ML20153C363

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SALP Rept 50-255/86-01 for Nov 1984 - Oct 1985
ML20153C363
Person / Time
Site: Palisades Entergy icon.png
Issue date: 02/12/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20153C360 List:
References
50-255-86-01, 50-255-86-1, NUDOCS 8602190148
Download: ML20153C363 (41)


See also: IR 05000255/1986001

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SALP 6

SALP BOARD REPORT

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

SYSTEMATIC ASS' , MENT OF LICENSEE PERFORMANCE

86001

Inspection Report No.

Consumers Power Company

Name of Licensee

Palisades Nuclear Generating Station -

Name of facility

November 1, 1984 to October 31, 1985

Assessment Period

B602190148 860 j55

PDR ADOCK O PDR

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I. INTRODUCTION

The Systematic Assessment of Licensee Performance:(SALP) program is an

integrated NRC staff effort to collect available observations and data on-

a periodic basis and to evaluate licensee performance based upon this

information. SALP is supplemental to normal regulatory processes used -

to ensure compliance to NRC rules and regulations. .SALP is-intended to

be sufficiently diagnostic to provide a rational basis for allocating NRC

resources and to provide meaningful guidance to the licensee's management

to promote quality and safety of plant construction and operation.

A NRC SALP~ Board, composed of staff members listed below, met on

January 6 1985, to review the collection of performance observations

and data to assess the licensee performance in accordance with the

guidance in NRC Manual Chapter 0516, " Systematic Assessment of Licensee

Performance." A. summary of the guidance and evaluation criteria is

provided in Section II of this report.

This report is the SALP Board's assessment of the licensee's safety

performance at-the Palisades plant for the period November 1, 1984

,

through October 31, 1985.

SALP Board for Palisades:

Name Title

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A. B. Davis Deputy Regional: Administrator

J. A. Hind Director, Division of Radiation

Safety and Safeguards (DRSS)

C. E. Norelius Director, Division of Reactor

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Projects (DRP)

C. J. Paperiello Director,. Division of Reactor

Safety (DRS)

A. Thadani Director, PWR Project Directorate

No. 8, NRR

T. V. Wambach Licensing Project Manager, NRR

R. M. Perfetti Project Engineer, NRR

i N. J. Chrissotimos Chief, Projects Branch 2, DRP

C. W. Hehl Chief, Projects Section 2A, DRP

E. R. Swanson Senior Resident Inspector,

Palisades

l C. D. Anderson Resident Inspector, Palisades

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L. A. Reyes Chief, Operations Branch, DRS

. W. D. Shafer Chief, Emergency Preparedness

and Radiological Protection Branch,

DRSS

3- L. R. Greger Chief, Facilities Radiation

Protection Section, DRSS

M. P. Phillips Chief, Emergency Preparedness Section,

DRSS

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F.' C. Hawkins Chief, Quality Assurance Programs

Section,'DRS

J. R. Creed. Chief, Safeguards Section, DRSS.

M. C. Schumacher Chief, Radiological Effluents and

Chemistry Section, DRSS

C.~ F. Gill Radiation Specialist, DRSS

J. P. Patterson Emergency-Preparedness Analyst,- DRSS

T. E.. Taylor. Reactor Inspector, DRS.

M. Pearson Licensing Assistant, DRP

J. F. Suermann Project Manager, DRP

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II. CRITERIA

The licensee performance is assessed in selected functional areas

depending whether the facility is in a construction, preoperational

or operating phase. Each functional area normally represents areas

significant to nuclear safety and the environment, and are normal

programmatic areas. Some functional areas may not be assessed because

of little or no licensee activities or lack of meaningful observations.

Special areas may be added to highlight significant observations.

One or more of the following evaluation criteria were used in assessing

each functional area.

1. Management involvement in assuring quality

2. Approach to resolution of technical issues from a safety

standpoint

3. Responsiveness to NRC initiatives

4. Enforcement history

5. Reporting and analysis of reportable events

6. Staffing (including management)

~ 7. Training effectiveness and qualification

'

However, the SALP Board is not limited to these criteria and others may

have been used where appropriate.

Based upon the SALP Board assessment each functional area evaluated is

classified into one of three performance categories. The definition

of these performance categories is:

Category 1: Reduced NRC attention may be appropriate. Licensee

management attention and involvement are aggressive and oriented toward

nuclear safety; licensee resources are ample and effectively used so

that a high level of performance with respect to operational safety or

construction is being achieved.

Category 2: NRC attention should be maintained at normal levels.

Licensee management attention and involvement are evident and are

concerned with nuclear safety; licensee resources are adequate and

are reasonably effective such that satisfactory performance with

respect to operational safety or construction is being achieved.

L Category 3: Both NRC and licensee attention ~should be increased.

Licensee management attention or involvement is acceptable and considers

nuclear safety, but weaknesses are evident; licensee resources appear to

be strained or not effectively used so that minimally satisfactory

i performance with respect to operational safety or construction is being

achieved.

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-Trend: -The SALP Board has'also categorized the performance trend in

each functional area rated over the course of the SALP assessment period.

The. categorization describes the general orfprevailing' tendency (the

performance gradient) during the SALP period. The performance trends

are-defined as follows:

Improved: Licensee performance has generally improved over

-the course of the SALP assessment period.

Same: Licensee performance has remained essentially constant

over the course of_the SALP assessment period.

Declined: Licensee performance has generally declined over

the course'of the SALP assessment period.

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III. SUMMARY OF RESULTS

The licensee's overall performance for this assessment period showed a

considerable decline, reflecting a continuation of the poor performance

noted in some areas at the end of the last assessment period. Three

functional areas (Maintenance, Surveillance and Quality Programs)

recorded a decline in performance to the Category 3 level and the

performance trend in two of these areas showed no overall improvement

over the course of the assessment period. Of the remaining seven areas

rated only three areas showed an improving performance trend and one-

area reflected a declining trend. None of the areas rated received a

Category 1 rating.

Rating Last Rating This

Functional Area Period Period Trend

A. Plant Operations 2 2 None

B. Radiological Controls 2 2 Improved

C. Maintenance 2 3 Same

D. Surveillance 2 3 Improved

E. Fire Protection 2 2 Improved

F. Emergency Preparedness 2 2 Declined

G. Security 2 2 Same

H. Refueling 1 NR* None

I. Quality Programs and

Administrative Controls 2 3 Same

J. Licensing Activities 2 2 Improved

  • NR - Not Rated (no basis for evaluation)

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IV. PERFORMANCE-ANALYSIS

A. Plant Operations

1. Analysis

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Evaluation of this functional area is based on portions of

twelve inspections conducted by the resident inspectors

encompassing direct observation of activities, review of logs

and records, verification of selected equipment lineups for

operability and followup on significant operating events to

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verify conformance to the Technical Specifications and

administrative controls.

During this operating cycle Palisades experienced one of its

-best operating runs (maintaining an availability factor of 87%)

and set several generation records. Plant power operation was

characterized by one nine month period of continuous reactor

operation, a low number of automatic reactor trips from power

-(two), three-power reductions to add oil which had leaked from

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a primary coolant pump motor, eight turbine. generator shutdowns

for electro-hydraulic system leaks on the turbine governor valve,

and two power reductions as required by Technical Specification

action statements. Except for the two reactor trips which

involved personnel errors, operators demonstrated their

proficiency and coordinated operating ability by rapidly

r removing the turbine generator from service in response to

j secondary plant problems a number of times without tripping the

reactor. 'The operators performance is commendable in light of

i the operating difficulties posed by operating a plant where

certain indicators are unreliable (HPSI flow and SIT level; see

!. Section IV.C. on Maintenance for more details).

Three violations were identified in this area. One, a Severity.

Level IV for late reporting of unidentified primary coolant

leakage in excess of 1 gpm (Inspection Report No. 50-255/84025),

was of concern since it showed.that operators were reluctant

to take action based on information and' indications which

should have been reliable. Corrective actions taken with

respect to this issue have been effective. The second, a

Severity Level IV for having two safety injection tanks below

the low level limit (Inspection Report No. 50-255/85002),was

of concern because operators failed to recognize the degraded

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equipment which eventually caused the violation. In this

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latter event, leaking fill and drain valves on the tank,

I primary coolant system check valve leakage and uncalibrated.and

! unreliable' level indicators for the tanks all contributed to

l make the operator's job of maintaining compliance difficult.

