IR 05000255/1993002

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Insp Rept 50-255/93-02 on 921229-930208.No Violations Noted. Major Areas Inspected:Previously Identified Items, Operational Safety Verification,Maint,Surveillance & Design Changes
ML20128N973
Person / Time
Site: Palisades Entergy icon.png
Issue date: 02/17/1993
From: Jorgensen B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18058B475 List:
References
50-255-93-02, 50-255-93-2, NUDOCS 9302240052
Download: ML20128N973 (17)


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i U. S. NUCLEAR REGULATORY COMMISSION REGION 111

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Report No. 50-255/93002(DRP)

Docket No. 50-255 License No. DPR-20 Licensee: Consumers Power Company 212 West Michigan Avenue Jackson, MI 49201

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facility Name:

Palisades Nuclear Generating Facility Inspection At:

Palisades Site, Covert, H1 inspection Conducted: December 29, through february 0,1993 Inspector :

J. K. Heller 0. G. Passehl 8/87/E3 Approved By:

n ief

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deactor Projects Section 2A DXTE

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Insotqtion Summary inspection f rom December 29._j992. throuah february 8.1931 (Report No. 50-255/9300?l0RPil Areas inspected: Routinn unannounced inspection by the resident inspectors of actions on previously identified items, operational safety verification,.

maintenance, surveillance, design changes, and quality program, activities, a

Results: Of the six areas inspected, no violations or deviations were identified in any areas.

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t The strengths, weaknesses, and Inspection Followup Items are discussed in paragraph 1, " Management Interview."

In summary, strengths were noted in the trending program for liquid leaks in'.ide containment, the detail used to analyze a " post-event" report, and the

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well-managed repair to a che:nical and volume control system charging line.

Weaknesses were noted in a personnel error that rendered an. emergency diesel generator inoperable, inadequate updating of a work order af ter the scope of the wo'rk order had changed, and in the administrative process-of writing and approving " periodic and predetermined activity control" documents.

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DETAILS 1.

Manauement Interview (71707)

The inspectors met with licensee representatives denoted in paragraph 9 on February 12, to discuss the scope and_ findings of the inspection.

In addition, the informational content of the inspection report with regard to documents reviewed during the inspection was-also discussed.

The licensee-did not identify any such documents or processes as proprietary.

Highlights of the exit interview are discussed below:

a.

Strengths noted:

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1)

The licensee's' trending program resulted in early detection of a leak in a containment air cooler (paragraph 3.b).

2)

The detail of a post-event review (paragraph 3.d).

3)

A well managed repair for the chemical and volume-control system charging line (paragraph 4.c),

b.

Weaknesses noted:

1)

Personnel error that resulted in an inoperable diesel generator (paragraph 3.c). The frequency of personnel

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error' appears to be increasing and will be evaluated in a subsequent report.

2)

Documentation problems pertaining to changing the work scope.

of a work order and the updating of a'" periodic and predetermined activity control" (PPAC) document.

Additionally, the administrative process for writing and approving a PPAC was not clear and concise. (paragraph 4.b).

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c.

The inspector cuestioned whether a surveillance test' established artificial concitions that may mask integrated system responso during an event (paragraph 5.a),

d.

An inspection followup item was discussed (paragraph 7'.b).

e.

Problems that occurred at other plants were discussed.

These-included tampering with plant records and lack of an acceptance criteria for operator. rounds (paragraphs 7.a and 7.b).

2.

Actions on Previous 1v Identified items (92701, 92702)-

(Closed)-Open item 255/90018-03(DRP): Heat trace circuit. overheated causing-the heat trace material to ignite.

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On August 13, 1990, a fire occurred in the "B" evaporator area.

Contractors were installing thermal insulation on the "B" evaporator when a heat trace temperature sensor wcs dislodged and -- when activated-

-- started sensing ambient room temperature instead of the~ output from the heat trace wiring. With the sensor registering ambient room

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temperature, the heat trace controller turned the heat trace full on.

This resulted in overheating of the heat trace material and smoldering of insulation. The fire was extinguished.

The heat trace and insulation were repaired.

The licensee re-trained the workers pertaining to the proper method to install the installation, sensors, and heat trace wiring.

No similar events have occurred to date.

