ML20195G373

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Insp Repts 50-456/98-14 & 50-457/98-14 on 980909-1019. Violations Noted.Major Areas Inspected:Licensee Operations, Maint & Engineering
ML20195G373
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 11/17/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20195G364 List:
References
50-456-98-14, 50-457-98-14, NUDOCS 9811200280
Download: ML20195G373 (20)


See also: IR 05000456/1998014

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U.S. NUCLEAR REGULATORY COMMISSION

REGIONlil l

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Docket Nos: 50-456, 50-457 I

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License Nos: NPF-72, NPF-77

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Report No: 50-456/98014(DRP); 50-457/98014(DRP)

uonsee: Commonwealth Edison Company

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Facility: Braidwood Nuclear Plant, Units 1 and 2

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' Location: RR #1, Box 84 l

Braceville,IL 60407 1

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Dates
September 9 through October 19,1998

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Inspectors:

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C. Phillips, Senior Resident inspector

J. Adams, Resident inspector

D. Pelton, Resident inspector ,

Approved by: Michael J. Jordan, Chief

Reactor Projects Branch 3

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9811200280 981117 s

, PDR ADOCK 05000456 &

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EXECUTIVE SUMMARY

Braidwood Nuclear Plant, Units 1 and 2

NRC Inspection Report 50-456/98014(DRP); 50-457/98014(DRP)

This inspection included aspects of licensee operations, maintenance, and engineering. The

report covers a 6-week period of resident inspection from September 9 through

October 19,1998.

Operations

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The shift managers, unit supervisors, and nuclear station operators routinely performed

good turnover briefings, pre-job briefings, control board operations, control of evolutions,

response to alarms, communications, direction of personnel, and control of work l

evolutions. However, unclear communications occurred between the control room

operators and a field operator during a pre-job brief, and control room operators failed to

recognize an illuminated annunciator alarm warning that the 18 emergency diesel

generator would not start. This resulted in preventing the automatic start of the

1B emergency diesel generator during sequencer surveillance test. (Section 01.1)

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The licensee identified at least eight recent configuration control errors consisting of ,

operator manipulation errors and inadequate OOS boundaries. Licensee corrective l

actions were extensive, but have not yet been effective. The majority of the problems

were the result of personnel errors. These errors had the potential to endanger

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personnel and equipment. The failure to arrest this trend has the potential to adversely

affect safety-related equipment in the future. A non-cited violation was issued for the

failure to follow procedures. (Section 04.1) i

Maintenance

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The prompt response by operators and maintenance personnel to a failure of a freeze

seal which isolated the 1 A auxiliary feedwater pump essential service water supply valve

limited flooding te, about 6000 gallons of water. The prompt response was attributed to

pre-planned licensee contingency actions and prevented additional equipment damage.

The licensee's root cause investigation identified several lessons-learned, which were

incorporated into the maintenance freeze seal procedure. The inspectors verified that

the licensee followed the previously existing maintenance freeze seal procedure.

(Section M1.1)

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The inspectors observed good Foreign Material Exclusion (FME) controls during

maintenance activities. During the inspection period, the licensee demonstrated a good

safety focus by identifying and taking appropriate corrective actions for a potential

increasing trend in the number of FME problems. (Section M1.2)

- The inspectors observed all or portions of 14 maintenance activities. The maintenance

activities were performed in accordance with the applicable procedures, which provided

the requisite information necessary to perform the work. Maintenance personnel

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demonstrated good general work practices and were knowledgeable of the associated

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Technical Specification limiting conditions for operation and high-risk work activity

requirements. '(Section M1.3)

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The inspectors observed the performance of all or portions of ten surveillance tests in

accordance with the Technical Specification and Updated Final Safety Analysis Report.

The surveillance tests adequately tested the systems. However, the inspectors

identified two minor administrative errors for the acceptance criteria in the emergency

diesel generator surveillance test procedures.- (Section M1.4)

Enaineerina

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Modifications were properly prepared, initiated, and documented on the Unit 1

condensate storage tank. Work was performed in a safe manner, and nondestructive ,

testing was properly performed and evaluated. (Section E1.1) -

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The inspectors identified the licensee did not test the control room ventilation system

design function to realign on the detection of smoke in the exhaust plenum as described

in UFSAR Section 6.4. The inspectors verified the testing of the control room ventilation

system met Technical Specification requirements. Licensee management stated the

control room ventilation system function to realign on the detection of smoke in the

exhaust plenum would be tested in the future. Currently, the control room operators 1

also have the ability to manually realign the control room ventilation system if necessary.

