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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML19352A1131974-06-21021 June 1974 Ao:On 740620,electrical Feed to Fast Insertion Pulser Interrupted Due to Power Supply Failure & Protective Fuse Blowing.Cause Unknown.Power Supply & Fuses Replaced ML20083R6631974-02-19019 February 1974 AO 4-2-8:on 740215,during Reactor Coolant Temp Channel Test, Limiting Safety Sys Setting Read Below Required Tech Spec for Channels II & Iv.Cause Under Investigation ML20083R6871974-02-19019 February 1974 AO 4-2-7:on 740201,both Doors of Personnel Air Lock to Containment Bldg Opened at Same Time.Caused by Erroneous Operation of Hand Wheel Door Lock by Offsite Employee Which Triggered Failure of Interlock.Interlock Inspected ML20083R7101974-02-0808 February 1974 AO 4-2-6:on 740125,control Rods Did Not Withdraw from Core to Insertion Limit in Conformance W/Tech Specs.Boron Added to Coolant Sys & Procedures re-emphasized to Personnel ML20083R6961974-02-0606 February 1974 AO 4-2-7:on 740201,both Doors of Containment Air Lock Opened at Same Period of Time.Caused by Offsite Employee Mistakenly Operating Wrong Hand Wheel Opening Inner Air Lock Door ML20083R7291974-02-0505 February 1974 AO 4-2-5:on 740123,coolant Sys Pressure Transient Experienced During Reactor Coolant Start.Caused by Insufficient Amount of Nitrogen Added to Pressurizer. Nitrogen Procedure Changed ML20083R7611974-02-0404 February 1974 AO 4-2-4:on 740121,small Leak Observed at Base of Fillet Weld Attaching Pipe Nozzle to Orifice Flange for Flow Transmitter 946D.Dye Penetrant Insp Indicated Pipe Also Cracked.Faulty Weld Ground Out & Flange Socket Redressed ML20083R8961974-02-0101 February 1974 AO 4-2-3:insp Determined Snubber on Component Cooling Water Return Line & Snubber on Secondary Blowdown Line Defective. Cause Under Investigation.Snubbers Replaced ML20083R7181974-01-31031 January 1974 AO 4-2-6:on 740125,reactor Brought Critical W/Control Rods Below Required Insertion Limit.Cause Under Investigation ML20083R7401974-01-28028 January 1974 AO 4-2-5:on 740123,while Placing Reactor Coolant Pump in Svc,Coolant Sys Pressure Exceeded Tech Spec Limit.Probably Caused by Insufficient Nitrogen Vol ML20084A0141974-01-25025 January 1974 AO 4-2-2:limiting Safety Sys Settings of Channels I & III Discovered Below Tech Spec Requirement.Cause of Setpoint Drift Problem Under Investigation ML20083R7681974-01-21021 January 1974 AO 4-2-4:on 740121,small Leak Observed in Upstream Orifice Flange Connection for Flow Transmitter 946D in Return Line to Reactor Coolant Loop.Dye Penetrant Insp of Weld Will Be Made ML20083R9151974-01-21021 January 1974 AO 4-2-3:insp Completed on 740118 Revealed Accumulator Oil Level Plunger of Two Snubbers Below Criteria Mark.Cause of Failure Will Be Determined During Insp of Disassembled Defective Snubbers.Snubbers Replaced ML20084A0481974-01-18018 January 1974 AO 4-2-1:low Steam Line Pressure Bistables Found Below Required Limit of 600 Psig.Cause of Setpoint Drift Under Investigation.Bistable Recalibr ML20084A0261974-01-15015 January 1974 AO 4-2-2:limiting Safety Sys Settings of Channels I & III Found Below Tech Spec Requirement.Cause of Setpoint Drift Under Investigation ML20084A1411974-01-0808 January 1974 AO 4-2-1:low Steam Line Pressure Bistables Found Below Required Limit of 600 Psig.Cause of Setpoint Drift Under Investigation.Bistable Recalibr ML20084A1941974-01-0404 January 1974 