No violations, deviations, unresolved or inspection followup items were identified.

3.

Operational Safety VerificaliQD (71707, 71710, 42700)

Routine facility operating activities were observed as conducted in the

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plant and from the main control room. Power operation of the plant was observed as applicable.

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The performance of reactor operators and senior reactor operators, shift i

engineers, and auxiliary equipment operators was observed and evaluated.

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included in the review were procedure use and adherence, records and.-

logs, communications, shift / duty turnover, and the degree of professionalism of control room activities.

Evaluation, corrective action, and response for off normal conditions

were examined. This included compliance to any reporting requirements.

Observations of the control room monitors, indicators, and recorders were made to verify the operability of emergency systems, radiation

monitoring systems,.and nuclear reactor protection systems.

Reviews'of surveillance, equipment _ condition, and tagout. logs were conducted.

Proper return to service of selected components was verified,

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a.

General The plant operated at essentially full power'during this reporting period.

b.

Containment Sumo level Monitorina proar3JD

-- NRC Inspection Report-No. 50-255/92027(DRP) discussed the_

licensee's December 23, 1992, repair of a service water leak from

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one of the containment ~ air coolers.

Detection of this problem demonstrated the licenree's ability to monitor-and trend leakage i

to the containment sump. -The containment sump level monitoring ~

program has proven to be effective in-detecting, measuring, and trending liquid leaks.inside containment.

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F The containment air cooler service water leak was initially identified when the licensee noted an unexpected containment sump level increase. The licensee initially speculated that the increase in sump level was due to increased leakage at the control rod drive (CRD) primt.ry coolant pressure boundary seals.

Leakage

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from these seals is monitored weekly and was trending upward (see i

paragraph 3.e, " Temporary Waiver of Compliance and Amendment to

Facility Operating License"). The increase in containment sump level indicated that the leakrate to the sump was approximately

1200 ml/ min.

CRD seal leakage is measured by auxiliary operators during weekly containment tours.

Operators expected a leakrate of approximately 1200 ml/ min but found a leakrate of approximately 700 ml/ min.

During the containment tour, the auxiliary operators discovered water in an area _where safety injection piping is located., The licensee analyzed a sample of the water and concluded that'it was

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service water from a containment air cooler.

This leakage

accounted for the additional leakrate of approximately 500 ml/ min.

  • The licensee's containment sump level monitoring program resulted in quick identification and early resolution of the containment

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air cooler leak. This is another example of a strong trending and

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monitoring program that was recognized in the previous SALP

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report, c.

Two Emergency Diesel Oenerators Inoperable

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j On January 6, '1993, at I a.m. the licensee declared an unusual i

l event when both emergency diesel generators _-(D/Gs) became inoperable.

The unusual event condition was exited about two minutes later, when one of the D/Gs was returned to operable status. The inspector reviewed the emergency plan and concluded

that this event was properly-classified and reported.

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An auxiliary operator was removing D/G 1-1 from service ~per switching and tagging order (S&TO) 93-0013. The operator had removed from service the electrical output breaker for D/G 1-1 and proceeded to activate the overspeed trip.

Instead of activating

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the overspeed trip for D/G'l-1, the operator _ activated the:

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overspeed trip for D/G l-2.

This made 0/G l-2 inoperable at.the

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L same time that D/G l-1-was inoperable.

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L-The auxiliary operator immediately recognized his error, reset th'e overspeed trip, and notified the control room of-his' error.> The-control room initially became aware of the error'when a D/G l-2 trouble alarm was received.

Prior to_ declaring D/G l-2. operable, the overspeed device was reset and a successful start _of the_D/G'

was completed.

The inspector interviewed the shift supervisor, shift engineer, control room operators, operations superintendent, and the.

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operations manager.

The above information was confirmed, and the inspector was informed that the shift supervisor considered i

Fitness-For-Duty testing but concluded it was not necessary based

on personal observations of the auxiliary operator before and

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after the error.

The inspector reviewed S&TO 93-0013. The S&TO was clear and concise.

The S&TO required dual verification. However, the error was self disclosing before a second auxiliary operator was

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assigned to perform the dual verification.