I Both of the above violations had root causes related to poor

( maintenance which contributed to the operators' lack of

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confidence in their indications in the first case and then in

the second case, when they believed them, resulted in the

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violation. The reliability of indicators needs to be improved

so that operators can believe what they indicate and take

action without evaluating the operability of the indicator.

The third violation, a Severity Level IV, was for a licensee

identified situation where both licensed Senior Reactor

Operators concurrently left the control room for a short time

during power operation (Inspection Report No. 50-255/85027).

This event was viewed as an isolated occurrence of a communica-

tion failure.

Of the six Licensee Event Reports (LER) related to the area of

operations (LER 85-004,85-010, 85-014,85-015, 85-016, and

85-021), all of them involved operator personnel errors.

In addition, one of the six LERs involved the inadvertent

operation of a power operated relief valve and two involved

operator errors which resulted in reactor trips. Additionally,

a voluntarily submitted report (LER 85-001), involved personnel

error, when operators disbelieved a panel indicating light

which resulted in several days of operation with certain safety

injection actuation features blocked.

None of the events had any serious safety significance although

a statistic of increasing personnel errors warrants close

scrutiny. The licensee does trend personnel errors, but has

not observed any commonality which would warrant other than

event specific corrective action.

Staffing the Operations Department has been adequate.

Experience level at the plant is fairly good in the Reactor

' Operator positions but the Senior Reactor Oparator positions

were lacking some depth due to attrition and the infusion of

less experienced replacements. One of the decisions made,

based on the attrition of operators, was to go back to a

5 shift rotation for the foreseeable future. In spite of the

lack of experience, most of the newly licensed SR0s are

competent and conscientious operators.

Operator attitudes have improved somewhat over the evaluation

period, and no situations which were adverse to safe operation ~

were identified. The operators are generally conscientious and

attentive while on duty. Plant licensed operators conduct

themselves in a professional manner and have not been observed

engaged in any of the activities prohibited by the plant

administrative procedure on control room conduct (prohibits

radios, hobbies and non job-related reading material). No

formal dress policy has been established, but dress has

improved during this period since the identification of the

dress issue. Good progress has been made in the general

housekeeping of the plant and specifically in the auxiliary

building hallways and accessible rooms. Operators take an

active role in the plant-wide housekeeping efforts by reporting

and correcting situations which are discovered during their

tours.

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Management and supervisory decisions were characterized by a

realistic view of safety, but did not, on two occasions of

note, take a conservative approach to plant operation. A

recent example is the primary coolant system (PCS) leakage

event of October 15, 1985 (LER 85-022) where the decision was

made to increase power from 30% with a 0.8 gpm unidentified

leakrate and one valve packing leaking water and steam at about

0.7 gpm (part of the identified leakage). The licensee later

shut down after the valve leakage increased to over 3.0 gpm.

Another example from earlier in the period rel~ ted

a to decisions

not to exercise one control rod due to possible aggravation of

seal leakage and declaring it inoperable. When a second rod

became inoperable, the licensee then exercised the first rod to

avoid shutting the plant down to effect repairs. These

actions, although technically within the requirements of the

Palisades lic~ense, are considered somewhat imprudent by the

NRC.

During the report period, examinations were administered to 2

reactor operators (R0s), 7 senior reactor operators (SR0s),

and 7 instructors. The overall pass rate was 75%, which is

slightly below the national average of 80%. In addition,

requalification examinations were administered to five SR0s

and three R0s in July 1985 with unsatisfactory results for all

three R0s and one SRO. These individuals were removed from

licensed duties. The NRC reviewed and accepted an accelerated

requalification program for these individuals. Subsequently,

all four individuals passed the August re-examination and

returned to licensed duties. The licensee attributes these

failures in part to the lack of qualified instructors familiar

with the Palisades Plant. Actions are underway to improve this

situation by the licensee " growing" their own certified

instructors.

2. Conclusion

The licensee is rated Category 2 in this area with no discernable

performance trend noted. Although improvement since early in

the period was evidenced by a reduction in cited violations, the

number of personnel errors stayed relatively the same.

3. Board Recommendations

None

B. Radiological Controls

1. Analysis

Five inspections were conducted during this assessment period

by region based inspectors. These inspections included

radiation protection, radioactive waste management, TMI Action

Plan Items, environmental protection, radiochemistry, and

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confirmatory measurements. The_ resident inspectors also

reviewed this area during routine inspections. Four violations

were identified as follows:

before filter elements were removed from the liquid

radioactive waste system. Because the elements were

removed, contaminated resin was pumped to the clean

radwaste system during resin sluicing operations.

(Inspection Report No. 50-255/85004)

control procedures in that an emergency door was routinely

used for auxiliary building ingress and egress without

required radiation safety approval, personnel commonly

used a shift log in/out option without required radiation

work permit (RWP) authorization, and two workers entered

a posted radiation area without being listed on a RWP and

without wearing the required self-reading dosimeters.

(Inspection Report No. 50-255/85010)

control procedures in that several pieces of unlabeled

contaminated tools and material were found outside the

radiologically controlled area and contract workers exited

the control area with hand tools that had not been surveyed.

(Inspection Report No. 50-255/85010)

release procedures in that incorrect iodine MPC values

were used in calculating several releases and on one

occasion, an actual release rate exceeded that authorized

by the shift supervisor. (Inspection Report

No. 50-255/85011)

These violations are indicative of a minor programmatic

breakdown in the areas of safety evaluations and procedure

adherence. Although licensee corrective actions have been

timely in most cases, procedure adherence problems were also

evident during the last assessment period. Licensee enforcement

history during this assessment period improved from the previous

assessment period.

Licensee staffing has generally improved during this assessment

period. One technician position was added and all positions are

filled. The staffir.g levels appear adequate to properly

1 establish acceptable radiation protection controls during

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station operation and to provide sufficient oversight of

contracted radiation protection technicians during outages. The

radiation protection and chemistry staff turnover rate, which

had been quite high in the past, has stabilized. This stability

appears to have helped the licensee improve performance in the

area of radiological controls, although experience levels on

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the average remain quite low. Licensee organization changes

during this assessment period removed one intervening management

layer between the RPM and the plant manager in response to NRC

concerns. Other organizational changes resulted in the

separation of the chemistry and the radiological services

departments at the manager level.

The licensee's management involvement has improved during this

period and is generally adequate, with occasions of both good

and poor performance. Audits are thorough and timely, with

good responsiveness to findings. Significant progress was made

in development of chemistry procedures to satisfy a nuclear

operations department directive of 1982. This work had lagged

somewhat during the previous assessment period. Administrative

procedures required by the Chemistry Program Manual were

completed but not all subordinate working procedures had been

fully or adequately implemented. Progress in this area was

addressed in a detailed internal audit performed in September

1985 and a followup audit was scheduled for early 1986. In

addition to these problems, the audit identified procedural-

inconsistencies that required reconciliation. In addition,

improved management oversight is warranted in the radwaste

area where the inspector identified nonconservative errors in

procedures used for calculating beta components of airborne

releases and also significant typographical errors in

semiannual reports. No significant releases were involved and

the licensee was quick to correct the errors after they were

pointed out. The licensee has implemented measures to improve

workers adherence to station radiation protection procedures by

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better identification of offenders and stronger disciplinary

actions. These improvements, in conjunction with increased

surveillances and program changes, are expected to reduce the

number of radiological incident reports. Management control

initiatives during this assessment period resulted in:

improved ALARA outage pl=nning; reduction of contaminated areas

in the auxiliary building; plant visits by senior health physics

staff personnel to several NRC Region III nuclear power stations

with a SALP 1 rating in the area of radiological controls; an

improved and revised alpha surveillance program; NVLAP

accreditation of the TLD dosimetry program; and several trending

programs. Several items, however, have remained open for prolonged

periods including: the need to improve the radiological incident

reporting system; repair of minor radioactive system leaks in

the auxiliary building; and a failure to quantify or

alternatively eliminate occasional low activity steam releases

from the heating boiler in accordance with a commitment made

during an earlier inspection.

The licensee's responsiveness to NRC initiatives has generally

been adequate during this assessment period. As noted above,

several NRC concerns remained open for prolonged periods. On

the other hand, improvements were made for a number.of NRC

identified weaknesses, including those concerning the

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unauthorized use of'an emergency door for auxiliary building

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access; access control logging procedures; radiation work permit

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(RWP) adherence; radioactive ~ material control; the need to

improve the quality and timeliness of neutron assessment for

containment entries during power operations; the need to expand

the scheduled surveys of uncontrolled areas to include such

items as tool cribs,-ladders, and scaffolding; environmental

i monitoring; gamma spectrometer calibration; the lack of a

contamination area tracking system; and the need to improve the

sensitivity of the portal monitors.

