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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML19343C2181975-12-23023 December 1975 AO 50-219/75-33:on 751212,during 6-month Load Test on Station a batteries,125 Volt Dc Distribution Ctr de-energized.Caused by Personnel Error in Following Procedure.Distribution Ctr re-energized ML20090C9991975-12-12012 December 1975 AO 75-33:on 751212,125-volt Dc Distribution Ctr of Station a Battery Inadvertently de-energized.Caused by Failure to Establish Proper Breaker Lineup Preparation for Conducting Battery Load Test.Procedure changed.W/751219 Memo ML19343C2191975-12-11011 December 1975 AO 50-219/75-32:on 751203,during Testing,Emergency Diesel Generator 1 Failed to Start When Simulated Loss of Power Condition Applied to Fast Start Logic Circuit.Caused by Failure of Relay to Operate Due to Varnish on Armature ML20126E8281975-12-0303 December 1975 AO 50-219/75-31:on 751124,during Operability Test of Torus to Drywell Vacuum Breakers,Alarm Sys 2 Failed to Annunciate in Control Room When V-26-4 Opened.Caused by Failure of Relay Due to Contacts Being Detective.Relay Replaced ML20090D0071975-11-25025 November 1975 AO 75-31:on 751124,drywell Vacuum Breaker Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-4 Opened. Caused by Component Failure.Corrective Action Under Investigation ML20090D0161975-11-0707 November 1975 AO 75-30:on 751106,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 17 a & C Tripped at Pressure Less than Min Required Value.Caused by Switch Repeatability.Pressure Switches Recalibr ML20090D0601975-11-0606 November 1975 AO 75-29:on 751027,torus Drywell Vacuum Breakers Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-8 Opened. Caused by Sticking Microswitch ML20090D0761975-10-28028 October 1975 AO 75-29:on 751027,torus to Drywell Vacuum Breaker Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-8 Opened.Caused by Component Failure.Corrective Action Under Investigation ML20090D0941975-10-24024 October 1975 AO 75-28:on 751015,standby Gas Treatment Sys 1 Inoperable. Caused by Air Solenoid Valve Coil Failure.Defective Solenoid Coil Replaced ML20090D1141975-10-17017 October 1975 AO 75-27:on 751008,low Reactor Pressure Core Spray Valve Permissive Pressure Switches RE17B & D Tripped at Pressure Less than Min Required Value.Caused by Switch Repeatability. Pressure Switches Recalibr ML20090D1041975-10-16016 October 1975 AO 75-28:on 751015,standby Gas Treatment Sys 1 Inoperable. Caused by Air Solenoid Valve Coil Failure.Defective Solenoid Coil replaced.W/751016 ML20090D1341975-10-0808 October 1975 AO 75-27:on 751008,low Reactor Pressure Core Spray Valve Permissive Pressure Switches RE17B & D Tripped at Pressures Less than Min Required Value.Caused by Switch Repeatability. Pressure Switches Recalibr ML20090D1501975-09-23023 September 1975 AO 75-26:on 750923,emergency Svc Water Pump 52C Failed to Start Automatically During Routine Surveillance Test of Containment Spray Sys Ii.Caused by Failure of Contact Switch in Time Delay Relay 16 K4B.Relay Replaced ML20090D2071975-09-0808 September 1975 AO 75-24:on 750829,electromatic Relief Valve Pressure Switches 1A83C & 1A83D Tripped at Pressures in Excess of Max Allowable Value.Caused by Instrument Setpoint Repeatability. Switches Reset ML19291C2641975-09-0808 September 1975 AO 73-19:when Closing Signal Was Applied to Breaker S1A,loss of Power Occurred at 4160-volt Ac Bus 1A Causing Trip of Various Pumps.Caused by Incorrect Setting of Current Transformer Ratio Matching Taps.Taps Set Properly ML20090D1941975-09-0808 September 1975 AO 75-25:on 750829,stack Gas Sample Sys Failed to Monitor Stack Releases Continuously While Reactor Was in Unisolated Condition.Caused by Malfunctioning Pump Lubricator.Thermal Overload Protection Reset ML20090D2151975-09-0202 September 1975 AO 75-24:on 750829,electromatic Relief Valve Pressure Switches 1A83C & 1A83D Tripped at Pressures