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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217H6231999-10-18018 October 1999 Discusses Completion of Licensing Action for GL 98-01 & Suppl 1, Yr 2000 Readiness of Computer Sys at Npps, to All Holders of Operating Licenses for NPPs ML20217J4331999-10-15015 October 1999 Forwards Insp Rept 50-461/99-19 on 990913-17.One Violation Re Individual Failure to Follow Radiation Protection Procedures When Accessing High Radiation Area Noted & Being Treated as Noncited Violation U-603280, Forwards Rev 27 to Clinton Power Station Physical Security Plan,Iaw 10CFR50.54(p).Encl Withheld from Public Disclosure, Per 10CFR50.54(p)1999-10-12012 October 1999 Forwards Rev 27 to Clinton Power Station Physical Security Plan,Iaw 10CFR50.54(p).Encl Withheld from Public Disclosure, Per 10CFR50.54(p) ML20217C0871999-10-11011 October 1999 Forwards Proprietary Attachment Inadvertently Omitted from Encl 2 to Submitting Responses to NRC RAI Re License Transfer Application for Plant.Proprietary Encl Withheld U-603276, Forwards Rev 8 to CPS USAR, Which Includes Changes from 970701 Through 990630 & Available Changes Approved After 990630 That Reduce Overall Burden of Submittal Changes for Forthcoming Reporting period.10CFR50.59 Rept Included1999-10-0808 October 1999 Forwards Rev 8 to CPS USAR, Which Includes Changes from 970701 Through 990630 & Available Changes Approved After 990630 That Reduce Overall Burden of Submittal Changes for Forthcoming Reporting period.10CFR50.59 Rept Included U-603279, Forwards non-proprietary & Proprietary Responses to NRC RAI Re License Transfer Application for Plant.Attached Responses Also Respond to Comments of Environ Law & Policy Center Dtd 990920.Proprietary Encl Withheld1999-10-0707 October 1999 Forwards non-proprietary & Proprietary Responses to NRC RAI Re License Transfer Application for Plant.Attached Responses Also Respond to Comments of Environ Law & Policy Center Dtd 990920.Proprietary Encl Withheld U-603275, Provides Updated Illinois Power Rept on Status of Decommissioning Funding for Clinton Power Station1999-10-0707 October 1999 Provides Updated Illinois Power Rept on Status of Decommissioning Funding for Clinton Power Station ML20217A9881999-10-0101 October 1999 Advises of NRC Plans for Future Insp Activities at Facility for Licensee to Have Opportunity to Prepare for Insps & to Provide NRC with Feedback on Any Planned Insps Which May Conflict with Plant Activities ML20217A7361999-10-0101 October 1999 Forwards Insp Repts 50-461/99-14 & 50-461/98-12 on 990729-0908.Two Violations Identified,One Re Failure to Place Control Switch in Proper Position to Identify Piece of out-of-svc Equipment & Being Treated as NCVs ML20217J1251999-09-30030 September 1999 Refers to Investigation 3-1997-040 Conducted from 971028- 980921 & Forwards Nov.Investigations Determined That During Jan 1997,supervisor Qv Dept Discriminated Against Qv Inspector in Retaliation for Inspector Contacts with NRC ML20217J1421999-09-30030 September 1999 Refers to Investigation 3-97-040 Conducted from 971028- 980921 & Forwards Nov.Investigation Concluded That Recipient Engaged in Deliberate Misconduct in That Recipient Discriminated Againt Qv Inspector for Having Contacted NRC ML20212G6751999-09-22022 September 1999 Forwards Comment Submitted to NRC by Environ Law & Policy Ctr Re Proposed License Transfer for Clinton Power Station U-603272, Provides Update to Final Response to GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. 3-D Monicore & Station Security Sys remediated.Y2K Readiness Disclosure for Cps,Encl1999-09-22022 September 1999 Provides Update to Final Response to GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. 3-D Monicore & Station Security Sys remediated.Y2K Readiness Disclosure for Cps,Encl U-603225, Provides Closure of Util Commitments Re Ci Cv Noted in Previous Ltr to Nrc.Basis for Expecting Valves to Remain in leak-tight Condition Throughout Operating Cycle & Basis That Justifies Not Performing mid-cycle Leak Testing,Encl1999-09-20020 September 1999 Provides Closure of Util Commitments Re Ci Cv Noted in Previous Ltr to Nrc.Basis for Expecting Valves to Remain in leak-tight Condition Throughout Operating Cycle & Basis That Justifies Not Performing mid-cycle Leak Testing,Encl ML20212G6981999-09-20020 September 1999 Requests That NRC Reject Proposed License Transfer for Clinton Power Station & That NRC State That Public Interest in Safe Nuclear Power Industry Will Not Be Subordinated to Interest in Maximizing Profit by Limiting Liability ML20217H3421999-09-17017 September 1999 Forwards Request for Addl Info Re Licensee 990723 Application for License Transfer & Conforming Administrative License Amend.Response Requested within 20 Days of Receipt of Ltr 05000461/LER-1996-010, Forwards LER 96-010-01, Plant Shutdown Due to Unidentified RCS Leakage from Degraded Reactor Recirculation Pump Seal Greater than TS Limit. Revised Rept Includes Cause of Event,Corrective Actions & Discussion of Similar Events1999-09-13013 September 1999 