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The licensee has satisfactory formal training / qualification

programs for radiation protection technicians, contract

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technicians, plant workers, and plant visitors. A radiation

protection and chemistry training and qualification program has

been implemented for a large portion of the staff. The licensee

has a good seven to nine week training program established for

radiation protection and chemistry technicians. About 90

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percent of the technicians currently on staff have completed

this training.

The licensee's approach to the resolution of radiological

s technical issues have generally been technically sound, thorough,

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and timely. Although the adequacy of radiological involvement

l in outage preplanning could not be directly assessed because no

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extended outage occurred during this assessment period, it

appears that there needs to be a better working relationship

between the ALARA group and the Planning department. In response

to this concern, the ALARA Coordinator and the Radiological

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Services Manager acknowledged the need to improve prejob planning,

including: routine advance planning over a longer period of time;

ALARA staff attendance at pre-outage meetings; and possible

relocation of the ALARA staff closer to the planning staff. A

review of a January 1985 entry into containment, while the

reactor was at 20 percent power, indicated that radiological

involvement and ALARA preplanning were adequate. The ALARA

program and corresponding management support appear to'have

been strengthened since the reorganization in November 1984,

j including: the appointment of a dedicated, full time ALARA

j coordinator; substantive commitments to INPO that should

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improve the ALARA program; improved ALARA goals and policies;

and increased efforts to improve job planning. During this

assessment period there was a significant improvement in the

overall radiological control program. Specific improvement

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areas include: procedure adherence, staffing, ALARA, access

control, contaminated area reduction, incorporation of good

4 radiation protection practices gleaned from SALP 1 plant visits,

the alpha surveillance program, the TLD dosimetry program,

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access control logging procedures, containment entry neutron

assessment, the uncontrolled area survey program, portal

j monitor sensitivity, and several trending programs.

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Personal. exposures during this assessment period were about

530 person-rem in 1984, and are estimated to be about 300

person-rem in 1985. These exposures are below the station

average over the previous five years (600 person-rem) and

less than the U.S. average for pressurized water reactors

(550 person-rem per reactor).

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. .The licensee's liquid radiological effluents continue to be

significantly lower than average for U. S. pressurized water

reactors. Reported noble gases effluents have shown an increase

during this assessment period but are still only about average

for U. S. pressurized reactors. '

.t is not yet certain whether

this apparent increase is real or an artifact of the new noble

gas-stack monitor. Licensee efforts are continuing to resolve

this matter. The solid radioactive waste volumes in 1984 and

1985 were significantly less than in recent years, and the

licensee has recently implemented a volume reduction program

and plans to begin segregation of dry active waste (DAW) in

the near future to reduce the amount of solid radwaste further.

Other planned improvements include: placing separate trash

containers in the RCA for potentially contaminated and clean

. DAW; limiting the issue of disposable " anti-C" clothing; and,

1 minimizing the amount of material, such as boxes or other

packing material, taken into controlled areas. No transportation

problems were identified during this assessment period.

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Confirmatory measurements comparisons during this period were

I limited to gross beta, tritium, and strontium comparison on a

liquid sample split near the end of the previous assessment

period. The licensee achieved agreement in all four

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comparisons. Counting room quality controls were generally

adequate. Performance tests on instruments are established,

completed as required, and are reviewed by a chemistry

supervisor. The absence of trend plotting of performance check

data and lack of a radiological crosscheck program with an

j independent laboratory were two weaknesses noted by the

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inspectors. Analysts interviewed and observed in the counting

room appeared knowledgeable regarding equipment and procedures.

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! 2. Conclusion

The licensee is rated Category 2 in this area. The licensee

received a rating of Category 2 in the last SALP period. An

improved performance trend was evident during this assessment

, period.

3. Board Recommendations

None

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C. Maintenance / Modifications

1. Analysis

Examination of this functional area consisted of two special

inspections by a Region III Maintenance Inspection Team, one

special inspection by two regional inspectors, one routine

inspection by a regional inspector, and portions of twelve

monthly inspections by the resident inspectors.

Activities inspected included the program and implementation of

maintenance and supporting activities (including calibration

and' control of test and measuring equipment), design changes

and modifications, and reviewing the cause and licensee

recovery efforts related to the failure of a shaft ~ joint on a

reactor coolant pump.

Seven violations were identified as follows:

a. Severity Level IV - Six examples were noted where

maintenance procedures related to preventive maintenance

and equipment control were not being followed. (Inspection

Report No. 255/85003).

b. Severity Level IV - Calibration was being performed

without a procedure. (Inspection Report No. 255/85003).

c. Severity Level V - A number of portable measuring and

testing devices were improperly controlled. (Inspection

Report No. 255/85003).

d. Severity Level V - Three examples were identified where

insufficient instructions were provided in maintenance

work orders. (Inspection Report No. 255/85003).

! e. Severity Level IV - Design considerations for redundancy,

diversity and separation were improperly applied to a

l modification of the Component Cooling Water (CCW)

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Containment Isolation valves. Purchase documents did not

specify appropriate requirements for Class IE components

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(Inspection Report No. 255/85018).

f. Severity Level IV - Failure to conclude that an unreviewed

safety question existed when changing the CCW isolation

circuitry (Inspection Report No. 255/85018).

g. Severity Level IV - Failure to environmentally qualify the

temperature switches for the Safeguards Pump room cooling

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fan (Inspection Report No. 255/85027).

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Individually, many of the above violations were not significant,

but collectively they indicate significant program implementa-

tion problems in this functional area. No violations were

identified in this functional area during the previous SALP

period, and, although one would normally expect a concentrated

team inspection to identify some deficiencies, it is significant

to note that roughly half of the violations noted above were

identified by the resident inspector while performing the

routine inspection program. Inspections resulting in violation

a. above and violation a. under Paragraph IV.I. (Quality

Programs and Administrative Controls) showed that the Preventive

Maintenance Program at the plant has not been either of

sufficient scope or adequately implemented to provide the

desired reliability. Additionally, machinery histories were

not being maintained in useable form and no trending was being

done. These problems contributed to the poor plant material

conditions observed. Violations b., c., and d. above are

considered additional examples of program implementation

failures.

The violation of greatest concern is item e. above. Not only

were design inputs found to be inadequate, but the independent

licensee reviews also failed to identify any of the problems

that existed with the design. The safety evaluation (item f.

above) did not accurately describe the change and did not

identify that the change created an unreviewed safety question.

The failures represent. training and program implementation

problems. The licensee committed to reviewing other minor

modifications for similar modification errors. Additional

reviews of design change packages identified further violations

of documentation requirements, as detailed under Paragraph IV.I.

(Quality Programs and Administrative Controls).

Item g. above was a result of poor transfer of responsibility

for the resolution of the issue from one organization to another

within the company. It was considered an isolated event with

respect to the enti.re environmental equipment qualification

issue.

As a result of concerns over the effectiveness and progress of

the licensee's remedial maintenance program, a Confirmatory

Action Letter (CAL) was issued on October 30, 1985 to confirm

that certain agreed upon goals would be met prior to restart

from the December 1985 - February 1986 refueling outage.

Satisfactory progress had not been made in reducing the

maintenance backlog and Control Room deficiencies between the

initial special maintenance inspection in February 1985 and the

followup inspection approximately six months later. Additionally,

the followup inspection found no corrective actions were

apparent on some of the earlier identified violations and action

was incomplete on others.

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One LER (Report 85-011) showed an inadequate understanding

of a Safety Injection System (SIS) circuit which resulted in an

inadvertent SIS actuation while shutdown. Three LERs (Reports84-024, 84-025, and 85-022) reported high PCS leakage due to

various equipment failures. A control rod seal failure was

apparently due to operation with high total dissolved solids

in the Primary Coolant System (PCS) from a worn and damaged

pump impeller. Another report (84-027) identified two charging

pump breaker closing coil failures due to lack of preventive

maintenance. Two Safety Injection Tanks were below the low

level limit at the same time (Report No.84-026); this was a

direct result of instrument unreliability and lack of

calibration. A continued concern exists for the state of

maintenance and reliability of indications and controls as

' described in Paragraph IV.A. (Plant Operations). Although the

situation improved somewhat over the SALP period, further

engineering and design changes will be required to solve the

existing problems. The licensee does have plans to correct

most of the identified maintenance problems during the upcoming

refueling outage and this issue will be further addressed before

startup under the CAL.