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Further review by the NRC is needed to determine if any enforcement is warranted on ,

this issue. An unresolved item was issued. (Section E1.2)

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The licensee failed to implement measures to determine the cause, and take

comprehensive and effective corrective action to preclude repetition of bolts being found

loose on two emergency diesel generator lubricating oil heat exchanger end bells

following the identification on July 10 and 12,1998. On August 18,1998, the inspectors

observed two similar problems with loose bolts on the 2A and 2B emergency diesel

generators lubricating oil heat exchanger end bells. Since August 18, the licensee's

efforts to identify and correct the causes for loose heat exchanger bolting were

aggressive and comprehensive. The inspectors concluded that identified corrective

actions should prevent recurrence of the problem with the loose bolts. A notice of

violation was issued for failure to initiate an investigation to determine the cause of a

condition adverse to quality until identified by the inspectors. (Section E2.1)

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Report Details

Summary of Plant Status

Unit 1 was shutdown for refueling outage A1R07 for the entire period. Unit 2 remained at or

near full power for the entire period,

l. Operations

- 01 - Conduct of Operations

01.1 Control Room Observation

a. Inspection Scooe (71707)

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The inspectors observed the conduct of operation during normal operating conditions,

shutdown conditions, refueling operations, and surveillance tests. The i, ;;;?ctors ,

interviewed nuclear station operators, unit supervisors, shift managers, and test i

directors,

b. ' Observations and Findinas

The inspectors observed control room operators throughout the inspection period. The

inspectors noted that the nuclear station operators were attentive, properly used

operating procedures, utilized self-checks when manipulating equipment, and used

three-way communications. The nuclear station operators promptly addressed alarms, -

referred to the annunciator response procedures, and promptly informed supervisors of

alarms. However, on October 10, while performing the 1B emergency diesel generator

emergency core cooling system sequencer surveillance test, the 1B emergency diesel

generator failed to start when bus 142 was de-energized. The licensee determined that

the diesel mode selector switch on the local control panel was not properly positioned

due to unclear communication between the control room operators and the field

operator during the pre-job brief. Additionally, an illuminated annunciator that indicated

the diesel mode selector switch was not correctly positioned for an automatic start was

not recognized by the control room operators. This is also discussed in setion O4.1 and

listed in Section M1.4.

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The inspectors attended the operations department shift turnover, pre-job briefings, and

heightened level of awareness briefings. The inspectors noted that the personnel

conducting the briefings were knowledgeable, major work activities were described,

limiting condition for operations (LCOs) were reviewed, communication methods were

discussed, contingency actions wem specified, and individual responsibilities were ]

. assigned. l

-The inspectors noted that the unit supervisors demonstrated good command and  !

control. The inspectors observed unit supervisors perform tumovers with the other unit

supervisor and announce to control room personnel changes in control room command

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and control responsibilities prior to leaving the control room. The inspectors observed

that unit supervisors worked closely with test directors during the performance of

surveillance tests for which a test director had been assigned,

c. Conclusions

The shift managers, unit supervisors, and nuclear station operators routinely performed

i good turnover briefings, pre-job briefings, control board operations, control of evolutions,

response to alarms, communications, direction of personnel, and control of work

evolutions. However, unclear communications occurred between the control room

operators and a field operator during a pre-job brief, and control room operators failed to

recognize an illuminated annunciator alarm warning that the 1B emergency diesel

l generator would not start. This resulted in preventing the automatic start of the

l 1B emergency diesel generator during sequencer sunteillance test.

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04 Operator Knowledge and Performance

i 04.1 Continued Confiouration Control Problems

a. Inspection Scope (71707)

The inspectors interviewed station management and operators to evaluate the reasons

behind and corrective actions for the most recent configuration control errors.

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l b. Observations and Findinas

l During this inspection period there were numerous configuration control problems, most

j involving the out-of-service (OOS) process . The inspectors categorized the problems

j into two areas. The first was operator errors involving the manipulation of the

equipment. The second were errors involving failures to establish adequate boundaries

for the work to be performed.

Between August 17,1998, and October 10,1998, the licensee identified that non-

licensed operators made five errors manipulating plant equipaent. Three of thuse

j errors were OOS cards placed on the wrong equipment. In addition, there were three

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instances of inadequate OOS boundaries established. The inspectors interviewed

operators involved with several of the configuration control errors. The operators were

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aware of management expectations regarding placing OOS cards and performing

l procedural steps. The operators all made assumptions in the field that were incorrect

l without making the proper verifications. There was no procedural guidance on how to

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place an OOS card. The proper method for placing OOS cards was a management

expectation. The operators interviewed had an excellent understanding of the correct

method for hanging an OOS card. A maintenance verification of the OOS prior to the

start of work was part of the OOS procedure. The OOS errors were identified either

durMg the maintenance verification or by the non-licensed operators. Therefore, there

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were no procedure violations identified in the failure to properly place the OOS cards.

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The inadequate OOS boundaries were on non-safety related equipment or on

equipment not required operable for the existing mode of operations.

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l However, one of the operator errors occurred during the restoration from a localleak

rate test. The non-licensed operator directing the test gave direction to the control room

to open an isolation valve before the vent valves were closed in violation of the

procedure. This resulted in spilling about 100 gallons of water in the Unit 1 auxiliary

l building. In addition the control room operator did not have a copy of the local leak rate

l test procedure available which was in violation of a station administrative procedure.

