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Category:NOTICE OF VIOLATION OF A REGULATION
MONTHYEARML20217K5821998-04-0202 April 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:On 971017,shift Supervisor Failed to Ensure That Equipment Could Be Removed from Svc,By Failing to Ensure That TS Requirements Were Met ML20132F8881996-10-18018 October 1996 Notice of Violation from Insp on 960727-0906.Violation Noted:On 960820,electrical Maint Technician Operated Supply Ventilation Fan to EDG 1-2 Room W/O Proper Authorization of Shift Supervisor ML20059C1281993-12-23023 December 1993 Notice of Violation from Insp on 931018-1103.Violation noted:930917 Primary Coolant Sys Temp Between 170 Degrees & 250 Degrees F,Average Cooldown Was Approx 48 Degrees F Per Hour ML20059G2071993-10-25025 October 1993 Notice of Violation from Insp on 930819-0929.Violation Noted:Licensee Cycle 10 Radiochemistry Testing Did Not Positively Identify Failed I-series Fuel ML20149D3601993-09-14014 September 1993 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $50,000.Noncompliance Noted:Shift Supervisor Failed to Explain Plans,Procedures & Safety Precautions to Auxiliary Operators Assigned to Perform CRDM mock-up ML20127M7821993-01-21021 January 1993 Notice of Violation from Insp on 921207-18.Violation Noted: Inservice Test Procedure QO-8B Contained Inadequate Acceptance Criteria to Verify That Listed Check Valves Exercised Full Open Position ML20212P8351987-03-0909 March 1987 Notice of Violation from Insp on 860724-1231 ML20214W1891986-09-26026 September 1986 Notice of Violation from Insp on 860723-0908 ML20206T5401986-07-0101 July 1986 Notice of Violation & Proposed Impostion of Civil Penalty in Amount of $50,000.Violation Noted:Inadequate Review & Corrective Action for Containment Isolation Valve Leakage Event Noted in May & Aug 1985 ML20205M3121986-04-11011 April 1986 Notice of Violation from Insp on 860119-0313 ML20154Q0381986-03-14014 March 1986 Notice of Violation from Insp on 860107-0228 ML20141N2321986-02-26026 February 1986 Notice of Violation from Insp on 860127-0207 ML20153E8281986-02-20020 February 1986 Notice of Violation from Insp on 860106-08 ML20151U9481986-02-0606 February 1986 Notice of Violation from Insp on 860113-21 ML20137H8581986-01-16016 January 1986 Notice of Violation from Insp on 851119-1223 ML20141H5731986-01-0909 January 1986 Notice of Violation from Insp on 851203-20 IR 05000919/20110181985-12-23023 December 1985 Notice of Violation from Insp on 850919-1118 ML20137H4681985-11-24024 November 1985 Notice of Violation from Insp on 850930-1004 IR 05000709/20080121985-09-13013 September 1985 Notice of Violation from Insp on 850709-0812 IR 05000710/20090041985-09-0505 September 1985 Notice of Violation from Insp on 850710-0904 IR 05000409/20050061985-06-0303 June 1985 Notice of Violation from Insp on 850409-0506 ML20128M2731985-05-21021 May 1985 Notice of Violation from Insp on 850423-26 & 0501-02 ML20055C1451982-07-22022 July 1982 Notice of Violation from Insp on 820601-30 1998-04-02
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARPNO-II-99-043, on 991013,Palisades Nuclear Plant Located Near South Haven,Mi Notified NRC That Package Received from Licensee Exceeded External Radiation Limits of 200 Mrem Per H Authorized by Regulations.Shipper & Carrier Notified1999-10-14014 October 1999 PNO-II-99-043:on 991013,Palisades Nuclear Plant Located Near South Haven,Mi Notified NRC That Package Received from Licensee Exceeded External Radiation Limits of 200 Mrem Per H Authorized by Regulations.Shipper & Carrier Notified IR 05000255/19980081998-05-28028 May 1998 Partially Withheld Insp Rept 50-255/98-08 on 980504-08 (Ref 10CFR73.71).No Violations Noted.Major Areas Inspected: Effectiveness of Access Control Functions & Testing & Maint Activities Related to Security Equipment