in Excess of Max Allowable Value.Caused by Instrument Setpoint Repeatability. Switches Reset ML20090D2011975-09-0202 September 1975 AO 75-25:on 750829,stack Gas Sample Sys Failed to Monitor Stack Releases Continuously While Reactor Was in Unisolated Condition.Caused by Malfunctioning Pump Lubricator.Thermal Overload Protection Reset ML20090D2241975-08-21021 August 1975 AO 75-23:on 750817-20,stack Effluent for Iodine & Particulates Not Monitored.Caused by Personnel Error.Filter Installed in Operating Stack Gas Sampling Train ML20090D2261975-08-11011 August 1975 Preliminary AO-50-219/75-22:on 750810,stack Gas Sample Line Low Flow Alarm Received.Caused by Stack Gas Sample Pump a Not Running.Thermal Overload Protection Reset ML20090D2471975-08-0404 August 1975 Preliminary AO-50-219/75-21:on 750801,during Routine Surveillance on B Isolation Condensor Sys,Steam Line Valve V-14-32 Failed to Close on Simulation of Steam Line High Flow.Caused by Low Torque Switch Setting.Torque Increased ML20090D2521975-07-17017 July 1975 AO 50-219/75-19:on 750708,during Monthly Surveillance Test on Reactor High Pressure Scram Sensors,Re 03A,B,C & D, A,B & D Tripped Above Normal Trip Points.Caused by Switch Repeatability.Sensors Recalibr ML20090D2561975-07-0909 July 1975 Preliminary AO 50-219/75-19:on 750708,during Monthly Surveillance Test on Reactor High Pressure Scram Sensors,Re 03A,B,C & D,A,B & D Tripped Above Normal Trip Points.Caused by Switch Repeatability.Sensors Recalibr ML20084E1151975-07-0101 July 1975 RO 50-219/75-18:on 750623,two 8-1/2 Inch Handhole Covers in Standby Gas Treatment Filter Train Not in Place.Cause Unknown.Handhole Covers Repositioned & Secured ML20090D2741975-06-27027 June 1975 AO 50-219/75-17:on 750619,during Surveillance Test,Core Spray Sys Parallel Isolation Valve V-20-15 Failed to Demonstrate Operability.Caused by Broken Tab on B Phase of Valve Motor Breaker Stab.Stab Replaced ML20090D2661975-06-24024 June 1975 Preliminary AO 50-219/75-18:on 750623,handhole Covers in Standby Gas Treatment Filter Train 1-1 Not in Place.Cause Under Investigation.Covers Repositioned & Secured ML20090D2781975-06-24024 June 1975 AO 50-219/75-16:on 750614,electromatic Relief Valve Pressure Switches 1A83P & E Tripped at Pressures Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Switches Reset ML20090D2731975-06-19019 June 1975 Preliminary AO 50-219/75-17:on 750619,during Surveillance Test,Core Spray Sys Parallel Isolation Valve V-20-15 Failed to Demonstrate Operability.Caused by Broken Tab on B Phase of Valve Motor Breaker Stab.Stab Replaced ML20090D2901975-06-16016 June 1975 Preliminary AO 50-219/75-16:on 750614,electromatic Relief Valve Pressure Switches 1A83B & E Tripped at Pressure Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Switches Reset ML20090D6561975-06-0606 June 1975 AO-50-219/75-14:on 750529,during Surveillance Test of Containment Spray Pump Operability,Essential Svc Water Pump 1-2 Failed to Develop Sufficient Discharge Pressure.Caused by Dirt in Check Valve V-3-68.Valve Cleaned & Repaired ML20090D2971975-06-0606 June 1975 AO 50-219/75-15:on 750530,calculations of TIP Traces Indicated Total Peaking Factor in One Core Location in Excess of Value of Pf Given in Tech Specs.Caused by Lack of Operating Experience W/New Core Loading ML20090D2981975-06-0202 June 1975 Preliminary AO 50-219/75-15:on 750530,calculations of TIP Traces Indicated Total Peaking Factor in One Core Location in Excess of Value of Pf Given in Tech Specs.Caused by Lack of Operating Experience W/New Core Loading ML20090D6581975-05-30030 May 1975 Preliminary AO-50-219/75-14:on 750529,during Surveillance Test of Containment Spray Pump Operability,Essential Svc Water Pump 1-2 Failed to Develop Sufficient Discharge Pressure.Caused by Dirt in Check Valve V-3-68.Valve Cleaned ML20090D6611975-05-14014 May 1975 AO-50-219/75-13:on 750507,during Surveillance Test,Time Delay Relay 6Kll Failed to de-energize