Forwards LER 96-010-01, Plant Shutdown Due to Unidentified RCS Leakage from Degraded Reactor Recirculation Pump Seal Greater than TS Limit. Revised Rept Includes Cause of Event,Corrective Actions & Discussion of Similar Events 05000461/LER-1999-011, Forwards LER 99-011-00 Re Improper Restoration of a APRM Which Caused Monitor to Not Meet Seismic Qualification Requirements.Rept Contains Listed Commitments1999-09-10010 September 1999 Forwards LER 99-011-00 Re Improper Restoration of a APRM Which Caused Monitor to Not Meet Seismic Qualification Requirements.Rept Contains Listed Commitments U-603269, Certifies That DB Livingston,License OP-31136,successfully Completed Facility Licensees Requirements to Be Licensed as Ro,Per 10CFR55 & Has Need for RO License to Perform Assigned Duties.Five Significant Control Manipulations,Listed1999-09-10010 September 1999 Certifies That DB Livingston,License OP-31136,successfully Completed Facility Licensees Requirements to Be Licensed as Ro,Per 10CFR55 & Has Need for RO License to Perform Assigned Duties.Five Significant Control Manipulations,Listed ML20211Q2671999-09-0808 September 1999 Informs That NRC Tentatively re-scheduled Initial Licensing Exams for License Operator License Applicants During Weeks of June 5 & 12,2000.Validation of Exams Will Occur at Station During Weeks of May 15,2000 U-603229, Provides Response to NRC RAI Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, Dtd 990528.Rev 0 to Calculation IP-M-0556 & Rev 0 to Calculation IP-M-0570,encl1999-08-25025 August 1999 Provides Response to NRC RAI Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, Dtd 990528.Rev 0 to Calculation IP-M-0556 & Rev 0 to Calculation IP-M-0570,encl U-603243, Forwards Response to NRC GL 99-02, Lab Testing of Nuclear-Grade Activated Charcoal. Util Performing Testing of ESF Ventilation Sys Charcoal Samples Using ASTM D3803- 1989 Methodology as Required by TS 5.5.71999-08-23023 August 1999 Forwards Response to NRC GL 99-02, Lab Testing of Nuclear-Grade Activated Charcoal. Util Performing Testing of ESF Ventilation Sys Charcoal Samples Using ASTM D3803- 1989 Methodology as Required by TS 5.5.7 ML20211D2201999-08-23023 August 1999 Confirms 990817 Telcon with J Neuschwanger & D Mcneil Re Arrangements Made for NRC to Inspect Licensed Operator Requalification Program at Plant U-603258, Forwards ISI Summary Rept, IAW ASME Section Xi,Article IWA-6000.Summary Rept Addresses ISI Activities Performed at Plant from 950429-990527,including Extended Sixth Refueling Outage1999-08-23023 August 1999 Forwards ISI Summary Rept, IAW ASME Section Xi,Article IWA-6000.Summary Rept Addresses ISI Activities Performed at Plant from 950429-990527,including Extended Sixth Refueling Outage ML20211B0871999-08-20020 August 1999 Responds to J Hopkins Inquiry Re Application for Order Consenting to License Transfer & Approving Conforming Administrative License Amend Filed by Ilpr & Amergen Energy Co on 990723 U-603259, Provides Notification That Cl Kreidler Has Resigned Position with Util,Effective 990818.License Status Should Be Changed to Expired1999-08-19019 August 1999 Provides Notification That Cl Kreidler Has Resigned Position with Util,Effective 990818.License Status Should Be Changed to Expired ML20211A8931999-08-19019 August 1999 Forwards Insp Rept 50-461/99-13 on 990611-0728.Two Violations Noted & Being Treated as Ncvs.Violation Re Three Examples Where Licensee Procedural Requirements for Minor Maint Work Were Not Followed U-603253, Notifies NRC That Je Smith,License SOP-30819-1,has Resigned from Position with Ilpr Effective 990813.Status of License Should Be Changed to Expired,Effective 9908131999-08-16016 August 1999 Notifies NRC That Je Smith,License SOP-30819-1,has Resigned from Position with Ilpr Effective 990813.Status of License Should Be Changed to Expired,Effective 990813 ML20210U3771999-08-12012 August 1999 Forwards Notice of Consideration of Approval of Transfer of FOL & Issuance of Conforming Amend & Opportunity for Hearing Re Amend Request for Approval of Clinton Power Station License NPF-62 Transfer to Amergen U-603250, Notifies NRC That Ma Freihofer (License SOP-31296-1) Has Resigned from Position with Illinois Power Effective 990729 & License Status Should Be Changed to Expired Effective 9907291999-08-10010 August 1999 Notifies NRC That Ma Freihofer (License SOP-31296-1) Has Resigned from Position with Illinois Power Effective 990729 & License Status Should Be Changed to Expired Effective 990729 U-603249, Notifies NRC That He Bouska (License SOP-3055-1) Has Resigned from Position with Illnois Power Effective 990809. & License Status Should Be Changed to Expired Effective 9908091999-08-10010 August 1999 Notifies NRC That He Bouska (License SOP-3055-1) Has Resigned from Position with Illnois Power Effective 990809. & License Status Should Be Changed to Expired Effective 990809 ML20210N2961999-08-0909 August 1999 Forwards Form of Nuclear Decommissioning Master Trust Agreement,Per CPS Application for License Transfer & Conforming Administrative License Amend U-603248, Requests