ML20217K5821998-04-0202 April 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:On 971017,shift Supervisor Failed to Ensure That Equipment Could Be Removed from Svc,By Failing to Ensure That TS Requirements Were Met IR 05000255/19970071997-06-0505 June 1997 Partially Deleted Insp Rept 50-255/97-07 on 970428-0513. Violations Noted.Major Areas Inspected:Mgt Support,Plant Support,Detection Equipment & Evaluation of Security Communication Activities IR 05000255/19960011997-01-24024 January 1997 SALP Rept 50-255/96-01 for Period from 950528-961123 ML20132F8881996-10-18018 October 1996 Notice of Violation from Insp on 960727-0906.Violation Noted:On 960820,electrical Maint Technician Operated Supply Ventilation Fan to EDG 1-2 Room W/O Proper Authorization of Shift Supervisor ML20059C1281993-12-23023 December 1993 Notice of Violation from Insp on 931018-1103.Violation noted:930917 Primary Coolant Sys Temp Between 170 Degrees & 250 Degrees F,Average Cooldown Was Approx 48 Degrees F Per Hour IR 05000255/19930301993-12-21021 December 1993 Insp Rept 50-255/93-30 on 931203.Violations Noted.Major Areas Inspected:Previous Violations Were Reviewed IR 05000255/19930011993-12-0101 December 1993 SALP 12 Rept 50-255/93-01 for 920401-931030 IR 05000255/19930281993-11-19019 November 1993 Insp Rept 50-255/93-28 on 931018-1103.Apparent Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Excessive Cooldown Following Identification of Nonisolable thru-wall Leak on Primary Coolant Sys IR 05000255/19930271993-11-16016 November 1993 Insp Rept 50-255/93-27 on 931025-28.No Violations Noted. Major Areas Inspected:Emergency Preparedness Exercise IR 05000255/19930201993-10-25025 October 1993 Insp Rept 50-255/93-20 on 930819-0929.Violations Noted.Major Areas Inspected:Licensee Activities Re Summer 1993 Refueling Outage Problems & Plant Restart Preparations ML20059G2071993-10-25025 October 1993 Notice of Violation from Insp on 930819-0929.Violation Noted:Licensee Cycle 10 Radiochemistry Testing Did Not Positively Identify Failed I-series Fuel IR 05000255/19930251993-10-21021 October 1993 Insp Rept 50-255/93-25 on 931005 & 06.No Violations of NRC fitness-for-duty Noted.Major Areas Inspected:Review of fitness-for-duty Concern Relating to Implementation of Testing for-cause & follow-up of Random Testing Program PNO-III-93-055, on 930917,indications of Leak Found in Pipe Connecting Top of Pressurizer to Two PORVs During Insp of Reactor Sys Piping.Issues Related to Cracked Pipe Being Reviewed by Region III & NRR & Repairs Underway1993-09-24024 September 1993 PNO-III-93-055:on 930917,indications of Leak Found in Pipe Connecting Top of Pressurizer to Two PORVs During Insp of Reactor Sys Piping.Issues Related to Cracked Pipe Being Reviewed by Region III & NRR & Repairs Underway ML20057B8581993-09-16016 September 1993 Exam Rept 50-255/OL-93-02 on 930914.Exam Results: Requalification Written Retake Exam Was Administered to One RO ML20149D3601993-09-14014 September 1993 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $50,000.Noncompliance Noted:Shift Supervisor Failed to Explain Plans,Procedures & Safety Precautions to Auxiliary Operators Assigned to Perform CRDM mock-up ML20057A1731993-09-0707 September 1993 Insp Rept 50-255/93-05 on 930614-17 & 29,0701 & 20-21 & 0803-04.No Violations or Deviations Noted.Major Areas Inspected:Isi Activities Including Review of Program, Procedures & Observation of Work Activities IR 05000255/19930181993-08-31031 August 1993 Augmented Insp Team Rept 50-255/93-18 on 930708-20.No Violations Noted.Major Areas Inspected:Review of Validation of Sequence of Events & Licensee Corrective Actions PNO-III-93-049A, provides Update on Degraded Neutron Absorbing Plates in Spent Fuel Pool at Plant.Licensee Determined That Sufficient Subcritical Margin Maintained in Spent Fuel Pool.State of Mi