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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20083R6631974-02-19019 February 1974 AO 4-2-8:on 740215,during Reactor Coolant Temp Channel Test, Limiting Safety Sys Setting Read Below Required Tech Spec for Channels II & Iv.Cause Under Investigation ML20083R6871974-02-19019 February 1974 AO 4-2-7:on 740201,both Doors of Personnel Air Lock to Containment Bldg Opened at Same Time.Caused by Erroneous Operation of Hand Wheel Door Lock by Offsite Employee Which Triggered Failure of Interlock.Interlock Inspected ML20083R7101974-02-0808 February 1974 AO 4-2-6:on 740125,control Rods Did Not Withdraw from Core to Insertion Limit in Conformance W/Tech Specs.Boron Added to Coolant Sys & Procedures re-emphasized to Personnel ML20083R6961974-02-0606 February 1974 AO 4-2-7:on 740201,both Doors of Containment Air Lock Opened at Same Period of Time.Caused by Offsite Employee Mistakenly Operating Wrong Hand Wheel Opening Inner Air Lock Door ML20083R7291974-02-0505 February 1974 AO 4-2-5:on 740123,coolant Sys Pressure Transient Experienced During Reactor Coolant Start.Caused by Insufficient Amount of Nitrogen Added to Pressurizer. Nitrogen Procedure Changed ML20083R7611974-02-0404 February 1974 AO 4-2-4:on 740121,small Leak Observed at Base of Fillet Weld Attaching Pipe Nozzle to Orifice Flange for Flow Transmitter 946D.Dye Penetrant Insp Indicated Pipe Also Cracked.Faulty Weld Ground Out & Flange Socket Redressed ML20083R8961974-02-0101 February 1974 AO 4-2-3:insp Determined Snubber on Component Cooling Water Return Line & Snubber on Secondary Blowdown Line Defective. Cause Under Investigation.Snubbers Replaced ML20083R7181974-01-31031 January 1974 AO 4-2-6:on 740125,reactor Brought Critical W/Control Rods Below Required Insertion Limit.Cause Under Investigation ML20083R7401974-01-28028 January 1974 AO 4-2-5:on 740123,while Placing Reactor Coolant Pump in Svc,Coolant Sys Pressure Exceeded Tech Spec Limit.Probably Caused by Insufficient Nitrogen Vol ML20084A0141974-01-25025 January 1974 AO 4-2-2:limiting Safety Sys Settings of Channels I & III Discovered Below Tech Spec Requirement.Cause of Setpoint Drift Problem Under Investigation ML20083R7681974-01-21021 January 1974 AO 4-2-4:on 740121,small Leak Observed in Upstream Orifice Flange Connection for Flow Transmitter 946D in Return Line to Reactor Coolant Loop.Dye Penetrant Insp of Weld Will Be Made ML20083R9151974-01-21021 January 1974 AO 4-2-3:insp Completed on 740118 Revealed Accumulator Oil Level Plunger of Two Snubbers Below Criteria Mark.Cause of Failure Will Be Determined During Insp of Disassembled Defective Snubbers.Snubbers Replaced ML20084A0481974-01-18018 January 1974 AO 4-2-1:low Steam Line Pressure Bistables Found Below Required Limit of 600 Psig.Cause of Setpoint Drift Under Investigation.Bistable Recalibr ML20084A0261974-01-15015 January 1974 AO 4-2-2:limiting Safety Sys Settings of Channels I & III Found Below Tech Spec Requirement.Cause of Setpoint Drift Under Investigation ML20084A1411974-01-0808 January 1974 AO 4-2-1:low Steam Line Pressure Bistables Found Below Required Limit of 600 Psig.Cause of Setpoint Drift Under Investigation.Bistable Recalibr ML20084A1941974-01-0404 January 1974 AO 3-2-18:on 731219,analysis of Monthly Pressurizer Pressure Tests Indicated Low Setting for One Bistable.Bistable Recalibr & Sensitivity of Bistable Setpoints Under Investigation ML20084A2321973-12-28028 December 1973 AO 3-2-17:on 731217,one Bistable Setting Exceeded Tech Spec Limit of 92%.Cause of Setpoint Drift Under Investigation. Channel Recalibr ML20084A2071973-12-21021 December 1973 AO 3-2-18:on 731219,analysis of Monthly Pressurizer Pressure Tests Indicated Low Setting for One Bistable.Channel Recalibr & Detailed Rept Re Instrument Drift Underway