The inspector reviewed the licensee's internal corrective action docun-nts and found that written statements from the individuals involved in this event were included; this exceeded the

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administrative requirements for the corrective action program.

The licensee internal investigation of this event was thorough.

1he inspector concluded that this was a~ classic case of the wrong train being removed from service. However, the inspector noted i

positive aspects to the event, including the willingness of the auxiliary operator to identify his-mistake and the timely response of the control room staff to the out-of-service condition.

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d.

Safeauards Transformer 1-1 Electrical fault

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During the midnight shift on January 28, 1993, a protective relay automatically removed the switchyard 345 kV

"f" bus and the safeguards transformer from service.

The safeguards transformer

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was the primary source of-power for the "C" and "D" 2400 volt safeguards vital-busses, as well as for the non-vital 2400 volt

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"E" bus. The loads transferred to the startup transformer (an alternate power supply). Also, momentarily lost was a non-safety

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related instrument bus, Y-01.

A number of systems were affected when Y-01 momentarily lost power

during the transfer to its alternate power source.

With Y-01 de-energized, the control valves for the moisture separator e

reheaters (MSR) went closed.

This resulted in tne unit settling at a new power level of 97 percent, due to an efficiency loss from the isolated MSRs.

Additionally, there was a voltage transient-

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that was sensed at the power supplies for turbine digital hydraulic controls (DEH).

This transient was similar to a previous transient that had tripped the plant because the DDI

controls did not transfer to an alternate' power supply.

As a result of modifications made subsequent to the last plant trip,

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the DEH successfully transferred to-the backup power supply.

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Trouble shooting activities on the safeguards transformer identified a grounded current transformer cable. This resulted in-

actuation of protective relays that tripped the safeguards -

transformer. -The cable was_ replaced and the safeguards transformer returned to service.

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Although there was no reactor trip, the licensee used the information. gathering techniques of their post-trip procedure to analyze and produce a " post-event" report for this event.

The detail included in the post-event report enabled the licensee _to perform a thorough analysis of this event.

This was-considered a strength, e.

Temporary Waiver of Comoliance (TWOC) and Amendment to Facility goeratina License The licensee was granted a TWOC from the biweekly Technical Specification surveillance frequency requirements for testing two control rod drive mechanisms. The TWOC was verbally granted on.

January 14, 1993, and approved in writing on clanuary 15, 1993.

The-TWOC allowed-the licensee to discontinue biweekly surveillance testing of control rods 20 and 31 until an amendment was granted that changed the surveillance test frequency of the two rods to quarterly. The amendment (number 155) was granted by letter datsd January 29, 1993.

Control rods 20 and 31 developed increased primary coolant leakage at the boundary seal during the current operating cycle.

The biweekly testing, which required movement of the control rods, was aggravating the leakage. The licensee stated that repeated testing of a control rod with a leaking seal could shorten seal life and increase the leakage of primary coolant past the control rod seals.

This could lead to a forced shutdown due to excessive primary coolant leakage.

The' licensee also stated in tht January 14, 1993,- letter that they.

would submit a subsequent itcense-amendment request to revise the test frequency of-all control rods during plant operation' from

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biweekly -to quarterly.-

No violations,- deviations, unresolved or ' inspection. followup items were identified.

4.

Maintenance (62703, 42700)

Maintenance activities in the plant were routinely inspected, including both corrective maintenance (repairs) and preventive maintenance.

Mechanical, electrical, and-instrument. and control group maintenance activities were included as available.-

The focus of the inspection was to assure the maintenance activities reviewed were conducted in accordance with approved procedures, regulatory guides and industry codes or standards, and in conformance with Technical-Specifications. The following items were considered-during this review: The Limiting conditions.for Operation were met while components or systems were removed from service; approvals were obtained prior to initiating the work;~ activities were accomplished,

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using a) proved procedures; and post maintenance testing was performed as applica)1e. The following activities were inspected:

a.

Lube Oil Pressure Deficiencies in._Charoina Pumo P-SSB The three work orders discussed below were reviewed after three separate occasions of lube oil pressure deficiencies in charging pump P-558. The first two work > orders addressed low pressure conditions; the third was a high pressure condition.

All three conditions occurred during a four week time frame.