Unrestricted License for Kc Scott,License SOP-31532.Scott Has Successfully Completed Facility Licensee Requirements to Be Licensed as Operator/Senior Operator Per 10CFR551999-08-0606 August 1999 Requests Unrestricted License for Kc Scott,License SOP-31532.Scott Has Successfully Completed Facility Licensee Requirements to Be Licensed as Operator/Senior Operator Per 10CFR55 U-603236, Forwards Revised Data Point Ref File Sheets for Clinton Power Station Computer Points That Input to ERDS1999-08-0202 August 1999 Forwards Revised Data Point Ref File Sheets for Clinton Power Station Computer Points That Input to ERDS ML20210J0541999-07-30030 July 1999 Forwards Three Original Signature Pages of Gr Rainey for Application for License Transfer & Conforming Administrative License Amend, for NRC Files U-603178, Forwards Four ASME Section XI Relief Requests Re Performance of non-destructive Exams for First 120-month Inservice Insp for CPS1999-07-29029 July 1999 Forwards Four ASME Section XI Relief Requests Re Performance of non-destructive Exams for First 120-month Inservice Insp for CPS U-603237, Informs That Util Will Provide Response to fire-related Questions One & Two of NRC RAI Re CPS Ipeee,By 0001311999-07-28028 July 1999 Informs That Util Will Provide Response to fire-related Questions One & Two of NRC RAI Re CPS Ipeee,By 000131 U-603240, Forwards Clinton Power Station semi-annual Fitness for Duty Rept for Period Ending 990630,IAW 10CFR26.711999-07-27027 July 1999 Forwards Clinton Power Station semi-annual Fitness for Duty Rept for Period Ending 990630,IAW 10CFR26.71 U-603235, Forwards Application for License Transfer & Conforming Administrative License Amend for OL NPF-62.Proprietary & Nonproprietary Asset Purchase Agreement Encl.Proprietary Info Withheld,Per 10CFR2.7901999-07-23023 July 1999 Forwards Application for License Transfer & Conforming Administrative License Amend for OL NPF-62.Proprietary & Nonproprietary Asset Purchase Agreement Encl.Proprietary Info Withheld,Per 10CFR2.790 ML20210A4401999-07-16016 July 1999 Forwards Insp Rept 50-461/99-10 on 990422-0610.Four Violations Being Treated as Noncited Violations ML20209G7671999-07-12012 July 1999 Ack Receipt of Encl FEMA Correspondence ,which Transmitted FEMA Evaluation Rept for 981118 Biennial EP Exercise at Clinton Power Station.No Deficiencies Were Observed ML20209D5691999-07-0707 July 1999 Forwards Insp Rept 50-461/99-12 on 990607-11.No Violations Noted.Insp Consisted of Selective Exam of Procedures & Representative Records,Observations of Work in Progress & Interviews with Personnel U-603231, Forwards Summary of Status of Plan for Excellence (Pee) Initiatives & Clinton Power Station (CPS) 1999 Business Plan.Encl Documents Provide Status & Disposition for Actions Not Completed to Date1999-07-0707 July 1999 Forwards Summary of Status of Plan for Excellence (Pee) Initiatives & Clinton Power Station (CPS) 1999 Business Plan.Encl Documents Provide Status & Disposition for Actions Not Completed to Date U-603214, Forwards Results of Analysis Performed on Recently Completed Vendor Contracts,Per GL 83-28, Required Actions Based on Generic Implications of Salem ATWS Events1999-07-0606 July 1999 Forwards Results of Analysis Performed on Recently Completed Vendor Contracts,Per GL 83-28, Required Actions Based on Generic Implications of Salem ATWS Events ML20196J9651999-07-0202 July 1999 Confirms Discussion Between Members of Staffs to Conduct Meeting on 990714 at Clinton Power Station to Discuss Results of Restart Insp & Licensee Progress in Addressing Remaining Long Term C/A Actions to Sustain Improvements ML20196J7131999-06-30030 June 1999 Informs of Closure of Response to Requests for Addl Info to GL 92-01,Rev 1,Supplement 1, Reactor Vessel Structural Integrity, for Clinton Power Station Unit 1 U-603218, Provides Final Response to GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. Attachment Provides Y2K Readiness Disclosure for Plant1999-06-28028 June 1999 Provides Final Response to GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. Attachment Provides Y2K Readiness Disclosure for Plant U-603212, Forwards Response to NRC 990315 Telcon Re Proposed Amend of License NPF-62,implementing Feedwater Leakage Control Sys Mode of RHR Sys1999-06-24024 June 1999 Forwards Response to NRC 990315 Telcon Re Proposed Amend of License NPF-62,implementing Feedwater Leakage Control Sys Mode of RHR Sys U-603227, Provides Updated Rept on Status of Decommissioning Funding for Plant.Updated Rept Provides Min Decommissioning Fund Estimate,Per 10CFR50.75(b) & (C) Utilizing NUREG-1307,Rev 8 Methodology1999-06-24024 June 1999 Provides Updated Rept on Status of Decommissioning Funding for Plant.Updated Rept Provides Min Decommissioning Fund Estimate,Per 10CFR50.75(b) & (C) Utilizing NUREG-1307,Rev 8 Methodology ML20196A3471999-06-16016 June 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-461/99-11 Issued on 990430.Corrective Actions Will Be Examined During Future Inspections 1999-09-08
