ML20090D104

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AO 75-28:on 751015,standby Gas Treatment Sys 1 Inoperable. Caused by Air Solenoid Valve Coil Failure.Defective Solenoid Coil replaced.W/751016
ML20090D104
Person / Time
Site: Oyster Creek
Issue date: 10/16/1975
From: Carroll J, Quintenz T
JERSEY CENTRAL POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20090D096 List:
References
AO-75-28, NUDOCS 8302240060
Download: ML20090D104 (3)


Text

Initial T'elephone m D;ts cf R:p;;rt Date:

Ohcr 16,1975 Occurrence: October 15, 1975 y

Initial Tritten Time of R: port Date:

October 16, 1975 Occurrence:

2325 OYSTER CREEK NUCLEAR GENERATING STATION FORKED RIVER, NEW JERSEY 08731 Abnormal Occurrence Report No. 50-219/75/28 IDENTIFICATION OF OCCURRENCE:

Failure of solenoid for valve V-28-24 (Standby Gas Treatment Orifice Valve) which subsequently rendered Standby Gas Treatment System #1 inoperabic.

This event is considered to be an Abnorrtl Occurrence as defined in the Technical Specifications, para-grrph 1.15D.

CONDITIONS PRIOR TO OCCURRENCE:

X Steady State Power Routine Shutdown Operation llot Standby Load Changes During

~ Cold Shutdown Routine Power Operation Refueling Shutdown Other (Specify)

Routine Startup Operation The major plant parameters at the time of the event were as follows:

Power:

Core 700 FMt Electric 191Mlje Flow:

Recire. 6.1x1g gpm Feed. 2.19x10 lb/hr.

Stack Gas:

3300 pei/sec.

DESCRIPTION OF OCCURRENCE:

On Wednesday, October 15, 1975 at approximately 2325 the " Emergency Exhaust System EF-1-8 Fan Trip" alarm was received in the Control Room. Subsequently it was found that the control circuit fuse for fan EF-1-8 was blown.

APPARENT CAUSE OF OCCUlUGNCE:

Design Procedure Manu facture Unusual Service Condition Installation /

Inc. Environmental Construction X Component Failure Operator Other (Specify) i l

Failure of the air solenoid valve coil for air operated valve V-28-24 is the cause of the abnormal oc6urrence.

8302240060 751024 PDR ADOCK 05000219 S

PDR

Abnsit.a1 Occurrsnce

(

Page 2 R;part No. 50-219/7S/28( )

/

ANALYSIS OF OCCURRENCE:

Since the Standby Gas Treatment System is a redundant system and full required processing capability is availabic through the other system (System #2) the only safety significance of this event is the loss of Standby Gas Treatment System redundancy.

CORRECTIVE ACTION:

Initial corrective action was to replace the. defective solenoid coil with a new one.

FAILURE DATA:

Basic Valve Data:

I Manufacturer:

Skinner Electric Valve Div.

New Britain, Conn.

Valve No.:

V53ADB2100 Voltage:

11S Volts

{

Power:

10 Watts Design Pressure:

100 psig J

PREPARED BY:

f4 5-"m Date: - /0/67

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T. Quir'tenz Asso, ngineer 2

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r TO:

James P.,0'Reilly Directorate of Regulatory Operations Region I

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631 Park Avenue x-King of Prussia, Pennsylvania 19A h[j;..pf, q

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m FROM:

Jersey Central Power G Light Company-Oyster Creek Nuclear Generating Station Docket #50-219 Forked River, New Jersey 08731

SUBJECT:

Abnormal Occurrence Report No. 50-219/75/ 28 The following is a preliminary report being submitted in compliance with the Technical Specifications, paragraph 6.6.2.

Prc1' inary Approval:

G

_ _ the tobhbf w,

J.

T.' Carroll, J Date CC:

Mr. A. Ciambusso Sb W

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