager and the regulatory assurance

supervisor. Almost all sanior station managers were involved in peer groups and

dedicate from one to two days per month working on peer group issues. Peer

group efforts resulted in the development of 28 nuclear station procedures,10 of

which have been implemented.

b.2 Commitment 95: "We are also taking special measures to assess and monitor

our performance to ensure that areas of weakness indicated by the I.aSalle and

Zion operational events are not present or are addressed at all of our nuclear

stations."

The licensee's response stated there would be three methods used to monitor

operations performance. The first was the use of performance indicators in

addition to the ones reported to the NRC. Examples included wrong unit /wmng

train events, control room caution tags, and lit annunciators. The second was an

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evaluation of the control room by the nuclear support group vice president. Third

was an evaluation of the control room by a team of peers from Byron, Dresden,

Quad Cities, and Braidwood.

The inspectors reviewed the performance indicators, the visit report from the vice

president, and the peer team report. The performance indicators demonstrated

that Braidwood had a greater number of OOS errors and wrong

unit / train / component events for 1997 than the other Comed stations. The

licensee initiateo self-assessments in those areas because of these perfonnance

indicators. The licensee, in addition to the single vice president visit, has had

visits from other station and corporate vice presidents to observe control room

performance. The shift operations supe visor stated that these visits occur on a

near weekly frequency. An operations department policy memorandum to -

formalize how often control board panel walkdowns should occur was changed as

a result of these visits. Licensee management took several actions based on the

results of the peer visit comments. For example, all operations department

personnel were required to watch a video tape of the NRC augmented inspection

team exit and some operations department personnel attended training

specifically on the Zion event.

c. Conclusion

The inspector s concluded that the licensee met commitments regarding peer group

implementation and actions to be taken to monitor operations performance.

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Commitments 68,69, and 95 are closed.

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11. Maintenance

M1 Conduct of Maintenance

Mti Surveillance Observation (61726)

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a. Inspection Scope

The inspectors observed the performance of all or parts of the following surveillance

tests. The inspectors also reviewed plant equipment and surveillance testing activities I

against the UFSAR descriptions and the TSs.

  • 2BwVS 5.2.f.3-2, "ASME (American Society of Mechanical Engi:wers]

Surveillance Requirements for Residual Heat Removal Pump 2RH01PB,"

Revision 4E1;

  • 2BwoS 3.2.1-3, " Unit Two Under voltage Simulated Start of the 2A Auxiliary

Feedwater Pump Monthly Surveillance", Revision OE1;

a BwOS 6.1.7.3-1, " Primary Contain fype C Local Leak Rate Tests of

Containment Purge Supply isolation Va!ves (VG)," Revision OE1;

- 2BwOS3.2.1-941, " Unit Two Quartetty Slave Relay Surveillance (Train A - K520

and 633)", Revision 2E2;

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2BwoS 3.2.1-802, " Unit Two ESFAS (Emergency Safety Features Actuation

System) Instrumentation Slave Relay Surveillance (Train A Automatic Safety

injection - K804)", Revision E1; and

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BwAP 100-12," Human Performance Awareness of Pre-Job Briefing / Meetings and

Self-Checking". Revision 5.

b. Observations and Findinos

The inspectors observed pre-job briefings for the surveillance tests which included job

scope, purpose, individual responsibilities, safety hazards, As-Low-As-Reasonably.

Achievable (Al. ARA) standards, communication of expectations, contingency actions,

human error traps, acceptance criteria, and lessons leamed from previous surveillance

tests. Emphasis was placed on self-checking.

c. Conclusion

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During surveillance testing, operations personnel and the involved system engineer were l

knowledgeable of system operation, testing setup, and testing methods. Operators

identified and resolved potential problems between plant configuration and procedural

guidance prior to starting the test. Surveil;ance tests were performed in accordance with

plant procedures and all acceptance criteria were met.