AO 3-2-18:on 731219,analysis of Monthly Pressurizer Pressure Tests Indicated Low Setting for One Bistable.Bistable Recalibr & Sensitivity of Bistable Setpoints Under Investigation ML20084A2321973-12-28028 December 1973 AO 3-2-17:on 731217,one Bistable Setting Exceeded Tech Spec Limit of 92%.Cause of Setpoint Drift Under Investigation. Channel Recalibr ML20084A2071973-12-21021 December 1973 AO 3-2-18:on 731219,analysis of Monthly Pressurizer Pressure Tests Indicated Low Setting for One Bistable.Channel Recalibr & Detailed Rept Re Instrument Drift Underway ML20084A2521973-12-18018 December 1973 AO 3-2-17:on 731217,one Bistable Setting Exceeded Tech Spec Limit of 92% Span.Caused by Instrument Drift.Channel Recalibr & Investigation Initiated for Detailed Analysis of Instrument Capabilities ML20084A2961973-12-0303 December 1973 AO 3-2-16:on 731116,setting for One Bistable Associated W/ Low Pressurizer Pressure Safety Injection Did Not Reach Tech Spec Limit.Cause Not Yet Determined.Channel Recalibr ML20084A3111973-11-19019 November 1973 AO 3-2-16:on 731116,during Cold Shutdown,Setting for One Bistable Did Not Reach Tech Spec Requirement.Channel Recalibr ML20084A3351973-11-12012 November 1973 AO 3-2-15:during 731026 Insp,Leaks Observed at Socket Weld Branch Connections for Vents S-47 & S-51.Caused by Fatigue Failure of Pipe to Socket Welds.Metallurgical Exam Initiated,Vent Valve Assemblies Replaced & RCS Inspected ML20084A3811973-11-0101 November 1973 AO 3-2-14:on 731017,prior to Maint on Pressurizer Safety Valves,Lift Pressure Settings Exceeded Tech Spec Limit. Valves Disassembled,Inspected & Seat Surfaces Repaired ML20084A3481973-10-31031 October 1973 AO 3-2-15:during 731030 Insp,Leaks Observed at Socket Weld Branch Connections for Vents S-47 & S-51.Cause & Corrective Actions Will Be Provided Upon Completion of Exam ML20084A4381973-10-26026 October 1973 AO 3-2-13:on 731011,reactor Tripped Off Line Due to Loss of Generator Field Relay Action.Caused by Gaseous & Particulate Radioactivity in Auxiliary Bldg.Investigation Concluded That No Release to Atmosphere Occurred ML20084A3861973-10-19019 October 1973 AO 3-2-14:on 731017,set Pressure of Safety Valves Exceeded Tech Spec Limit.Valves Will Be Disassembled,Inspected & Seating Surfaces Repaired ML20084A4111973-10-12012 October 1973 AO 3-2-13:on 731011,reactor Tripped Off Line Due to Loss of Generator Field Relay Action.Caused by Gaseous & Particulate Radioactivity in Auxiliary Bldg.Samples Analyzed & Investigation Initiated ML20084A3901973-09-27027 September 1973 AO 3-2-12:on 730913,during Maint of Closure Mechanism of 80-ft Elevation Outer Door of Vapor Container,Inner Door Partially Opened for Short Period.Cause Unknown.Procedures Revised & Supplemented to Prevent Recurrence ML20084A4441973-09-0606 September 1973 AO 3-2-11:on 730822,discovered That Instrument Setting of One of Four Channels of Low Steam Line Pressure Controllers in High Steam Flow Safety Circuit Below Tech Spec Requirements.Caused by Instrument Drift.Channel Recalibr ML20084A4671973-08-23023 August 1973 AO 3-2-11:on 730822,instrument Setting for One Channel of Low Steam Line Pressure Controllers in High Steam Flow Safety Circuit Found Below Tech Spec Requirements.Caused by Instrument Drift.Channel Recalibr & Satisfactorily Tested ML20084A4961973-08-16016 August 1973 AO 3-2-10:on 730802,discovered That Limiting Safety Sys Setting of Channel III of overpower-overtemp delta-T Reactor