Technical Specification 6.8.1.a states, in part, that written procedures shall be

established, implemented, and maintained covering the applicable procedures l

, recommended in Appendix A, of Regulatory Guide 1.33, Revision 2, February 1978. ,

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Regulatory Guide 1.33, Revision 2, Appendix A, Section 1.d, requires administrative

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procedures for procedure adherence; and Section 8.b.1.a requires procedures for

containment leak rate tests.

BwAP 100-20, " Procedure Use And Adherence," Revision 9, Step D.8.c.4, states, in

part, that each step of a continuous use procedure must be performed as written, in the

order written. Step D.8.a.4, states, in part, that when more than one individual is

performing steps in a procedure at different locations, individuals at each location should

i have a copy of the procedure to follow and refer to as the activity proceeds.

Contrary to the above, on October 8,1998, an operator in the control room failed to

l perform continuous use procedure 18wOSR 3.6.1.1-22, " Primary Containment Type C

! Local Leakage Rate Test Of Safety injection System," Revision 0, Steps 2.39 and 2.40,

in the order written. Step 2.40 was performed by operators in the control room before

l the completion of Step 2.39 by non-licensed operators in the Unit 1 auxiliary building

i curved wall area. In addition, the control room operator did not have a copy of

l 1BwOSR 3.6.1.1-22 available to follow and refer to while performing these steps.

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The licensee temporarily suspended all local leak rate tests and the non-licensed

operator directing the local leak rate test was temporarily relieved of all field work. The

local leak rate test supervisor and all operators assigned to the local leak rate team met

and discussed this incident and current Braidwood operating standards. The localleak

rate team supervisor was made responsible for ensuring that the control room operators

j have a copy of the local leak rate procedure before the start of the test.

This non-repetitive, licensee-identified and corrected violation is being treated as a

non-cited violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy

(50-456/98014-01(DRP); 50-457/98014-01(DRP)).

The inspectors met with senior station management regarding the configuration control

errors. The licensee had initiated many corrective actions including procedure

guidance, training, second verification of all OOSs, and where necessary personnel

discipline. In addition, operations managers and supervisors were called in for a

l special meeting to discuss the problems with configuration control. Station

! management perspective was that the OOS process was sound and that current

problems were related to personnel performance issues.

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c. Conclusions

- The licensee identified at least eight recent configuratiori control errors consisting of 4

. operator manipulation errors and inadequate OOS boundaries. Licensee corrective

actions were extensive but have not yet been effective. The majority of the problems l

were the result of personnel errors. These errors had the potential to endanger

personnel and equipment. The failure to arrest this trend has the potential to adversely -i

affect safety-related equipment in the future. - A non-cited violation was issued for the 1

failure to follow procedures.

07 Quality Assurance.in Operations

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07.1 Strateoic Reform initiative Number 4 'Alian and intearate Resources" l

a. inspection Scoce'(71707)

The inspectors reviewed the implementation of the Nuclear Generation Group Strategic

Reform initiative Number 4 at Braidwood. The strategic reform initiatives were outlined

in a February 17,1998, letter from Comed (Kingsley) to the NRC (Callan). The

inspectors selected Action Step Number 4 to review, which dealt with incorporating peer

group initiatives into the Site Wide Integrated Operational Plan. '

b. Observations and Findinas

The inspectors reviewed the list of initiatives generated by the Peer Groups and

approved by the Nuclear Generating Group. The only items that were included in the

Site Wide Integrated Operational Plan were those considered by station management to

be resource intensive. Other items were tracked in the licensee's nuclear tracking  ;

system data base. The licensee was making good progress toward completion of the .j

initiatives. j

c. Conclusions

Select, resource intensive, Peer Group initiatives approved by the Nuclear Generating j

Group were verified to be included into the Site Wide Integrated Operational Plan in

accordance with Strategic Reform Initiative Action Step Number 4. Other Peer Group i

initiatives were tracked in the licensee's nuclear tracking system with good progress

toward completion.

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11. Maintenance

M1 Conduct of Maintenance

M1.1 Lost Freeze Seal on the Essential Service Water Sucolv to the1 A Auxiliary Feedwater

Pumo

a. Inspection Scope (62707)

The inspectors responded to a loss of a freeze seal for the removal of the 1 A auxiliary  !

feedwater pump essential service (SX) water supply valve 1 AF017A. The inspectors  :

interviewed the maintenance personnel responsible for the freeze seal and the

ope;ators that responded to the event. The inspectors reviewed Problem Identification

Form (PlF) A1998-03316 and its associated prompt investigation report; Braidwood

Maintenance Procedure (BwMP) 3300-18, " Application of Liquid Nitrogen Freeze Seal to I

All Piping," Revisions 7 and 8; BwMP 3300-18, Attachment Two, " Freeze Seal Log"; and l

BwMP 3300-18, Attachment Three," Contingency Actions."