M3 Maintenance Procedures and Documentation

M3.1 Unit 2 Essential Service Water System Walkdown

a. Inspection scope (61726)

As part of a detailed walkdown of the accessable portions of the Unit 2 SX system, the

inspectors performed a review of the following completed surveillance test procedures:

  • 2BwOS 0.5.SX.1, "American Society of Mechanical Engineers (ASME)

Requirements for Essential Service Water Valves," Revision 2

(Completed 1/21/98);

Surveillance," Revision OE1 (Completed 11/22/97);

  • 2BwCS SX - Q1, " Unit 2 Essential Service Water System Manual Ball Valve Cycle

Quarterty Surveillance," Revision 1E1 (Completed 10/13/97 and 12/26/97); i

+ 2BwVS 0 5-3.SX.1-1, "ASME Surveillance Requirements for 2A Essential Service

Water Pump," Revision 1E1 (Complete 10/10/97 and 12/19/97);

  • 2BwVS 0.5 3.SX.1-2, "ASME Surveillance Requirements for 28 Essential Service g

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Water Pump," Revision 1E1 (Complete 10/21/97 and 1/5/98);

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ASME Pump Trending Data for the 2A and 2B Essential Service Water Pumps

(4th Quarter 1995 Through 3rd Quarter 1997);

ASME Valve Trondmg Data for 2SX005,2SX016A and B,2SX027A and B,

2SX112A and B, 2SX114A and B,2SX169A and B,2SX173, and 2SX178

(1st Quarter 1996 Through 3rd Quarter 1997); and

. BwAP 100-18. " Braidwood Station Independent Verification Procedure,"

Revision 3.

b. Observations and Findinas

The inspectors reviewed completed surveillance test procedures and ASME pump and

valve performance data. The inspectors noted that all the surveillance test procedures

reviewed were complete and were being performed at the proper frequency, and that the

licensee was property documenting that the system acceptance criteria were being

satisfied. Step E.1.d, of BwAP 100-18, Revision 3, states, in part, that independent

verifications of proper system alignment shall be required during the performance of

safety-related surveillance tests in which valves are repositioned. However, on February

26, the inspectors identified that Step F.1.4 of 2BwVS 0.5-3.SX.1-1 and 2BwVS 0.5-

3.SX.1-2 directed operators to stroke 2SX2179NB, the isolation valves for the 2N2B SX

pump lube oil cooler, and 2SX2180NB, the isolation valves to the cooling water inlet tc

the 2NB SX pump lube oil heat exchanger; and that Step F.1.7 of 2BwVS 0.5-3.SX.1-1

and 2BwVS 0.5-3.SX.1-2 directed operators to close 2SXO46NB,2N2B SX room ar.d

lube oil cooler heat exchanger outlet valves; but failed to stirect operators to perform the

required independent verification.

The licensee issued Problem identification Form # A-1998-00756 to document the  !

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problem and initiate corrective actions. As part of the detailed walkdown, the inspectors

verified that the valves were in their correct position.

Technical Specification 6.8.1.a states, in part, that written procedures shall be .

established, implemented, and maintained covering the applicable procedures )

recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. I

Regulatory Guide 1.33, Appendix A, Section 1.c, states that thors shall be administrative

procedures for equipment control of safety-related systems, the failure to follow BwAP

100-18, Revision 3, was a violation of TS 6.8.1.a. as described in the attached NOV

(50-456/98002-02(DRP); 50-457/98002-02(DRP)).

c. Conclusions

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Technical Specific 4;on and American Society of Mechanical Engineers surveillance l

requirements for the essential service water system were being met by the performance

of surveillance tests. However, the inspectors identified that safety-related valves were

manipulated during the performance of Unit 1 and Unit 2 Technical Staff Surveillance

tests and independent verifications of proper system alignment were not subsequently

conducted as required by Braidwood Administrative Procedure 10018. A violation was

issued.