Informed1993-08-31031 August 1993 PNO-III-93-049A:provides Update on Degraded Neutron Absorbing Plates in Spent Fuel Pool at Plant.Licensee Determined That Sufficient Subcritical Margin Maintained in Spent Fuel Pool.State of Mi Informed IR 05000255/19930051993-07-30030 July 1993 Insp Rept 50-255/93-05 on Stated Date.No Violations Noted. Major Areas Inspected:Independent NDE of Components & Welds in Order to Ascertain Accuracy of NDE Performed by Licensee PNO-III-93-038, on 930701,licensee Discovered Highly Radioactive Object on Floor of upender-tilt Pit in Refueling Area of Containment.There Have Been No Radiation Overexposures as Result of Event1993-07-0101 July 1993 PNO-III-93-038:on 930701,licensee Discovered Highly Radioactive Object on Floor of upender-tilt Pit in Refueling Area of Containment.There Have Been No Radiation Overexposures as Result of Event PNO-III-93-027, on 930504,listed Individuals Filed Suit Against NRC on Dry Cask Storage Sys at Plant.Util Planning to Begin Movement of Sf Into Storage Casks on 9305071993-05-0404 May 1993 PNO-III-93-027:on 930504,listed Individuals Filed Suit Against NRC on Dry Cask Storage Sys at Plant.Util Planning to Begin Movement of Sf Into Storage Casks on 930507 IR 05000255/19930021993-02-17017 February 1993 Insp Rept 50-255/93-02 on 921229-930208.No Violations Noted. Major Areas Inspected:Previously Identified Items, Operational Safety Verification,Maint,Surveillance & Design Changes ML20127M7821993-01-21021 January 1993 Notice of Violation from Insp on 921207-18.Violation Noted: Inservice Test Procedure QO-8B Contained Inadequate Acceptance Criteria to Verify That Listed Check Valves Exercised Full Open Position IR 05000255/19920281993-01-21021 January 1993 Insp Rept 50-255/92-28 on 921207-18.Violations Noted.Major Areas Inspected:Licensee Program on Check Valves,Self Assessment & Incorporation of GL 89-04, Guidance on Developing Acceptable Inservice Test Programs IR 05000255/19920271993-01-13013 January 1993 Insp Rept 50-255/92-27 on 921117-1228.No Violations Noted. Major Areas Inspected:Operational Safety Verification, Engineering & Technical Support,Maintenance,Surveillance & Quality Control Activities IR 05000255/19920231992-11-25025 November 1992 Insp Rept 50-255/92-23 on 921006-1116.Noncited Violations or Deviations Noted.Major Areas Inspected:Operational Safety Verification,Reactor Trip,Maint Surveillance,Quarterly Mgt Meeting & Dry Cask Storage Project Insps IR 05000155/19900201990-11-0707 November 1990 Insp Repts 50-155/90-20 & 50-255/90-27 on 900925-28 & 1015-19.Violations Noted.Major Areas inspected:fitness-for- Duty & Corrective Actions for Audit Findings IR 05000255/19900161990-07-0606 July 1990 Insp Rept 50-255/90-16 on 900618-22 & 25.No Violations Noted.Major Areas Inspected:Mgt Support,Protected & Vital Areas,Detection & Assessment Aids,Package & Vehicle Access, Compensatory Measures & Training & Qualification IR 05000255/19890111989-05-0101 May 1989 Partially Withheld Physical Security Insp Rept 50-255/89-11 on 890410-14 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected:Mgt Support,Protected & Vital Area Barriers & Access Control,Including Personnel,Packages & Vehicles PNO-III-89-007, on 890130 Unit Taken off-line to Repair Primary to Secondary Tube Leak in B Sg.Caused by Leakage Increase Since 890124 & Reaching Licensee Administrative Limit of 0.1 Gpm.Plans Include Preventive Plugging of Tubes1989-02-0101 February 1989 PNO-III-89-007:on 890130 Unit Taken off-line to Repair Primary to Secondary Tube Leak in B Sg.Caused by Leakage Increase Since 890124 & Reaching Licensee Administrative Limit of 0.1 Gpm.Plans Include Preventive Plugging of Tubes IR 05000255/19880131988-05-24024 May 1988 Partially Withheld Insp Rept 50-255/88-13 on 880502-05 (Ref 10CFR73.21).Major Areas Inspected:Security Plan/ Implementing