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b. Observations and Findinas  !

On September 21, a freeze seal isolating the SX water to the 1 A auxiliary feedwater

pump SX water supply valve,1 AF017A, failed releasing approximately 6000 gallons of

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SX water to the auxiliary building. The Unit i nuclear station operator told the

inspectors that the control room operators were notified immediately of the loss of the

freeze seal. The unit supervisor directed equipment operators to implement

pre-planned contingency actions. The contingency actions were completed effectively

within five minutes of the start of the event. The inspectors were told that the

contingency actions were discussed in detail during the pre-job brief for the

maintenance activity and field operators had possession of the keys necessary to unlock

the valves identified for closure by the contingency actions.

The inspectors walked down the associated section of the piping following the event.

The inspectors noted that sufficient liquid nitrogen was available for the freeze seal, the

freeze seal tamperature log was maintained, the freeze seal jacket and temperature

monitors were properly installed on the pipe, and the freeze seal temperatures were

below the maximum allowable temperature. The inspectors verified that a copy of the

freeze seal procedure was at the work site, that the freeze seal procedure

BwMP 3300-18 was followed, that no spread of contamination occurred as a result of

the flooding, and that no equipment was rendered inoperable due to water intrusion.

The licensee performed a prompt investigation of the loss of the freeze seal and

identified an apparent cause and severallessons learned. The licensee suspects that

the silt and water mixture in the line may have affected the integrity of the seal. The

licensee identified several lessons learned from their review of the event which were

incorporated into the freeze seal procedure BwMP 3300-18. The inspectors attended a

subsequent pre-job brief for an SX water freeze seal and noted that the lessons-learned

were incorporated in the briefing.

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c. Conclusions l

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The prompt response by operators and maintenance personnel to a failure of a freeze

seal which isolated the 1A auxiliary feedwater pump SX water supply valve limited

flooding to about 6000 gallons of water. The prompt response was attributed to pre-

planned licensee contingency actions and prevented additional equipment damage.

The licensee's root cause investigation identified several lessons-learned which were

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incorporated into the maintenance freeze seal procedure. The inspectors verified that

the licensee followed the previously existing maintenance freeze seal procedure.

M1.2 Foreian Material Exclusion Problems,

a. Insoection Scope (62707)

The inspectors observed the foreign material exclusion (FME) controls implemented and

used during the performance of maintenance activities. The inspectors reviewed PIFs

issued to address FME issues and interviewed operations and maintenance personnel.

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b. Observations and Findinas

The inspectors observed good FME controls utilized throughout the plant. The

inspectors also noted that areas requiring heightened levels of FME controls such as the

spent fuel pit area or the refueling cavity were properly controlled. Between

. September 19 and October 4, the licensee identified eight FME issues. The licensee

initiated a PIF to investigate a potential trend in FME problems, but later determined

there was not a trend. However, communication sessions with both licensee and

contractor personnel were held to raise awareness concerning FME controls.

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c c. Conclusions

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The inspectors observed good FME controls during maintenance activities. During the

inspection period, the licensee demonstrated a good safety focus by identifying and

taking appropriate corrective action for a potential increasing trend in the number of

FME problems.

M1.3 Maintenance Activity Observations

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a.' inspection Scope (62707)

. The inspectors observed all or portions of the following maintenance activities
  • .1 A centrifugal charging pump gear drive unit oil spray valve replacement in

accordance with work request (WR) 970086904-01;

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- Installation of SX system line stop prior to/during A1RO7 in accordance with

e WR 980003392-01;

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Replacement of the 1A SX pumo discharge valve in accordance with I

- WR 980003298-01' I

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Electrical inspection of motor operated safety injection valve 1S18813 in l

accordance with WR 970133749-08;

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Reinstallation and torquing of the 1 A SX pump discharge check valve in

accordance with WR 980091882-02;

Troubleshooting of the Unit 2 rod control system in accordance with

WR 980000439-01;

18 month inspections of the 1 A emergency diesel generator in accordance with

WR 970051160-01;

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Installation of the 1A emergency diesel generator governor modification in

accordance with WR 960061285;

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Installation of the 1 A emergency diesel generator fuel oil filter / strainer

modification in accordance with WR 970011809; I

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Installation of the 1B emergency diesel generator fuel oil filter / strainer

modification in accordance with WR 970010950-01;

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Installation of the 1B emergency diesel generator governor modification in

accordance with WR 960061289;

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18 month inspections of the 1B emergency diesel generator in accordance with

WR 970030021-01;

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Replacement of the 125 volt DC 1E battery 111 in accordance with

WR 980002678-01; and

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Replacement of the 125 volt DC 1E battery 112 in accordance with

WR 980002680-01,

b. Observations and Findinas

The inspectors attended the heightened-level-of-awareness briefings; reviewed all or

portions of the above work packages; reviewed high-risk work check sheets, if

, applicable; walked down the work areas with maintenance personnel; questioned

personnel concerning the scope of the work, including system status, and precautions

for electrical safety; observed the establishment of required system conditions; observed

the use of FME controls; reviewed applicable welding procedures and " hot work"

permits; and observed the use of quality control" hold points." The inspectors also

l reviewed the associated Technical Specification LCO, if applicable, and reviewed the

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control room logs for LCO entries and exits. The inspectors noted no problems during

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the above reviews, interviews and observations.