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M8 Follow up Maintenance (92902)

M8.1 (Open) Violation 50-456/97022-02(DRP): 50-457/97022-02(DRP): This violation was

issued in inspection Report No. 97022 for the failure to follow procedures regarding the  ;

control of access to maintenance and test equipment. The inspectors reviewed problem

identification form (PlF) A1998-00587 and interviewed the maintenance staff supervisor. i

in response to the violation, the licensee formed a team of station employees to address i

the licensee's need to better control maintenance and test equipment. Braidwood l

Administrative Procedure (BwAP) 400-4, " Control of Portable Measurement and Test

Equipment," Revision 10E1, requimd that when test equipment was sent offsite to be 1

calibrated and was found to be out-of-tolerance, an evaluation of the system or l

equipment that was measured or tested with the out-of-tolerance test equipment, was to ,

be performed. In accordance with SWAP 400-4, the evaluation at the discretion of the i

station maintenance and test equipment coordinator and had 90 days after that to i

complete it. The team identified that there was a backlog of about 75 evaluations '

needing to be completed. The entire backlog of evaluations was addressed and i

completed by February 13. Some field instruments had to be rechecked, but none were i

found to be out-of-calibration. The licensee planned to change the evaluation process to

shorten the time requirement for conducting the evaluation, but this had not been

accomplished by the end of the inspection period. This violation will remain open pending

completion oflicensee actions.  ;

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M8.2 (Closed) Violation 50-456/95015-03: 457/95015-03(DRP): As a result of an inspection  !

conducted from October 1 through November 14,1995, the inspectors identified a

violation of requirements contained in BwAP 100-21, " Foreign Material Exclusion, (FME)" l

Revision 1.0. the inspectors reviewed the corrective actions taken by the licensee in I

response to this violation. The licensee implemented a new corporate procedure, l

Nuclear Station Work Procedure (NSWP) A-03, " Foreign Material Exclusion," Revision 0,  !

and increased the emphasis on proper FME controls during training. The inspectors also  ;

reviewed the FME related problems documented since the licensee completed its l

corrective actions for the violation. Although actions taken by the licensee have not  !

completely eliminated FME problems, the total number and severity of FME related i

problems has decreased and the inspectors have not noted FME problems during recei.t

maintenance related inspections. This violation is closed.

111. Ennineerina

E3 Engineering Procedures and Documentation  ;

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E3.1 Operability Determinations

a. Inspection Scope (37551)  !

The inspectors reviewed the following documents: ,

  • Operability Evaluation 97-159, "UFSAR assumes the pressurizer power operated

relief valves are manually opened during an inadvertent safety injection";

i

- Operability Evaluation 98-005, " reactor coolant svstem leak rate calculatk.a may

be non-conservative due to crediting non-reactor coolant system leakage";

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BwAP 33040, " Operability Determinations," Revision SE1; j

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19wOS 4.6.2.1.d-1, " Unit One Reactor Coolant System Water inventory

l Balarce 72 Hour Surveillance," Revision 15;

Braidwood Updated Final Safety Ar.alysis Report Sections 5.2.5 and 15.5.1; and q

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Braidwood TSs 3.4.6.2 and 3.4.4.  !

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l b. Observations and Findanas

The inspectors verified that the documentation of the operability evaluations met

BwAP 330-10 requirements, that the licensee complied with TSs, and that the

assumptions used in the operability evaluations were valid. The inspectors had no l

concems with the licensee's determinations of operability or the proposed correcibe I

! actions.

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c. Conclusion

The inspectors concluded that the two operability determinations regarding the reactor i

coolant system leakage calculations and the automatic operation of the pressurize r power

j. operated relief valves reflected good engineering judgement and safety focus.

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E3.2 Review of Plant Modifications

a. Inspection Scope (37551)

The inspectors reviewed the following documents:

E20-0-96-235-1 post-modification test procedure, " Addition of a Fire

Damper / Pressure Control Damper Assembly at the Wall Between the Auxiliary

j Building and Turbine Building," Revision 0;

  • Preferred Metal Technologies, Inc., Test Procedure #1001-LT-1, "Operatienal 1

Testing of Pressure Relief / Fire Damper Assembly," Revision 1; j

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  • BwVS 7.7.d-1, " Auxiliary Building Non-accessible System Filter Plenum Tost," l

l Revision 4; and  !

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= 10 CFR 50.59 Safety Evaluation BRW-SE-1998-57.  !

The inspectors observed the physical installation of the pressure control and fire damper

assembly, observed the operation of the pressure control damper, and obseived control  !

room instrumentation measuring the differential pressure between the auxiliary and

turbine buildings. ,

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b. Observations and Findinas l

The inspectors reviewed the post-modification test procedure that was used following the  !

installation of the pressure control and fire damper assembly. The inspectors noted that

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the post-modification test procedure was well-written, identified criteria for acceptable

performance, and contained a level of detail sufficient to ensure the modification

performed as designed. The inspectors observed that all acceptance criteria of the post-

modification test were met.

