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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B4041993-07-28028 July 1993 LER 93-004-00:on 930629,identified Noncompliance W/Srs of TS 4.3.2.1,Table 3.3-3.8.b.Caused by Personnel Error.Retest Sucessfully Performed & Personnel Involved Have Taken Part in Discussion of Importance of Review process.W/930728 Ltr ML20046B1601993-07-28028 July 1993 LER 93-003-00:on 930628,TS Violation Occurred Due to Personnel Error Re non-licensed Operator Performing Evolution W/O Consulting Governing Procedure.Reactor Bldg Purge Supply Valves closed.W/930728 Ltr ML20028H4411990-12-27027 December 1990 LER 90-001-01:on 900209,Part 21 Rept Received from Gilbert Commonwealth Re Possible Loss of One Train of Chilled Water Sys in Event of High Energy Line Break.Conceptual Design Developed to Reduce Heat Load on coils.W/901231 Ltr ML20043F3941990-06-0404 June 1990 LER 90-008-00:on 900505,energizing of Sequencer Initiated Undervoltage Sequence Causing ESF Bus a to Deenergize. Caused by Incorrectly Installed Undervoltage Circuit Agastat Relay.Relay rewired.W/900604 Ltr ML20043B6031990-05-23023 May 1990 LER 90-007-00:on 900423,during Offsite Relay Testing,Oil Circuit Breaker Supplying Bus 3 Tripped Open,Resulting in Loss of Power to ESF Train B & Diesel Generator B Start. Caused by Deficient Procedure.Testing stopped.W/900523 Ltr ML20043A4231990-05-10010 May 1990 LER 90-006-00:on 900412,unplanned ESF Actuation Occurred When Train B Emergency Diesel Generator Automatically Started.Caused by Personnel Error.Feeder Breaker from Battery reopened.W/900510 Ltr ML20042G7691990-05-0808 May 1990 LER 90-005-00:on 900410,steam Generator Tube Eddy Current Exam Yielded Insp Category C-3 Results.Caused by Primary Water Stress Corrosion Cracking in Hot Leg Tubesheet Area. Defective Tubes Plugged or repaired.W/900508 Ltr ML20042G1761990-05-0707 May 1990 LER 90-003-00:on 900406,computer Software Error Caused Nonconservative Radiation Monitor Setpoints.Caused by Software Developer Personnel Error.Setpoints Readjusted & Procedures/Software evaluated.W/900507 Ltr ML20042G1791990-05-0707 May 1990 LER 90-004-00:on 881114,investigation Determined That Two Leads for Cabinet XPN-6002 Had Been Previously Disconnected in 881114 Refueling Outage,Rendering Transmitter LT-1976 Inoperable.Caused by Personnel error.W/900507 Ltr ML20042E1601990-04-11011 April 1990 LER 90-002-00:on 900318,inadvertent ESF Actuation Occurred When Emergency Start Signal Reset.Caused by Procedure Inadequacy When Emergency Start Signal Still Present on Train B.Sys Operating Procedure revised.W/900411 Ltr ML20012C4231990-03-12012 March 1990 LER 90-001-00:on 900209,Gilbert/Commonwealth,Inc Informed Util of Vendor Requirement to Rept Design Deficiency Re Failure of Safety Function,Per Part 21.Util Evaluating What Design Mods Can Be Made to Correct deficiency.W/900312 Ltr ML20006B1231990-01-26026 January 1990 LER 89-022-00:on 890913,discovered That Chilled Water Pump B Returned to Svc W/O Performing Adequate Section XI of ASME Boiler & Pressure Vessel Code Required post-maint Operability Test.Caused by Personnel error.W/900126 Ltr ML19354E1641990-01-17017 January 1990 LER 89-021-00:on 891218,when Operator Directed to Stop Svc Water Pump C by Positioning Handswitch to auto-after Stop Position,Pump Started,Causing ESF Actuation.Caused by Failed Circuit Board.Board replaced.W/900117 Ltr ML20005G1511990-01-0808 January 1990 LER 88-008-01:on 880607,AE (Gilbert Assoc) Notified Util of Design Defect Yielding Potential for Steam Propagation Path Which Could Affect Safe Shutdown Equipment.Caused by Design Error.Also Reportable Per Part 21.W/900108 Ltr ML20005E6941990-01-0202 January 1990 LER 89-019-00:on 891203,as Result of Plant Trip on 891202, Results of Reactor Coolant Sample Not Reviewed & Recognized as Being Out of Tolerance.Caused by Personnel Error.Another Sample of RCS Taken & Analyzed,Per Tech Spec.W/900102 