Trip Circuitry Below Tech Spec Requirements.Caused by Improper Adjustment of Channel.Channel Recalibr ML20084A9691973-07-0303 July 1973 Telecopy AO 3-2-9:on 730702,first Stage Turbine Pressure Setting Discovered Slightly in Excess of Tech Spec Limits. Cause Unknown.Investigation Underway ML20084B0261973-06-11011 June 1973 AO 3-2-7:on 730601,one of Two Motor Actuators for MOV 851A Improperly Moved to Closed Position Following Initiation of Automatic Safety Injection as Result of Spurious Signal from High Steam Line Flow Logic.Caused by Logic Malfunction ML20084A9831973-06-0808 June 1973 Telecopy AO 3-2-8:on 730607,during Performance of Periodic Tests & Calibr Checks Re Reactor Coolant Flow,Flow Trip Settings Discovered Slightly Below Tech Spec Requirements. Cause Unknown.Investigation Underway ML20084B0391973-06-0101 June 1973 Telecopy AO 3-2-7:on 730601,during Power Level Testing, Spurious Safety Injection Signal Initiated Automatically Starting High Head Pumps.One of Two Valves Tying Discharges Driven to Closed Position.Cause Unknown ML20084A9921973-05-29029 May 1973 AO 3-2-6:on 730519,within Minutes After Starting High Head Safety Injection Pump 23,accumulator Level Observed Not Changing & Pump Discharge Pressure Decreased to Existing Rcs.Caused by Personnel Error ML20084B0131973-05-25025 May 1973 AO 3-2-5:on 730518,pressure Transient within RCS Experienced Due to Closure of Certain Air Operated Valves in Reactor Coolant Letdown Sys.Caused by Moisture Freezing in Air Supply Line Refrigerant Dryer of Instrument Air Sys ML20084B0981973-05-14014 May 1973 Ao:On 730511,during Pressurization,Preparatory to Starting Reactor Coolant Pumps for Performance of Hydrostatic Leak Test of Rcs,Leak Apparently Occured in Valve 204B Located in Loop 21 Charging Line.Caused by Defect in Stud Holes ML20084B1101973-05-0404 May 1973 Ao:On 730426,MSIV 22 Failed to Close in Response to Manual Signal by Control Room Operator.Caused by Binding of Linkage Connecting Solenoid Armature to Valve.Solenoids Thoroughly Cleaned of All Lubricant 1974-06-21
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H8501999-10-14014 October 1999 Safety Evaluation Supporting Amend 197 to License DPR-64 ML20206U2551999-02-0909 February 1999 Safety Evaluation Supporting Amend 187 to License DPR-64 ML20236Y1571998-08-0303 August 1998 Part 21 Rept Re ASTM A351,GR. CF8 Matl at Indian Point Being Out of Specifications in Molybdenum & Chromium.Cause & Corrective Actions Are Not Stated ML20236V4281998-07-13013 July 1998 Safety Evaluation of TRs WCAP-14333P & WCAP-14334NP, PRA of RPS & ESFAS Test Times & Completion Times. Repts Acceptable ML20236T5511998-06-24024 June 1998 Consolidated Edison Co of Ny,Indian Point Unit 2,Drill Scenario Number 1998C ML20248B2371998-03-31031 March 1998 Revised Monthly Operating Rept for March 1998 for Indian Point Station Unit 2 ML17264A9381997-07-10010 July 1997 Deficiency Rept Re Potential Safety Hazard Associated w/FM-Alco 251 Engin,High Pressure Fuel tube-catalog: 4401031-2 in Which Dual Failure Mode Exists.Caused by Incorrect Forming Process ML18153A1431997-06-10010 June 1997 Part 21 Rept Re Possible Machining Defect in Certain Stainless Steel Swagelok Tube Fitting Bodies.Facilities Have Been Notified About Possible Problem ML20210E3591997-03-27027 March 1997 Part 21 Rept Re Sorrento Electronics Inc Has Determined Operation & Maint Manual May Not Adequately Define Requirements for Performing Periodic