The inspectors reviewed the 10 CFR 50.5g safety evaluations for the pressure control

and fire damper modification. The inspectors determined that the safety evaluation was

well-wntion, complete, and prepared in accordance with Nuclear Station Work

Procedure A-04, "10 CFR 50.59 Safety Evaluation Process," Revision O.

The inspectors observed the physical installation of the pressure control and fire dampers

and did not identify any obstructions or interforance that could prevent the proper

operation of the dampers. The inspectors observed operation of the pressure control

damper and noted that the damper responded smoothly to changes in air flow between

the auxiliary and turbine buildings. The inspectors observed control room instrumentation

measuring the differential pressure between the auxiliary and turbine buildings during

daily inspections of the control room and noted that the indicated differential pressure

' was consistently maintained within its acceptable range.

. c. Conclusion

The inspectors performed a review of post-modification and surveillance testing

procedures for a modification that installed a pressure control and fire damper assembly

,

between the auxiliary and turbine buildings and concluded that all acceptance criteria

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associated with those procedures were met. The post-modification test procedure was

well-wntion and verified that the modification performed as designed. The surveillance

test procedure was well-written and verified that TS and Updated Final Safety Analysis

l Report requirements for the non-accessible filter ventilation system were satisfied. The

l physical installation of modification hardware was not obstructed by adjacent equipment.

The inspectors concluded that the pressure control and fire damper assembly property

controlled the differential pressure between the auxiliary and turt>ine buildings.

j E7 Follow up -Engineering (92903)

E7.1 Enoineerina Reauest and Enoineerina Reauest Overdue Review

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a inspection Scope (92703)

The inspectors reviewed the contents of the engineering request data base.

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l b Observations and Findinos

The licensee committed in the March 28,1997, response to the NRC's request for

information pursuant to 10 CFR 50.54(f) to report to the NRC the number of high pnority i

(A or B and significant with respect to safety, risk or operability) engineering requests and l

the number of high priority engineering requests outstanding past the assigned due date. l

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The inspectors reviewed the contents of the engineering request database and noted that

there were 461 high pnority work requests. The inspectors observed that 253 of these

high prionty engineering requests had no due dates assigned. The inspectors also,

identified that there were 134 engineering requests in the database with no oriority j

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identified,37 of which were from 1997 or earlier. The inspectors brought this to licensee

management attention and engineering requests were prioritized and due dates were

assigned pending availability of resources. None of the engineering requests from 1997,

or eartier were prioritized as high.

c. Condusion

The inspectors concluded that the licensee was not aware of the 134 engineering

requests in its database that had not been prioritized. The inspectors alsc, concluded that

253 high priority engineering requests had no due dates assigned. The 253 high priority

engineering requests without due dates assigned made up about 54 percent of the high .

priority bactiog. With this high percentage, the inspectors concluded that the number of

high pnonty overdue engineering requests was not a good performance indicator of

backlog reduction which was a performance indicator committed to in the licensee's

March 28,1997, response to the NRC's request for information pursuant to

10 CFR 50.54(f).

IV, Plant Support

R1 Radiological Protection and Chemistry (RP&C) Controla

R1.1 Scent Rosin Transfers

a. Inspection Scope (71750)

The inspectors attended the ALARA and the heightened level of awareness (HLA)

briefings for the transfer of resin from the boric acid system's boron recycle evaporator

feed domineralizer OAB01DA, the chemical and volume control system's mixed bed

domineralizer 1CV01DB, and the fuel pool cooling system's spent fuel pit

domineralizer 1FC01D. The inspectors observed radweste tunnel access point radiation

protection postings and access controls. The inspectors reviewod the following

documentation:

  • Braidwood Radiation Protection Procedure (BwRP) 6020 3T9, " Radioactive Spent

Resin Transfers," Revision 1;

Radiation Areas," Revision 6;

= BwAP 100-12," Human Performance Awareness of Pre-Job Briefings / Meetings

and Self-Checking," Revision 5;

- Radiation Survey of the 383 foot elevation redweste tunnel post-transfer survey

map (dated Februry 19,1998); and

  • Radiation Protection Policy Memo (RWP) # 16, "Al. ARA Pre-Job Requirements,"

Revision 0.