The inspector reviewed these work orders to determine if the quality of maintenance was satisfactory, and if enforcement action was appropriate.

The inspector found that the overall work was satisfactory.

The licensee identified and resolved several root causes during the course of its repair efforts. Not all of the problems were identified during the initial troubleshooting activities because-some were masked by others.

The inspector found the licensee made reasonable attempts at finding all of_ the problems.

Support _from the system engineer and maintenance supervision was adequate.

However, in the case of the high oil pressure condition, the licensee could have been more proactive in adjusting the pressure output of the oil pump, which was identified as the root cause.

This was apparently a simple fix that the licensee let lapse:for three weeks.

(1)

Work Order 2404744, "P-55B; Correct Low Lube Oil Pressure."

The licensee found during performance of Technical S)ecification test Q0-17, " Inservice Test Procedure -

Ciarging Pumps," that 1ube oil pressure in charging pump P-55B was slightly low at 19 psig. - The acceptance criteria stated in the-00-17 procedure was 20 to 50 psig.

The licensee declared P-55B inoperable and commenced repair activiths.

No Technical Specification Action Statements applied since charging pumps P-55A and P-55C were operable.

In addition to the work order, an upper tier Corrective Action Report (Deviation Report) was issued.

Maintenance and system engineering personnel performed extensive troubleshooting.

The root causes identified were:

(a)

A worn oil pump. The oil pump was replaced twice because the-first replacement pump also exhibited low discharge pressure when tested.

(b)

A minor crimp in the oil pump suction line.

The suction line was replaced.

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(c)

Loose. oil pump shaft packing follower and ca) screws.

Both the original and replacement oil pumps 1ad this problem. Maintenance personnel did an excellent job

in identifying this problem.

The need to verffy the tightness of the capscrews was nct in

the procedure nor was it a vendor recommendation.

The inspector considers this finding to be a strength en the part of the mechanics. The licensee identified the need to-enhance the charging pump maintenance procedure CVC-M-22,

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" Charging Pump Maintenance for P-SSB and ?-550."

The pump was initially run with the crankcase cover removed

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with no visual evidence of gross oil leakage observed.

The crankcase was installed, and the pump was returned to operable service after successful performance of Q0-17..

(2)

Work Order 24204953, "P-553; 011 Pressure at 10 psig."

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This low oil pressure event occurred almost three weeks after the pump underwen' the maintenance described in the

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previous paragraph. Cha ging pump P-55A, the normal in-service pump, was removeo from servico to repair its leaking

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seals.

Charging pump P-SSB was started to replace P-55A, i

and had run for about 45 minutes when an auxiliary operator reported P-558 running with an oil pressure of 10 psig.

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licensee issued another Deviation Report.

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Maintenance personnel found the root cause to be a crack in the copper tubing on the discharge side of'the pump. The crack had likely been present during the low pressure condition described in the previous paragraph.

The inspector determined that it was. reasonable.that maintenance mechanics had not identified the presence of the

crack during the preceding event.

The crack was located under a fastener that connected the discharge tubing to the

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pump. Adequate lube oil pressure was obtained during the previous post maintenance test, and the pump was operated with the crankcase cover removed with no evidence of gross oil seepage.

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The licensee's opinion was that the crack probably was -

forced shut during-the preceding work order activity and had-vibrated loose during subsequent running of the pump..The inspe: tor agreed this was probably the case.. Improper installation of the fastener was ruled out because the installation passed inspection by a-maintenance. supervisor.

Technical Specification test 00-17 was satisfactorily performed after the cracked oil-line was replaced._ The

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discharge pressure of.the oil pump was 38 psig.

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Work Order 24205064, "P-55B; Lube 011 Pressure Too-High At 59 psig."

A couple of days after the low (10 psig) oil pump discharge l

pressure condition was corrected (see the preceding.

paragraph), the system engineer noted oil pump discharge pressure to be 59 pstg.

The system engineer initiated a

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work request to decrease the oil pressure.

No Technical Specification Action Statement applied since the other two i

charging pumps remained operable.

The licensee determined that there was no immediate

operability concern since the ASME Section XI recuirements_

were met. Additionally, th9 pum) curve showed acequate output flow at the observed disclarge pressure.