Ltr ML20005E6611990-01-0202 January 1990 LER 89-020-00:on 891202,turbine Controls Failed to Respond to Attempt to Counter Loss of Load & Turbine Manually Tripped.Caused by Relay Contact Failure in Turbine Electrohydraulic Control circuitry.W/900102 Ltr ML20011D4691989-12-20020 December 1989 LER 89-015-02:on 890825,presssurizer Safety Valve Body Inlet Temp Increased to Greater than 450 F & Acoustic Leak Monitor Alarmed,Causing RCS to Depressurize & Reactor Trip. Caused by Loss of Loop Seal.Valve replaced.W/891220 Ltr ML19332F0131989-11-30030 November 1989 LER 89-018-00:on 891027,shift Engineer Observed That Control Room Alarm Did Not Occur When Sample Pumps Stopped.On 891031,radiation Monitors RM-A3 & RM-A4 Declared Inoperable. Caused by Inadequate procedures.W/891130 Ltr ML19327B4921989-10-24024 October 1989 LER 89-017-00:on 890918,responsible Engineer Reviewed Plant Parameters & Concluded That Initial Conditions Required by Surveillance Test Procedure 209.001 Not Satisfied.Caused by Personnel Error & Procedural inadequacy.W/891024 Ltr ML19327B3451989-10-24024 October 1989 LER 89-015-01:on 890825,pressurizer Safety Valve Body Inlet a Temp Increased to Greater than 450 F & Plant Shutdown Initiated.Cause Being Evaluated.Plant Parameters Monitored & Stabilized in Mode 3.W/891024 Ltr ML19325C6501989-10-0707 October 1989 LER 89-016-00:on 890908,shutdown Occurred Due to Inoperable Msiv.Caused by Crushed Conduit That Resulted in Short Circuit of Test Circuit Wiring.Conduit/Test Circuit Wiring repaired.W/891006 Ltr ML20006B2751989-06-27027 June 1989 LER 89-011-01:on 890528,manual Reactor Trip Initiated Following Failure of Pressurizer Safety Valve When Valve Became Unseated,Causing Rapid Depressurization of Rcs.Temp Detectors Installed on Safety valve.W/900123 Ltr ML20024F5131983-08-31031 August 1983 LER 83-091/03L-0:on 830802,while in Mode 1,borated Water Vol of Accumulator a Decreased to 7,354 Gallons.Caused by Valve Leakage in ECCS Check Valve Leakage Detection Sys.Valves Verified in Locked Position.Flange installed.W/830831 Ltr ML20024F4551983-08-31031 August 1983 LER 83-090/03L-0:on 830818,while Increasing Reactor/Turbine Power from 14 to 20%,rod Insertion Limit Violated.Caused by Operating Personnel Failure to Establish Plant Parameters. Emergency Boration initiated.W/830831 Ltr ML20024F2221983-08-31031 August 1983 LER 83-093/03L-0:on 830802,refueling Water Storage Tank Level Transmitter LT-991 Failed High.Caused by Internal Component Failure.Transmitter replaced.W/830831 Ltr ML20024F5901983-08-31031 August 1983 LER 83-092/03L-0:on 830817,east Wall Fire Barrier in Control Bldg Room CB-36-02 Declared Degraded When Unsealed Conduit Found in Newly Installed Juction Box.Caused by Personnel error.W/830831 Ltr ML20024D9111983-08-0101 August 1983 LER 83-075/03L-0:on 830703,emergency Feedwater Valve IFV-3536 to Steam Generator a Tripped Shut on High Flow & Failed to Reset.Caused by Signal Comparator Card Failure. Card replaced.W/830801 Ltr ML20024D8301983-08-0101 August 1983 LER 83-078/03L-0:on 830709,Th Inputs to Subcooling Monitor Channel a Declared Inoperable Due to Low Indications.Caused by Intermittent Opening on Input Connections.Connectors tightened.W/830801 Ltr ML20024D7981983-08-0101 August 1983 LER 83-076/03L-0:on 830707,during Mode 1,pressurizer Power Relief Valve PCV-444B-RC Failed to Stroke Fully.Caused by Low Pressure Nitrogen Reservoir Failing to Charge Up to Pressure.Valves Will Be Inspected & readjusted.W/830801 Ltr ML20024D6981983-07-29029 July 1983 LER 83-074/03L-0:on 830603,during Emergency Diesel Generator a Operability Surveillance Test,Normal 115 Kv Power Supply to Vital Bus Lost & Diesel Generator Output Breaker Tripped Open.Caused by Electrical surge.W/830729 Ltr ML20024D8571983-07-28028 July 1983 LER 83-072/03L-0:on 830701,smoke Detector SMK-CB-3,Zone W-W, Would Not Reset at Integrated Fire & Security Panel.Caused by Failure to Teletype Printed Control