within 15 After Pressure Sensor RE-15C Tripped.Caused by Component Failure.Relay 6Kll Replaced ML20090D6641975-05-0707 May 1975 Preliminary AO-50-219/75-13:on 750507,during Surveillance Test,Time Delay Relay 6Kll Failed to de-energize within 15 After Pressure Sensor RE-15C Tripped.Caused by Component Failure.Relay 6Kll Replaced ML20090D6531975-05-0606 May 1975 AO-50-219/75-12:on 750426,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 17B & C Found to Trip at Pressure Less than Tech Spec Value.Caused by Switch Repeatablilty.Switches Recalibr ML20090D6701975-04-28028 April 1975 Preliminary AO-50-219/75-12:on 750426,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 178 & C Found to Trip at Pressure Less than Tech Spec Value.Caused by Switch Repeatability.Switches Recalibr ML20090D6751975-04-18018 April 1975 AO-50-219/75-11:on 750410,leakage of Main Line Drain & Bypass Line Exceeded Tech Spec Rate.Caused by Failure of Packing on Valve V-1-110.Valve to Be Repacked ML20090D7001975-04-14014 April 1975 AO-50-219/75-10:on 750404,reactor Bldg to Torus Vacuum Breaker Valves V-26-16 & 18 Leak Rates Exceeded Tech Spec Limits.Caused by Component Failure.Valves Adjusted &/Or Repaired ML20090D6811975-04-11011 April 1975 Preliminary AO-50-219/75-11:on 750410,leakage of Main Line Drain & Bypass Line Exceeded Tech Spec Rate.Caused by Failure of Packing on Valve V-1-110.Valve to Be Repacked ML20090D7131975-04-0808 April 1975 AO-50-219/75-09:on 750329,breaker 1C Tripped Resulting in Fault on Bus 1C.Caused by Fault on Cable 86-25.Cables Replaced ML20090D7061975-04-0707 April 1975 Preliminary AO-50-219/75-10:on 750404,reactor Bldg to Torus Vacuum Breaker Valves V-26-16 & 18 Leak Rates Exceeded Tech Spec Limits.Caused by Component Failure. Valves Adjusted &/Or Repaired ML20090D7271975-04-0303 April 1975 AO-50-219/75-08:on 750325,power Operation Continued W/ Average Linear Heat Generation Rate of Fuel Assemblies in Excess of Max Linear Heat Generation Rate.Caused by Failure to Properly Monitor Reactor Core.Rate Reduced ML20090D7211975-03-31031 March 1975 Preliminary AO-50-219/75-09:on 750329,breaker 1C Tripped Due to Fault on Bus 1C.Caused by Fault on Cable 86-25.Cables Replaced ML20090D7651975-03-27027 March 1975 AO-50-219/75-07:on 750319,during Standby Gas Treatment Sys (SGTS) Test,Dehumidifying Heater EHC-1-5 in SGTS 1 Failed to Energize.Caused by Plugged Orifice in Air Supply to Controller.New Type of Differential Relay Installed ML20090D7361975-03-26026 March 1975 Preliminary AO-50-219/75-08:on 750325,power Operation Continued W/Average Linear Heat Generation Rate of Fuel Assemblies in Excess of Max Linear Heat Generation Rate. Caused by Improper Reactor Core Monitoring.Rate Reduced ML20090D7761975-03-20020 March 1975 Preliminary AO-50-219/75-07:on 750319,during Stanby Gas Treatment Sys (SGTS) Test,Dehumidifying Heater EHC-1-5 in SGTS 1 Failed to Energize.Caused by Plugged Orifice in Air Supply to Controller.New Type of Relay Installed ML20090D7801975-03-19019 March 1975 AO-50-219/75-06:on 750310,stack Gas Sample Sys Failed to Continuously Monitor Stack Releases While Reactor in Unisolated Condition.Caused by Circuit Design.Request to Modify Circuit for Stack Gas Sample Pumps Submitted ML20090D7901975-03-13013 March 1975 AO-50-219/75-05:on 750306,during Monthly Surveillance Test, Containment Spray Pump 51A Failed to Start When Subjected to Simulated Signals.Caused by Breaker Trip Bar Failing to Reset After Previous Breaker Trip.Trip Bar Bushings Cleaned ML20090D7811975-03-11011 March 1975 Preliminary AO-50-219/75-06:on 750310,stack Gas Sample Sys Failed to Monitor Stack Releases While Reactor in Unisolated Condition.Caused by faulty-circuit Design 1975-09-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F1891998-05-0505 May 1998 Risk Evaluation of Post-LOCA Containment Overpressure Request ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20151Y4651998-03-31031 