Surveillance of SR Applications.Caused by Hardware Failures.Revised RM-23A ML1005008001997-02-28028 February 1997 Conditional Extension of Rod Misalignment TS for Indian Point 3. ML20115J3981996-07-22022 July 1996 Interim Part 21 Rept Re 3/4 Schedule 80 Pipe Furnished to Consolidated Power Supply.Investigation Revealed Only One Nuclear Customer Involved in Sale of Matl ML20096E5101995-12-31031 December 1995 Resubmitted Rev 13 to QA Program 05000286/LER-1994-010, :on 941007,concluded That at Least Two EDGs Inoperable During June 1992 Surveillance Test of Carbon Dioxide Fire Protection Sys.Caused by Inadequate Procedural Guidance.Surveillance Test Revised1994-11-0707 November 1994
- on 941007,concluded That at Least Two EDGs Inoperable During June 1992 Surveillance Test of Carbon Dioxide Fire Protection Sys.Caused by Inadequate Procedural Guidance.Surveillance Test Revised
ML17059A3611994-07-0606 July 1994 Emergency Action Level Verification & Validation Rept. ML17311A0181994-05-13013 May 1994 New York State EAL Upgrade Project Verification & Validation Rept. ML20029C7801994-03-31031 March 1994 Monthly Operating Rept for Mar 1994 for Indian Point Unit 1. W/940415 Ltr ML20056E5171993-08-31031 August 1993 Technical Review Rept, Tardy Licensee Actions ML20062J2281993-07-23023 July 1993 Consolidated Edison Co of Ny Indian Point Unit 2,Drill Scenario 1993 ML20044B8461993-03-0404 March 1993 Part 21 Rept Re Possible Safety Implications in Motor Operated Valve Evaluation Software Program Re Use of Total Thrust Multiplier.Utils Advised of Problem & Recommended Corrective Action in Encl Customer Bulletin 92-06 ML20118A2681992-12-31031 December 1992 Consolidated Edison Co of Ny Indian Point,Unit 2 Exercise Scenario,1992 ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20096H2301992-05-21021 May 1992 Special Rept:On 920504,south Side Lower Electrical Tunnel Detection Sys 8 Taken Out of Svc for Mod to Reposition Detection Sys Run of Conduit.Detection Sys Declared Operable on 920520 After Mod Completed & Sys Retested ML20079F9181991-05-31031 May 1991 Structural Evaluation of Indian Point,Units 2 & 3 Pressurizer Surge Lines,Considering Effects of Thermal Stratification ML20059E9461990-08-31031 August 1990 Nonproprietary Rev 2 to Indian Point 2 Tube Fatigue Reevaluation ML20059G2011990-07-31031 July 1990 Final Rept on Steam Generator Insp, Repair & Restoration Efforts During 1990 Midcycle Insp ML20058K4121990-06-30030 June 1990 Status Rept,Indian Point Unit 2 Mid-Cycle Steam Generator Insp Presentation to Nrc ML20058K4151990-06-30030 June 1990 Steam Generator Insp,Repair & Restoration Program Presentation to Nrc ML20043A4891990-05-30030 May 1990 Nonproprietary Indian Point Unit 2 Steam Generator Insp, Repair & Restoration Program JPN-90-035, New York Power Authority Annual Rept for 19891989-12-31031 December 1989 New York Power Authority Annual Rept for 1989 ML19332B9371989-11-30030 November 1989 Nonproprietary Info Presented to NRC Re Indian Point Unit 2 Steam Generator Secondary Side Loose Objects. ML19332D6661989-10-31031 October 1989 Nonproprietary Rev 2 to Indian Point Unit 2 Steam Generator Girth Weld/Feedwater Nozzles Rept Spring,1989 Outage. ML20247J8161989-07-31031 July 1989 Safety Evaluation for UHS Temp Increase to 95 F at Indian Point Unit 3 05000286/LER-1989-013-01, :on 890702,contractor Security Guard Was Found Asleep at Duty Post.Caused by Cognitive Personnel Error. Contract Security Officer Involved in Event Was Dismissed. All Security Personnel Reapprised of Responsibilities1989-07-28028 July 1989