Procedures,Mgt Effectiveness,Security Organization,Testing & Maint & Security Sys Power Supply IR 05000255/19880091988-04-27027 April 1988 Insp Rept 50-255/88-09 on 880411-15.No Violations or Deviations Noted.Major Areas Inspected:Activation of Emergency Plan,Licensee Action on Previously Identified Items & Changes to Emergency Preparedness Program PNO-III-87-140, on 871111,oiler on Feedwater Block Valve Exploded in Turbine Bldg,Injuring Two Workers.One Individual Taken to Local Hosp & Later Transferred to Kalamazoo,Mi Hosp for Surgery & Second Worker Treated at Plant1987-11-12012 November 1987 PNO-III-87-140:on 871111,oiler on Feedwater Block Valve Exploded in Turbine Bldg,Injuring Two Workers.One Individual Taken to Local Hosp & Later Transferred to Kalamazoo,Mi Hosp for Surgery & Second Worker Treated at Plant PNO-III-87-134, on 871015,w/unit Cold Shutdown for Maint, Operators Tripped Operating Shutdown Coolant Pump in Response to Alarms & Indications of Fluctuation Pressure within Pump1987-10-16016 October 1987 PNO-III-87-134:on 871015,w/unit Cold Shutdown for Maint, Operators Tripped Operating Shutdown Coolant Pump in Response to Alarms & Indications of Fluctuation Pressure within Pump PNO-III-87-131, on 871007,util & Bechtel Power Corp Issued Joint Press Release Announcing Tentative Agreement to Form New Joint Venture Which Would Own & Operate Facility.Util Would Continue to Operate Facility Under Contract for 3 Yrs1987-10-0707 October 1987 PNO-III-87-131:on 871007,util & Bechtel Power Corp Issued Joint Press Release Announcing Tentative Agreement to Form New Joint Venture Which Would Own & Operate Facility.Util Would Continue to Operate Facility Under Contract for 3 Yrs PNO-III-87-097A, on 870714,preliminary Review of Incident Determined That Startup Transformer 1-2 Faulted.Cause of Initial Fault Still Under Investigation1987-07-15015 July 1987 PNO-III-87-097A:on 870714,preliminary Review of Incident Determined That Startup Transformer 1-2 Faulted.Cause of Initial Fault Still Under Investigation PNO-III-87-097, on 870714,plant Lost Offsite Power Causing Reactor Trip.Caused by Ground Fault in One of Three Startup Transformers.Main Generator Will Be Disconnected from Main Transformer Which Will Feed Power to Plant1987-07-14014 July 1987 PNO-III-87-097:on 870714,plant Lost Offsite Power Causing Reactor Trip.Caused by Ground Fault in One of Three Startup Transformers.Main Generator Will Be Disconnected from Main Transformer Which Will Feed Power to Plant PNO-III-87-095, on 870709,reduction in Power Occurred Due to Handswitch Failure on Cooling Tower Pump B Discharge Valve. on 870710,decreasing Oil Pressure in Primary Coolant Pump Noted.Possibly Caused by Pump Vibration Creating Oil Leak1987-07-10010 July 1987 PNO-III-87-095:on 870709,reduction in Power Occurred Due to Handswitch Failure on Cooling Tower Pump B Discharge Valve. on 870710,decreasing Oil Pressure in Primary Coolant Pump Noted.Possibly Caused by Pump Vibration Creating Oil Leak IR 05000255/19870161987-07-0808 July 1987 Insp Rept 50-255/87-16 on 870608-12.No Violations Noted. Major Areas Inspected:Confirmatory Measurements Program Including Comparison of Licensee Analyses W/Region III Mobile Lab,Radiological Environ Program & Open Item PNO-III-87-085, on 870620,while Reducing Power for Governor Valve Test on Main Turbine,Turbine Was Taken Off Line After Discovery of electro-hydraulic Control Fluid Leak on 4 Governor Valve1987-06-22022 June 1987 PNO-III-87-085:on 870620,while Reducing Power for Governor Valve Test on Main Turbine,Turbine Was Taken Off Line After Discovery of electro-hydraulic Control Fluid Leak on 4 Governor Valve PNO-III-87-081, on 870610,earthquake Measuring 5.0 on Richter Scale Occurred Near Lawrenceville,Il.Unusual Events Declared by Six Power Stations But No Damage Observed.Ground Motion Felt at