ML20052C424

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LER 82-016/03L-0:on 820329,during Refueling Outage Mechanical Snubber 23 on Reactor Water Cleanup Sys Found Inoperable.Caused by Overloading Snubber During One Time Event.Snubber Replaced W/Hydraulic Snubber HSSA-10
ML20052C424
Person / Time
Site: Dresden Constellation icon.png
Issue date: 04/23/1982
From: Rhee S
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20052C419 List:
References
IEB-81-01, IEB-81-1, LER-82-016-03L, LER-82-16-3L, NUDOCS 8205040786
Download: ML20052C424 (2)


Text

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T 8 89 oATg 74 75 REPoMT omTE 80 EVENT DESCRIPTION AND PROSA8LE CONSECUENCES h l ITTT1 IDuring refueling outage while conducting routine snubber inspection (per I.E. Bulletin I r.usu l81-01 and Tech. Spec. 4.6.I.1) operation of mechanical snubber no. 23 on RWCU system was l

ni,i lfound questionable. The snubber was sent to Wyle Lab for testing. The result from test l

( g ; indicated it was inoperable. Safety significance is minimal because even without the g

,,,,,gsnubber piping stresses were within code allowables. First occurrence of mechanical  ;

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,, ,,,g time event. The snubber was replaced with hydraulic snubber (HSSA-10). Station is eval g uating possible design changes to mitigate the chance of future failures.

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  • On 3-29-82, following receipt of test results from Wyle Laboratory that indicated the snubber was inoperative, this report was reclassified as a 30 day letter.

Further investigation into the cause of failure is in progress.

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  • SEE RECLASSIFICATIdN STA UNIT YEAR No. ,

P /A T 1 l T l TLE O F DEVI ATION CCCURRED Unit 3 Mechanical Snubber Failed Stroke Test 2-15-82 0800 CATE *!vr

$v STEM AFFECTED PL AN T s T A Tus A T TIME cr EVENT TEsTimo 1200 Rx H 9 0 Cleanup MODE Ra f tf ol . PealvAT) 0 . LOAO(MAE) 0 y 3 OESCRIPTION OF EVENT During the stroke test of Pacific Scientific Mechanical Snubber #23 in the Unit 3 drywell, operation of Snubber ( 3-1201-SR-3) found questionable.

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NOTIF ICATION MADE YES NO E QU I PVEN T F A ILUR E 7g716 Ovrs O NO .OR< aE0uEsT NO. REsPons, rte septRvis0R Sang Rhee oATE 2/17/82 PART 2 l 0PER A TI NG ENGINEER * $ COA 9AENTS Consultations with a Pacific Scientific Factory Rep. disclosed that the snubber was operable but not over its full range, ie., it would not go to full compression. It stopped short by about 1 inch. Discussion with EDS indicated that the snubber was not required to function in the full compression range. The snubber is being sent to Wyle Labs for testing, dis-assembly and repair.

EVENT OF PUBL I C INTEREST O 24aHOUR NRC NOTIFICATION REQ'O Tom Tongue (courtesy) 7-23-82 1300 TECH. SPEC. VIOLATION

  • NotifieIof" REGiCN lii DATE TiuE O NON REPORTABLE OCCURRENCE 7ghagpEL g OPY Tom Tongue 3-29-82 1300

] 14 DAY REPO R T A BL E/ T. S. REGION lli DATE TIME

  • 30 DAY REPO R T A BL E / T. .

CECO CORPORATE NOTIFICATION MADE

] ANNU AL/ $PECL REPORT RE Q'D IF ABOVE NOTIFICATION l$ PER 10CFR21 A*I*R* '

5-DAY ARI TTEN REPORT RE0'D PER 10CFR21 L.E.R. 82-16/03L-0 3-29-82 1522 Changed to 30 day ler. 3-29-82 TELEpH F. A. Palmer 2-24-82 1322 (over) CECO CORPORATE OFFICER 1-74-R9 DATE TIME PRELIMINARY REPORT Michael Wright 2-23-82 COMPLE TED AND REVIE*AED cPERAt NG ENGINEER M O A W/ / / ,

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