- on 890702,contractor Security Guard Was Found Asleep at Duty Post.Caused by Cognitive Personnel Error. Contract Security Officer Involved in Event Was Dismissed. All Security Personnel Reapprised of Responsibilities
ML20248D3631989-06-30030 June 1989 Rev 1,to Indian Point Unit 3 Reactor Vessel Fluence & Ref Temp PTS Evaluations ML20248B3171989-06-30030 June 1989 Rev 1 to Nonproprietary WCAP-12294, Indian Point Unit 2 Steam Generator Girth Weld/Feedwater Nozzles Rept,Spring 1989 Outage ML20247J8071989-05-31031 May 1989 Containment Margin Improvement Analysis for Indian Point Unit 3 ML20247N5331989-05-31031 May 1989 Nonproprietary Indian Point Unit 2 Steam Generator Girth Weld/Feedwater Nozzles Rept Spring,1989 Outage ML20247G5171989-04-30030 April 1989 Monthly Maint Category I Rept Pages from Monthly Operating Rept for Apr 1989 for Indian Point 05000286/LER-1989-007, :on 890321,unauthorized Access Into Protected Area by Former Employee Utilizing Photo Identification Badge of Another Contract Employee Occurred.Caused by Security Guard Error.Security Retrained1989-04-17017 April 1989
- on 890321,unauthorized Access Into Protected Area by Former Employee Utilizing Photo Identification Badge of Another Contract Employee Occurred.Caused by Security Guard Error.Security Retrained
ML20244C3311989-04-10010 April 1989 Safety Evaluation Supporting Amend 137 to License DPR-26 ML20248F4211989-03-31031 March 1989 NSSS Stretch Rating-3,083.4 Mwt Licensing Rept 05000286/LER-1989-001, :on 890204,initiated Safety Injection Via High Steam Flow Safety Injection Logic.Caused by Uneven Refilling of Steam Flow Instrumentation Lines.Safety Injecton Terminated & Plant Cooldown Proceeded1989-03-0303 March 1989
- on 890204,initiated Safety Injection Via High Steam Flow Safety Injection Logic.Caused by Uneven Refilling of Steam Flow Instrumentation Lines.Safety Injecton Terminated & Plant Cooldown Proceeded
ML20235V5931989-03-0202 March 1989 Special Rept:During Cycle 6/7 Refueling Outage Scheduled from Feb-May 1989,openings Will Be Made in Plant Penetration Fire Barriers in Order to Install Various Mods. Fire Watches Posted & Fire Detection Tests Completed 05000286/LER-1989-003-01, :on 890205,security Gate Found Unlocked.Caused by Cognitive Personnel Error.Upgrade of Security Procedure 4, Compensatory Measures to Clearly Define Methods of Establishing,Maintaining & Closing Posts Performed1989-02-23023 February 1989
- on 890205,security Gate Found Unlocked.Caused by Cognitive Personnel Error.Upgrade of Security Procedure 4, Compensatory Measures to Clearly Define Methods of Establishing,Maintaining & Closing Posts Performed
ML20248F3001988-12-31031 December 1988 10CFR50.59(b) Rept of Changes,Tests & Experiments Completed in 1988 ML20246E2711988-12-31031 December 1988 Con Edison 1988 Annual Rept ML20196D3011988-10-31031 October 1988 Reactor Vessel Matl Surveillance Program for Indian Point Unit 2 Analysis of Capsule V ML20155H2541988-09-30030 September 1988 Rev 2 to Indian Point Unit 2 (NRC Bulletin 88-008 Thermal Stresses in Piping Connected to RCS) Indentification of Unisolable Piping & Determination of Insp Locations ML20154M5661988-08-31031 August 1988 Monthly Operating Rept for Aug 1988 for Indian Point Station Unit 2 1999-02-09
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WiHi:m E. C;ldw:H,Jr.
