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Other: ML20076E880, ML20079M106, ML20080E109, ML20100G880, ML20100G888, ML20100H212, ML20112G667, ML20127J807, ML20135B301, ML20135D754, ML20137H372, ML20137S741, ML20141P181, ML20154K144, ML20197C598, ML20197G513, ML20205C845, ML20206B459, ML20207K470, ML20211P495, ML20215E408, ML20215G100, ML20235G758
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MONTHYEARML20076E8801983-05-17017 May 1983 Responds to NRC 830413 Order Re Environ Qualification of safety-related Electrical Equipment,Per 10CFR50.49.Environ Qualification Records Audit Will Be Completed by 831231 Project stage: Other ML20080E1091983-08-15015 August 1983 Provides Followup to Util Re Environ Qualification of safety-related Electrical Equipment. Justification for Continued Operation W/Components Not Fully Qualified Provided Project stage: Other ML20079M1061984-01-0909 January 1984 Advises NRC Re Status of Three Commitments Made in Util Concerning Environ Qualification of safety-related Electrical Equipment.Valve Actuators Tested & Successfully Passed HELB Tests Project stage: Other ML20100G8881984-09-11011 September 1984 Four-Minute Isolation of Postulated Steam Line Breaks at Fort St Vrain Nuclear Generating Station Project stage: Other ML20112G6671984-12-27027 December 1984 Informs of Efforts to Environmentally Qualify Certain post-accident Monitoring Equipment Per 10CFR50.49.Equipment Identified in Reg Guide 1.97 & Existing in Harsh Environ Will Be Qualified by 850331 Project stage: Other ML20108A2121985-02-0404 February 1985 Informs of Receipt of Generic Ltr 84-24 on 850121 & Request for Addl Info on Environ Qualification of Electrical Equipment on 850128.Responses to Both Ltrs Will Be Provided by 850328 Project stage: Request ML20100H2121985-03-25025 March 1985 Forwards Response to NRC 841227 Order Re Certification of Compliance w/10CFR50.49 (Generic Ltr 84-24).Util Previously Submitted Ltrs Re Environ Qualification of safety-related Equipment in Response to IE Bulletin 79-01B Project stage: Other ML20100G8801985-03-28028 March 1985 Forwards Addl Info Re Environ Qualification Program. Response to NRC 850128 Concerns & Summary of Completion Schedule for Outstanding Items Encl Project stage: Other ML20237L1731985-03-29029 March 1985 Notification of 850403 Meeting W/Util in Bethesda,Md to Discuss Equipment Qualification Project stage: Meeting ML20127J8071985-06-11011 June 1985 Maintains Util Position of Full Compliance w/10CFR50.49 in Response to Eh Johnson 850611 Inquiry Re Environ Qualifications of Electrical Equipment Important to Safety. Responses to Each Concern Presented in Encl Project stage: Other ML20237L1551985-06-25025 June 1985 Submits Daily Highlight.Notifies of 850702 Meeting W/Util in Bethesda,Md to Discuss State of Compliance of Plant W/ Equipment Qualification Rule 10CFR50.49 Project stage: Meeting ML20244D4841985-07-10010 July 1985 Provides Feedback on Current NRR Conclusions Re Facility Compliance W/Equipment Qualification Rule & Operator Action Needed to Terminate Design Basis Events.Summary of 850702 Meeting W/Util in Bethesda,Md Encl Project stage: Meeting ML20132B9171985-07-11011 July 1985 Discusses Resolution of Technical Issues of Aging & Operability Times Per 850702 Meeting Re Environ Qualification Program.Hold on Reactor Power to 15% Proposed as Initial Limitation Project stage: Meeting ML20132F0721985-07-19019 July 1985 Safety Evaluation Documenting Deficiencies in Licensee Program for Environ Qualification of Electric Equipment Important to Safety.Licensee Response to Generic Ltr 84-24 Inadequate.However,Operation at 15% Power Authorized Project stage: Approval ML20132F0231985-07-19019 July 1985 Forwards Safety Evaluation Re Environ Qualification of Electric Equipment Important to Safety & Authorizes Interim Operation in dry-out Mode at Max 15% of Rated Power,Based on Listed Conditions,Until Technical Review Completed Project stage: Approval ML20134M0161985-08-20020 August 1985 Submits Discussion of Technical Issues Re Environ Qualification Program Raised During Meetings W/Nrc.Aging & Operability Time Program Operator Response Time,Temp Profiles & Shutdown Cooling Paths & Equipment Evaluated Project stage: Meeting ML20135D7541985-08-30030 August 1985 Advises That Rev of Emergency Procedures Committed to in Deferred to Coincide W/Final Environ Qualification Program Documentation.Procedure Revs at This Time Will Cause More Confusion than Clarity for Operators Project stage: Other ML20135B3011985-08-30030 