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217H6231999-10-18018 October 1999 Discusses Completion of Licensing Action for GL 98-01 & Suppl 1, Yr 2000 Readiness of Computer Sys at Npps, to All Holders of Operating Licenses for NPPs ML20217J4331999-10-15015 October 1999 Forwards Insp Rept 50-461/99-19 on 990913-17.One Violation Re Individual Failure to Follow Radiation Protection Procedures When Accessing High Radiation Area Noted & Being Treated as Noncited Violation ML20217A7361999-10-0101 October 1999 Forwards Insp Repts 50-461/99-14 & 50-461/98-12 on 990729-0908.Two Violations Identified,One Re Failure to Place Control Switch in Proper Position to Identify Piece of out-of-svc Equipment & Being Treated as NCVs ML20217A9881999-10-0101 October 1999 Advises of NRC Plans for Future Insp Activities at Facility for Licensee to Have Opportunity to Prepare for Insps & to Provide NRC with Feedback on Any Planned Insps Which May Conflict with Plant Activities ML20217J1421999-09-30030 September 1999 Refers to Investigation 3-97-040 Conducted from 971028- 980921 & Forwards Nov.Investigation Concluded That Recipient Engaged in Deliberate Misconduct in That Recipient Discriminated Againt Qv Inspector for Having Contacted NRC ML20217J1251999-09-30030 September 1999 Refers to Investigation 3-1997-040 Conducted from 971028- 980921 & Forwards Nov.Investigations Determined That During Jan 1997,supervisor Qv Dept Discriminated Against Qv Inspector in Retaliation for Inspector Contacts with NRC ML20212G6751999-09-22022 September 1999 Forwards Comment Submitted to NRC by Environ Law & Policy Ctr Re Proposed License Transfer for Clinton Power Station ML20217H3421999-09-17017 September 1999 Forwards Request for Addl Info Re Licensee 990723 Application for License Transfer & Conforming Administrative License Amend.Response Requested within 20 Days of Receipt of Ltr ML20211Q2671999-09-0808 September 1999 Informs That NRC Tentatively re-scheduled Initial Licensing Exams for License Operator License Applicants During Weeks of June 5 & 12,2000.Validation of Exams Will Occur at Station During Weeks of May 15,2000 ML20211D2201999-08-23023 August 1999 Confirms 990817 Telcon with J Neuschwanger & D Mcneil Re Arrangements Made for NRC to Inspect Licensed Operator Requalification Program at Plant ML20211A8931999-08-19019 August 1999 Forwards Insp Rept 50-461/99-13 on 990611-0728.Two Violations Noted & Being Treated as Ncvs.Violation Re Three Examples Where Licensee Procedural Requirements for Minor Maint Work Were Not Followed ML20210U3771999-08-12012 August 1999 Forwards Notice of Consideration of Approval of Transfer of FOL & Issuance of Conforming Amend & Opportunity for Hearing Re Amend Request for Approval of Clinton Power Station License NPF-62 Transfer to Amergen ML20210A4401999-07-16016 July 1999 Forwards Insp Rept 50-461/99-10 on 990422-0610.Four Violations Being Treated as Noncited Violations ML20209G7671999-07-12012 July 1999 Ack Receipt of Encl FEMA Correspondence ,which Transmitted FEMA Evaluation Rept for 981118 Biennial EP Exercise at Clinton Power Station.No Deficiencies Were Observed ML20209D5691999-07-0707 July 1999 Forwards Insp Rept 50-461/99-12 on 990607-11.No Violations Noted.Insp Consisted of Selective Exam of Procedures & Representative Records,Observations of Work in Progress & Interviews with Personnel ML20196J9651999-07-0202 July 1999 Confirms Discussion Between Members of Staffs to Conduct Meeting on 990714 at Clinton Power Station to Discuss Results of Restart Insp & Licensee Progress in Addressing Remaining Long Term C/A Actions to Sustain Improvements ML20196J7131999-06-30030 June 1999 Informs of Closure of Response to Requests for Addl Info to GL 92-01,Rev 1,Supplement 1, Reactor Vessel Structural Integrity, for Clinton Power Station Unit 1 ML20196A3471999-06-16016 June 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-461/99-11 Issued on 990430.Corrective Actions Will Be Examined During Future Inspections ML20207D1261999-05-28028 May 1999 Forwards Request for Addl Info Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20206P0641999-05-12012 May 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Aj Mendiola Will Be Section Chief for Clinton Power Station.Organization Chart Encl ML20206K4351999-05-0707 May 1999 Discusses NRC OI Investigation Rept 3-99-002 Re 981018 Personnel Error Which Resulted in Loss of Offsite Power Which Caused Loss of Only Operating Shutdown Cooling Subsystem ('A' RHR Pump) ML20206J7461999-05-0505 May 1999 Forwards Insp Rept 50-461/99-04 on 990301-0407.Four Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20206L5191999-05-0303 May 1999 Informs That on 990420-21 NRC Senior Managers Met to Evaluate Nuclear Safety Performance of Operating Reactors, Fuel Cycle Facilities & Other Matl Licenses ML20206G9691999-04-30030 April 1999 Forwards Insp Rept 50-461/99-11 on 990408-21 & NOV Re Failure to Correctly Translate Design Basis for Hydrogen Mixing Compressors Into EDG Load Calculation ML20206G6671999-04-30030 April 1999 Discusses Insp Rept 50-461/99-01 on 990208-0325.Number of Weaknesses Were Identified