March 1998 Non-proprietary Version of Rev 1 to GENE-E21-00143, ECCS Suction Strainer Hydraulic Sizing Rept ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20212E2291998-03-0404 March 1998 Rev 11 to 1000-PLN-7200,01, Gpu Nuclear Operational QAP, Consisting of Revised Pages & Pages for Which Pagination Affected ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203B2781998-02-16016 February 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Systems & Procedures ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20217C7591997-12-31031 December 1997 1997 Annual Environmental Operating Rept for Oyster Creek Nuclear Generating Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20202E8511997-10-21021 October 1997 Rev 0 to Scenario 47, Gpu Nuclear Oyster Creek Nuclear Generating Station Emergency Preparedness (Nrc/Fema Evaluated) 1997 Biennial Exercise. Pages 49 & 59 of Incoming Submittal Were Not Included ML20211M9481997-10-0303 October 1997 Supplemental Part 21 Rept Re Condition Effected Emergency Svc Water Pumps Supplied by Bw/Ip Intl Inc to Gpu Nuclear, Oyster Creek Nuclear Generation Station.No Other Nuclear Generating Stations Effected by Notification ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20211B7461997-09-24024 September 1997 Part 21 Rept Re Failure of Emergency Service Water Pump Due to Threaded Flange Attaching Column to Top Series Case Failure.Caused by Dissimilar Metals.Pumps in High Ion Svc Will Be Upgraded to 316 Stainless Steel Matl ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station 1999-09-30
[Table view] |
Text
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fersNy Central Power & Light Company J N'j MADISON AVENUE AT PUNCH BOWL ROAD e MORRISTOWN, N.J.07960 = 201-539-6111
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, jjf,,*, Pubhc Utihties Corporation August 2, 1974 Mr. A. Giambusso l Deputy Director for Reactor Projects Directorate of Licensing United States Atomic Energy Commission Washington, D. C. 20545
Dear Mr. Giambusso:
Subject:
Oyster Creek Station Docket No. 50-219 Abnormal Occurrence Report No. 50-219/74/42 The purpose of this letter is to forward to you the attached Abnormal Occurrence Report in compliance with paragraph 6.6.2.a of the Technical Specifications.
Enclosed are forty copics of this submittal.
Veiy truly yours, 3
I o Ivan R. Finf,r'ock ,./Jr.
Vice President cs Enclosures cc: Mr. J. P. O'Reilly , Director '
i Directorate of Regulatory Operations, Region I j
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Jersey Central Power & Light Company &
MADISON AVENUE AT PUNCH BOWL ROAD
General gyj{ Public Utihties Corporation
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OYSTER CREEK NUCLEAR GENERATING STATION l
FORKED RIVER, NEW JERSEY 08731 l Abnormal Occurrence i Report No. 50-219/74/42 -
Report Date August 2,1974 j Occurrence Date
! July 25, 1974 Identification of Occurrence i
Violation of the Technical S7ecifications, paragraph 2.3.7, main steam line low pressure switches RE23A, B, C, and D were found to trip at pressures Icss than the minimum required value of 860 psig. This event is considered to be an abnormal occurrence as defined in the Technical Specifications, paragraph 1.15A.
Conditions Prior to Occurrence The plant was at steady state power with major parameters as follows:
Power: Reactor,1898 FMt Electric, 653 FMe Flow: Recirculation, 15.8 x 10'+ gpm Feedwater, 7.05 x 106 lb/hr Reactor Pressure: 1020 psig Stack Gas: 13,065 pCi/sec Description of Occurrence On Thursday, July 25,1974, at 1015, while performing a routinc surveillance test on the four main stean line low pressure switches, it was discovered that switches RE23A, B, C, and D t ri[' ped at 849, 854, S59, and 855 psig, respectively. These values are below the minimum required trip point of 860 psig which is derived by adding to the Technical Specification limit of 850 psig, a 10 psig head correction factor.