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b. Observations and Findinos

On February 19, the inspectors attended the ALARA and the HM briefings for the

transfer of resin from three domineralization tanks. The inspectors verified that the

ALARA briefing was performed and documented in accordance with Radiation Protection

Policy Memo # 16. The inspectors verified that the HlA briefing was performed and

documented in accordance with BwAP 100-12. The inspectors verified that the auxiliary

building 393 foot elevation access points to the radweste tunnel were locked and posted

in accordance with posting requirements specified in BwRP 5310-2.

The inspectors verified that a post-transfer survey of the radweste tunnel was performed

and posted. The post-transfer dose rates in the radweste tunnel were slightly elevated

when compared to the pre-transfer dose rates at several locations. The inspectors

determined that the posting requirements were correct for the radiation levels in the

radweste tunnel. The radweste system engineer told the inspectors that plans were

being prepared to conduct a more extensive flush of the affected lines to reduce the

radwaste tunnel dose rates to pre-transfer levels.

c. Conclusion

The inspectors concluded that the ALARA and HLA briefings for the transfer of resin from

three domineralization tanks were propedy performed and documented. All topics

specified in Radiation Protection Policy Memo # 16 and BwAP 10012 were discussed.

The inspectors concluded that the auxiliary building 383 foot elevation access points to

the redweste tunnel were property posted and access was prohibited by locked doors.

The inspectors concluded that post-transfer surveys were completed and were posted.

R2 Status of RP&C Facilities and Equipment

R2.1 Radiation Monitors

a. Inspection Scope (71750)

The inspectors routinely monitored the status of radiation monitors stationed in the plant.

The inspectors also reviewed Procedure BwRP 5800-6, " Administrative Controls for

Health Physics instrumentation," Revision 2, and Braidwood Updated Final Safety

Analysis Report, Section 12.5, " Health Physics Program."

b. Observations and Findinos

The inspectors routinely checked the status of detectors stationed in the auxiliary I

building, fuel handling building, radweste building, and technical support center. All I

detectors were found to be property calibrated and in good operational condition. ]

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The inspectors also inspected the radiation department calibration facildy located in the l

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auxiliary building on the 401 foot elevation. All instruments in the facility were properly

labeled and otherwise controlled. The facility was somewhat cluttered due to the large

number of instruments stored there; however, calibrated and ready for use instruments

were appropriately segregated from instruments requiring calibration or repair.

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l Procedure BwRP 5800 6 requirements for out-of-calibration and defective instruments

were appropriatelyimplemented.

c. Conclusion

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The radiation protection department's control of radiation monitoring devices was good.

l_ instruments were controlled as required by plant procedures.

R2.2 Plant Radiation And Postina of Notices to Workers

a. InspectK>n Scope (71750)

!

The inspectors monitored posting and labeling of radiologically controlled areas. The I

i inspectors also checked licensee postings required by 10 CFR 1g.11, " Posting of Notices

L to Workers." The inspectors also reviewed Procedures BwRP 501G-1, " Radiological i

Posting and Labeling Requirements," Revision 7E1; BwRP 6020-2, " Radiological Air

! Sampling Program," Revision 3E1; and BwRP 6020-3, " Radiological Surveys,"

Pevision 7, against the references of 10 CFR 20. l

c. Conclusion

, The inspectors concluded that the radiation protection department's control of radiation  !

l postings was good. Postings were controlled in accordance with plant procedures and

10 CFR 20. Survey maps for radiologically posted areas in the auxiliary building, fuel

! handling building, and radweste building were current. The inspectors conduded that the

licensee was in compliance with 10 CFR ig.11 posting requirements. l

F1 Control of Fire Protection Activities

F1.1 Messed Fire Watch

a. Inspection Scope (71750)

The inspectors reviewed the compensatory measures in place for the unavailability of the

l cart >on dioxide fire suppression system. The inspectors toured the areas and interviewed

j the fire marshal and an individual posted as a fire watch. The inspectors reviewed

i BwAP 1100-13, " Fire Watch inspection," Revision 6; BwAP 1100-1, " Fire Protection