The root cause evaluation identified an apparent problem with the pressure adjustment on the new oil pump when it was installed as discussed in (1) above.

The output pressure of the oil pumps is adjusted by an internal set screw. The maintenance procedure required that the pressure adjustment-on a new oil pump be taken from the as4found setting from the old oil pump.

In this-case, the mechanical setting was transferred to the new pump as stated in the maintenance procedure.

The problem was that this resulted in an oil pressure setting on the new pump which slowly-increased out of specification with extended pump operation.

The system engineer wrote a Work: Request to_ adjust.the setting but this was not performed until.approximately three-weeks later. This was not a timely _ action contidering potential pump operability questions.

Had there been another charging pump inoperable during this-time, then the-

~ licensee might have unnecessarily entered a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> Technical Specification Action Statement on the charging pumps.

The system engineer stated in the Deviation Report that in the future, System Engineering would be more proactive ini

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prompting corrective correction, b.

Kork Order 24100585. "PASM Panel Instrument Calibration nor Eeriodic and Predetermined Activity Control (PPAC) PCS-025."

The inspector did_not observe-the~ performance of this work-order, but performed a_ technical review of-selected subsections #to

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determine how temperature-elements TE/ TIS-1902 and TE/ TIS-1903:

were calibrated. - This review.was performed to resolve questions-identified in paragraph 5.a "Q0-1-Safety injection-System" of-this report pertaining to the isolation capab_ility of those temperature elements.

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i The inspector reviewed the following: microfilm and computerized i

version of the work order which was performed on March 16, 1992;

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revision 15 of Piping and Instrumentation Diagram (P&lD) M-219.

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sheet Ib dated July 9, 1992, for the process sampling system; PPAC 025 dated October 27, 1992; and, administrative procedure AD 5.14

" Periodic and Predetermined Activity Control."

In addition, the

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inspector interviewed the system engineer for the sampling system, the recently re-assigned project engineer for the PPAC system, and

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the instrument and control (I&C) superintendent.

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The results of the inspector reviews and interviews are documented bel ow, i

(1)

P&lD M-219 documented the temperature rating at the output of the sample coolers was 105 degrees fahrenheit and identified that valves will automatically isolate the sample

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sink if high temperature is detected.

(2)

Step 19 of PPAC PCS025 performed a calibration of TE/ TIS-1902 and required verification that SV-1915 (low pressure safety injection sample bleed valve) goes closed.

This is incorrect; P&lD M-219-1B documented that TE/ TIS-1902 will

isolate a portion of the sample sink by closing SV-1916

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(reactor coolant sample block valve) and will isolate a

bypass line by closing SV-1917 (reactor coolant sample bleed valve) when high temperature is detected.

TE/ TIS-1902 does not operate SV-1915.

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The computerized version of the work order that performed the PCS025 on March 17, 1992, verified that SV-1915 went closed, and the microfilm version contained a " pen and ink" change that verified that the SV-1916 went closed.

The inspector reviewed the microfilm version and was unable to find a technical reason or reference to the documents reviewed to justify the " pen and ink" change.

(3)

Step 20 of PPAC PCS025 performed a calibration ~ of TE/ TIS-1903 and required verification that SV-1916 goes closed.

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This should be SV-1914.

P&lD M-219-1B documented that TE/ TIS-1903 will isolate the sample sink by closing SV-1914

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(low pressure safety injection sample block valve) and bypass valve SV-1915 when high temperature is detected.

TE/ TIS-1903 does not operate SV-1916.

The computerized version of the work' order that performed the PCS025 verified that SV-1916 was closed, and-the

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microfilm version-contained a " pen' and -ink" change that =

verified SV-1914 went closed.

The inspector reviewed the-

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microfilm version and was. unable-to find a technical reason or reference to the documents reviewed to' justify the " pen-and ink" change.

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(4)

The inspector looked at the sample sinks and found that a mimic of the system configuration was on the control panel.

The mimic identified which valves go shut when high temperature was sensed at a temperature element.

The inspector questioned whether the mimic may have been used as the justification for the " pen and ink" changes.

If the mimic was used then the inspector questioned if the " pen and ink change" received the proper technical-review.

The use of unjustified " pen and ink" changes in documenting steps 19 and 20 of PPAC PCS025 was discussed with the 1&C superintendent and at the management interview.