Many existing maintenance problems have arisen due to equipment

age. Previously, a number of older problems had not been faced

squarely and resolved, but rather solutions were sought which

could be " lived with". Examples of these older problems

include the nuclear instruments, control rod drive indication

and seals, and Safety Injection Tanks, valves, and indications.

One example of the current management's desire to solve the

problems that have plagued operators was their successful

pursuit of the solution to the electro-hydraulic vibration

problems on the turbine governor valves. However, a number of

backlogged issues remain to be solved.

One major improvement in this appraisal period was the overhaul

of the maintenance work order system. With full employee

participation, a team was established which addressed the

" log jams" of the existing system and improved the controls

to improve the erficiency of the workers. This was considered

a key step towards reducing tho backlog. Other improvments

include: the system assessment program where major systems

were walked down to identify deficiencies; improved work order

prioritization through the use of an aggressive and experienced

Senior Reactor Operator; improved supervision of work in progress;

improved quality of work execution; and added engineering

support for resolution of chronic problem instrumentation.

2. Conclusion

The licensee is rated a Category 3 in this area. This rating

is lower than that for the previous SALP period and reflects

the actual performance level noted in this area at the end of

16

L

. ..

the last period. Deficiencies found in the areas of preventive

maintenance, design changes and documentation, corrective

maintenance, work supervision, machinery history and trending

support this rating. The performance trend improved over the

period in several of the areas noted above, but the lack of

results in lowering a large maintenance backlog resulted in the

overall performance trend remaining the same. The level of

performance overall continues to be a major concern at the

facility.

3. Board Recommendations

The Board recommends continuation of the increased level of

NRC inspection effort and licensee management involvement in

this area. The Board notes that subsequent to the issuance of

the CAL (but after the appraisal period ended) the licensee

implemented steps to reduce the maintenance backlog and the

number of outstanding Control Room deficiencies. The licensee

also initiated steps to implement various maintenance trending

programs.

D. Surveillance and Inservice Testing

1. Analysis

Evaluation of this functional area is based on parts of twelve

inspections by the resident inspectors and two inspecticns by

Region III specialist inspectors.

Six violations were identified as follows:

a. Severity Level IV - The PCS low flow trip setpoints for

both four pump and three pump operation were nonconservative

due to failure to perform a test (Inspection Report

No. 255/84027).

b. Severity Level IV - Safety Injection Tanks were not

sampled within the required frequency (Inspection Report

No. 255/85005),

c. Severity Level V - Temperature readings were not taken

as required by the procedure (Inspection Report

No. 255/85008).

d. Severity Level V - Electrolyte level not measured and

recorded as required (Inspection Report No. 255/85008).

e. Severity Level IV - Containment isolation check valves

were not stroke tested quarterly (Inspection Report

No. 255/85023).

17

.' ..

f. Severity Level IV - Procedure was not followed concerning

operability status of untested components (Inspection

Report No. 255/85023).

Although these violations do not represent a serious safety

problem, when added to the number of additional licensee

identified inadequate or incomplete surveillances, they indicate

the variety of shortcomings in the surveillance program.

Violations a. and e. above were indicative of weaknesses in the

scheduling for some surveillance tests. Violations b. c. and f.

and LER 85-003 indicate implementation of the surveillance

program was not given sufficient attention to ensure completion.

Item d. above, and item 1. from functional area I (Quality

Programs), and LERs85-019 and 85-020 are evidence that program

requirements were not correctly translated into written

procedures. Although perceived at times as narrow in scope,

the licensee's corrective actions have be.en generally effective

in preventing similar occurrences. A twofold' increase in the

number of cited violations was noted over the last assessment

period.

Other event reports included the failure of personnel

performing a Safety Injection System Test to recognize that

a blocking relay was left energized during several days of

operation (LER 255/85-001). The condition was indicated by a

panel light which when pursued by the resident inspector was

finally resolved. In another event report (LER 255/85-018)

eight pressure transmitters were calibrated incorrectly

resulting in nonconservative setpoints for the high pressure

reactor trip. This potentially serious error was due to

unfamiliarity with the equipment used for the calibration.

Subsequent review determined that the error was within the

assumptions made in the safety analysis. These two events

display cognitive personnel errors which would likely have

been avoided through better training.

As a result of the identified violations and a changeover in

personnel who administer the surveillance program, the licensee

embarked on initiatives to validate their program and computerize

the scheduling. Both efforts have for the most part been

completed. One of the results of the reviews of their program

was the identification and correction of at least four

deficiencies in their program and procedures. Provided that

these initiatives continue to be successful, the licensee

would not be expected to experience any further scheduling or

programmatic problems in the area of surveillance. Implementa-

tion of the program and procedural adherence will continue to

require licensee attention.

2. Conclusion

The licensee is rated Category 3 in this area due to program

weaknesses noted during the appraisal period and a significantly

18

_ _ _ . - __

.

worse enforcement history for the period compared to the last

appraisal period. The licensee's performance reflected an

increase in both the number of violations and the severity level

of the violations. An improving performance trend, however,

., was evident late in the appraisal period as a result of program

i adjustments and personnel changes made in the surveillance area.

3. Board Recommendations

The Board recommends that increased licensee management

attention be focused on both a review of the surveillance

program itself and the implementation of the program.

'

E. Fire Protection ard Housekeeping

1. Analysis

,

Evaluation of compliance to fire protection requirements and

i good housekeeping practices was accomplished as part of twelve

routine inspections by the resident inspectors, who were

i assisted by Regional Fire Protection Specialists on one

occasion and part of the Maintenance Team inspection on

another occasion. Three violations were identified as follows:

'

a. Severity Level V - Administrative controls for

housekeeping were not being followed (Inspection

Report No. 255/85002),

b. Severity Level IV - Poor housekeeping: water, combustible

debris in a class IE cable tray, combustible material,

i

contaminated tools, aerosol can in safety related

electrical cabinets (Inspection Report No. 255/85003).

l,

!' c. Severity Level V - No fire watch or fire extinguisher

present during hot work (Inspection Report No. 255/85018).

Violation k. under functional area I (Quality Programs and

Administrative Controls) also represents a fire protection

violation, with the main concern being the adequacy of the

program and procedures. The above referenced violations are

a contrast to no violations in the previous assessment period.

This is especially of concern since one would not expect

problems in this area without a large contract work force

1 onsite, and there was not a major outage during this period.

j Violation b. involved housekeeping in some obscure places but

1

was typical of the inspectors' observations. Well travelled

areas were well lighted, painted, and kept clean. Other areas

manifested a lack of routine cleaning and maintenance efforts.

In general, the licensee made headway in stopping minor

j equipment leaks and cleaning up the problem areas. A number

)

i

1

4 19

. - - - - . - - . _ _ - - - - - . -

..

of previously controlled contamination areas have been cleared

and opened for access in street clothes. This has been a real

benefit to operators and other workers.

With respect to final implementation of 10 CFR 50, Appendix R

requirements, all identified modifications are scheduled for

completion during the February 1986 refueling outage; however,

there are still two exemption requests being reviewed by the

Office of Nuclear Reactor Regulation. The first concerns

separation of_certain instruments inside containment. The

second concerns the use of high pressure coolant injection as

a source of primary makeup water if a fire occurs in the

charging pump area. These reviews are expected to be complete

during early summer 1986.

2. Conclusion

Although the performance trend in this appraisal period

improved, the licensee continues to be rated Category 2 in this

area, which is the same rating achieved in the last appraisal

period.

3. Board Recommendations

None

F. Emergency Preparedness

1. Analysis

Three inspections were conducted during the period to evaluate

the following aspects of the licensee's emergency preparedness

program: emergency detection and classification; protective

action decisionmaking; notifications and communications;

implementation of changes to the emergency preparedness program;

shift staffing and augmentation; emergency preparedness training;

dose calculation and assessment; public information program; and

independent audits of the emergency preparedness program. One

inspection involved the observance of the annual exercise. In

addition three management meetings were held; (one was held in

May 1985 and two were held in September 1985).

One Severity Level IV violation was issued because the licensee

had not provided the required annual training for some

individuals designated to fill key positions in the onsite

emergency organization. The training records, as reviewed by

the inspectors, were imp 1ssible to reconcile when comparing the

training records with the requirements of the training matrix.