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. U. U Abnormal Occurrence Report No. 50-219/74/42 Page 2 The "as found" and "as Icft" switch settings were:
"As Found" Settings "As Left" Settings RE23A 849 psig 861 psig RE23B 854 psig 860 psig RE23C 859 psig 862 psig RE23D 855 psig 862 psig Apparent Cause of Occurrence The cause of this occurrence is the recognized probicm of switch repeatability.
Analysis of ' Occurrence As indicated in the bases of the Technical Specifications, "The low pressure isolation of the Main Steam Lines at 850 psig was provided to give protection against fast reactor depressurization and the resultant rapid cooldown of the vessel. Advantage was taken of the scram feature which occurs when the Main Steam Isolation Valves are closed to provide for reactor shutdown so that high power operation at low reactor pressure does not occur, thus providing protection for the fuel cladding integrity safety limit."
The adverse consequences of reactor isolation occurring at reactor pressure approximately 11 psig below the specified minimum value of 860 psig is limited to those effects attendant to a greater than normal reactor cooldown rate. The fuel cladding integrity safety limit only comes into effect for power operation at reactor pressures less than 600 spig or for power operation greater than 354 FMt with less than 10'4 recirculation flow. Therefore, the consequences of a 11 psig lower than normal reactor isolation and scram set point has no threatening effect whatsoever on the fuel cladding integrity.
1he effects of a too rapid cooldown due to the lower isolation pressure are inconsequential since there is less than 2'F difference between the saturation tenperature for 850 psig and 839 psig.
Corrective Action Set point accuracy and tolerance in not only these instruments but in others as well are under investigation by Jersey Central Power 6 Light Company, GPU Service Corporation, and General Electric Company personnel. This investigation was described in detail in Abnormal Occurrence No. 50-219/74/35.
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! ~ ' Abnardal Occurrence Report No. 50-219/74/42 Page 3 [
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Failure Data
~
Manufacturer data pertinent to these switches are as follows:
Meletron Corporation (subsidiary of Barksdale)
Los Angeles, California Pressure Actuated Switch l Model 372 j Catalog No. 372-6SS49A-293 l - Range 20-1400 psig -
} Proof Psi 1750 G Previous abnormal occurrence reports involving these switches are:
i
- 1. Letter to Mr. A. Giambusso from Mr. D. A. Ross, dated December 24, 1973.
- 2. Abnormal Occurrence Report No. 50-219/74/1
] 3. Abnormal Occurrence Report No. 50-219/74/9 1
- 4. Abnormal Occurrence Report No. 50-219/74/10 I
- 5. Abnormal Occurrence Report No. 50-219/74/12
- 6. Abnormal Occurrence Report No. 50-219/74/22 i
- 7. Abnormal Occurrence Report No. 50-219/74/35 a
j 8. Abnormal Occurrence Report No. 50-219/74/37
) 9. Abnormal Occurrence Report No. 50-219/74/41 l
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O ER CPIEK 1RICLEAR.GD?BRATING ST ION'
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Abnozcal occurrence
,- . Report No. 50-210/74/'42 IDDITIFICATION Violation of the Technical Specifications, paragrcph 2.3.7, OP OCCURPRICB: .
. Hain Steam Line Low Pressure Switches RE23A, B, C, and D, found
. to trip at pressures less then the minicus requi'red'value of
, 860 psig. '
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7his event is censidered to be(en abnormal occurrenco 'as de-fined 16 the Technical Specifications, paragraph I'.15A.
. ,, . ',e - 4, ; , (, 2 Steady Sthte Powor.. "
ElDITIC'iS PRIOR -
X '
Routino. Shutdown-10 OCCUarmiCE: llot Stendby >
Operation y Cold shutdcun Load 01 angas During
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Refualing 5:iutdein '
P,outine Poner Operation Routino Startup-
Other (Specify)
_ Operation . . <
Power: Reactor, 1898 l.Ht Bloc. , 653 1.'.le Flow:* Rocirc.,15.8 X 104 gpa.
Food., 7.05 X IOC lb/hr.
Ronctor Prossuro: 1020 psig Stack Gas: ~ 13,065 pCi/ soc . '
DESCRIPTicN OF On Thursday, July 25,1974, at 1015, while performing a routino OCCURRCICE:
survellicnco test on tho four Hain Steam Lino Low Pressuro Switches, it was discovered that switches RB23A, B, C,. and D tripped at 849, 854, 859, and 855 psigf 'roshoctiv[> y. Thos'e values aro below the ninitum required trip point of 860 psig _._
which is' derived by adding to the Technical Specification limit of 850 psig a 10 psig head correction factor.