(5)

Based on the above, the inspector reviewed AD 5.14 and.found that the procedure was not' clear as to:

(a)

the administrative mechanism to change a PPAC that was incorporated into a work order. As shown above,-the inspector was unable to find that a technical review was performed when a change was made to PPAC PCS025:

implemented by the work order.

(b)

how to change the-controlled copy of the PPAC when an error was identified. As shown above, the-inspector found that the controlled copy of PPAC PCS025 contained errors approximately seven months after it-was last performed. Additionally. PPAC PCS025 was not targeted for a revision.

(c)

the administrative mechanism to issue.a PPAC'and what technical reviews were required before the PPAC was issued for unrestricted use. As shown above, the inspector identified technical and administrative errors that should have been identified during the initial review / approval process.

The inspector discussed the items' addressed above with the system-engineer, 1&C cuperintendent, and the recently assigned PPAC-project engineer.

The inspector was informed that the licensee-was aware of these types-of weaknes:es.

This had prompted the-maintenance manager to temporarily assign an individual as the.

PPAC project engineer. This position was filled in October of 1992 and resulted in programmatic changes that should address the weaknesses addressed above.

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The inspector noted that the weaknesses identified above' appeared administrative and did not result in inoperable-equipment.

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c.

Work Order 24D5676. " Manual operation of Charaina Pumn p-55A

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discharae isolation valve was severely limited."

This repair required isolation of the normal charging path for the chemical and volume control system.

This required a well-planned

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maintenance effort because any delay could result in charging via an alternate flow path. That would introduce concentrated boric acid into the primary coolant system and possibly force a plant

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shutdown.

The inspector toured the work site before the repair activity was authorized.

He found that the repair equi) ment and replacement parts were are-staged at the work site. Tie inspector attended

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the-prejob artefing and found that the meeting was well conducted,

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orderly, and demonstrated that communication barriers did not -

exist between the work groups involved.

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The inspector observed the performance of this work activity and-

concluded, after interviews with the operators and mechanics, that i

this was a well coordinated and managed repair activity.

No violi.. ions, deviations, unresolved or inspection followup items were-identified.

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5.

.Sjfrveillance (61'726, 42700)

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The inspector reviewed Technical Specifications required surveillance testing as described below and verified that testing was parformed in accordance with adequate procedures.

Additioni.11y, test-irstrumentation was calibrated, Limiting Conditions for Operation were met, removal and restoration of the affected components were properly accomplished, and'

test results conformed with Technical Specifications and procedure recuirements.

The results were reviewed by personnel other than the incividual directing the test and deficiencies identified during' the lasting were properly reviewed and resolved by appropriate management personnel.

The following activities were inspected:

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a.

-00-1 Safety in.iection System.

The inspector did not observe the performance of this test but-l performed a limited post test review after the event discussed in-

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paragraph 3. d, " Safeguard Transformer 1-1 Electrical Fault;" The

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test was written to demonstrate the operability:of the safety

' injection system initiation circuitry by using the internal: test feature of the system.

The inspector's review'of the prerequisite section (Section 5.) of'

00-1 raised?a question whether this section was creating artificial. conditions.that could mask the integrated system response during an actual safety injection signal-(SIS).

The~

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prerequisite section required closure of primary system sample

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isolation control valves CV-1910 and CV-1911 before performance of l

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the test.- These valves are in-series containment penetration

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isolation valves from the primary coolant system to a sample sink that are located in the auxiliary building. The valves were

considered to be outside the scope of the test because they do not i

change position during a SIS.

However, the prints show that

s cooling water to the sample sink is isolated during a SlS.

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Closing CV-1910 and CV-1911 prior to performance of the test

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ensured that hot primary coolant system (PCS) water was not introduced to the sample sink during the test.

CV-1910 and CV-1911 are normally open for approximately five hours per day to r

facilitate sampling activities.

i The inspector reviewed the corrective action file and found a

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deviation report (DR-PAL-80-160) that discussed performance of the-i test with CV-1910 and CV-1911 open.

That report documented that i

delays in completion of the test permitted a sustained flow of hot

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primary coolant to a sample sink that did not have cooling water I

i available because of the SIS.