ML20084A2521973-12-18018 December 1973 AO 3-2-17:on 731217,one Bistable Setting Exceeded Tech Spec Limit of 92% Span.Caused by Instrument Drift.Channel Recalibr & Investigation Initiated for Detailed Analysis of Instrument Capabilities ML20084A2961973-12-0303 December 1973 AO 3-2-16:on 731116,setting for One Bistable Associated W/ Low Pressurizer Pressure Safety Injection Did Not Reach Tech Spec Limit.Cause Not Yet Determined.Channel Recalibr ML20084A3111973-11-19019 November 1973 AO 3-2-16:on 731116,during Cold Shutdown,Setting for One Bistable Did Not Reach Tech Spec Requirement.Channel Recalibr ML20084A3351973-11-12012 November 1973 AO 3-2-15:during 731026 Insp,Leaks Observed at Socket Weld Branch Connections for Vents S-47 & S-51.Caused by Fatigue Failure of Pipe to Socket Welds.Metallurgical Exam Initiated,Vent Valve Assemblies Replaced & RCS Inspected ML20084A3811973-11-0101 November 1973 AO 3-2-14:on 731017,prior to Maint on Pressurizer Safety Valves,Lift Pressure Settings Exceeded Tech Spec Limit. Valves Disassembled,Inspected & Seat Surfaces Repaired ML20084A3481973-10-31031 October 1973 AO 3-2-15:during 731030 Insp,Leaks Observed at Socket Weld Branch Connections for Vents S-47 & S-51.Cause & Corrective Actions Will Be Provided Upon Completion of Exam ML20084A4381973-10-26026 October 1973 AO 3-2-13:on 731011,reactor Tripped Off Line Due to Loss of Generator Field Relay Action.Caused by Gaseous & Particulate Radioactivity in Auxiliary Bldg.Investigation Concluded That No Release to Atmosphere Occurred ML20084A3861973-10-19019 October 1973 AO 3-2-14:on 731017,set Pressure of Safety Valves Exceeded Tech Spec Limit.Valves Will Be Disassembled,Inspected & Seating Surfaces Repaired ML20084A4111973-10-12012 October 1973 AO 3-2-13:on 731011,reactor Tripped Off Line Due to Loss of Generator Field Relay Action.Caused by Gaseous & Particulate Radioactivity in Auxiliary Bldg.Samples Analyzed & Investigation Initiated ML20084A3901973-09-27027 September 1973 AO 3-2-12:on 730913,during Maint of Closure Mechanism of 80-ft Elevation Outer Door of Vapor Container,Inner Door Partially Opened for Short Period.Cause Unknown.Procedures Revised & Supplemented to Prevent Recurrence ML20084A4441973-09-0606 September 1973 AO 3-2-11:on 730822,discovered That Instrument Setting of One of Four Channels of Low Steam Line Pressure Controllers in High Steam Flow Safety Circuit Below Tech Spec Requirements.Caused by Instrument Drift.Channel Recalibr ML20084A4671973-08-23023 August 1973 AO 3-2-11:on 730822,instrument Setting for One Channel of Low Steam Line Pressure Controllers in High Steam Flow Safety Circuit Found Below Tech Spec Requirements.Caused by Instrument Drift.Channel Recalibr & Satisfactorily Tested ML20084A4961973-08-16016 August 1973 AO 3-2-10:on 730802,discovered That Limiting Safety Sys Setting of Channel III of overpower-overtemp delta-T Reactor Trip Circuitry Below Tech Spec Requirements.Caused by Improper Adjustment of Channel.Channel Recalibr ML20084A9691973-07-0303 July 1973 Telecopy AO 3-2-9:on 730702,first Stage Turbine Pressure Setting Discovered Slightly in Excess of Tech Spec Limits. Cause Unknown.Investigation Underway ML20084B0261973-06-11011 June 1973 AO 3-2-7:on 730601,one of Two Motor Actuators for MOV 851A Improperly Moved to Closed Position Following Initiation of Automatic Safety Injection as Result of Spurious Signal from High Steam Line Flow Logic.Caused by Logic Malfunction ML20084A9831973-06-0808 June 1973 Telecopy AO 3-2-8:on 730607,during Performance of Periodic Tests & Calibr Checks Re Reactor Coolant Flow,Flow Trip Settings Discovered Slightly Below Tech Spec Requirements. Cause Unknown.Investigation Underway ML20084B0391973-06-0101 June 1973 Telecopy AO 3-2-7:on 730601,during Power Level Testing, Spurious Safety Injection Signal Initiated