in C/A Program Re Approval Process for Issuing Condition Repts,Program Effectiveness Reviews & Issue Resolution.Six non-cited Violations Noted ML20206F2111999-04-27027 April 1999 Informs That NRC Considers Util Actions Associated with demand-for-info Pursuant to 10CFR50.54(f) Re C/A Program Performance at Clinton Power Station,Satisfactory & Therefore DFI Closed ML20206F2141999-04-27027 April 1999 Documents Completion of NRC Review of Specific Corrective Actions Util Committed to Complete Prior to Restarting Clinton Power Station & Forwards NRC Manual Chapter 0350 Restart Action Plan ML20206F1741999-04-27027 April 1999 Informs of Completion of Review of Actions Taken by Illinois Power as Specified in NRC CAL-III-97-09 Issued on 970806. Considers Actions Taken to Be Satisfactory & CAL Re 970805 W Circuit Breaker Failure at CPS Closed ML20205S6921999-04-21021 April 1999 Forwards Insp Rept 50-461/99-06 on 990217-0407.Four Violations Noted Re Professional Atmosphere of Main Control Room & Being Treated as Non-Cited Violations ML20205T5711999-04-21021 April 1999 Forwards Insp Rept 50-461/99-03 on 990208-0318.Eight Violations Occurred & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20205M9421999-04-13013 April 1999 Forwards Emergency Response Data System Implementation Documents.Data Point Library Updates for Kewaunee (271), San Onofre (272) & Clinton (273) Encl.Also Encl Plant Attribute Library Update for Grand Gulf (274).Without Encls ML20205P3921999-04-0909 April 1999 Forwards Emergency Preparedness Exercise Insp Rept 50-461/99-08 on 990309-12.No Violations Identified.Exercise Weakness Re Maintenance of Status of Repair Teams Identified During Insp ML20205H3001999-04-0101 April 1999 Confirms Plans to Have Meeting on 990416 at Clinton Power Station to Discuss Results of Plant Performance Review Process & Discuss Progress in Addressing Remaining Open Items in NRC Specific Checklist Which Need Resolution ML20205G2141999-04-0101 April 1999 Ack Receipt of ,Which Transmitted Changes Identified as Rev 26 to CPS Security Plan,Per 10CFR50.54(p) ML20205G5471999-03-26026 March 1999 Advises of Completion of Plant Performance Review on 990202 to Develop Integrated Understanding of Safety Performance. Three Areas of Concern Are Operator Performance,Cap Implementation & Resolution of Engineering Design Issues ML20205C5181999-03-26026 March 1999 Ack Receipt of Revising 2 Previously Communicated Corrective Action Commitments Contained in . Corrections Reviewed & NRC Have No Questions at Present Time ML20204J5071999-03-24024 March 1999 Forwards Insp Rept 50-461/98-29 on 981214-990217.No Violations Noted.Insp Conducted to Review Circumstances Surrounding Unsatisfactory Licensed Operator Performance That Staff Identified During Sept 1998 Operator Exam ML20204F4281999-03-18018 March 1999 Forwards Insp Rept 50-461/99-02 on 990107-0216.Violations Noted.Violation Re Engineering & Work Mgt Personnel Failure to Ensure Overdue Preventive Maint Items Were Completed ML20204E6311999-03-10010 March 1999 Forwards Insp Rept 50-461/99-05 on 990208-12 & Notice of Violation Re Inadequate Radiological Surveys Were Performed in Residual Heat Removal Heat Exchanger Room ML20207K2841999-03-0909 March 1999 Confirms Discussion Between Members of Staffs to Have Meeting on 990325 at Illinois Power Energy & Environ Ctr. Purpose of Meeting to Discuss Performance Improvement Initiatives ML20203F2541999-02-10010 February 1999 Informs That Beginning 990216,DE Hills Will Be Chief of Operations Branch Which Includes Operator Licensing Function ML20202J8541999-02-0505 February 1999 Forwards Notice of Proposed No Significant Hazards Consideration & Opportunity for Hearing ML20202H9941999-02-0303 February 1999 Forwards SE Accepting Changes in Quality Assurance Program Continuing to Meet Requirements of App B to 10CFR50 ML20202G4951999-02-0101 February 1999 Forwards Insp Rept 50-461/98-28 on 981214-18.No Violations Noted.Inspector Concluded That Risk Assessment Process for Evaluating on-line & Outage Maint Activities Has Been Developed ML20202H6851999-01-26026 January 1999 Forwards Request for Addl Info Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20202D7871999-01-22022 January 1999 Confirms Discussion Between Members of Staff to Have Meeting on 990205 at NRC Office in Lisle,Il to Discuss Performance Improvement Initiatives.Meeting Will Be Open to Public ML20203A0501999-01-22022 January 1999 Requests Expedited Publication of Encl Notice of Consideration of Issuance of Amend to Facility Operating License,Proposed NSHC Determination & Opportunity for Hearing on 990129 ML20206S0931999-01-22022 January 1999 Forwards Insp Rept 50-461/98-20 on 981118-0106 & Notice of Enforcement Discretion.Inspectors Identified That Operations Personnel Did Not Initiate Condition Repts for Several Nonconforming Conditions Documented in Main Control Room ML20199E1431999-01-12012 January 1999 Refers to Info Provided on 981229 That Was Requested by NRC in .Informs That Info Has Been Reviewed & Forwards List of Mods & Other Engineering Work Products Which Will Be Reviewed During Ssei ML20198S8221999-01-0505 January 1999 Confirms Discussion Between Members of Staff to Have Meeting on 990114 in Clinton,Il to Discuss Licensee Performance Improvement Initiatives 1999-09-08