The hot water damaged some of the

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valves down stream of the sample sink.

According to P&lD diagram M-219-18, the temperature rating at the output of the sample sinks is 105 degrees fahrenheit.

Additionally, there is a temperature element (TE-1902) downstream i

of the sample sink that should close,a supply line isolation valve

if high temperature was detected.

The emergency operating

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procedures required verification that valves CV-1910 and 1911.are

closed following a SIS.

The inspector was unable to determine the i

time duration from a SIS until the emergency operating procedures l

required verification that CV-1910 and CV-1911 were closed.

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The inspector discussed the topic of integrated system response i

with the operation superintendent who acknowledged that the isolation ~ feature of TE-1902'should be tested. He stated that i

performance of an integrated system test would put. unnecessary

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stresses on the sample sink heat exchanger and that the isolation feature should be confirmed during calibration of the TE-1902.

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The inspector reviewed the periodic and predetermined activity control (PPAC) index and found that the calibration of TE-1902 was aerformed by the post accident sampling panel instrument caliaration PPAC number PCS025.- This activity is discussed in paragraph 4.b, " Work Order 24100585 - PASM Panel-Instrument Calibration"'of this report.

It did not accomplish complete, -

well documented testing of temperature-based isolation _feitures of TE-1902.

The inspector acknowledged that an integrated-system test was not the intent of Q0-1, and that performance of an integrated system each quarter may put unnecessary stresses on the system.- However,

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the test as written may mask a design problem or equipment problem

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not identified during a calibration activity.

This topic was discussed at the management interview.

b.

DWO - 13 LLRT of the Containment Airlock c.

M0 - 76 Emeroency Diesel Generator'l-1 Monthly Surveillance

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00 - 17A Inservice Test of Charaina Pumn P-55A e.

MO - 03 Reactor Protective Matrix Relav

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No violations, deviations, unresolved or inspection followup items were identified.

6.

Desian Chanaes (37700)

Specification change (SC) Number 91-135 " Modification of the 2400/4160

Volt Breaker indication for Bus lA, IB, IC, and~10."

The inspector found that the overall preparation of SC 91-135 was assigned to a project angineer who was responsible for the project from-conception to completion.

There were several subsections of this--SC that pertained to preparation of the work instructions, work orders, or-test procedures.

These subsections were ass *gned to different work groups but still. remained the responsibility of the project engineer.

Several positive attributes were noted.

The overall design change.

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package, as well as each subsection received individual 10 CFR 50.59 evaluations.

The work instructions and test procedures were very detailed, easy to follow, and the author did not take shcrt cuts when preparing the test procedures or work instructions.

For example, the work Instructions and test procedures were unique to a breaker,

,

On the negative side, the' package did not adequately restate the commitment and commitment dates.that had been made to the NRC..This

,

contributed to the communication problem between the NRC and the utility discussed in paragraph 6.a, " Incorrect Information Provided to the NRC" of Inspection Report No. 50-255/92027(DRP).

No' violations, deviations, unresolved or inspection followup items were identified.

7.

O_qality Proaram Activities (37701, 38702, 40704, 92720)

The effectiveness of management controls, verification and oversight-

. activities, in the conduct of_ jobs observed during.this inspection,-was evaluated.

The-inspector frequently attended management and supervisory" meetings involving plant status and plans and focusing on-proper co-ordination-among departments.

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The results of licensee auditing and corrective action programs were routinely monitored by attendance at Corrective Actinn Review Board (CARB) neetings and by review of Deviation Reports, Event Reports, Radiological Deficiency Reports, and security deficiency reports. As-applica61e, corrective action program documents were forwarded to the NRC Region 111 technical specialists for 9 formation and possible followup evaluation.

a.

I mperina with Plant Records.

The inspector discussed two recent events with plant management.

These events occurred at other nuclear power plants and pertained to falsification of plant records.- The first event resulted when an operator failed to repor' and document control rod movement errors.

The operator incorrectly moved control rods and conspired with several operators to cover up the error. The error was identified and reported by ar.other member of the plant staff when the conspirators were overheard discussing the coverup. The event resulted in strong disciplinary action by the utility and intensive inspection activity by the NRC because the event demonstrated a lack of trustworthiness and integrity on the part of the operators.