Five Other Plants1987-06-11011 June 1987 PNO-III-87-081:on 870610,earthquake Measuring 5.0 on Richter Scale Occurred Near Lawrenceville,Il.Unusual Events Declared by Six Power Stations But No Damage Observed.Ground Motion Felt at Five Other Plants ML20214T9121987-06-0404 June 1987 Exam Rept 50-255/OL-87-01 on 870504-08.Exam Results:Both Senior Operator Candidates Passed.Exam & Answer Key Encl ML20214U3261987-06-0404 June 1987 Requalification Exam Rept 50-255/OL-87-02 of Exam Admininstered on 870505-08.Exam Results:Five Senior Operators & Four Operators Passed Exams IR 05000255/19860351987-05-28028 May 1987 Insp Rept 50-255/86-35 on 861216-870216.Violations Noted: Inadequate Review of Mod Package,Inadequate Procedures for Conduct of 10CFR50.59 Evaluations & Failure to Identify Modified Breakers as Class 1E IR 05000255/19870071987-04-20020 April 1987 Partially Withheld Insp Rept 50-255/87-07 on 870320-30 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected: Licensee Actions Re Opening of Physical Barrier,Security Plan & Implementing Procedures & IE Info Notice 86-083 PNO-III-87-053, on 870412,reactor Manually Tripped as Result of Leak in Electrohydraulic Control (EHC) Sys for Main Turbine.Caused by Fatigue Failure of Impeller of Pump in EHC Sys.Pump Repaired1987-04-13013 April 1987 PNO-III-87-053:on 870412,reactor Manually Tripped as Result of Leak in Electrohydraulic Control (EHC) Sys for Main Turbine.Caused by Fatigue Failure of Impeller of Pump in EHC Sys.Pump Repaired PNO-III-87-044C, on 870405,unit Completed Testing Activities at 30% Level & Increased Power at 45% for Further Testing & Review.Power Held at 45% for Repair of Valve in Cooling Tower Sys & Oil Flow in Main Feedwater Pump Bearing1987-04-10010 April 1987 PNO-III-87-044C:on 870405,unit Completed Testing Activities at 30% Level & Increased Power at 45% for Further Testing & Review.Power Held at 45% for Repair of Valve in Cooling Tower Sys & Oil Flow in Main Feedwater Pump Bearing PNO-III-87-044B, on 870403,unit Tied to Util Electrical Grid for First Time Since 860519 Reactor Trip.Licensee Began Plant Startup on 870327 But Returned to Cold Shutdown to Replace Failed Nuclear Instrument1987-04-0303 April 1987 PNO-III-87-044B:on 870403,unit Tied to Util Electrical Grid for First Time Since 860519 Reactor Trip.Licensee Began Plant Startup on 870327 But Returned to Cold Shutdown to Replace Failed Nuclear Instrument 1999-10-14
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NOTICE OF VIOLATION
{
t Consumers Power Company Docket-No. 50-255 Palisades Nuclear Plant License No. DPR-20 .;
During an NRC inspection conducted on July 8 through July 20, and August 19 ,
through 27, 1993, violations of NRC requirements were identified. In ,
accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C, the violations are listed -
below: '!
A. 10 CFR 50.59 (b)(1) requires in part that the licensee.have a- l written safety evaluation which provides'the bases for determination that a change in the facility as described in the Safety Analysis Report does nnt involve an unreviewed' safety -
question. Section 3.3.2.6 of the Updated Safety Analysis Report describes use of hafnium poisoned assemblies as part of a-neutron -i fluence reduction program.
Contrary to the above, the licensee's 50.59 evaluation of extended I use of hafnium poisoned 1-series fuel assemblies for cycles 10 and 11 did not provide complete bases for the determination that there .
was no unreviewed safety question. Specifically, the evaluations ,
did not include consideration of the effects of the neutron spectrum at the periphery of the core (which was proportionally .. ,
higher in " fast" neutrons and lower in " thermal" neutrons compared a to non-periphery locations) on mechanical properties of the -!
assemblies. These evaluations were therefore incomplete. .