The violation was indicative of a programmatic breakdown in

recordkeeping coupled with the significant change in personnel

in emergency response roles due to the transfer of personnel

20

.

.

from the discontinued Midland Plant to Palisades. The licensee's

corrective actions were thorough, including a review of the

administrative content of all training records and the

appointment of a new training administrator.

The licensee's performance in the August exercise was the

poorest of any Region III facility during 1985, in contrast to

a very good exercise in 1984. Six major exercise weaknesses

were identified as follows: (1) control room participants were

not given time by controllers to evaluate messages prior to

formulating an Alert classification; (2) lack of coordinated

effort between the Control Room and Technical Support Center;

(3) failure to adequately assess and trend radiological field

data; (4) poor and erratic contamination control techniques in

the Operational Support Center; (5) the Emergency Operations

Facility lacked sufficient space and communications equipment

to meet NUREG-0696 guidance; and (6) the offsite monitoring

teams did not decontaminate their vehicles upon leaving the

plume. With the exception of the fifth weakness, all of these

weaknesses related to poor adherence to procedures by response

personnel. On the positive side, the exercise scenario was a

very complicated one, and its complexity made dose assessment

evaluations and technical decisionmaking more difficult for

participants.

'

Management involvement in the emergency preparedness program

has needed improvement. While the licensee has been very

responsive to significant issues brought forward by the NRC,

they had failed to correct the problems prior to NRC management

meetings. The first example of this involved licensee failure

to adequately classify emergency conditions. Although this

issue had been brought up in the preceding SALP period, the

actions taken by the licensee had been ineffective prior to the

management meeting held in May to discuss timely classification

of emergencies and subsequent notifications to offsite

authorities, although the commitment to make classifications

based on initial leek rate calculations was met. As a result

of this meeting, licensee management took action to relieve the

Shift Engineer / Shift Techn % 1 Advisor of some of his emergency

duties. In additior, special training was conducted for all

SR0s on Emergency Action Levels, as well as simulator time

which addressed emergency plan duties as well as recovery of

the plant during accidents. This simulator time was expanded

from five days per year to eight days. The results of these

activities have been the elimination of conditions where

emergency classifications were missed.

Two management meetings were held as a result of the exercise

during which the licensee presented a comprehensive corrective

action program which should result in the improvement of the

1

21

- ._

_ - _ - _ _ _ - - -. -_ -__ - -

. _ _ - _ _ _ . -

.' .

licensee's performance during future exercises. The licensee's

corrective actions included a comprehensive review of EALs,

conduct of several table top exercise / discussions, revising

procedures to make them clearer, clarification of responsibili-

ties and authorities in the emergency organization, involve

General Office personnel in offsite monitoring team drills, and

upgrade the training program. All of these actions included

specified realistic completion dates.

During this SALP period, a significant change was made to the

emergency plan involving the elimination of the General Office

Control Center concept of operations. Licensee personnel

worked closely with their NRC counterparts to ensure that the

change was well coordinated and would meet all applicable NRC

requirements and guidance. This activity demonstrated

excellent responsiveness to technical issues from a safety

standpoint, ensuring that no decrease in the effectiveness of

the plan would occur as a result of the changes.

The licensee is maintaining nine key staff positions with

eleven additional support personnel available for duty in

30 minutes. An additional complement of 15 individuals can be

available in 60 minutes. Augmentation capabilities have been

adequately demonstrated by periodic drills. Both primary and

alternate persons have held key positions in emergency drills

and in the annual exercise, thus testing, where possible, a

second line of emergency expertise.

2. Conclusion

The licensee is rated a Category 2 in this area, the same as

for the previous SALP period. However, with the poor

performance demonstrated in the August exercise, the overall

trend is considered to have declined during this appraisal

period.

3. Board Recommendations

The Board notes that a subsequent inspection conducted after

the end of this SALP period showed that the licensee had made

considerable strides in improvinq their performance in

emergency preparedness. All cortective action completion dates

have been met, and the preliminary indications are that the

training and other activities committed to have resulted in an

improvement in this functional area.

G. Security

1. Analysis

Two routine inspections were conducted by region based inspectors

during this assessment period. The resident inspector also made

periodic inspections of security activities assessing routine

program implementation.

22

.' ..

One violation was identified as follows:

Severity Level IV - Physical Protection of Safeguards

Information: Some safeguards information was not properly

protected. (Inspection Report No. 255/84-24)

The violation did not represent a significant degradation in

the licensee's program to protect unclassified safeguards

information. In the previous SALP, four violations,

representative of significant programmatic weaknesses, were

identified.

The Corporate Property Protection Department's involvement in

site activities and in the performance of audits continued in

this evaluation period. Appropriate actions were taken by site

management in response to audit recommendations. Audit personnel

were qualified and experienced in the area of physical security.

In addition to the annual audit, required by the security plan,

the Corporate Property Protection Department conducted numerous

effective surveillances throughout the assessment period.

The key changes in plant management appear to have had some

positive impact on the overall security program. The security

organization managers appear to be receiving better support and

the new plant managers appear more receptive to ideas and

communication. They are more involved in working with and

monitoring the security organization and have begun to provide

a more cohesive approach to overall security program support.

This support is necessary due to the minimal manning levels of

security management, whose time is further split with functions

other than security. The Guard force size is likewise adequate.

Security records were generally complete, well maintained and

available.

The timeliness of resolution of technical issues was generally

adequate. However, we noted that although some actions were

taken regarding a problem with two vital area doors, final

resolution was not yet achieved. The problems were identified

in a special maintenance inspection in February 1985 and despite

actions by maintenance and engineering staffs those actions

were not successful. Consequently, a more thorough analysis

was completed, but those actions also did not achieve the

results expected as ordered replacement parts did not, in fact,

fit. The final solution is pending receipt of completely new

doors and frames. Additionally a problem regarding the closure

of an important vital area door, identified in October 1984,

has not been completely resolved. Although important progress

has been made, additional corrective actions were still

continuing at the conclusion of this evaluation period.

23

. ..

There have been few long-standing regulatory issues attributable

to the' licensee, with the exception of.the procurement of an

acceptable intrusion detection system for the protected area.

The licensee has adhered to this implementation schedule which

calls for completion of system installation and testing by

December 1986. Progress in the committed schedule has been

satisfactory.

Although there were no events reported to the NRC under the

provisions of the licensee's plan or 10 CFR 73.71(c) some

minor similarities were noted in the items required to be

logged (approximately 12). These similarities or events did

not demonstrate a significant adverse trend. The licensee did I

adequate review of the logged events in accordance with their

procedures. The number and type of logged events in relation

to possible reportable events is not representative of either a

positive or negative trend.

Key positions within the security organization were identified

and authorities were defined in security implementing procedures.

Staffing was minimally adequate. Although no significant

deficiencies in guard force performance were noted, interviews

with several guards and high personnel turnover rates appear

to be indicative of declining guard morale. A continuing

unresolved labor discute between the union and the security

force contractor has resulted in the lack of a contract for

two years. This has impacted individual guards, for example

expected pay raises have apparently not been forthcoming. The

disputes between the contractor's management and the guard union

may lead to a further decline in morale and an associated

degradation of performance and should be closely monitored by

the licensee's management.

The Training and Qualification Program contributes to an

adequate understanding of job responsibilities and fair

adherence to procedures with a modest number of personnel

errors.

2. Conclusion

The licensee is rated Category 2 in this area, the same as the

last SALP period. The licensee's performance has remained the

same over the course of the SALP assessment period.

3. Board Recommendations

None.

24

-. - . . - . - . ~ . _ _ _ _ - _ . _ - _ - - = . - . . -

. ..

1

H. Refueling

There were no refueling outages during this assessment period and

this functional area'was not rated.

I. Quality Programs and Administrative Controls Affecting Quality

.f

1. Analysis

! The assessment of performance in this functional area was based

i -on inspection by the Resident and Region based specialist

inspectors and on the effectiveness of the licensee's overall

management control system in achieving excellence of regulatory

performance.

.,

!

'

Specific directed quality assurance inspections were made

in the following areas: quality assurance program, audits,

,

QA/QC administration, design changes and modifications, test

i and experiments program, surveillance procedures and records,

surveillance testing and calibration control. Related

,

activities necessary t'o support inspections of other functional

l

areas were also inspected.

i Ten violations were identified as follows:

i

i

a. Severity Level IV - Inadequate corrective action for

' missed preventive maintenance of 480/460 volt switchgear

and administrative procedures overdue for biennial review

l (Inspection Report No. 255/85003).

b. Severity Level IV - QA audit findings were not assigned

{ the appropriate level of corrective action (Inspection

Report No. 255/85003).