Automatically Starting High Head Pumps.One of Two Valves Tying Discharges Driven to Closed Position.Cause Unknown ML20084A9921973-05-29029 May 1973 AO 3-2-6:on 730519,within Minutes After Starting High Head Safety Injection Pump 23,accumulator Level Observed Not Changing & Pump Discharge Pressure Decreased to Existing Rcs.Caused by Personnel Error ML20084B0131973-05-25025 May 1973 AO 3-2-5:on 730518,pressure Transient within RCS Experienced Due to Closure of Certain Air Operated Valves in Reactor Coolant Letdown Sys.Caused by Moisture Freezing in Air Supply Line Refrigerant Dryer of Instrument Air Sys ML20084B0981973-05-14014 May 1973 Ao:On 730511,during Pressurization,Preparatory to Starting Reactor Coolant Pumps for Performance of Hydrostatic Leak Test of Rcs,Leak Apparently Occured in Valve 204B Located in Loop 21 Charging Line.Caused by Defect in Stud Holes ML20084B1101973-05-0404 May 1973 Ao:On 730426,MSIV 22 Failed to Close in Response to Manual Signal by Control Room Operator.Caused by Binding of Linkage Connecting Solenoid Armature to Valve.Solenoids Thoroughly Cleaned of All Lubricant 1974-02-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H8501999-10-14014 October 1999 Safety Evaluation Supporting Amend 197 to License DPR-64 ML20206U2551999-02-0909 February 1999 Safety Evaluation Supporting Amend 187 to License DPR-64 ML20236Y1571998-08-0303 August 1998 Part 21 Rept Re ASTM A351,GR. CF8 Matl at Indian Point Being Out of Specifications in Molybdenum & Chromium.Cause & Corrective Actions Are Not Stated ML20236V4281998-07-13013 July 1998 Safety Evaluation of TRs WCAP-14333P & WCAP-14334NP, PRA of RPS & ESFAS Test Times & Completion Times. Repts Acceptable ML20236T5511998-06-24024 June 1998 Consolidated Edison Co of Ny,Indian Point Unit 2,Drill Scenario Number 1998C ML20248B2371998-03-31031 March 1998 Revised Monthly Operating Rept for March 1998 for Indian Point Station Unit 2 ML17264A9381997-07-10010 July 1997 Deficiency Rept Re Potential Safety Hazard Associated w/FM-Alco 251 Engin,High Pressure Fuel tube-catalog: 4401031-2 in Which Dual Failure Mode Exists.Caused by Incorrect Forming Process ML18153A1431997-06-10010 June 1997 Part 21 Rept Re Possible Machining Defect in Certain Stainless Steel Swagelok Tube Fitting Bodies.Facilities Have Been Notified About Possible Problem ML20210E3591997-03-27027 March 1997 Part 21 Rept Re Sorrento Electronics Inc Has Determined Operation & Maint Manual May Not Adequately Define Requirements for Performing Periodic Surveillance of SR Applications.Caused by Hardware Failures.Revised RM-23A ML1005008001997-02-28028 February 1997 Conditional Extension of Rod Misalignment TS for Indian Point 3. ML20115J3981996-07-22022 July 1996 Interim Part 21 Rept Re 3/4 Schedule 80 Pipe Furnished to Consolidated Power Supply.Investigation Revealed Only One Nuclear Customer Involved in Sale of Matl ML20096E5101995-12-31031 December 1995 Resubmitted Rev 13 to QA Program ML17059A3611994-07-0606 July 1994 Emergency Action Level Verification & Validation Rept. ML17311A0181994-05-13013 May 1994 New York State EAL Upgrade Project Verification & Validation Rept. ML20029C7801994-03-31031 March 1994 Monthly Operating Rept for Mar 1994 for Indian Point Unit 1. W/940415 Ltr ML20056E5171993-08-31031 August 1993 Technical Review Rept, Tardy Licensee Actions ML20062J2281993-07-23023 July 1993 Consolidated Edison Co of Ny Indian Point Unit 2,Drill Scenario 1993 ML20118A2681992-12-31031 December 1992 Consolidated Edison Co of Ny Indian Point,Unit 2 Exercise Scenario,1992 ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20096H2301992-05-21021 May 1992 Special Rept:On 920504,south Side Lower Electrical Tunnel Detection Sys 8 Taken Out of Svc for Mod to Reposition Detection Sys Run of Conduit.Detection Sys Declared Operable on 920520 