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l c. Conclusions

The inspectors observed all or portions of 14 maintenance activities. The maintenance

activities were performed in accordance with the applicable procedures, which provided

the requisite information necessary to perform the work. Maintenance personnel

demonstrated good general work practices and were knowledgeable of the associated

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- Technical Specification limiting conditions for operation and high-risk work activity '

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requirements.

l M1.4 Miscellaneous Surveillance Test Observation

a. Insoection Scope (61726)

The inspectors observed all or portions of the following surveillance activities:

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Unit 1, Braidwood Engineering Surveillance Procedure (1BwVSR) 3.8.4.7-111,

" Unit One 125 Volt ESF (Engineered Safety Feature] Battery Bank 111 Service

Test," Revision 0;

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18wVSR 3.8.4.7-112, " Unit One 125 Volt ESF Battery Bank 112 Service Test," l

Revision 0; l

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1BwVSR 384-2, " Unit One 125 Volt ESF Battery Charger 112 Setpoint and

Alarm Test," Revision 0;

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1BwVSR 8.1.1.2.f-13, "1 A Emergency Diesel Generator ECCS [ Emergency Core

Cooling Systems] Sequencer Surveillance " Revision 10; I

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1BwVSR 8.1.1.2.f-15, "1 A Emergency Diesel Generator Loss of ESF Bus

Voltage With No SI [ Safety injection) Signal," Revision 8; '

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1BwVSR 8.1.1.2.f-21, "1 A Emergency Diesel Generator 24 Hour Endurance Run

and Hot Restart Test 18 Month," Revision 2;

Surveillance," Revision 10;

18wVSR 8.1.1.2.f-22, "1B Emergency Diesel Generator 24 Hour Endurance Run

and Hot Restart Test 18 Month," Revision 2;

1BwVSR 8.1.1.2.f-20, "1B Emergency Diesel Generator KW [ Kilowatt) Load

Rejection and Simulated Si in Conjunction With UV (Undervoltage] During Load

Testing," Revision 11; and

Braidwood Engineering Surveillance Procedure (BwVS) 900-8, " Emergency

Diesel Generator Engine Analysis," Revision d.

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b. Observations and Findinos

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For each surveillance test, the inspectors verified the establishment of initial conditions

required for the surveillance test and observed the operation of equipment, the ,

communications between the licensed operators in the control room and non-licensed

operators, and the restoration of affected equipment. The inspectors determined that

each of these activities were performed in accordance with the applicable procedure.

The inspectors verified the data obtained met the required acceptance criteria specified

in the surveillance test procedures. The inspectors also reviewed the associated i'

portions of the Updated Final Safety Analysis Report (UFSAR) and the Technical

Specifications and determined that the surveillance test procedures demonstrated the

systems performed as designed.

However, the inspectors did observe two examples where the acceptance criteria in the

surveillance test procedures were not consistent with the requirements of Technical i

Specifications. Surveillance test 2BwOS 8.1.1.2.a-1, "2A Emergency Diesel Generator .

Monthly (Staggered)," which verified that the emergency diesel generator can start from

ambient condition and accelerate to at least 600 revolutions per minute (rpm) in less

than or equal to 10 seconds meeting Technical Specification 4.8.1.1.2.a.4. The

inspectors noted that 2BwOS 8.1.1.2.a-1 indicated an rpm acceptance criteria as

l. "588 to 612" which was not consistent with the Technical Specification. This

l inconsistency was discussed with the system engineer who agreed that the acceptance

! criteria must match the Technical Specification requirement. The inspectors reviewed

nine previously completeJ emergency diesel generator mtnthly surveillance procedures

and determined that each time the recorded rpm value was greater than 600 rpm. The

l licensee revised all the monthly surveillance procedures to be consistent with the

Technical Specification. On September 26, the inspectors observed the performance of l

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18wVS 8.1.1.2.f-21. This surveillance procedure was used to demonstrate compliance

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with Technical Specification 4.8.1.1.2.f.7, which verified that the emergency diesel

l generator operate for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, stop and restart within five minutes accelerating to at

least 600 rpm in less than or equal to ten seconds. The inspectors noted that the

surveillance procedure did not include the 600 rpm acceptance criteria as specified in

the Technical Specification. This inconsistency was discussed with the system engineer

who had the procedure revised to reflect the Technical Specification rpm requirement.

The inspectors concluded that no operability concern existed.