August 1985 Forwards Justification to Operate Facility at Reduced Power Level.Requests That NRC Provide Concurrence for Facility to Be Operated at 8% Power Level for Period of Time Not to Exceed 45 Days.Operation Does Not Pose Undue Safety Risk Project stage: Other ML20205C8451985-09-10010 September 1985 Forwards Info Supporting 850830 Request to Operate at 8% Power to Facilitate Core Dryout for 45 Days,Per 850826,0903 & 04 Telcons.Moisture Removal Needed to Maintain Conditions Prescribed in FSAR & Tech Specs Project stage: Other ML20205C4811985-09-11011 September 1985 Provides Commitment That Operating Procedures & Operator Training Described in Providing Addl Info in Support of Request to Operate at Up to 8% Power Will Be Complete Prior to Withdrawal of Control Rods Project stage: Withdrawal ML20137S7411985-09-23023 September 1985 Forwards Addl Calculations,Clarifying Util Re Predicted Fuel/Pcrv Liner Temps Resulting from Design Basis Event from 8% Power & Subsequent Reactor Cooling Utilizing Liner Cooling Sys.Calculations Confirm Original Position Project stage: Other ML20137H3721985-11-26026 November 1985 Memorandum & Order Granting Extension of 851130 Deadline for Environ Qualification of Electrical Equipment to 860531 & Approving Proposal to Allow Operation w/35% Reactor Power Limit During Interim.Served on 851127 Project stage: Other ML20151N7211985-12-27027 December 1985 Forwards Response to 851105 Request for Addl Info Needed to Determine If Environ Qualification Program Complies W/ Requirements of 10CFR50.49.Sys Description & Temp Profiles Used in Environ Qualification Program Also Encl Project stage: Request ML20141P1811986-01-29029 January 1986 Rev 00 to Justification/Analysis:Environ Qualification of Square D Pressure & Temp Switches Project stage: Other ML20141M8081986-02-14014 February 1986 Advises That DBAs Re Permanent Loss of Forced Circulation & Rapid Depressurization of Reactor Vessel Must Be Addressed in Equipment Qualification Program.Util Cooperation W/Program Mods Confirmed During 851029 Meeting Project stage: Meeting ML20154K1441986-02-28028 February 1986 Forwards Addl Info Re Environ Qualification,Per 851105 Request.Encl Info for Three Line Break Scenarios in Reactor Bldg Will Allow Independent Verification of Temp Profiles Obtained from Ga Technologies Using Computer Programs Project stage: Other ML20142A0441986-03-12012 March 1986 Summary of 860221 Onsite Meeting W/Util,Inel,D Benedetto Assoc,S&W,Tenera,Ned & NPD Re Equipment Qualification Program & Steam Line Rupture Detection & Isolation Sys Project stage: Meeting ML20141P1771986-03-14014 March 1986 Summary of 860130 Meeting W/Util,Inel,Tenera & Sargent & Lundy Re Equipment Qualification (EQ) Program.List of Attendees,Test Profiles & Review of Sample EQ Package Encl Project stage: Meeting ML20205S2591986-04-10010 April 1986 Summary of 860326 Site Meeting W/Util,Dibenedetto Assoc,Inc, Sandia & Sargent & Lundy Re Status of Qualifications of 10CFR50.49 Cables & Maint Records History Review.Viewgraphs & Attendees List Encl Project stage: Meeting ML20204A3181986-05-0101 May 1986 Provides Status Summary of Environ Qualification Program. Addl Details on Program Contained in 860501 Draft Environ Qualification Submittal.Major Equipment Replacements Listed Project stage: Draft Other ML20197G5131986-05-12012 May 1986 Requests Concurrence Re Inclusion of DBA in Environ Qualification Program Per Berkow .Util Will Not Environmentally Qualify Electric Equipment to Mitigate DBA-1 & DBA-2 Since Equipment Not Exposed to Harsh Environ Project stage: Other ML20198H4561986-05-27027 May 1986 Summary of 860505 Meeting W/Util Re Status of Equipment Qualification Program.Considerable Work Remains Before Approval of Full Power Operation Can Be Granted.Staff Recommended Util Continue to Complete Program Project stage: Meeting ML20205S2341986-06-0101 June 1986 Summary of 860502 Meeting W/Util & Inel in Bethesda,Md Re Equipment Qualification Program Problem Areas.Attendees List & Supporting Documentation Encl Project stage: Meeting ML20206R6241986-06-20020 June 1986 Forwards Environ Qualification Submittal Re Activities to Assure Compliance w/10CFR50.49 & Incorporating Comments on Draft 860502 Submittal.Evaluations Will Be Available for Review Before Request for Release to Full Power Project stage: Draft Request ML20203B6181986-07-15015 July 1986 Summary of 860613 Meeting W/Util in Bethesda,Md Re Status of Plant Equipment Qualification Program.List of Attendees, Environ Qualification of Plant