I c. Severity Level IV - The root causes for equipment

malfunctions were not being identified. (Inspection

,

Report No. 255/85003).

'

d. Severity Level V - Two rubber products were not controlled

for shelf life (Inspection Report No. 255/85003).

l

e. Severity Level IV - Failure to perform 10 CFR 50.59 review

l of leaving East Safeguards Pump room cooler isolated

(Inspection Report No. 255/85009).

i

f. Severity Level IV - Four examples were noted where QA

'

records were missing or were not retrievable. (Inspection

l

Report No. 255/85017).

1

! g. Severity Level IV - Five examples were identified where

l objective evidence did not exist that plant modifications

l were properly installed. (Inspection Report No. 255/85017).

i

l

25

_

. . - - _ - _

, ,. . _ ,_. . -_. _.

..

h. Severity Level IV - Failure to perform 10 CFR 50.59. review

when East Safeguards pump room roof hatches were removed

(Inspection Report No. 255/85018).

.

I i. Severity Level IV - Corrective actions were not timely

i after a QA audit identified a Technical Specification

,

i

violation (Inspection Report No. 255/85027).

I j. Severity Level IV - Three examples were identified where

i corrective actions were not completed as committed in

response to a prior Notice of Violation (Inspection

Report No. 255/85024). .

,

) Violations "a", "b" and "i" provide seven examples of the

failure to obtain or address adequate corrective action to

i prevent recurrence of noted quality-related problems.

!~ Violation "b" indicated a reluctance to assign high visibility

, corrective action status to audit findings. One of the six

!~ examples of failure to follow procedures listed unuer

i Paragraph IV.C. (Maintenance) (see violation "a") detailed

failures to implement. effective jumper, link and bypass

'

i controls despite repeated findings by the NRC and other

inspecting organizations. Subsequent review of this violation

, and others resulted in a further violation - item "j" above.

t An unresolved item identified in one of the inspections

i

disclosed that the quality trend program did not provide for

reporting of repetitive occurrences by cause o- type of

'

occurrence so that action to prevent recurrence can be taken.

] These findings indicate that management attention has not

resulted in timely and adequate corrective action necessary

i to correct the cause of quality problems at all levels of

! corrective action.

Items which required reporting or higher levels of response

]

were generally handled in a timely and appropriate manner. The

i licensee's Corrective Action Review Board and onsite Licensing

Group were major contributors to the success in this area.

f

} As discussed above and in Inspection Report No. 255/85003, a

number of adverse conditions were discovered where procedures

i were not used or not followed resulting in violations.

Management does not yet appear to have taken the action

necessary to assure rigorous compliance with procedures. In

one case, a quorum of the Plant Review Committee decided on a

'

course of action which violated an administrative procedure

! (Paragraph-IV.D. violation "e").

i

'

Violations "c." ud "d." above are considered examples of

l inadequate Audit Program implementation. Both would likely

j have been identified by experienced auditors reviewing the

,

related areas. Otherwise, the audit program was found to be

I

i

1

'

i

26

!

i

, - - - -n--,,,, , , - - , ~-n-, , , . - ~ -, - . - - - , , .. .. --- n m n , n -- -.- - - n..-_ .-,---nm-.,.-.,.,,,- n,,m,,,, -----n-en--,,-,-,r,-

. . .- . - - -. . -_

, ..

a= well managed with the organization adequately staffed with

qualified personnel. Good use was made of " surveillance" type

'

activities at the plant, although some problems were r,oted in

the achievement of corrective actions as previously noted.

Violations "f." and Ug." indicate significant problems in

records preparation, storage and retrieval. A number of

records /providing objective evidence that installat_ ion of

design changes had been satisfactorily completed could not

be retrieved or were inramplete or missing. This indicates

problems in the preparation, checking, storage and retrieval

of QA records related to design charges.

i

Violations "e." and'"h." and item f. in Paragraph IV.C.

J (Maintenance) all relate to inadequate or missing 10 CFR 50.59

'

! safety evaluations. These violations, however, were somewhat

dissimilar in root cause; and one related to maintenance, while

'

the other two related to either operations or design engineering.

The licensee's corrective action to the 10 CFR 50.59 violations

included providing special training sessions for personnel who

may be involved in the modification of systems, and the writing

i of safety evaluations or reviewing them.

l

The design change process, design and procurement control

i were found to be adequate with the exception of one minor

modification (item e. under Paragraph IV.C., Maintenance).

A review of otner minor modifications is underway to assure

that no other similar violations of design control oc':urred.

s

Two Licensee Event Reports (LERs) identified in this area were

asscciated specifically with tracking system errors (LERs 84-23

and 85-17) but were not linked by any common fault.

. t

'

2. Conclusion

,

The licensee is rated Category 3 in this area. Program implemen-

'

tation problems were noted in the area of minor modifications.

Moreover, inspections indicate that the effectiveness of the

i

corrective action program has deteriorated. The problem does

not seem to be limited to a specific activity but appears to

5 bridge several activities in this functional areae A substantial

's increase in the number and significance of violations contributed

to this rating. Overall controls and management oversight

activities related to the maintenance and surveillance areas

were not effective in achieving the desired level of performance.

Based on plant conditions and operational problems experienced

throughout the period, the performance trend this area was

considered to have remained the same.

1

6

27

!

_ - _ - - . _ , - , _ . _ _ _ _ _ ____ . _.. .,, _... _ __ _ _ _ , _ _ _ _ _ , _ . _ _ .

..

3. Board Recommendation

Increased NRC activity should be provided in this functional-

area. A thorough review of QA program implementation including

maintenance, calibration, design changes, material storage, and

record storage and retrieval should be performed during the

next SALP period. ' Emphasis should be placed on reviewing the

corrective action system and adherence to procedures.

J. Licensing Activities

1. Analysis

The basis for this appraisal was the licensee's performance in

support of licensing actions that were either completed or had

a.significant level of activity during the current rating

period. These actions, consisting of amendment requests,

exemption requests, responses to generic letters, TMI items,

and other actions, include the following specific items:

Multiplant Action Items (MPAs) completed or having a

significant level of review include:

  • Appendix R Exemptions (Local Tending of Diesel Generator)

Final Design Modification submitted; Others Completed

  • TMI Item II.E.1.1 AFW System Technical Specifications

Final Submittal made incorporating resolution of NRC

comments

  • Environmental Qualification of Safety Related Equipment,

Completed

Safety Parameter Display System (SPDS) - Modified

submittal made - under review

Detailed Control Room Design Review (DCRDR) Plan -

Completed

Procedures Generation Package - Draft Safety Evaluation

Report (SER) w/open items

R.G. 1.97 - Request for Additional Information sent -

Licensee to respond May 1986

  • G.L. 83-28 Salem ATWS, 9 items completed, 9 remaining

items - submittals in - under review

10 CFR 50.73 (G.L. 83-43), Completed

28

< ,

.' .. ,

Plant Specific Action Items completed or having a significant

level of review include:

  • Main Steamline Isolation Valve and Main Feedwater

Isolation Valve Probabilistic Risk Assessment

SER in final draft

  • Allegation of inadequate cable tray supports, submittal

under review

  • Technical Specification change for D/G surveillance

_

interval, Complete

  • Detailed Control Room Design Review Program Plan, Complete
  • Technical Specifications for Containment Purge and

Ventilation, Complete

  • Technical Specification change for Plant Review Committee

(PRC) approval, Complete

  • Environmental Qualification Implementation Extension,

Complete

  • Radiological Effluent Technical Specifications (RETS)

Modification, Complete

  • ECCS analysis errors, Complete
  • Technical Specification change deleting Reactor Internals

Vibration Monitoring, Complete

  • Supplement 1 NUREG-0737 Confirmatory Order, Complete
  • Technical Specification change - Reactor Vessel

Pressure / Temperature Limits, Complete

A total of 30 licensing actions were completed.

t

Management Involvement and Control in Assuring Quality

With rare exception, there was evidence of prior planning and

assignment of appropriate priorities. Corporate management

made frequent visits to the site and was involved in site

'

activities. Licensing management visited NRC in Bethesda for

pre-submittal planning meetings for the PRA submittal, steam

generator inspection plan, fire protection exemption requests

and the up-coming submittals for spent fuel storage expansion.