After Mod Completed & Sys Retested ML20079F9181991-05-31031 May 1991 Structural Evaluation of Indian Point,Units 2 & 3 Pressurizer Surge Lines,Considering Effects of Thermal Stratification ML20059E9461990-08-31031 August 1990 Nonproprietary Rev 2 to Indian Point 2 Tube Fatigue Reevaluation ML20059G2011990-07-31031 July 1990 Final Rept on Steam Generator Insp, Repair & Restoration Efforts During 1990 Midcycle Insp ML20058K4151990-06-30030 June 1990 Steam Generator Insp,Repair & Restoration Program Presentation to Nrc ML20058K4121990-06-30030 June 1990 Status Rept,Indian Point Unit 2 Mid-Cycle Steam Generator Insp Presentation to Nrc ML20043A4891990-05-30030 May 1990 Nonproprietary Indian Point Unit 2 Steam Generator Insp, Repair & Restoration Program. ML20042F1441989-12-31031 December 1989 New York Power Authority Annual Rept for 1989. W/900430 Ltr ML19332B9371989-11-30030 November 1989 Nonproprietary Info Presented to NRC Re Indian Point Unit 2 Steam Generator Secondary Side Loose Objects. ML19332D6661989-10-31031 October 1989 Nonproprietary Rev 2 to Indian Point Unit 2 Steam Generator Girth Weld/Feedwater Nozzles Rept Spring,1989 Outage. ML20247J8161989-07-31031 July 1989 Safety Evaluation for UHS Temp Increase to 95 F at Indian Point Unit 3 ML20248B3171989-06-30030 June 1989 Rev 1 to Nonproprietary WCAP-12294, Indian Point Unit 2 Steam Generator Girth Weld/Feedwater Nozzles Rept,Spring 1989 Outage ML20248D3631989-06-30030 June 1989 Rev 1,to Indian Point Unit 3 Reactor Vessel Fluence & Ref Temp PTS Evaluations ML20247N5331989-05-31031 May 1989 Nonproprietary Indian Point Unit 2 Steam Generator Girth Weld/Feedwater Nozzles Rept Spring,1989 Outage ML20247J8071989-05-31031 May 1989 Containment Margin Improvement Analysis for Indian Point Unit 3 ML20247G5171989-04-30030 April 1989 Monthly Maint Category I Rept Pages from Monthly Operating Rept for Apr 1989 for Indian Point ML20244C3311989-04-10010 April 1989 Safety Evaluation Supporting Amend 137 to License DPR-26 ML20248F4211989-03-31031 March 1989 NSSS Stretch Rating-3,083.4 Mwt Licensing Rept ML20235V5931989-03-0202 March 1989 Special Rept:During Cycle 6/7 Refueling Outage Scheduled from Feb-May 1989,openings Will Be Made in Plant Penetration Fire Barriers in Order to Install Various Mods. Fire Watches Posted & Fire Detection Tests Completed ML20248F3001988-12-31031 December 1988 10CFR50.59(b) Rept of Changes,Tests & Experiments Completed in 1988 ML20246E2711988-12-31031 December 1988 Con Edison 1988 Annual Rept ML20196D3011988-10-31031 October 1988 Reactor Vessel Matl Surveillance Program for Indian Point Unit 2 Analysis of Capsule V ML20155H2541988-09-30030 September 1988 Rev 2 to Indian Point Unit 2 (NRC Bulletin 88-008 Thermal Stresses in Piping Connected to RCS) Indentification of Unisolable Piping & Determination of Insp Locations ML20154M5661988-08-31031 August 1988 Monthly Operating Rept for Aug 1988 for Indian Point Station Unit 2 ML20154M5691988-07-31031 July 1988 Revised Page to Monthly Operating Rept for Jul 1988 for Indian Point Station Unit 2 ML20151N7881988-07-31031 July 1988 Rev 1 to Charpy Toughness & Brittle Transition Temp Characterization of HAZ High Hardness Zone of Indian Point Unit 2 Steam Generator Girth Weld by Gleeble Weld Thermal Cycle Simulation ML20006B4741988-05-31031 May 1988 Nonproprietary Indian Point Unit 2 Evaluation for Tube Vibration Induced Fatigue. ML20151N7821988-05-31031 May 1988 Fracture Sensitivity Study of Girth Weld 6 Repaired Configuration,Indian Point Unit 2 ML20153F9161988-04-28028 April 1988 Changes,Tests & Experiments - 1986 ML20151T4681988-01-31031 January 1988 Experimental & Finite Element Evaluation of Spent Fuel Rack Damping & Stiffness 1999-02-09
[Table view] |
Text
Wilh:m E. C:tdwell, Jr.
vn h+s o., e Conschdated idison Company of New York. Inc.