Safe Shutdown Cable & Cable Qualification Binders Encl Project stage: Meeting ML20204H6531986-07-31031 July 1986 Responds to 860724 Request for Documentation Re Use of Thermal Lag Analysis in Environ Qualification of Electrical Equipment in Plant.Thermal Analysis Will Be Performed Per Rev 3 to CENPD-255-A Project stage: Request ML20206P5971986-08-15015 August 1986 Summary of 860724 Meeting W/Util,Inel,Wyle Labs,Sargent & Lundy & Tenera in Bethesda,Md Re Util Draft Documentation to Justify Qualification of safety-related Cabling at Plant. List of Attendees Encl IR 05000267/19860251986-10-30030 October 1986 Insp Rept 50-267/86-25 on 860816-0930.Violations Noted: Failure to Follow Procedures,To Review Mod Control Procedures & to Sufficiently Document Design Verification Project stage: Request ML20197C5631986-10-30030 October 1986 Forwards Draft FATE-86-117, Review of Convection Heat Transfer Coefficients Utilized in Fort St Vrain Main Steam Line Break Analyses, Technical Evaluation Rept (Ter).Ter Addresses Details Used in Temp Profile Calculations Project stage: Draft Approval ML20197C5981986-10-31031 October 1986 Review of Convection Heat Transfer Coefficients Utilized in Fort St Vrain Main Steam Line Break Analyses, Technical Evaluation Rept Project stage: Other ML20214Q0951986-11-25025 November 1986 Summary of 861027 Meeting W/Util to Discuss Schedule for Ie/Nrr Insp of Equipment Qualification Program.Attendance List & Viewgraphs Encl Project stage: Meeting ML20214U7071986-12-0202 December 1986 Summary of 861120 Meeting W/Util,Ornl,Ga Technologies & Eg&G Re Temp Profiles for Equipment Qualification.List of Attendees & Viewgraphs Encl Project stage: Meeting ML20215E4081986-12-12012 December 1986 Forwards Analyses of Three Steam Line Break Scenarios for Reactor Bldg & Three Scenarios for Turbine Bldg Using Convective Heat Transfer Coefficient of 1.0,per NRC 861120 Request Project stage: Other ML20215G1001986-12-19019 December 1986 Forwards Second Formal Submittal Re Turbine Bldg Temp Profiles Resulting from Steam Line Breaks,Per 861120 Request.Composite Temp Profile Curves Originally Submitted as Basis for Environ Qualification Program Appropriate Project stage: Other ML20207K4701986-12-31031 December 1986 Final Review of Convection Heat Transfer Coefficients Utilized in Fort St Vrain Main Steam Line Break Analysis, Technical Evaluation Rept Project stage: Other ML20207K4021987-01-0202 January 1987 Forwards Final FATE-86-117, Review of Convection Heat Transfer Coefficient Utilized in Fort St Vrain Main Steam Line Break Analysis, Technical Evaluation Rept,For Info Project stage: Approval ML20207Q4431987-01-16016 January 1987 Confirms 870126-30 Equipment Qualification Insp,Per 870113 Meeting at Region IV Ofcs.Mgt Entrance Meeting Scheduled for 870126 at Site Visitors Ctr & Exit Meeting Tentatively Scheduled for 870130 at Plant Site Project stage: Meeting ML20210P5241987-01-29029 January 1987 Forwards Draft Evaluation of Confinement Environ Temps Following High Energy Line Breaks Proposed for Fort St Vrain Environ Qualification Program, Technical Evaluation Rept,In Response to Util 861212 & 19 Submittals Project stage: Draft Other ML20210P6451987-01-31031 January 1987 Draft Evaluation of Confinement Environ Temps Following High Energy Line Breaks Proposed for Fort St Vrain Environ Qualification Program, Technical Evaluation Rept Project stage: Draft Other ML20211P4951987-02-25025 February 1987 Informs of Present Status & Plans Re Completion of Environ Qualification Program,Per Open Items Identified During 870130 Site Insp.Program & Implementing Procedures to Assure Environ Qualification in Place.Status of Open Items Encl Project stage: Other 1986-10-31
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PublicService
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Company of Colorado 2420 W. 26th Avenue, Suite 100D, Denver, Colorado 80211 August 30, 1985 Fort St. Vrain Unit No. 1 P-85302 b b O N8 N I. '
Regional Administrator Region IV U.S. Nuclear Regulatory Commission
- SEP - 5 M 611 Ryan Plaza Drive, Suite 1000 Arlington, TX 76011 Attn
- Mr. Dorwin R. Hunter Docket No:
50-267
SUBJECT:
Low Power Operation of FSV
REFERENCE:
(1) NRC Letter, Martin to Lee, dated 07/19/85 (G-85288)
(2) PSC Letter, Warembourg to Martin, dated 8/20/85 (P-85293)
Dear Mr. Hunter:
In Reference 1, Public Service Company (PSC) received authorization from the NRC to operate Fort St. Vrain at a power level no greater than 15% until equipment qualification issues are resolved.
