ML20049H829

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LER 82-008/03L-0:on 820127,RCS Leak of Less than 0.1 Gallon Per Minute Discovered in Letdown Cooler A.Caused by tube-to-shell Leak in Cooler.Letdown Cooler a Isolated & Will Be Replaced W/Spare Cooler
ML20049H829
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 02/26/1982
From: Charles Brown
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20049H828 List:
References
LER-82-008-03L, LER-82-8-3L, NUDOCS 8203040169
Download: ML20049H829 (2)


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l4j l letdown cooler "A".

This. created an event reportable under T.S. 6.9.1.9.d. Letdown coolerI L l gl3j l"A" is still operable under these conditions and redundancy was provided by letdown E

j o l6 j l cooler "a". Letdown cooler "A" was isolated. There was no effect upon the health or i l

3gjj g safety of the general public. This is the first occurrence of this type and the eleventh l report under this Specification'. ]

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.s 40 41 42 43 47 CAtJ5E CESCRIPTION AND CCRRECTIVE ACTIONS "A"+ I l i l o l lThe cause of this event is attributed to a tube-to-shell leak in letdown cooler I

ijil l Letdown cooler "A" was isolated and will be replaced.

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SUPPLEMENTARY INFORMATION 8

. Report No.: 50-302/82-008/03L-0 Facility: Crystal River Unit 3 f

Report Date: February 26. 1982 Occurrence Date: January 27, 1982

. Identification of Occurrence:

A leak was discovered in letdown cooler "A", creating 1 an event reportable under Technical Specification 6.9.1.9.d.

Conditions Prior to Occurrence:

l Mode 1 power operation (100%).

Description of Occurrence:

At 0740, during normal operation, an increasing activity level was found in the service water system at RML-3. After i various component isolation, a leak was discovered in let-down cooler "A". Letdown cooler "A" was isolated. Redun-1 dancy is provided by letdown cooler "B". ,

i Designation of Apparent Cause:

The cause of this event is attributed to a tube-to-shell leak.

Analysis of Occurrence:  !

I

, There was no effect upon the health or safety of the general

, public and the letdown cooler is still operable and shall be i used only under unusual conditions. There was no unplanned release.

Corrective Action:

I

, Letdown cooler "A" was isolated and will be replaced with a spare cooler.

. Failure Data:

This is the first occurrence concerning the letdown coolers

.and this is the eleventh report under this Specification.

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