4 Irvo g Place. ! Jew York, fJ Y 10003 leh'phor o (212) 460-5181 May 29, 1973 Re: Indian Point Unit No. 2 AEC Docket No. 50-247 Facility Opera ' License DPR-26 '9
/ Y D Mr. John F. O' Leary, Director
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Directorate of Licensing 'i
'bIJJ U. S. Atomic Energy Commission 3U4 M 1078A I j
Washington, D. C. 20545 Yx $f
'A nis ' ;r . l Dear Mr. O' Leary The following report of Abnormal Occurrence No. 3-2-6 is provided pursuant to the requirements of Section 6.6.1.D of the Technical Specificati.ons to Facility Operating License No. DPR-26.
On May 19, at 0215 hours0.00249 days <br />0.0597 hours <br />3.554894e-4 weeks <br />8.18075e-5 months <br />, No. 23 Iligh Head Safety Inj ection Pump was started in order to add water to the Safety Injection System Accumulators. Within a few minutes after starting the pump, and after first observing normal pumping characteristics, it was noted that the accumulator level was not changing and that the pumps discharge pressure had decreased to that exist-ing in the Reacter Coolant System. Safety Injection Pump No. 23 was thereupon shut down.
Investigation revealed that a motor-operated valve, (MOV) 1810, in the common suction line from the Refueling Water Storage Tank to the fligh IIcad Pumps was closed. The motor operated valve was opened and a re-start of the pump was attempted with-out success. Apparently, the pump had seized as a result of having been operated without a source of water. Safety Injection Pump No. 23 was then replaced with an identical pump which was tcsted satisfactorily.
Investigation into the cause of the improper valve lineup revealed that several key operations personnel had assumed that MOV 1810 was in its normal position, i.e., open and deenergized as required by the Technical Specifications which gegod oEoSShl E a 3521' * ")
COPY SENT TEGION .
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Mr. John F. O' Leary May 29, 1973 define prerequisite conditions for reactor criticality, and did not obtain verification of the valve status prior to starting the pump. In fact, the valve was shut in order to facilitate maintenance work which had been performed on the system. The occurrence, therefore, was the direct result of standard operating procedures not being followed by the operating personnel prior to starting this high head pump.
Safety implications attendant to the occurrence are non-existent. This evaluation is based on the fact that the Unit No. 2 reactor had not yet been brought to initial criticality, and completion of the required precriticality check-off list would have assured the proper position of MOV 1810 before reactor startup even if pump failure had not occurred. Further-more, the subject check-off list is required to be completed prior to reactor startup at any time, regardless of the reason for shutdown, or its duration. For this reason, we consider it extremely unlikely that the Unit No. 2 reactor would ever be brought to operating status while MOV 1810 is in the closed position. We wish to note that Technical Specification 3.3.A.1 specifically requires that MOV 1810 be in the open, deenergized position while the reactor is in service.
Very truly yours
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01210 FR DC NEWYORK NY 40105-21742P EDT PMS JAMES P OREILLY DIRECTOR A I REWLATORY OPERATIONS REGION 1
, US ATOMIC ENERGY COMM ,
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, NEVARK REPT NEWARK NJ 07102 ,
RE: INDIAN POINT UNIT NO 2 F ACILITY OPERATING LICENSE DPR-26 4 '.