[Table view] |
See also: IR 05000461/1996010
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Noveuber 19, 1996
John G. Cook
Senior Vice President
Illinois Power Company
500 South 27th Street
Decatur,IL 62525
Dear Mr. Cook:
On October 4,1996, the NRC completed two inspections at your Clinton facility: a
Special inspection into the circumstances surrounding the September 5,1996,
recirculation pump seal package failure and an independently chartered Operational Safety 11
Team inspection (OSTI) which was initiated as a result of operator performance in the' I
recirculation pump seal package failure event. The enclosures to this letter present the
results of those inspections.
As will be discussed below, on September 5,1996, the operations department put in
motion a sequence of events which revealed sigoificant deficiencies throughout the
organization at the Clinton facility. These deficiencies included procedural adequacy and
adherence problems, lack of rigor in conducting plant operations, and weak engineering
support to operations. And, most significantly, the deficiencies included serious lapses in
safety focus by both plant management and staff. It appears that plant management and
staff made decisions which placed plant production ahead of plant operational safety. .This
matter is the subject of an ongoing Office of Investigations review.
Our review of the activities associated with the September 5, event, and additional i
confirmatory findings from the OSTI, identified a number of actions and practices which 1
are inconsistent with procedural and pr'ogrammatic controls for assuring safe operation of l
a nuclear power plant. These actions and practices were also evident in the April reactor l
scram when station management decided to maintain the unit in a hot standby condition, 4
.thereby minimizing down time. This decision resulted in degraded safety relief valves. In l
both events, actions necessary to place the unit in the safest, most stable condition were
not taken. Further, the decision to maintain the unit in hot standby following the June
r_eactor ccram resulted in a lost opportunity to address the degrading "B" recirculation
pump seal package.
~ Specifically during the September 5, event, operators were attempting to place the unit in
single loop operation to allow continued unit operation by isolating a reactor coolant leak in
the "B" reactor recirculation pump shaft seal package. While attempting to isolate the
loop, seal pressure, temperature, and leak rate were not decreasing quickly enough to
ensure continued unit operation. To increase the pump shaft seal's cool down rate and
reduce leakage, shift supervision directed actions which were inconsistent with both
Clinton procedures and vendor recommendations for isolating the seal package. After this
procedural noncompliance, sealleakage increased to greater than 5.0 gallons-per-minute,
the technical specificaticn (TS) allowable leakage rate. The shift crew entered the
emergency plan, declared a Notice of Unusual Event, and made appropriate notifications. f
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J. Cook -2-
The plant was now in a TS limiting condition for operation (LCO) which required reducing
the leakage within four hours or shutting the plant down. Based on the four-hour
limitation, additional procedural steps were not followed in another attempt to reduce the
leakage to less than the TS limit to allow for continued unit operation. These activities
exacerbated the seal condition resulting in a seal failure and leakage exceeding the
installed instrumentation's ability to accurately monitor the leakage. The crew, although
recognizing the seal failure, did not recognize the instrumentation's limitations. It was not
until a relief Shift Technical Advisor arrived that leakage rates were properly calculated.
Even though shift management was aware that these actions would furthe: degrade the
seals and was aware that a previous seal failure had resulted in leakage in excess of the
criteria for declaring an Alert under the emergency plan, an Alert was not dxlared
following all of the obvious indications that a seal failure had occurred.
After the seal package failed, shift supervision continued to delay commencing the reactor
shutdown, maximizing the operating time and fully expecting the leakage to drop below
the TS limit so that single loop operation could be maintained. Finally, four hours after the
l
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seal package failed (two hours after the LCO expired), with a leakage rate still greater than
twice the TS limit, a briefing was held for the planned orderly shutdown of the unit. Plant
shutdown continued to be inappropriately protracted with plant operation continuing to
within 46 minutes of the 12-hour shutdown requirement being exceeded.