Communications improved significantly. There were a few

exceptions to timeliness of submittals, such as the pressure /

temperature limit change in the Technical Specifications and

i

29

o

.__

.' ..

the diesel generator surveillance interval change. There were

changes in the licensing management made late in the report

period. Insufficient time has elapsed to judge the new

management.

Approach to Resolution of Technical Issues from a Safety

Standpoint

In general, the licensee demonstrated an understanding of the

issues, exhibited conservatism,'and provided viable, sound and.

thorough approaches. There were a few instances, however, where

a number of revisions had to be made by the licensee. These

included the revised Technical Specifications for Auxiliary

Feedwater, the justifications for continued operation associated

with extension of the EQ deadline for certain components, and

the yet to be completed resubmittal of Technical Specifications

for leak detection systems. The administrative requirements on ,

the licensee's part for approvals and committee reviews is

multiplied by the number of resubmittals that must be made.

These items could probably have been more expeditiously handled

if meetings were held with the staff or telephone calls made

prior to the formal submittal process. Similarly, the

. licensing process for the staff becomes more burdensome with

the pre-notice requirements for additional submittals.

'

Responsiveness to NRC Initiatives

Responses were generally timely; however, there were occasions

where responses were delayed. Two notable cases that have

experienced delays are the submittals associated with NUREG-0737,

Supplement 1 and the Technical Specifications for leak detection

equipment. Otherwise, the licensee has been very responsive in

meeting deadlines. A significant improvement has been made in

responding to informal requests for information. Commitments

,

made in telephone conversations and in the course of meetings

'

are followed up and this previous weakness (adverse comment in

the last three SALP reports) has been corrected.

"

Staffing

The licensing staff is excel. lent. There is a main licensing

, contact for all routine issues and the normal licensing

'

activities. Special projects, such as fire protection, spent

fuel storage, NUREG-0737, and auxiliary feedwater system

Technical Specifications have other licensing personnel

assigned for project management and co-ordination. However,

support for some of the projects has been light. As noted

previously, support for the activities associated with

NUREG-0737, Supplement 1 has had some problems with attrition

of operating personnel such that initially proposed schedules

had to be slipped. Also, there is apparently insufficient

support to respond to the NRC reviewer's questions regarding

the Technical Specification for leak detection systems.

30

_ _ _ _ __ _ _, . _ _ __ _. . _ _ _ .

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___

..

2. Conclusion

The licensee is rated Category 2.in this area, which is the

same rating given in the previous appraisal period. The

performance trend, as noted.in several areas above, improved

during the appraisal period.

3. Board Recommendations

None.

,

31

. ..

V. SUPPORTING DATA AND SUMMARIES

A. Licensee Activit,ier

Due to heat transfer limitations resulting from steam generator tube

plugging done in the previous SALP period, reactor power was limited

to 98% maximum output for this SALP period. There were no major

planned outages (maintenance, refueling, etc.) during this SALP period.

In contrast to the previous SALP period where the plant experienced

extended outages (the year to date availability factor for 1984 ns

only 15.2 percent), the average monthly availability factor for 4 e

twelve months of this SALP period was approximately 90 percent. The

licensee experienced a relatively good operating cycle from startup on

November.21, 1984 to shutdown for a refueling / Environmental Equipment

Qualification outage on November 30, 1985 (one month after the end of

the appraisal period). In fact, several plant generation records were

set.

During the SALP period three power reductions were made to add oil

which was leaking from a reservoir on a reactor coolant pump (RCP).

Loss of condenser vacuum and numerous (eight) problems with the

turbine governor valve electrohydraulic control system required taking

the turbine off the line several times while maintaining the reactor

critical.

The reactor tripped automatically two times from power. The first

time on August 11, 1985 was due to equipment deficiencies and operator

error in co.ntrolling the main generator voltage. This trip was

followed with a two wod outage to repair RCP seal leakage and control

rod drive seals and to perform diesel generator preventive maintenance.

A second trip on August 30, 1985 was caused by incorrect isolation of

an auxiliary generator trip feature.

A manual shutdown on October 15, 1985 was required due to excessive

primary coolant system leakage from a shutdown cooling system valve.

The plant remained shutdown for four days.

No significant licensing actions or modifications were completed

during the operating cycle.

B. Inspection Activities

(1) There were two special team inspections in the maintenance area

conducted by Region III personnel during the assessment period.

The results of these inspections are discussed in Section IV.C.

(Maintenance).

(2) Facility Name: Palisades Nuclear Generating Station

Docket No: 50-255

Inspection Reports No. 50-255/84-23 through 50-255/84-25

No.'50-255/84-27 through 50-255/84-29

32

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No. 50-255/85001 through 50-255/85013

i No. 50-255/85015 throuch 50-255/85019

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No. 50-255/85021 through 50-255/85025

No. 50-255/85027

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TABLE 1

Inspection Activity and Enforcement

Functional

Areas No. of Violations in each Severity Level

I II III IV V

A. Plant Operations 3

B. Radiological Controls 4

C. Maintenance 5 2

D. Surveillance 4 2

E. Fire Protection 1 2

F. Emergency Preparedness 1

G. Securi ty 1

H. Refueling NOT RATED

I. Quality Programs and

Administrative Controls 9 1

J. Licensing Activities NA NA NA NA NA

TOTALS 28 7

34

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C. Investigations and Allegations Review

On December 24, 1984, a former licensee employee contacted

Region III in regard to alleged test cheating during the auxiliary

operators examination. Although the circumstances alleged were not

substantiated, inspection of the matter disclosed that the licensee

did not have procedures in place to prevent such an occurrence from

potentially taking place. The allegation was documented in

Paragraph 3 of Inspection Report No. 50-255/85009. The allegation

was closed June 3, 1985.

On December 28, 1984, Region III received a call from a-private

citizen who had concerns regarding alleged procedural violations

involving radwaste processing. This was the same allegation as one

received earl.ier in the year, which was referenced in Paragraph 9

of Inspection Report No. 50-255/85004; no violations were cited.

Additional inspection was conducted and reported in Paragraph 10

of Inspection Report No. 50-255/85010. The allegation was closed

March 4, 1985.

On December 29, 1984, Region III received an anonymous telephone

call regarding security at the plant (mainly involving industrial

relations concerns such as low security guard morale caused by

understaffing, lost pay checks, security force overtime hours and

no union contract). The concerns were reviewed by a Region III

security specialist and no violations were identified. The results

were documented .in an internal Region III memorandum to files, which

is exempt from public disclosure due to 10 CFR 73.21 information

being contained therein. The matter is closed.

A January 10, 1985 report of a Midland plant (another Consumers

Power Company facility) allegation review conducted for Region III

by Brookhaven National. Laboratory contained allegations related to

the Palisades facility (see the Category E allegations). The

allegations related to the concerns of a former contractor employee

that: (1) quality control reports failed to reflect problems he had

discovered; (2) transition welds did not meet ASME code requirements;

(3) these were inadequate levels and weld transitions; and (4) there

was excessive fitting of pipe. On May 25, 1985 Region III sent a

letter to the alleger requesting more specific information. On

July 1, 1985 Region III sent a followup letter via certified mail to

the alleger and the receipt-was returned to Region III. No additional

information was received from the alleger and attempts to locate him

were unsuccessful through the end of the assessment period. Region III

intends to close out the allegation in late 1985 or early 1986 without

further action based on the lack of responsiveness of the alleger and

the inability to locate him.

On June 12, 1985, Region III received a letter from a former

licensee employee who alleged that in the event of an emergency at

the plant the operators would leave their posts to be with their

,

35

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I

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families (based on informal conversations the alleger took part in-

when he was a station employee). Based on a lack of specificity or

actual violation noted, the past allegation history of the

individual, and the fact that the alleger's suggested remedial

measures went beyond the scope of existing law and were outside the

jurisdiction of the agency, the matter was closed and documented in

a memorandum dated August 9, 1985 from the Region III Administrator

to the Director of the Office of Nuclear Reactor Regulation (NRR);

the memorandum indicated no further action would be taken by

Region III.but.that any generic implications prompting a review of

licensed operator requirements should be pursued if NRR deemed it

necessary.

An allegation was made on June 15, 1985 by a contractor employee

regarding potentially in~ adequate (re: seismic considerations)

cable tray supports and the possible failure to report the deficiency

pursuant to 10 CFR Part 21. The alleger was recontacted by Region III

and asked to provide additional information. Subsequently, per a

June 26, 1985 conference call between Region III and NRR, lead

responsibility for resolving the allegation was transferred to NRR.