DEAR MR OREILLY O
IN ACCORDANCE WITH THE REQUIREMENTS OF TECHNICAL SPECIFICATION
'. 6.6.1.B 0F FACILITY OPER ATIN LICENSE DPR WE WISH TO INFORM YOU OF AN ABNORMAL OCCURRENCE WHICH WAS IDENTIFIED S
ON MAY 19 1973 AT APPROXIMATELY 0215 HOURS-sr.m uing @
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C WITH THE UNIT NO 2 REACTOR IN A SHUTDCWN CONDITION, AND THE RE ACTOR COOLANT SYSTEM PRESSURE AND TEMPERATURE AT 413 PSIG AMD 225 F , RESPECTIVE LY, N O 22 HICH HEAD SAFETY INJECTION PUMP WAS STARTED INORDER TO ADD VATER TO THE SIS ACCUMULATORS- '
l" WITHIN A FEV MINUTES AFTER STARTING THE PUMP-I*
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AND AFTER FIRST OBSERVING NORMAL PUMPING. CHARACTERISTICS, IT WAS l NOTED THAT ACCUMULATOR LEVEL WAS NO CHANGING, AMD THAT THE PUMP i '
- DISCHARGE PRESSURE HAD DECREASED TO THAT EXISTING IN THE REACTOR COOLANT SYSTEM. S AFETY INECTION PUMP N0'23 VAS THEREUPON SHUT DO,WN-INVESTIGATION REVEALED THAT A MOTOR -OPERATED VALVE , NO 1810,- 1
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IN THE COMMON SUCTION LINE FROM THE FEFUELING EATER STORAGE. ~ ,_
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TANK TO THE SIS PUMPS WAS CLOSED APO }THIS, RESULTED .IN .THE ~ ' , .,
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- o o n THE MOTOR-OPER ATED V ALVE VAS OPENED AND A RE-START OF THE PUMP WAS ATTEMPTED WITHOUT SUCCESS-APPARENTLY, THE PUMP SEIZED AS A RESULT OF HAVING BEEN OPERATED VITHOUT A SOURCE OF VATER. SAFETY INJECTION PUMP NO 23 2AS 4
REPLACED WITH A SPARE AND, AFTER HAVING BEE N S ATISFACTCRILY TESTED,
_, WAS RETURNED TO SERVICE ON'MAY 21, 1973 O
AN INVESTIGATION AS TO THE CAUSE OF NO 23 SAFETY INJECTION PUMP BEING OPERATED WITH AN IMPROPER VALVE LIhEUP IS PRESENTLY BEING CONDUCTED. AT THIS POINT IN TIME, IT APPE ARS O
THAT A MAJOR CONTRIBUTING F ACTOR IS THAT SEVERAL KEY OPER ATIONS PERSONNE L ASSUMED THAT MOV 1810 .WAS IN ITS NORMAL POSITION-1E OPEN AND DEENERGIZED, AND DID NOT ACTUALLY OBTAN VERIFICATION 9,
OF ITS STATUS PRIOR TO STARTING THE PUMP. A REPORT 0N THE sr-w m 3
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RESULTS OF THIS IN'IESTIGATION , AND ANY MEASURES TAKEN TO '
PHEVENT RECURRENCE, WILL BE FROVIDED WITHIN TEN (10) DAYS AS REQUI
' RED BY THE F ACILITY LICENSE.
~-l MR ELDON BRUNNE4 OF YOUR OFFICE WAS NOTIFIED OF THIS INCIDEUT BY MR JOHN MAKEPE ACE , CHIEF ENGINEER, UNIT NO 2, BY TELEPHONE ON MAY 19, 1973 IN ADDITION, AND IN ACCORDANCE WITH l
THE TE CHMICA L SPECIFICATION 6.2, THE CHAIRMAN OF OUR NUCLEAR rACILITITES S AFETY COMMITTEE WA5 NOTIFIED OF THE OCCURRENCE THE SAME DAY J
'4.ILLI AM E CALDWELL JR '" {j 1g - --
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io.....~,,...., ~nus nim ..s Licensce: Consolidated Edison Cor.:pany 3 11 . D. Thornburg, e.:a Docket No.- 50-247 Chic!, FSM B
.Bnor al occurrence: TWX dated 5/21/73 K j r o . .. .;, 4
-.o .ns ni . .a u N 2C:UQ (5)
'E Central Files (1) c.ra '~~ ~ ~ ~ ~The attached report from the subject licensee is Recul atorv St andards :3)
Dir. of I,1 censing (13, i forwarded in accordance with RO Ffanual Chapter 1000, toi...-...,c.o anus ai-.ans The action taken by the licensee is considered
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eart appropriate. Followup will be performed during the next inspection Es anpropriate. Copics of F =O M (*e e me .nd vain a& M AA RS the report have been forwarded to the PDR, Local
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/)L ~~ PDR, NSIC, DTIE and State representatives. The
,E. J. Brunner, RO:I licensee will submit a 10 day written report to PHU8*4 MLL DATE 5/29/73 Licensing.
USE OT.etR SDL FOR ADClisO884 REMAasLS . cro: 107 o - e46-est b
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