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c. Conclusions

The inspectors observed the performance of all or portions of ten surveillance tests in

accordance with the Technical Specification and Updated Final Safety Analysis Report,

The surveillance tests adequately tested the systems. However, the inspectors

identified two minor administrative errors for the acceptance criteria in the emergency

diesel generator surveillance test procedures.

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Ill. Eno!neerina

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l E1 Conduct of Engineering

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E1.1 Modification to the Unit 1 Condensate Storaae Tank (CSTL

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! a. Inspection Scope (37551)

The inspectors reviewed Engineering Change Notice (ECN) 001157M, " Increase the

Height of the Unit 1 Condensate Storage Tank (CST) by 10 Feet, and Install

a 6" Butterfly Drain Valve (1CD260)"; Design Change M20-1-97-002-B, " Increase the

Height of the Unit 1 Condensate Storage Tank by 10 Feet"; Operability Evaluation

Form 93-029, " Failure to Arm the SX (water) Suction Swap-Over when the Control

Switch is in "after-close" and an Arming Signal is Present"; Application for Amendment

to Appendix A, Technical Specifications, to Facility Operating Licenses," Condensate

Storage Tank Level," dated December 30,1997; and Work Package 960022332-01,

l " Increase Height of CST by 10 Feet." The inspectors interviewed system engineering

l. and contractor personnel and performed a walk-down of the CST before, during, and

after the modification installation.

j b. Observations and Findinas

l The ECN, the design change package, the associated operability determination and

l proposed license amendment were properly documented. Worker safety practices,

l cutting, welding, and nondestructive testing were good and were properly documented.

l No problems were noted with the work performed or with the work and modification

packages.

c. Conclusions

(. Modifications were properly prepared, initiated, and documented on the Unit 1

l condensate storage tank.- Work was performed in a safe manner, and nondestructive

! testing was properly performed and evaluated.

E1.2 Failure to Test All of the Automatic Realianment Functions of the Control Room

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Ventilation System.

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l a. Inspection Scope (37551)

The inspectors reviewed 10 CFR 50, Appendix B; UFSAR Chapter 6.4; Braidwood

Technical Specification 4.7.6.e.2; NUREG-0800, " Standard Review Plan"; NUREG-

l 1002, " Safety Evaluation Report Related to the Operation of Braidwood Station, Units 1

l and 2"; Braidwood Operating Surveillance Procedure (BwOSR) 3.7.10.3, " Control Room

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Ventilation System Emergency Makeup System 18 Month Surveillance," Revision 0;

i 1BwOSR 3.3.2.7-602A, " Unit One Quarterly Slave Relay Surveillance (Train A - K602

and K647); 1BwOSR 3.3.2.7-602B, " Unit One Quarterly Slave Relay Surveillance

(Train B - K602 and K647); 2BwOSR 3.3.2.7-602A, " Unit Two Quarterly Slave Relay

Surveillance (Train A - K602 and K647); and 2BwOSR 3.3.2.7-602B, " Unit Two

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Quarterly Slave Relay Surveillance (Train B - K602 and K647). The inspectors

interviewed system engineering, operations, fire protection, and regulatory assurance

personnel.

b. Observations and Findinas

The inspectors performed a review of portions of the control room ventilation system

design bases including a comparison of the UFSAR described functions, UFSAR

described system testing, and Technical Specification required surveillance testing.

Specifically, the inspectors reviewed the control room ventilation system's UFSAR

described automatic realignment functions.

The UFSAR, Section 6.4, describes three possible automatic realignments of the control

room ventilation system. The system will automatically realign upon detection of high

radiation in the outside air intakes, upon receipt of a safety injection signal, or upon

detection of ionization products (smoke) in the return air duct or mixed air plenum. The

UFSAR, Section 6.4.5 states that the control room ventilation system and its

components are thoroughly tested in a program which includes periodic testing and that

written test procedures will establish minimum acceptance values for all tests. However,

the inspectors determined that the system's automatic realignment upon detection of

smoks in the return air duct or mixed air plenum was not periodically tested. The

licensee pointed out that there was no Technical Specification surveillance requirement

pertaining to the control room ventilation system's automatic realignment upon detection

of smoke. In addition, control room operators can manually realign the control room

ventilation if necessary. Based on questions raised by the inspectors, the licensee

planned to develop a periodic test of the control room ventilation system's automatic

realignment upon detection of smoke.

Since the test was not required by technical specifications, the licensee contested the

inspectors position that the failure to periodically test the control room ventilation

system's automatic realignment upon detection of smoke was a violation of 10 CFR 50,

Appendix B, Criterion Ill. Criterion lit requires that measures be established to assure

that applicable regulatory requirements and the design basis are correctly translated into

specifications, drawings, procedures, and instructions. Therefore, this matter is

unresolved and will be forwarded to NRC headquarters, NRR for resolution

(50-456/98014-02(DRP); 50 457/98014-02(DRP)).

c. Conclusions

The inspectors identified the licensee did not test the contrd room ventilation system

design function to realign on the detection of smoke in the exhaust penum as described

in UFSAR Section 6.4. The inspectors verified the testing of the control room ventilation

system met Technical Specification requirements. Licensee management stated the

control room ventilation system function to realign on the detection of smoke in the

exhaust plenum would be tested in the future. Currently the control room operators also

have the ability to manually realign the control room ventilation system if necessary.

