ML20024B672

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Updated LER 82-053/03X-1:on 821215,while Performing LPCI Valve Operability surveillance,2A LPCI HX Bypass Valve Position Identification Lost.Breaker Trip Setting Found to Be One Setting Too Low.Cause unknown.W/830624 Ltr
ML20024B672
Person / Time
Site: Dresden Constellation icon.png
Issue date: 06/24/1983
From: Ata H, Scott D
COMMONWEALTH EDISON CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
DJS-83-540, LER-82-053-03X, LER-82-53-3X, NUDOCS 8307110189
Download: ML20024B672 (3)


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q Io i:I l Durine normal operation, while performing LPCI valve operability surveillance I io la l I (DOS 1500-1) the 2A LPCI heat exchanger bypass valve (1501-11A) position l l

) 10 la l l indication was lost. Safety significance was minimal since LPCI was operable. I q: .

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af Commonwealth Edison Dresden Nucle:r Power Sttti:n R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 June 24, 1983 DJS Ltr #83-540 James G. Keppler, Regional Administrator Region III U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 Updated Reportable Occurrence Report #82-53/03X-1, Docket #050-237 is being submitted to your office in accordance with Dresden Nuclear Power Station Technical Specification 6.6.B.2. (b), conditions leading to operation in a degraded mode permitted by a limiting condition for operation or plant shutdown required by a limiting condition for operation. This revised report includes the findings following further investigation of the cause of the event. It also revises the corrective action based on these findings and corrects the report dete. The report date 01/03/82 was incorrect. The correct report date is 01/03/83.

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. Scott Station Superintendent Dresden Nuclear Power Station DJS/kjl cc: Director of Inspection & Enforcement Director of Management Information & Program Control U.S. NRC, Document Management Branch File /NRC T

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SUPPLEMENT TO DVR '

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DVR NO.

STA UNIT. YEAR NO.

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2 - 82 - 87 PART I l TITLE OF EVENT OCCURRED . - - -

1 LPCI Heat Exchanger Bypass Valve 1501-11A Breaker Trip 12/15/82 1845 i DATE TIME REASON FOR SUPPLEMENTAL REPORT kl

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. Update cause description and corrective action and correct the report date.

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ACCEPTANCE BY STATION REVIEW

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SUPPLEMENTAL REPORT APPROVED

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