This is a Severity Level IV violation (Supplement 1). 1 i
B. 10 CFR 50, Appendix B, Criterion XI, requires that a test program ;
be established to assure that all testing required to demonstrate
~
that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures. i Contrary to the above, the licensee's' Cycle 10 radiochemistry !
testing did not positively identify failed I-series fuel, nor was additional testing performed between cycles 10 and 11 to assure I-series fuel would perform satisfactorily for a sixth cycle, which constituted a unique fuel performance demand. ,
l This is a Severity Level IV violation (Supplement I).
C. 10 CFR 50, Appendix B, Criterion XVI, requires in part that measures be established to assure that conditions adverse to ,
quality are promptly identified and corrected. In the case of :
significant conditions adverse to quality the measures shall i assure that the cause of the condition is determined and corrective action taken to preclude repetition.
l 93110B0036 931027 J PDR ADOCK 05000255 1 O PDR
x N '.
u y
Notice of Violation 2 )
I l
Contrary to the above, when the upper guide structure (UGS) was j lifted from the reactor on July 6, 1993, and a fuel bundle from ;
core location Z-ll stuck onto the UGS, it marked the third u occasion for this.same interference between core components.
]
This is a Severity Level IV violation (Supplement I). .;
D. Technical Specification 6.8.1.b requires that written procedures - -!
be established, implemented and maintained for activities covering refueling operations.
- 1. Licensee procedure RVI-M-1, Revision 16, " Removal'and j storage of the Upper Guide Structure," provided instructions :
for installation for a TI-2000 load cell readout device ,
only. .
Contrary to the above, on July 6,1993, while lifting the ;
UGS, a J-300 load cell readout device was used. {
l
- 2. Licensee procedure RVI-M-1, Revision 16, " Removal and -l storage of the Upper Guide Structure," Section-5.3.6.g, j includes a stipulation to follow Work Order No. 24301781 for t steps to use a load cell. Step 3.3.A.7 of the work order j requires that the load cell readout device be zeroed. :
'l Contrary to the above, on July 6,1993, while performing i procedure RVI-M-1, the load cell . readout device was not - :
zerced. ;
- 3. Licensee procedure RVI-M-1, Revision 16, " Removal and storage of the Upper Guide Structure," Section 5.3.14, 1 specifies an upper load limit of 62,000 pounds. 1 Contrary to the above, on July-6,1993, while performing procedure 'RVI-M-1, af ter the UGS was raised approximately ;
six inches, indicated load reached 62,800 pounds, which is in excess of the upper load limit. '
- 4. Licensee procedure FHS0-18, " Recovery of Bundle SAN-8," -l requires in steps 4.2.6 and 5.2.1 that chainfall tension be :l limited to a combined load of 1500 - 1600 pot'!ds. J 1
Contrary t'o-the above, on July 7,1993, the chainfalls were '
l tightened to a combined load of 2300 pounds. !
This is a Severity Level IV violation (Supplement ~I). f l
\
m
4
e W
4 1 -l Notice of Violation 3 l,
. Pursuant to the provisions of 10 CFR 2.201, Palisades Nuclear Plant. is hereby j required to submit a written statement or explanation to the U.S. Nuclear j
. Regulatory Commission, ATTN: Document Control Desk, Washington, D.C.'20555 with a copy to the Regional Administrator, Region III, and a copy:to the NRC Resident Inspector at the facility that is the subject of this Notice, within 30 days of the date of the letter transmitting this Notice of Violation- a (Notice). 1This reply should be clearly marked as a " Reply to a Notice of ~ l' Violation" and should include for each violation: (1) the' reason for the.
violation, or, if contested, the basis for disputing the' violation, (2) the l corrective steps that have been taken and the results achieved, (3) the . .'
corrective steps that will be taken to avoid further violations, and (4). the date when full compliance will be achieved. If an adequate reply is not <
received within the time specified in'this Notice, an order or a Demand for Information-may be issued to show cause why the license should not be .;
modified, suspended, or revoked, or why such other action as may be proper ,
should not be taken. Where good cause is shown, consideration will be given- ~;
to extending the response time.
1 i
DatedaggGlen Ellyn, Illinois this,7__5 day of October 1993 :
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