Further review by the NRC is needed to determine if any enforcement is warranted on

this issue. An unresolved item was issued.

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E2 Engineering Support of Facilities and Equipment

E2.1 Loose Bolts on Emeraency Diesel Generator Lubricatina Oil Heat Exchanaers

a. Insoection Scope (37551)

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Inspectors conducted inspections of all Unit 1 and 2 emergency diesel generators; '

discussed the observation of loose bolts with the shift manager, system engineer,

seismic engineer, and station management; reviewed machinery history documents for

the emergency diesel generators; and reviewed the licensee's corrective actions. The

inspectors reviewed the applicable sections of the Cooper Bessemer vendor's manual;

WR #960094684, " Upper Lube Oil Cooler Has Slight Oil Leak"; PlF #A1998-02783, i

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" Loose Bolts Found on 2A DG [ Emergency Diesel Generator] Lube Oil Heat

Exchanger"; PIF A1998-02783 Prompt investigation Report; Root Cause Report NTS

(Nuclear Tracking System) number 457-200-98-CAQS00008, " Loose Bolts Found on l

2A Emergency Diesel Generator Lube Oil Cooler Due to Not Using Industry Operating

Experience," Revision 0; PlF A1998-2400, " Loose Bolts Found on 2B DG [ Emergency

Diesel Generator) Lube Oil End Bell"; and PIF A1998-2406, Loose Bolts Found on

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1B Emergency Diesel Generator Lube Oil Heat Exchanger."

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b. Observations and Findinas

On August 18,1998, the inspectors observed that ten of the sixteen bolts on the 2A and

one bolt on the 2B emergency diesel generator lubricating oil heat exchanger end bells

were loose. The licensee initiated an action request for the tightening of the bolts,

checked heat exchanger bolts on the all of the emergency diesel generator lubricating

oil heat exchangers, performed an operability assessment for the 2A emergency diesel

generator, conducted a prompt investigation, and initiated a root cause analysis of the

event. The inspectors verified the assumptions used in the operability assessment and

agreed with the licensee's determination of operability.

The inspectors reviewed the vendor's manual and WR#960094684 for the most recent

maintenance activity on the 2A emergency diesel generator lubricating oil heat

exchanger packed end. The inspectors noted that the installation instructions in the

work request were consistent with the instructions in the vendor's manual and that the

vendor's manual did not specify a torque value for the bolts.

The inspectors conducted a review of the maintenance history records for all of the

emergency diesel generators and noted ten similar problems, four of which were

identified this year. In February 1998, the licensee identified a oilleak from the

2A emergency diesel generator lubricating oil heat exchanger packed end bell but failed

to check the bolts for tightness. On July 10,1998, painters observed several loose

bolts on the 2B emergency diesel generator lubricating oil heat exchanger end bell and

documented the deficiency in PIF A1998-2400. The licensee responded by tightening

the loose bolts on the 2B emergency diesel generator lubricating oil heat exchanger and

inspecting the other emergency diesel generators lubricating oil heat exchangers.

Operators checked all of the other emergency diesel generator heat exchangers for

loose bolts and identified loose bolts on the 1B emergency diesel generator lubricating

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oil heat exchanger end bell. The additionalloose bolts identified were tightened and

were documented in PlF A1998-2406. However, following the identification of these

significant conditions adverse to quality on two of the four emergency diesel generators

(safety-related equipment identified as important in the licensee's risk analysis), the

licensee failed to implement measures to assure that the cause of the bolt loosening

was determined and corrective action taken to preclude repetition. The licensee initiated

such action on August 18,1998, after inspectors observed the same condition on the

2A and 23 emergency diesel generators.

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10 CFR Part 50, Appendix B, Criterion XVI, " Corrective Actions," requires, in part, that

measures be established to assure that conditions adverse to quality, such as failures,

malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformances are promptly identified and corrected. In the case of significant

conditions adverse to quality, the measures shall assure that the cause of the condition

is determined and corrective action taken to preclude repetition. The licensee's failure

to implement measures to determine the cause and take comprehensive and effective

corrective action to preclude repetition of the loose bolts on the emergency diesel

( generator lubricating oil heat exchangers was a violation of 10 CFR Part 50,

Appendix B, Criterion XVI (50-456/98014-03(DRP); 50-457/98014-03(DRP)).

The licensee's investigation of the event determined that the lack of uniform tightening,

and " creep" (a phenomenon that will result in the loss of pre-load on the bolts due to the

partially plastic behavior of elattomeric gaskets) as causes or contributing factors.