In Reference 2, additional information concerning PSC's progress towards resolving these issues was submitted to the NRC.
As a result of recent discussions with the NRC, PSC has been advised not to restart Fort St. Vrain until further justification is provided to the NRC. to this letter contains PSC's justification to operate ort St. Vrain at a reduced power level.
c PSC requests that the NRC provide concurrence for Fort St. Vrain to
' l),
be operated at power levels up to 8% for a period of time not to exceed 45 days, based on the conclusion that such operation does not Ll pose undue risk to the health and safety of the public.
PA
{4 p\\y 9509100514 850830 f
PDR ADOCK 05000267
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PDR
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2 PSC staff will be available to meet with the NRC in Bethesda the week of September.3.
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.Should you have any further questions, please contact M.H. Holmes, (303)'571-8409.~
Very truly yours, t
h /Y Ww D.W. Warembourg, Ma er Nuclear Engineering Division DW:JS:jrp Attachment.
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I Attachment I to P-85302 Page 1 i
4.
l INTRODUCTION i
Public Service Company has comitted to and embarked upon multiple i
efforts to minimize moisture ingress into the PCRV.
Recently, the plant has undergone extensive modifications and refurbishment programs to provide added assurance that moisture in the PCRV will not adversely effect reactor vessel internal components. Consistent with the desire to prevent moisture ingress, limiting the moisture level is also desirable.
For this. reason, PSC considers it prudent to continue to reduce the levels of moisture in the reactor vessel.
This would ensure that in the next several months, while the reactor is shutdown to resolve 10CFR50.49 ' issues, the moisture will be significantly reduced from the present levels.
PSC plans to begin work in early October 1985, for the purpose of resolving technical issues associated with 10CFR50.49. Part of this work is expected to include the installation of an automatic steam line rupture detection / isolation system.
While complete. moisture dry-out.cannot be accomplished until higher power levels are achieved, operating the reactor at low power levels provides the diffusion mechanism by which additional moisture can be withdrawn. Low power operation during_ the months of September-October 1985 would minimize moisture over the subsequent outage and would pose no undue risk to the health and safety of the public.
This short-term low power operation would also result in economic benefits to PSC.
The moisture level in the reactor vessel has thus far been reduced to an equilibrium value of about 300 ppm by the pressurizing of the PCRV to the range of 300 psia, increasing the reactor coolant flowrate, and -
increasing the reheat steam temperature to about 290 degrees F.
The current moisture removal
- rate, however,.has been reduced significantly due to the location of the water in the PCRV liner
' insulation.
In order to increase the diffusion of moisture out of the insulation and into the -primary coolant, for removal by the-helium purification system, the coolant flow and temperatures must be increased. This will -require nuclear fission power to generate higher core outlet temperatures and hence increased steam production to drive the helium circulators at increased speed, t-Increasing reactor coolant temperatures through-the use of core generated power will help to dry the reactor coolant system and PCRV.
We have reevaluated the 15% reactor power level conditions and have determined that an 8% power level will be nearly as effective as 15%
power in reducing the moisture level.
LOWER STRESS LEVELS AT 8% POWER LEVELS The combination of.the margins between actual and allowable pipe stresses and the short duration of operation at 8% power provides reasonable assurance that a significant steam leak would not occur during operation in September-October 1985.
PEAK TEMPERATURES AS A RESULT OF A STEAM LINE BREAK A double-ended steam line break was analyzed with the Contempt-G Code for a power level of 8%. The breaks chosen were the cold reheat steam line in the reactor building and the hot reheat steam line in the turbine building, based on past determination that these were the worst cases (FSAR Section 1.4.6 and Appendix I).
The peak temperatures calculated for these accidents are shown in Table 1.
These temperatures are based upon isolation of the break in 4 minutes. These peak temperatures are significantly lower than those for the 100% power-level steam line breaks.
