ML20040F496

From kanterella
Jump to navigation Jump to search
LER 82-001/03L-0:on 820103,outer Seal on Vacuum Breaker 3-1601-32B Found Leaking in Excess of Tech Spec Limit. Caused by Worn Rubber O-ring Seal.Seal Will Be Replaced & Valve Retested During Present Refueling Outage
ML20040F496
Person / Time
Site: Dresden Constellation icon.png
Issue date: 01/29/1982
From: Rowley E
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20040F495 List:
References
LER-82-001-03L-02, LER-82-1-3L-2, NUDOCS 8202090267
Download: ML20040F496 (2)


Text

M@@NSEE EVEG87 @EPORT ~

CoNTRot stoCx: ' I I I I I j@ <PtE4sE mNr oR TvPE Au. REQumEo iNPonuATiom l o l ta ]9 l I I LucENsEE 7 lDlR l S l i43 l@l 0 l 0 l - l 0ucENsE cooE is l 0 l NvMeER 0 l 0 l 0 l - l 0 l 2s0 l@l 2s 4l license 1l l l TvPE 1 l 140l@l57 CAT l sa l@

CCN'T ,

Ioi1l 7

$uRc5 l L gl , 5 l 0 l 0 l 0 l 2 l 4 l9 Ql 0 l 1l 0 l 3 l 8 l2 @l 0l 1l 2 l 9 l 8 l 2 l@ l 8 60 61 CoCXET NUMSER 68 69 EV ENT QATE 74 7s REPCRT QATE 30 l EVENTDESCRIPTION AND PROSA8tE CONSEQUENCES h lo (2l l During unit refueling outage, while local leak rate testing, it was determined that the l g ; outer seal on vacuum breaker 3-1601-32B was leaking (31.66 SCFH) in excess of Tech. Spec.[

, ,,;4.7.A.2 limit (29.38 SCFH). This event was of minimal significance because the inner  ;

seal did not leak, preventing through leakage. No effect on public health or safety. g Similar occurrence: DVR 12-2-77-96.

l o l 71 I I

10181 l l NE So$E su$ciEE COMPONENT CCof suSCo'QE su E loisl 7 8 I s li l@ W@ La_j@ l v l 4 I t lv Ir lv l@ Lcj@ Lcj @

9 10 11 12 13 18 20

. 19

_ SEQUENTIAL QCCURRENCE REPORT Revision LER EVENT YEAR REPORT No. CooE TYPE No.

@ ,ag/Ro 18121 l-l I010111 l-l 10131 it I l-1 101

_ 21 22 23 24 28 27 28 29 30 31 02 IAEN "AcT/EE oEIEr **Nc7 u wouRs ^5sTTT!E s PEIMS$e. "s'u"E@EE MA PAC RER l33A gl34Z l g l5Z l g l4 Zl@ 37 3 3 l 0 l 0 l 0 40

@l 41 0 l lNl@ 42lNl@ l43N l@ l A l 5 l 8 l 547 l@

de CAUSE DESCRIPTION AND CCRRECTWE ACTIONS

,i,a;jThe cause of this leakage was a worn rubber 0-ring seal. This seal will be replaced and I

,,,,,gthe valve retested during the present refueling outage. No further action is deemed l y

necessary. ,

l i l 31 l I ii 1 1 I I 7 8 9 80

  1. ii*2EuY s  % power oTNEnsTATus @$iEo[EOv' ciscovEnv oEseniPrioN @

l7 t I se l l H l@ l 0 l 0 l 032l@l11 N/A l l B l@l Local leak rate testing l i 44 as 4e so RELpEn Location o,P RELEASE @

l t l s l U @cP RELEASE l Amount Zg N 7AAcTiviTv l @

N/A l l P~.RsoNNEL uPorbhEs l , g 7 l l 0"l'7*g"0 lglT l N/A l

PERSONNEL INJU IEs NUMSER CEscalmCN@

l7 t l a8 l9l 0 l 0 l 011l@l12 N/A _j 8J E QE n PT1o N/A i; l* t l 9*l *l Z l@l l Pusu$7v 8202090267 820129 NRC USE CNLY i PDR ADOCK 05000249 ,

l2}ol 7 8 9 E @cEsenimoN@

l 10 N/A S PDR l 68 69 ll ll llllll l1j{

gg . ; ,

815-942-2920, X-523 NAME OF PREPARER PHONE: {

- . . - _ .- - -_.-_ _ -..,,- . _ . - _ ._ , ._ _ - - . h.

/ -

DEVIATION REPORT t 1f ) Commonwealth E " son DvR No.

,g m- -

- 82 ~ 1

( ,f 7 TA 3

UNIT YEAR NO.

, P ART I l TITLE OF DEVI ATION OCCURRED 1-3-82 0330 Failure of the Seal on the Vacuum Breaker 3-1601-32B nArt vivr SYSTEM AFFECTED 1600 PLANT STATUS AT TIME OF EVENT TESTING Pressure Suppression uoDE Shutdown . PWR(MWT) 0 . LOAD (MAE) 0 g, O DESCRIPTION OF EVENT The outside seal of the vacuum breakers positioning arm was found leaking during the local leak rate test of Vacuum Breaker 3-1601-32B. Leakage was 31.70 SCFH.

Tech Spec limit is 29.38 SCFH.

10 CFR50.72 NRC RED PHONE O 0 NOTIFICATION MADE YES NO EQUIPMENT FAILURE 17886 GYES O NO .0Rx RE0ueST NO. RESPO~SiBtE suPraviSOR M EdeY DArE M4 P ART 2 l 0PERATING ENGINEER'S COMMENTS The unit was in cold shutdown during the discovery of the exCessRe leakage. The seal will be repaired and retested prior to startup from refueling.

O EVENT OF PUBLIC INTEREST C 24= HOUR NRC NOTIFICATION REQ'D TELEPH Mike Jordan (courtesy) 1-5-82 1400 0 TECH. SPEC. VIOLATION REGION III DATE TIME O NON REPORTABLE OCCURRENCE TELEGM/TELECOPY C 14 DAY REPO R TA BL E/ T. S. ,

REGION 118 DATE TIME

@ 30 DAY REPORTABLE /T.S.6.6.B.2.d Ceco CORPORATE NOTIFICATION MADE

] ANNUAL /SPECL REPORT REC'D IF ABOVE NOTIFICATION IS PER 10CFR21 A.I.R. e

] 5. DAY WRITTEN REPORT REQ'D PER 10CFR21 L.E.R. 482-01/03L-0 TELEPH . . a mer M-N UN CECO CORPORATE OFFICER DATE TIME PRELIMINARY REPORT COMPLETED AND REVIEWED Michael Wright 1-5-82 OPERATING ENGINEER , D ATE) / '

INVESTtGATED REPORT & RESOLUTION

  • l' ACCEPTED BY STATION REVIEW ). N , . . .. e _ J d .

j.

U sl.2.9/ 8x . NINO '

RESOLUTION APPROVED AND AUTHORIZED FOR DISTRIBUTION ,

% A, ~ sp

$6 5176 (FORM 15 52.ft 10 61 O WPr #M j il I

?

U