Throughout the event, operators' actions were complicated by preexisting equipment
deficiencies. The originally installed leakage rate instrumentation has been a continuing
problem at Clinton. A modification installed to provide similar information had its
indication capped at 8 gallons-per-minute, well below the actual leakage achieved during
the September 5 event. While providing leakage rates, the modification did not support
continued leakage rate information or emergency classification assessments when most
needed. Safety relief valves, cycled 85 times in the April event discussed earlier, were
leaking and contributed to operators diverting their attention from the plant shutdown to
enter an Emergency Operating Procedure to reduce suppression poollevel.
Even after the unit was placed in a shutdown condition, the operations department still
appeared to be driven by schedule pressures rather than conservative operating practices.
For example, while placing the feedwater system in a cleanup mode, the operations
department determined there was a need to expedite the cleanup rate and again operated
equipment / components outside of procedural controls. This procedural non-compliance
resulted in the spinning of the feedwater pump without oil to the bearings which could
have caused serious damage to the pump.
l Following the event, our observations indicated that the Clinton staff believed that the
i actions taken during the event were appropriate. The failures to follow procedures,
inadequate procedures, operator performance issues, and inadequate management
involvement were not promptly identified nor understood. it was not until the NRC had
2
extensively intervened, through a number of calls with senior plant management over a
period of several days that action was taken to initiate a thorough and comprehensive
assessment. This commitment was formalized in our Confirmatory Action Letter dated
l
l
_ - _ . . .
s - .- l
.
D
I J. Cook -3-
L
September 11,1996. The initial assessment, while drawing appropriate overall
conclusions, did not provide a solid basis for some of the conclusions. For example, while
the initial assessment concluded that procedures were not followed, the detailed report
indicated that procedural steps were followed, or a procedure deficiency existed, when in
fact the problem was that procedural steps were not followed. Following subsequent
discussions with the NRC, the Clinton staff's revised assessment corrected these issues.
In summary, our assessment of the recirculation pump seal package failure event identified
three significant concerns. First, the operations department lacked an appropriate safety
focus as exhibited by: (1) the failure to follow procedures in an extraordinary attempt to
keep the unit in an operating condition, and (2) the protracted unit shutdown. Secondly, l
the failure to correct known material condition deficiencies that complicated operators' i
actions and responses indicated a lack of management sensitivity and priority to the
removal of barriers affecting operator performance. Finally, the engineering department's ,
support to operations was weak as exhibited by' poor corrective actions for the original
leakage instrumentation problems and the deficient compensatory modification.
While the examples differed, the same issues were independently confirmed during the
l' OSTl. A number of problems with procedure adequacy and adherence were identified.
' Two cases of preconditioning for a diesel generator surveillance and an inadequate local
leak rate test procedure were identified. The preconditioning is of concern because this
could mask materiel condition issues affecting the operability of the diesel generators.
Problems with procedure adherence were further exemplified by operators failing to follow
the procedure for isolating spent fuel pool cooling and thereby allowing a 1000 gallon per
- day leak. In addition, when an operator was asked why they (operators) were having
difficulty with a specific procedure, he responded that they were trying to do this the right
way because the NRC was watching. This statement demonstrates a poor attitude toward
and understanding the importance of procedure adherence.
The OSTI identified, through control room observations, a lack of management oversight
and a full appreciation for the responsibilities held by licensed operators. At one point the
"at the controls" operator left the designated control area without obtaining a relief. Short
term relief turnovers were weak, and variations in crew communications and formality
were observed. That these activities would occur during a major NRC team inspection,
with inspectors in the. control room, indicates to us that these problems may be more
widespread.
Engineering support to operations was weak and the engineers exhibited a weak safety
. focus. Engineering and operations on occasion conducted tests on facility systems with
i the reactor at power to identify potential impacts on safety systems. For example, cyc%d
l condensate was isolated from the residual heat removal system to determine the potential
l impact. This test resulted in the residual heat removal system being declared inoperable.
1- These special tests did not receive the required safety evaluations (10 CFR 50.59) or site
reviews for acceptability. Further, engineers indicated it was acceptable to perform
actions by combining steps from disparate procedures without further review. Conducting
l unreviewed, unauthorized tests demonstrate'.s a lack of a safety focus by engineers and
[ licensed operators.
L
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%
J. Cook -4-
i
The OSTI also noted that often engineers seemed focused on finding a way to justify
system operability rather than performing an in-depth evaluation and analysis
demonstrating system operability and compliance with the FSAR. The operability
evaluation program was poor with the process for operability evaluations not fully
described. The Clinton staff did not know how many or what operational evaluations were
in-place. Further, the staff had no mechanism of tracking evaluations. This is of
significant concern to us because degraded plant equipment needs to be promptly
evaluated to ensure appropriate safety margins are maintained.
Most of these significant issues described in this report including several apparent
l violations with multiple examples, were identified by the NRC, including: 12 examples of
l failing to follow procedures,8 examples of inadequate / inappropriate procedures,4
l examples of failure to perform safety evaluations (10 CFR 50.59), two examples of
inadequate corrective actions, an example of an operator leaving the " control" area
without relief, and an example of operations management not performing appropriate
administrative activities. The failure of the Clinton staff to recognize the significance of ,
the issues identified and to promptly and appropriately respond to the them shows a lack l
of appreciation for the importance of adherence to NRC requirements. l
l Based on the results from the inspections and as noted above, several apparent violations
l of NRC requirements were identified and are being considered for escalated enforcement
l action in accordance with the " General Statement of Policy and Procedure for NRC
Enforcement Actions" (Enforcement Policy), NUREG-1600.