TIME AVAILABLE TO RESTART FORCED CIRCULATION COOLING BEFORE FUEL FAILURE CAN OCCUR For the 100% reactor power case, it has been established (FSAR Section 10.3.9) that there is a time period of 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> before forced circulation core cooling must be resumed to prevent any of the fuel from reaching the minimum temperature of 2900 degrees F at which fuel failure is postulated to occur, i
Operation of the FSV reactor at a power level and duration not to exceed 8% and 45 days respectively would resu.l t in a decay heat inventory which is a fraction of that for the 100% reactor power Case.
Preliminary calculations indicate that a time period of approximately 70 hours8.101852e-4 days <br />0.0194 hours <br />1.157407e-4 weeks <br />2.6635e-5 months <br /> is available before forced circulation core cooling must be restored for the 8% power level to avoid any fuel temperatures reaching 2900 degrees F.
The harsh environment resulting from the low peak temperatures given in Table 1 are short lived. The 70-hour time period discussed above thus provides ample margin to enable personnel. to both perform the manual operations necessary to align the safe shutdown cooling paths and to effect any necessary repairs.
Since fuel temperatures do not reach 2900 degrees F, no release of fission products occurs and thus there are no resulting undue risks to the health and safety of the public.
ECONOMIC CONSIDERATIONS Aside from other considerations, there would be an important economic benefit to PSC if the NRC were to authorize operation of FSV in a
" dry-ou t" mode for the purpose of allowing the removal of moisture from the reactor vessel. Power levels not to exceed 8% reactor power, a level which is insufficient to generate electricity, would suffice for this purpose.
Without this authorization from the NRC, PSC could be exposed to an economic penalty of approximately_ $140,000 per day for each day that rise-to-power operations are delayed while moisture is being removed from the core.
If the moisture removal process requires'a month to complete, this exposure would amount to $4.2 million.
The bases for these figures are presented below:
1.
In August 1984, The Colorado Public Utilities Commission (CPUC) issued a decision requiring potential refunds to customers for periods when the revenues collected under base rates attributable
.to Fort St. Vrain exceed the value of the energy produced by the station during such period.
If the CPUC decision.is eventually upheld in the courts and as long as Fort St. Vrain is nonoperational, the potential refund, which began in November 1984, increases by increments of $320,000 per month up to a monthly maximum of approximately $3.8 million beginning in October 1985. Each day that moisture removal activities delay rise-to-power operations represents -a refund liability of
$126,667 ($3,800,000/30) to PSC.
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m 2.
In March 1985, PSC decided to delay fabrication of Segment Eleven (11) fuel because the fabricated fuel on hand was not in balance with projected fuel needs.
GA Technology's fuel fabrication facility is currently in a holding mode.
Each day's delay in achieving an effective full-power day translates into a day's delay in reactiviating the fuel fabrication process. Based on GA Technology's cost estimate, the average monthly charge to hold the facility and maintain security for the period August 1985 through December 1985 will be approximately $365,600 or $12,190 per day.
3.
On September 30, 1985, PSC is required to pay the Department of Energy $6,613,650 for 48,990 SWUs under the terms of the Utility Services Contract.
By borrowing these funds at an assumed 10%
interest rate, PSC will have to pay approximately $55,000 a month (or $1,833 per day) in interest charges until the enriched uranium is utilized for fabricating Segment 11 fuel.
CONCLUSION Based upon the discussions above, PSC has concluded that operation of FSV at 8% power, for a period of time not to exceed 45 days poses no undue risk to the health and safety of the public. Continued moisture removal is an important operational factor given the design bases of the FSV reactor. Potential environmental temperatures that might result from a postulated steam line break at low power are significantly lower than those for 100% power. There is ample time following a postulated steam line break to both perform manual operations as well as effect repairs, if required, prior to reestablishing forced circulation core cooling. Additionally, since fuel temperatures do not approach the 2900 degrees F calculated for possible fuel failure, no fission product releases occur and thus there is no resulting risk to the health and safety of the public.
PSC is continuing to agressively undertake actions to resolve 10CFR50.49 issues.
In the interim, operation of the FSV reactor under conditions stated above would enhance moisture removal from the reactor vessel.
This operation is prudent from design considerations, is economically beneficial and presents no undue risk to public health and safety,
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4 TABLE 1 Peak Temperatures as a Result of a Steam Line Break.
s i
. Peak Temperature i
1 20 Feet Building Average Reactor Building 221 degrees F 170 degrees F (cold reheat steam line) 134 degrees F i
Turbine Building 207 degrees F i
(hotreheatsteamline)
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