ML20040C583

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LER 81-082/03L-0:on 821221,discovered Containment Isolation Valve CFV-27 Inoperative.On 811223 Five Other Valves Were Inoperative.Caused by Failure of Control Relays.Relay Coils & Plungers Replaced
ML20040C583
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 01/19/1982
From: Charles Brown
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20040C568 List:
References
LER-81-082-03L, LER-81-82-3L, NUDOCS 8201290045
Download: ML20040C583 (2)


Text

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, o ,7 y l At 2045, while performing SP-130, Containment Isolation Valve CFV-27 was discovered to be. inoperative, an event contrary to T.S. 3.6.3.1. CFV-27 was verified closed and main-l

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tenance was initiated, operability was restored at 1445 or, r,ecember 22, 1981. The same g i 10141 l I event occurred on December 23, 1981, at 0922 for Containment Isolation Valves CFV-28 and; 1015] I MSV-148, and at 1340 for Containment Isolation Valves MUV-41, CFV-26, and DW-160. Theseg

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Containment Isolation Valves were closed. Operability was restored at 1130 and 1510 re I This ll o l 7 l l spectively. There was no ef fect upon the health or safety of the steneral public.

is the first occurrence for these valves, and the 38th occurrence reported under this I lo;s; l Specification.

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o .. . SUPPLEMENTARY INFORMATION Report No.: 50-302/81-082/03L-0 Facility: Crystal River Unit 3 Report.Date: January 19, 1982 Occurrence Date: December 21, 1981 Identification of-Occurrence:

Containment isolation valves were inoperable contrary to Technical Specification 3.6.3.1.

Conditions Prior to Occurrence:

Mode 1 power operation (100%),

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Description of Occurrence:

At 2045 while performing Surveillance Procedure SP-130, Containment Isolation Valve CFV-27 was discovered inopera-4 tive. Containment Isolation Valve CFV-27 was verified closed, and-maintenance was initiated. Operability was restored at 1445 on December 22, 1981. The same event occurred on December 23, 1981, for Containment Isolation Valves CFV-28 and MSV-148 at 0922, and Containment Isolation Valves MUV-41; CFV-26; and DWV-160 at 1340. These Containment Isolation Valves were closed and maintenance was initiated. Operability was restored on December 23, 1981, at 1130 and 1510 respectively.

Designation of Apparent Cause:

The cause of this event is attributed to the failure of the control relay for these valves.

Analysis of Occurrence:

There was no effect upon the health or safety of the general public.

Corrective Action:

The relays' coils and plungers were replaced and the functional

] test was satisfactory. These relays are functionally tested under our surveillance program, and they are being repaired under Modification Appreval Record 31-5-20 as repair parts be-come available.

4 Failura Data:

This is the firt occurrence for these valves, and this is ,

the thirty-eighth report under this Specification.

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