Board in Cathode Ray Tube Circuitry.Component replaced.W/830728 Ltr ML20024B6801983-07-0606 July 1983 LER 83-055/03L-0:on 830609 & 10,smoke Detectors in Control Bldg Zone a Failed.Caused by Welding in Area.Fire Watch Patrol Initiated & Affected Detectors & Deluge Resettled. W/830706 Ltr ML20024B7091983-07-0606 July 1983 Updated LER 83-054/03L-1:on 830601,power Failure Occurred, Defeating One Gpm Leakage Alarm for Reactor Bldg Sump.Caused by Loose Power Supply Module Fuse Holder Grounding Power Supply.Module replaced.W/830706 Ltr ML20024B7761983-07-0606 July 1983 LER 83-058/03L-0:on 830607,smoke Detector IXA-4993G Failed to Respond to Simulated Alarm.Caused by Broken Base Assembly in Detector Due to Open Circuit Preventing Alarm Condition. Component replaced.W/830706 Ltr ML20024B9821983-07-0101 July 1983 LER 83-056/03L-0:on 830606,feedwater Flow Transmitter (FT-468) Steam Generator B Failed Low.Caused by Failure of Power Supply Card.Card replaced.W/830701 Ltr ML20024C0371983-07-0101 July 1983 LER 83-057/03L-0:on 830606,nitrogen Low Pressure Alarm on Low Pressure Accumulator for PORV Received in Control Room. Caused by Valve Position Indicator Lights Not Showing Full Actual Position.Limit Switches adjusted.W/830701 Ltr ML20024C2601983-06-30030 June 1983 LER 83-54/03L-0:on 830601 Plant Auxiliary Relay Rack XPN-6034 Balance Declared Inoperable Due to Power Failure. Caused by Loose Fuse Holder on Power Supply Module Grounding Supply.Module replaced.W/830630 Ltr ML20024C1031983-06-22022 June 1983 LER 83-051/03L-0:on 830524,control Room Evacuation Panel Pressurizer Relief Tank Level Indicator ILI-470A Removed from Svc Due to Low Readings.Caused by Instrument Drift. Upgraded Electronic Cards installed.W/830622 Ltr ML20023D4561983-05-13013 May 1983 LER 83-036/03L-0:on 830414,during Performance of Channel Calibr,Pressurizer Safety Valve Position Indication on Valves Failed to Function Properly.Caused by Excessive Current Flow During Contact Closure.Switch Assembly Changed ML20023B6481983-04-29029 April 1983 LER 83-032/03L-0:on 830331,detection Zone Nnn in Control Bldg Failed to Respond to Simulated Smoke Condition During Investigation of Alarm.Alarm Previously Received on 830329. Caused by Short in Smoke Detector.Detector Reinstalled ML20023B4391983-04-29029 April 1983 LER 83-033/03L-0:on 830331,while in Mode 5,source Range Detectors N-31 & N-32 Lost for Approx 5 Minutes.Caused by Maint Personnel Error in Placing Trains of Solid State Protection Sys in Wrong Position.Personnel Cautioned ML20028G0861983-02-0101 February 1983 LER 83-001/01T-0:on 830119,w/plant in Mode 1,three Refueling Water Storage Tank Level Transmitters Failed High. Caused by Frozen Instrument Lines.Transmitters Thawed. Insulated Encls Will Be Installed ML20028F4721983-01-21021 January 1983 LER 82-065/03L-0:on 821222,electrical Power Lost to Train a Radiation Monitoring Sys.During Investigation of Loss of Power,Maint Personnel Accidently Short Circuited Train B. Caused by Blown Power Fuses Due to Personnel Error ML20028E0091983-01-14014 January 1983 LER 82-060/03L-0:on 821215,Surveillance Requirement 4.3.3.6 Discovered Unperformed in Modes 1,2 & 3.Caused by Personnel Error.Procedure Revised ML20028E1831983-01-13013 January 1983 LER 82-059/03L-0:on 821215,w/plant in Mode 1,several Fire Doors Not Verified Closed.Caused by Doors Not Being Included in Auxiliary Operator Logs Rev & Therefore Not Checked.Log Being Revised to Ensure That Doors Checked ML20028E1301983-01-13013 January 1983 Revised LER 82-016/03L-2:on 821216,main Control Board Indicator PI-951 for Reactor Bldg Pressure Failed Low.Caused by Failure of Loop Power Supply Circuit Board When Exposed to Ambient Conditions.Circuit Board Replaced ML20028E0771983-01-13013 January 1983 LER 82-058/03L-0:on 821214,urgent Failure Alarm Due to Loss of Power Occurred During Restoration of Rod Control Sys Upon Completion of Power Operational Testing.Caused by Oxidation