ML20052G590

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LER 82-029/03L-0:on 820331,hydraulic Snubber MSH-168 Found Leaking Hydraulic Fluid.Caused by Leaking Shaft Seal.Snubber Shaft Seal Replaced
ML20052G590
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 04/28/1982
From: Charles Brown
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20052G580 List:
References
LER-82-029-03L, LER-82-29-3L, NUDOCS 8205180489
Download: ML20052G590 (2)


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Supplementary Information k Report No.: 50-302/82-029/03L/0 Facility: Crystal River Unit 3 Report Date: April 28, 1982 Occurrence Date: March 31, 1982 Identification of Occurrence:

Hydraulic snubber (MSH-168) was inoperable contrary to Technical Specification 3.7.9.1.

Conditions Prior to Occurrence:

Mode 3 - hot standby (0%).

Description of Occurrence:

At 2340, hydraulic snubber (MSH-168) was found leaking.

The hydraulic snubber was removed and functionally tested.

It was found to be inoperable. Maintenance was initiated and operability was restored at 1430 on 4/1/82.

Designation of Apparent Cause:

The cause of this event is attributed to a leaking shaft seal.

Analysis of Occurrence:

The plant was in not standby at the time of discovery.

There was no effect upon the health or safety of the general public.

Corrective Action:

The hydraulic snubber (MSH-168) shaft seal was replaced, the snubber was functionally tested satisfactorily, and reinstalled. No further corrective action is deemed necessary.

Failure Data:

This is the seventh report under this Specification.

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