The second event pertained to a failure of several chemistry technicians to verify that liquid discharge limits to a river were

.

not exceeded, in this case a state permit for discharge-limits

'

may not have been complied with because the required inspections were not performed.

Legal action from the state is pending.

Both events were discussed with the licensee.

The licensee was aware of the events and had emphasized the need for a working atmosphere that encouraged identification and documentation of personnel errors, b.

Failure of Plant Review Committee to Review Security Implementina Procedures.

During a review of the procedure revision processes, the licensee discovered that they.were not in literal complianca with Te'chnical.

Specification (TS) 6.8.1.d and 6.8.2.

TS 6.8.1.d requires written procedures be established,-implemented, and maintained covering the site security plan.

TS 6.8.2 requires.that procedures required by TS 6.8.1 be approved by.the appropriate senior department manager and, by reference to TS 6.5.3, be approved by the Plant Review Committee (PRC).

The security implementing procedures have never been approved.by the PRC.

The NRR project manager reviewed this Item and-determined that.the licensee had requested, by letter dated September 23, 1988, deletion of a sentence from TS 6.8.2 that stated: "PRC is responsible for the review 'of each procedure of 6.8.1 above,- and changes thereto (except for Security Implementing Procedures which

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are. reviewed and approved in accordance with the Site Security

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Plan)."

The NRC approved the request via TS Amendment No. 127,

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eliminating the exception for security implementing procedures.

f When Amendment No. 127 was approved, the licensee never changed

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their administrative procedures to reflect the required PRC

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reviews of the Security implementing Procedures.

Instead, the licensee continued to review the Security Implementing Procedures

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in accordance with the Site Security Plan.

The licensee has revised the procedure review process to capture PRC review of security implementing procedures.

Also, the

licensee is preparing a TS change request to delete PRC review of

security plant procedures.

r The inspector reviewed this item for enforcement action. The

'

inspector was unable to determine if this is an administrative i

problem or if there is a technical reason to require PRC review of the' security implementing procedures. Additionally, the inspector was unable to determine if inadequate reviews were performed or_

i items were missed because the PRC did not review security

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implementing procedures. The inspector has requested a technical

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L review of this item by Region III security specialists.

Pending

their review, this is considered an Inspection Followup Item ~

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(255/93002-Ol(DRP))

c.

Inoperable Eouipment

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The inspector discussed an event that occurred at another plant pertaining to-the lack of an acceptance criteria in the operator's l

log sheet.

In that case the log sheet did not provide-an s

acceptance criteria for diesel generator lube oil level. The

'

failure to provide an acceptance criteria resulted in an inoperable diesel generator when the diesel generator tripped due

p to low lube of' pressure.

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One inspection followup item was identified.

No violations, deviations, i

or unresolved items were identified.

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8.

Inspection followuo iteml

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i Inspection Followup Items are matters which have been. discussed with the L

licensee, and will be reviewed further by the_NRC.

These involve some action on the part of the NRC, licensee, or both. An inspection

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Followup Item disclosed during;the inspection is' discussed in-paragraph 7. b.

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-Persons Contacted

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-Consumers Power Company.

  • G. B.JSlade,: Plant General Manager.

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  • T., J.-Palmisano, Plant Operations Mantger s.

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  • P. M. Donnolly, Safety.& Licensing Director f

K. M. Haas, Radiological Services Manager

  • J. L. Hanson,10perations Superintendent
  • R. B. Kasper,' Maintenance Manager;
  • K. E. Osborne, System Engineering Manager-

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D. D. Hice, Chemistry Superintendent D. J. Malone, Radiological Service Superintendent i

W. L. Roberts, Senior Licensing Engineer K. A. Toner, Electrical /I&C/ Computer Engineering Manager 1. A. Buczwinski, Engineering Programs Manager

  • C R. Ritt, Administrative Nanager tutchar_Recul a tory Commission (NRG1

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  • J. K. Heller, Senior Resident inspector O. Passehl, Resident Inspector

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  • Denotes some of-those present at the management-interview on February 12, 1993.

Other members of the plant staff,.and several members of the contra'ct-

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security force, were-also contacted during the-inspection period.

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