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Program," Revision 3; and BwAP 1110-1 A4, " Carbon Dioxide Fire Suppression Systems,"

Revision 2.

b. Observations and Findanas

The inspectors venfied continuous fire watches were posted in the Unit 1 and 2 lower

cable spreading rooms and at the Unit 1 and 2 cable tunnels, and that houriy fire watches

were established in the emergency diesel generator and the diesel-driven auxiliary

feedwater pump rooms as required by BwAP 1110-1 A4 due to the unavailability of the

carbon dioxide fire suppression system.

The inspectors toured the Unit 1 lower cable spreading room area 1Z with the fire

marshal. Area 1Z was divided into two separate rooms,1Z1 and 1Z2. The inspectors

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observed that a continuous fire watch was seated in Room 1Z2 and that no one was

posted in Room 1Z1. The inspectors later verified that one person can act as a

continuous fire watch between two rooms as long as the rooms were easily accessible to

one another and the other room was visited at least every 15 minutes with a margin of

five minutes in accordance with BwAP 1100-13. However, the inspectors spoke with the

fire marshalin Room 1Z1 for a period of about 40 minutes and observed that the fire

watch did not enter the room. The individual assigned as the fire watch told the

inspectors that he did not understand that he was supposed to also act as a fire watch in

Room 1Z1 and did not enter Room 1Z1 for the entire hour he was posted in Room 1Z2. -

The inspectors noted that it was the third time that individual was assigned as the fire

watch for that post on January 29.

The inspectors reviewed the fire watch post orders. The post orders stated that the

location of the continuous fire watch was the Unit i lower cable spreading room but did

not specsfy that the lower cable spruding room was made up of Subzones 1Z1 and 1Z2.

The post orders stated that the fire watches were to document the inspection by using a

bar code scanner in the area to be inspected. If the scanner failed to work, the 15 minute

inspection was to be documented in the fire watch log. The inspectors noted that fire

watch supervisors had reviewed the fire watch log, but the fact that Room 1Z1 had not

been entered could not be determined by reviewing the fire watch log because the

inspections had not been documented. The inspectors questioned the lead fire watch

supervisor about the post order requirement to log the inspections every 15 minutes. The

supervisor stated that the documentation of the 15 minute inspection was no longer

required.

The failure to follow Procedure BwAP 1110-13 to establish a continuous fire watch in the

Unit i lower cable spreading room wits the station carbon dioxide suppression

system OOS was a violation of TS 6.8.1.g as described in the attached NOV

(456/98002-03(DRP)).

c Conclusion

The inspectors concluded that the continuous fire watch requirement for the Unit i lower

cable spreading room was not met at least three times on January 29. The inspectors

concluded that the fire watch was not adequately supervised because the instructions to

the individual assigned to the fire watch were unclear, the stated post-order requirements

were not enforced, and supervisory review of the watch documentation as well as,

observation of the fire watch did not identify,these problems. A violation was issued.

F8 Follow up Plant Support (Fire Protection) (92904)

F8.1 (Closed) Violation 50-456/93022-01a(DRS): 50-457/93022-01a(DRS): The licensee failed

to take timely corrective actions for an impaired fire door between the auxiliary building

and the turbine building. The door was a rated fire protection barrier between safety and 1

non-safety-related areas of the plant. When high differential pressure problems between

the turbine building and the auxiliary building were experienced, plant staff blocked the

door open to allow air to flow between the two areas to partially equalize the air pressure.

The licensee allowed this impairment to exist since March 1991. On January 20,1998,

the licensee completed long-term corrective actions with the installation of a pressure

control and fire damper assembly between the turbine and auxilistv building.

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The inspectors reviewed the post-modification testing of the pressure control and fire

damper assembly, observed operation of the pressure control damper, and verified the

impaired fire door between the auxiliary building and the turbine building was closed.

The inspectors had no further concems. This item is closed.