w We Pres 4aat s
.l Consohdated Edison Company of New York. Inc.
4 Irving Place. New York. N Y 10003 Tetephone (212) 400-5181 June 11, 1973 Re:
Indian Point Unit No. 2 AEC Docket No.
Facility Operating 50-247 g HpsN
}/r' l
Mr. John F. O' Leary, Director Directorate of Licensing 6/g',Il g ' v/j rt m
U. S. Atomic Energy Commission ef 78/y0-j fr y,.
Washington, D. C.
20545 4/f'7>jt.g f. ' ?,
Y
Dear Mr. O' Leary:
.\\i Mr es The following report of Abnormal Occurrence No.
3-2-7 is pro-T vided pursuant to the requirements of Section 6.6.1.B of the Technical Specifications to Facility Operating License No.
DPR-26.
On June 1, 1973, at 0202 hours0.00234 days <br />0.0561 hours <br />3.339947e-4 weeks <br />7.6861e-5 months <br />, automatic safety injection was initiated as a result of a spurious signal from the high steam line flow logic.
By design, this signal caused a trip of the reactor whica at the time was operating at essentially acro power for physics testing.
The three high head safety injection pumps started as expected; however, one of two motor actuators (for MOV 851A), which controls the flow path from pump No.
22 to supply either of the injection headers, improperly moved to a closed position.
Mr. A. Fasano of the Region I Regulatory Operat.'ons Office of the U. S. Atomic Energy Commission was notified by telephone on June 1, 1973 of the occurrence.
In addition, a telegram
)
was sent on the same date to confirm the notification.to the Director of the Region I Of Investigation into the cause of the improper operation of MOV 851A revealed that the fault was due to a logic malfunction.
- Normally, MOV 851A would only be required to close if high head pump No.
failed to start.
23 The logic circuitry that furnishes this pro-tection includes a timer component which served to delay actu-ation of the particular MOV until six seconds after the initiation of the safety injection signal.
allow sufficient time for pump No.This timing, however, did not 23 to start in this instance.
Instead, the logic controlling the actuation of MOV 851A sensed that the pump had not yet started and supplied a closing signal.
i To prevent this situation from recurring, the timers in the operating logics for MOV 051A and B were reset for 15 seconds.
It is noteworthy, that on June 6, 1973, following another simi-
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gDRADOCK 05000247
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Mr. John F. O' Leary June 11, 1573 Re:
Indian Point Unit No. 2 AEC Docket No. 50-247 Facility Operating License DPR-26 larly spurious safety injection signal, these logic circuits operated properly (i.e., all three high head pumps started and MOV 851A and B remained in their proper, open position).
There are no significant safety implications related to this occurrence because all three high head pumps did, in fact, start and render both headers capable of supplying safety injection flow.
Furthermore though MOV 851A and.B do, under certain circumstances, operate automatically in the closed direction, they can at any time be reopened manually, should it be necessary.
In light of these reasons, therefore, it is considered that the safety of the facility was not compro-mised.
Our Nuclear Facilities Safety Committee has reviewed the circum-stances of this occurrence and concurs that it does not represent a significant hazards consideration.
Very truly yours
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