.The allegation' remained open at the-end of the assessment period.

D. Escalated Enforcement Actions

1. Civil Penalties

There were no c ual penalties issued during the assessment

period.

2. Orders

Thee were no orders issued during the assessment period.

E. Management Conferences and Confirmatory Action Letters

1. Conferences

March 12, 1985 - Meeting with licensee management

representatives to discuss SALP 5 (Inspection Report

No. 50-255/85001).

May 3, 1985 - Meeting with corporate and site representatives

to discuss the role of the shift engineer and shift supervisor

regarding emergency classifications and notifications.

July 19, 1985 - Site tour by Regional Administrator and

presentation by licensee on Palisades Plant Plan.

September 5, 1985 - Meeting between Chief, Emergency

Preparedness Branch, Region III and Plant Manager at the site

to discuss concerns identified in last emergency preparedness

exercise.

36

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.' ..

September 20, 1985 - Meeting between Region III Emergency

, Preparedness representatives and Plant Manager / staff to discuss

emergency preparedness issues and develop activities plan to

improve licensee performance.

September 23, 1985 - Special Management meeting. conducted to

discuss weaknesses in the Palisades emergency preparedness

annual exercise of August 20, 1985 and to emphasize Region III's

concern with the overall trend and performance of Palisades

-emergency preparedness program.

October 2, 1985 - Enforcement Conference to review event

involving the failure to perform certain Technical

Specifications required surveillances.

October 17, 1985 - Management meeting between the Regional

Administrator and Consumers Power Company representatives to

discuss maintenance and other issues of mutual interest.

October 24, 1985 - Plant tour by'the Regional Administrator and

management meeting with licensee's Vice President for Nuclear

Operations / staff to discuss the licensee's maintenance program.

t

2. Confirmatory Action Letters (CAL)

July 16, 1985 - Letter confirming actions to be taken by

the licensee as a result of failures noted in the licensed

operator and senior operator NRC administered requalification

examinations conducted on July 1, 1985.

October 30, 1985 - Letter confirming the licensee's actions

to reduce the maintenance backlog which was still found

unacceptable after the maintenance team followup inspection.

F. LICENSEE EVENT REPORTS (LER), CONSTRUCTION DEFICIENCY REPORTS, AND

,

10 CFR 21 REPORTS

1. Licensee Event Reports (LER)

Note: Effective with the issuance of 10 CFR 50.73 (January 1,

1]84) reporting requirements were'significantly changed.

Therefore data for this SALP period are not directly

comparable with prior SALP statistics.

'

'LER No. 84023 through 84027

85001 through 85023

Of the twenty-nine reports submitted during this appraisal

period (SALP 6), six were classified as voluntary reports.

The proximate cause codes for this period's reports, as well

as those of previous periods, are as follows:

37

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n 3

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.

l

CAUSE CODE SALP 4 SALP 5 SALP 6

Personnel Error 3 15 14

Design Deficiency 5 6 1

Deficient Procedure 3 8 2

Component Failure 46 20 10

Other 15 10 1

72 59 28

In general, the LER's provided adequate information to give

a description of the occurrence, the: direct consequences of

the event and the licensee's corrective actions. Some event

reports that contained inadequate or incorrect information

were updated, when the deficiencies were pointed out to the

licensee. In some reports, however, the licensee's use of

tactful expression clouded the real issue of the event.

Three LERs (LER 85-010,85-013 and 85-016) collectively

reported two automatic trips from power and four subcritical

actuations of the reactor protection system due to nuclear

instrument noise.

Nevertheless, the number of events which were attributed'to

personnel error, in part or entirely in this SALP period

remained the same as the prior SALP period. Specific concerns

about these errors were discussed in their respective functional

areas in Section IV of this report. A second statistic of

concern is the number of events attributed to equipment or

component failure. A number of repetitive material problems

continued to plague the plant and are in need of attention,

although the number of events associated with this cause code

was greatly reduced from previous SALP periods. These were

previously discussed under Paragraph IV.C. " Maintenance."

During this assessment period, the NRC's Office for Analysis

.and Evaluation of Operational Date (AE0D) began using a new

methodology to assess the quality of LERs submitted by

licensees. A copy of the AE0D report on the Palisades plant

will be provided to the licensee under separate cover. Summary

comments, however, are provided here. In general, AE00 found

the LERs to be of above-average quality based on the

requirements contained in 10 CFR 50.73. The Palisades LERs

have the third highest overall average score of the 24 units

that have been evaluated to date using this methodology. This

was accomplished (1) without the use of an outline format which

the other high scoring units use, and'(2) in spite of the fact

that two of the ten LERs were of below average quality. If

Palisades were to implement the use of a good _ format and

improve their review process so as to identify and correct

those few LERs which are not meeting current requirements or

which contain minor deficiencies, Palisades could submit even

38

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higher quality LERs in the future. (Note: The AE0D report

only sampled ten of the twenty-nine LERs submitted during the

appraisal period.) AE00 noted the areas most needing

improvement in the LERs were: safety assessment inform'ation;

manufacturer and model number information; date and time

information; previous similar events; EIIS codes; text

presentation and readability; abstract; and coded fields.

2. Construction Deficiency Reports

There were no reports issued.

3. 10 CFR 21 Reports

There were no reports issued.

G. LICENSING ACTIVITIES

1. NRR Site and Corporate Office Visits

May 8, 1985 -

Site visit by J.-Zwolinski for his plant

orientation. Toured plant and met with

Vice President R. DeWitt, Plant Manager

J. Firlit, and other plant management

personnel.

May 9, 1985 -

Corporate office visit by J. Zwolinski to

meet with corporate licensing and engineering

staff. Discussed existing and future

licensing activities and priorities.

July 15, 1985 - Site visit to meet with CPCo and Be; Fuel

Corporation personnel regarding concu.ns

about cable trays in Switchgear Room. Held

meeting and toured Switchgear Room.

2. Commission Briefing

September 18, 1985 - Commission briefed on Main Steam Line

j Break Single Failure Issues at Palisades

3. Schedule Extension Granted

February 25, 1985 - Granted extension to November 30, 1985

for Equipment Qualification, 10 CFR 50.49

4. Relief Granted

None

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5. Exemptions Granted

July 12, 1985 - Granted exemption from the requirements of

Section III.G.3 of Appendix R to 10 CFR 50 for the Engineered

Safeguards Room and the Corridor Between.the Charging Pump Room

and IC Switchgear Room.

6. -Licensee Amendments Issued

Amendment No. 85, issued November 9, 1984, Radiological

Effluent Technical Specifications (RETS)

Amendment No. 86, issued December 10, 1984, Plant Review

Committee Review Process

Amendment No. 87, issued April 29, 1985, Two Modifications Made

to RETS issued in Amendment No. 85

Amendment No. 88, issued June 6, 1985, One time extension of

allowable outage time for emergency diesels from seven to 10

days for the month of May 1985

Amendment No. 89, issued August 21, 1985, Revised Pressure /

Temperature Limits for Reactor Vessel per Appendix G to 10 CFR 50

Amendment No. 90, issue'd August 26, 1985, Limiting Conditions

for Operation and Surveillance-Requirements for Containment

Purge and Vent

Amendment No. 91, issued September 5, 1985, Deletes

Specification 4.13 Reactor Internals Vibration Monitoring

Amendment No. 92, issued October 28, 1985, Revises Diesel

Generator Surveillance Frequency from every 18 months to each

refueling cycle

7. Emergency / Exigent Technical Specification

On May 24, 1985 an emergency Technical Specification change was

made to extend allowable outage time for diesel generators.

This change was formally issued as Amendment No. 88.

8. Orders Issued

Order Modifying License to Confirm Additional Licensee

Commitments on Emergency Response Capability (Supplement 1 to

NUREG-0737) was issued on July 1, 1985.

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9. .NRR/ Licensee Management-Conference

On August 21, 1985 CPCo Director of Licensing and two of his i

staff met with the Director, Division of Licensing, ONRR and

members of his staff to present an overview of the

single-failure issues associated with the main steam line break

accident analysis for Palisades.

t

41~

. _ _ .- - _ _ _ _ _ _ _ _ _ - _ _ _ _ . _ _ _ - - _ - _ _ _ - _ _ - _ _ _ _ - - _ _ _ - _ - - _ _ _ - _ _ _ _____-. - _ _ - _ - _ _ _ - _ _ _ _ _ _ _ _ _ - _ _ - - - _ -