No Notice of violation is presently being issued for these inspection findings, in addition,
the number and characterization of apparent violations described in the enclosed inspection
reports may change as a result of further NRC review.
A pre-decisional enforcement conference to discuss these apparent violations will be
scheduled. The decision to hold a pre-decisional enforcement conference does not mean
- that the NRC has determined that a violation has occurred or that enforcement action will
I be taken. The conference will be held to obtain information to enable the NRC to make an
!
enforcement decision, including a common understanding of the facts and circumstances
surrounding the violations, their root causes, your opportunities to identify the apparent
violations sooner, your corrective actions, and the significance of the issues.
l
l In addition, this is an opportunity for you to point out any errors in our inspection reports
l and for you to provide any information concerning your perspectives on 1) the severity of
l the violations: 2) the application of the factors that the NRC considers when it determines
l the amount of a civil penalty that may be assessed in accordance with Section VI.B.2 of
I the Enforcement Policy; and 3) any other application of the Enforcement Policy to this
case, including the exercise of discretion in accordance with Section Vll.
;
You will be advised by separate correspondence of the results of our deliberations on this
-
manner. No response regarding these apparent violations is required at this time.
I
_ . . _ . _ _ _ __
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l
! ,
J. Cook -5-
- Docket No. 50-461
l
l cc w/ encl: Mr. Wilfred Connell, Vice President l
l P. Yocum, Plant Manager
l
Clinton Power Station
j R. Phares, Manager-Nuclear Assessment
!
P. J. Telthorst, Director - Licensing
l
Nathan Schloss, Economist
Office of the Attorney General
l K. K. Berry, Licensing Services Manager
l General Electric Company
Chairman, DeWitt County Board
State Liaison Officer
Chairman, Illinois Commerce Commission
.
Office of Enforcement (3)
J. Goldberg, OGC
G. Marcus, NRR
i i
l
l
Distribution:
!
! Docket File w/ encl DRP w/enci
OC/LFDCB w/ encl y ;PUBLIC IE-01 w/enci
l SRI Clinton, Dresden, Rill PRR w/ encl
LaSalle, Quad Cities CAA1 w/enci (E-mail)
l Project Manager, NRR w/ encl A. B. Beach, w/enci
l B. L. Burgess, w/enci W. L. Axelson, w/ encl
B. McCabe, OEDO
-
Document: R: INSPRPTS\ CLIN \CLl96010; 96011
g ,r .. . . . , . ,sni. . $ wi.. . . in. n.. c c.,, ,, ism . .ss..nf i e - c.,, ism .ss..nf i =-
0FFICE RIII , 8 RIII 6 RIII 3 ,/ REII RIII
NAME Mrkt/LeTd Granth Bu M /01
i
[[Mll
w
Axelson/ Beach
- DATE 11//f[96 11/)h/96 11/5/96 11/\,/;/96 11/ /96
0FFICIAL RICORD COPY
No k e a l2d hv d, f.u9 0] reciea0 ecoet lollrr ce
.
hoc $ vo o(jecbarf 4 Ws denty (Srat cN), ,
I ,q )h6
,
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'
. l
.-
'
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!
l
l J. Cook -5- ;
i 1
I
In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter
and its enclosures will be placed in the NRC Public Document Room (PDR).
Sincerely,
/s/A. Bill Beach l
A. Bill Beach I
Regional Administrator
l
Docket No. 50-461 l
cc w/ encl: Mr. Wilfred Connell, Vice President
P. Yocum, Plant Manager
Clinton Power Station l
R. Phares, Manager-Nuclear Assessment
P. J. Telthorst, Director - Licensing
Nathan Schloss, Economist
Office of the Attorney General
K. K. Berry, Licensing Services Manager
General Electric Company
Chairman, DeWitt County Board
State Liaison Officer
Chairman, Illinois Commerce Commission
Office of Enforcement (3)
J. Goldberg, OGC
G. Marcus, NRR
Distribution.
Docket File w/ encl DRP w/enci
OC/LFDCB w/enci PUBLIC IE-01 w/enci
SRI Clinton, Dresden, Rill PRR w/enci
LaSalle, Quad Cities CAA1 w/enci (E-mail)
Project Manager, NRR w/enct A. B. Beach, w/ encl
B. L. Burgess, w/ encl W. L. Axelson, w/ encl
B. McCabe, OEDO
See orevious concurrence
Document: R: INSPRPTS\ CLIN \CLl96010; 96011
-i . iwi.. 4. en. n.. c - c.,, -itu .it.cnf.ui c - c.,r itm .st. nf.=i n-
g gi.. . . , .e ini.
0FFICE RIII RIII RIII RIII RIfif
l NAME Wright / Leach Grant Burgess /0I Caldwell Axkl3n/ Beach
j DATE 11/ /96 11/ /96 11/ /96 11/ /96 11/M/96
0FFICIAL RECORD COPY l
l
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