Further information obtained by the licensee from the Electric Power Research Institute

Bolting Procedure Handbook discussed the periodic tightening of bolts as a common

way to address the loss of pre-load due to " creep." Additionalinformation obtained

through discussions with other members of the Cooper Bessemer Diesel Generator

Owners Group supported the need for periodic tightening of the lubricating oil heat

exchanger end bell bolts since the members with periodic requirements for tightening

reported no events. The licensee identified two root causes for this event. The first was

not establishing and using specific tightening values for the emergency diesel generator

lube oil cooler end bell fasteners. The second root cause was not performing periodic

'

hot re-tightening of the emergency diesel generator lube oil cooler end bell fasteners.

Based on the root causes, the licensee identified, documented, and initiated the

,

implementation of corrective actions to prevent recurrence.

c. Conclusions

The licensee failed to implement measures to determine the cause, and take

comprehensive and effective corrective action to preclude repetition of bolts being

found loose on two emergency diesel generator lubricating oil heat exchanger end bells

following the identification on July 10 and 12,1998. On August 18,1998, the inspectors

observed two similar problems with loose bolts on the 2A and 2B emergency diesel

generators lubricating oil heat exchanger end bells. Since August 18, the licensee's

efforts to identify and correct the causes for loose heat exchanger bolting were

aggressive and comprehensive. The inspectors concluded that identified corrective

actions should prevent recurrence of the problem with the loose bolts. A notice of

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l violation was issued for failure to initiate an investigation to determine the cause of a

condition adverse to quality until identified by the inspectors.

E8 Followup Engineering (92903)

E8.1 (Closed) Violation 50 457/97021-03: " Failure to initiate PIF as required by station ,

procedure." Inspectors identified on November 10,1997 that the licensee had failed to  !

follow nuclear station work procedure NSWP-A-15, " Comed Nuclear Division Integrated

Reporting progmm," Revisioni and Braidwood administrative procedure BwAP 330-10,

" Operability Determinations," Revision 3E1 requirements to issue a PlF when problems

were recognized with a tempering feedwater line snubber and with various main feed

water line snubbers. The licensee counseled the involved engineering personnel about

the circumstances surrounding this violation including the need to follow station

procedures concerning the documentation of conditions adverse to quality. The

licensee also performed a review of NSWP-A-15 and BwAP 330-10 to determine if

changes were necessary to ensure a PlF would be generated when required. The

licensee determined that no changes to these procedures were required. Since this

review, the licensee replaced BwAP 33.0-10 with nuclear station

procedure NSP-CC-3001, " Operability Determination Process," Revision O. This

procedure was also reviewed by the licensee and found to contain appropriate

guidance. The inspectors reviewed NSWP-A-15 and NSP-CC-3001 and concur with the

licensee's conclusions. This item i:, closed.

V. Manaaement Meetinas

X1 Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at

the conclusion of the inspection on October 19,1998. The licensee acknowledged the

findings presented. The inspectors asked the licensee whether any materials examined

during the inspection should be considered proprietary. No proprietary information was

identified.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

I *T. Tulon, Site Vice President

l K. Schwartz, Station Manager

!

.R. Wegner, Operations Manager

R. Byers, Maintenance Superintendent

. A. Haeger, Health Physics and Chemistry Supervisor  !

L *R. Graham, Work Control Superintendent

L T. Simpkin, Regulatory Assurance Supervisor

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J. Kuchenbecker, System Engineering Supervisor l

l T. Luke, Engineering Manager i

  • M. Cassidy, Regulatory Assurance - NRC Coordinator i

blB.G

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' M. Jordan, Chief, Reactor Projects Branch 3

  • C. Phillips, Senior Resident inspector
  • J. Adams, Resident inspector

D. Pelton, Resident inspector

  • Denotes those who attended the exit interview conducted on October 19,1998.

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l INSPECTION PROCEDURES USED

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l lP 37551: Onsite Engineering

1- IP 61726: Surveillance Observations

IP 62707: Maintenance Observation

)

IP11707: Plant Operations

IP 92903: Followup - Engineering

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l ITEMS OPENED AND CLOSED

Opened

50-456-457/98014-01 NCV failure to follow procedures

l 50-456-457/98014-02 URI contested need to have a test procedure

j 50-456-457/98014-03 VIO failure to take timely corrective actions

,

Closed

50-457/97021-03 VIO failure to follow procedures

50-456-457/98014-01 NCV failure to follow procedures

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LIST OF ACRONYMS USED

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AF Auxiliary Feedwater

CFR Code of Federal Regulations

ESF Engineered Safety Features

l FME Foreign Material Exclusion

LCO Limiting Condition for Operation

NRC Nuclear Regulatory Commission

NRR Nuclear Reactor Regulations

OOS Out-of-Service -

PlF Problem identification Form

SI Safety injection

SX Essential Service Water

UF3AR Updated Final Safety Analysis Report

VIO Violation

WR Work Request

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