F8.2 (Closed) Unresolved item 50-456/96016-06(DRS): 50 457/96016-06(DRS): The

inspectors noted that the fire door between the auxiliary building and the turbine building

was open (a condition documented in Violation 50-456/93022-1a; 50-457/93022-1a), but

a permanent watch had been assigned to the blocked open door. The licensee stated

that the watch was stationed as a compensatory measure for a licensee identified high

energy line break concem. The watch was assigned to close the door during a high

energy line break in the turbine building. The inspectors were excomed about the high

energy line break watch's ability to close the impaired door during a high energy line

break event. On January 20,1998, the licensee completed long-term corrective actions

with the installation of a pressure control and fire dan per assembly between the turbine

and auxiliary building. The inspectors reviewed the post-moddication testing of the

pressure control and fire dampers, observed operation of the pressure control damper,

and verified the impaired fire door between the auxiliary building and the turbine building

was closed. The inspectors hed no further concems. This item is closed.

V Mananoment Meetinas

X1 Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at

the conclusion of the inspection on March 9,1998. The licensee acknowledged the

findings presented. The inspectors asked the licensee whether any materials examined

during the inspection should be considered proprietary. No proprietary information was

identified.

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PARTlM. LIST OF PERSONS CONTACTED

pcensee

  • T. Tulon, Site Vice President

K. Schwartz, Station Manager

  • R. Wegner. Operations Manager
  • R. Byers, Ma'.ntenance Superintendent

l *A. Haeger, Heelth Physics and Chemistry Supervisor

l R. Graham, Work Control Superintendent

l *T. Simpkin, Regulatory Assurance Supervisor

  • C. Dunn, System Engineering Supervisor
  • J. Meister, Engineering Manager
  • M. Riegel, Q&SA Manager
  • M. Cassidy, Regulatory Assurance - NRC Coordinator

d.RQ

M. Jordan, Chief, Reactor Projects Branch 3

C. Phillips, Senior Resident inspector

  • J. Adams, Resident inspector

D. Pelton, Resident inspector

IDI$E

T. Esper

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  • Denotes those who attended the exit interview conducted on March 9,1998.

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INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observations

IP 62707: Maintenance Observation

IP 71707: Plant Operations

IP 71750: Plant Support Activities

IP 92901: Follow up - Plant Operations

IP 92902: Follow up- Plant Maintenance

IP 92903: Follow up - Engineering

l IP 92904: Follow up - Plant Support

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ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-457/98002-01 NCV Failure comply with TS

50-456/98002-02; 50-457/98002-02 VIO Failure to follow procedures

l 50-456/98002-03 VIO Failure to follow procedures

Closed

50-456/93022-01a; 50-457/93022-01a VIO Failure to take corrective actions

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50-456/95015-03; 50-457/95015-03 VIO Failure to follow procedures

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50-456/96016-06; 50-457/96016-06 URI High energy line break compensatory

action concems

Discussed

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50-456/97022-02; 50-457/97022-02 VIO Failure to follow procedures

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LIST OF ACRONYMS USED

Al. ARA As Low As Reasonably Achievable

ASME American Society of Mechanical Engineers

BwAP Braidwood Administrative Control Procedure

BwGP Braidwood General Operating Procedure

BwOP Braidwood Operating Procedure

BwOS Braidwood Operations Surveillance Procedure

BwRP Braidwood Radiation Protection Proc * dure

l BwVS Braidwood Technical Staff Surveillance Procedure

CFR Code of Federal Regulations

CV Chemical and Volume Control System

ESFAS Emergency Safety Feature Actuation System

FME Foreign Material Exclusion

Hl.A Heightened Level of Awareness

LCO Limiting Condition for Operation

NCV Non-Cited Violation

NRC Nuclear Regulatory Commission

NRR Nuclear Reactor Regulations

NSO Nuclear Station Operator

l OOS Out-of-Service

! P&lD Piping and instrumentation Diagram

!

pcm percent millirho

PDR Public Document Room

l PIF Problem Identification Form

i RCS Reactor Coolant Sy., tem

RHR Residual Heat Removal

RP Radiation Protection

RP&C Radiological Protection & Chemistry

SX Essential Service Water

( TS Technical Specification

l UFSAR Updated Final Safety Analysis Report

! URI Unresolved item

l US Unit Supervisor

VIO Violation

l VQ Primary Containment Purge

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