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beh found" and "as Icft" switdih. tings' wore: '
.- I "As Found" Settings '
- "As.left"' Settings
' i l RB23A 849 psig 861 psig
) RE23B 854 psig , 860 psig RB23C 859 psig ./ 862 psig.
RB23D 855'psig 862 psig APPt. RENT cat 1SH X Design _ Procedure OF 0CCURRENCE: 14anufacture _ Unusual Servico Condition Installation / ~~'
. Ince Envirennental Construction . Co penent Failuro Operator-
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Other (Spacify)
>=,,." The cause .of this occurrence is switch repeatebility, which is a recognized problon. M ANA1.YSIS OF As indicated in the bases of the Technical Spacifications, ,
OCCURFECE: .
,; , . "The low pressure isolation of the }!ain Stena Lines at 850
.w psig was provided to give protection against. fast reactor' depressurizatib and the resultant rcpid cooldown.of the vessel. Advantcge was taken of the scran fodure which occurs when tho }!ain Stoan Isolation valves aro closed to-provide for reactor shutdown so that high pc ter oporation at low reactor pressure does not occur, thus providing protoc-tion for the fuel cladding integrity safety limit."
Tho adverso conscquences of roactor isolation occurring at reactor pressuro approxicatoly 11 psig below the specified minit:um value of 860. psig is limited'to those offects atten-dont to a greator than nomal reactor cooldown rate. The fuel cladding integrity safety limit only comes into offect
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ir for- or operation, at.roactor press os .lo:is then. 600/ psig. .
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,3 A n' e s. e point'hns no threatening offect' whatsoever on~,the fuel" ac, .
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Tho .cffects of a too rapid.ccoldown duo.to tho lower isola-
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tion pressure are incensequential since thoro is'1 css than-W 26p difference between the saturation temperaturo.for 850' psig and 839 psig.
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CORPICTIVE f' Sctpoint' accuracy nnd tolor::nco..in.notienly:theso inctrucents ACTION: ' - '
but in others as well is under. investigation by cc pany. and GPU:personnot with General'Elcetric Co:panye ,
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FAII173 DATA: Manufacturer data pertinent to,these switches are as; follows:
, Heletron Corp. (srbsidiary of Darksdale) .,.
' Ins Angeles, Califomia e ,. ;
,. Pressuro Actuated Switch. y ii.' :
Hodel 372
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Cataloa 0372-6SSOA-293 -
(- f / fE -
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Range 20-1400-13sig -
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Proof. Psi.1750 C. -
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Previous Abnorral Occurrence: Twports invol'ving. i.imse swit'ches
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are:
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- 1. Lotter to Hr. A. Ginrbusso from Mr. D. A. Rens dated Decc:bar 24, 1973. .
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2i Abnorr.210:curronco Report.No. 74-1. , '
- 3. Abnorual Occurrence Reitort No. 74-9..
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Rcport .No. . 5'J-219/74/42 3 'An + Q e: . >< % . M. U" ii,;a. .. , ; lyi.,,. a;: ..g,pogo'4 i 'ci'r ' '
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.' 4. Abnormal Occurrence Roport No. 74-10
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Abnor=al Occifrrence R.e.nort No. 74 , ,' '... ..>.
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- 6., ".Abnomalr0ccurrencei Report No. ' 74-22
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, ,. .,,. ' , ' '8. 'Ab'nor:ala0ccurrenco" Report No. 74- 37.
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'9. - Abnordal Occurrence Report No. 74-41.
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Prepared by: -
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- Dato
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o o qs Jams P'. O'Ecilly To:
Directorate of Regulatory Operations Region 1 ,
631 Park Avenuo King of Pntssia, Pennsylvania 19406 Pan: Jersey Central Powcr G Light.Co:pany-Oyster Cicek Huclear Generating Station.
Docket 850 219 07651 Forked River, New Jorsey ..
Subject:
Abnormal Occurrence Report.No. 50 219/74/42
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'Iho following i~s a prolicinary report being st6nitted-i in. corpli=1ce with the Technical:Specificaticas, paragraph-6.6.2.- 7 ;4
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[Jw T. .Carro11',. Jr. Date
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