Between Fuse & Fuse Block Mating Surfaces ML20028E1241983-01-11011 January 1983 LER 82-057/03L-0:on 821213,turbine Bldg Sump Normal Discharge to Site Settling Ponds Temporarily Bypassed Via Auxiliary Pump & Fire Hose.Caused by Sump Pumps Becoming Clogged W/Debris from Const Repair Work Being Done ML20028D3231983-01-0707 January 1983 LER 82-056/03L-0:on 821209,surveillance Test Procedure, Nis Power Range Heat Balance, Not Performed in Specified Intervals.Caused by Personnel Oversight.Administrative Procedures for Control of Surveillances Revised ML20028D1161983-01-0505 January 1983 LER 82-053/03L-0:on 821206,during Mode 1,spurious High & Low Meter Indications Observed on Main Control Board Indicator FI-494 for Steam Generator C Flow.Caused by Failure of Circuit Board FY-494.Board Replaced 1993-07-28
[Table view] Category:RO)
MONTHYEARML20046B4041993-07-28028 July 1993 LER 93-004-00:on 930629,identified Noncompliance W/Srs of TS 4.3.2.1,Table 3.3-3.8.b.Caused by Personnel Error.Retest Sucessfully Performed & Personnel Involved Have Taken Part in Discussion of Importance of Review process.W/930728 Ltr ML20046B1601993-07-28028 July 1993 LER 93-003-00:on 930628,TS Violation Occurred Due to Personnel Error Re non-licensed Operator Performing Evolution W/O Consulting Governing Procedure.Reactor Bldg Purge Supply Valves closed.W/930728 Ltr ML20028H4411990-12-27027 December 1990 LER 90-001-01:on 900209,Part 21 Rept Received from Gilbert Commonwealth Re Possible Loss of One Train of Chilled Water Sys in Event of High Energy Line Break.Conceptual Design Developed to Reduce Heat Load on coils.W/901231 Ltr ML20043F3941990-06-0404 June 1990 LER 90-008-00:on 900505,energizing of Sequencer Initiated Undervoltage Sequence Causing ESF Bus a to Deenergize. Caused by Incorrectly Installed Undervoltage Circuit Agastat Relay.Relay rewired.W/900604 Ltr ML20043B6031990-05-23023 May 1990 LER 90-007-00:on 900423,during Offsite Relay Testing,Oil Circuit Breaker Supplying Bus 3 Tripped Open,Resulting in Loss of Power to ESF Train B & Diesel Generator B Start. Caused by Deficient Procedure.Testing stopped.W/900523 Ltr ML20043A4231990-05-10010 May 1990 LER 90-006-00:on 900412,unplanned ESF Actuation Occurred When Train B Emergency Diesel Generator Automatically Started.Caused by Personnel Error.Feeder Breaker from Battery reopened.W/900510 Ltr ML20042G7691990-05-0808 May 1990 LER 90-005-00:on 900410,steam Generator Tube Eddy Current Exam Yielded Insp Category C-3 Results.Caused by Primary Water Stress Corrosion Cracking in Hot Leg Tubesheet Area. Defective Tubes Plugged or repaired.W/900508 Ltr ML20042G1761990-05-0707 May 1990 LER 90-003-00:on 900406,computer Software Error Caused Nonconservative Radiation Monitor Setpoints.Caused by Software Developer Personnel Error.Setpoints Readjusted & Procedures/Software evaluated.W/900507 Ltr ML20042G1791990-05-0707 May 1990 LER 90-004-00:on 881114,investigation Determined That Two Leads for Cabinet XPN-6002 Had Been Previously Disconnected in 881114 Refueling Outage,Rendering Transmitter LT-1976 Inoperable.Caused by Personnel error.W/900507 Ltr ML20042E1601990-04-11011 April 1990 LER 90-002-00:on 900318,inadvertent ESF Actuation Occurred When Emergency Start Signal Reset.Caused by Procedure Inadequacy When Emergency Start Signal Still Present on Train B.Sys Operating Procedure revised.W/900411 Ltr ML20012C4231990-03-12012 March 1990 LER 90-001-00:on 900209,Gilbert/Commonwealth,Inc Informed Util of Vendor Requirement to Rept Design Deficiency Re Failure of Safety Function,Per Part 21.Util Evaluating What Design Mods Can Be Made to Correct deficiency.W/900312 Ltr ML20006B1231990-01-26026 January 1990 LER 89-022-00:on 890913,discovered That Chilled Water Pump B Returned to Svc W/O Performing Adequate Section XI of ASME Boiler & Pressure Vessel Code Required post-maint Operability Test.Caused by Personnel error.W/900126 Ltr ML19354E1641990-01-17017 January 1990 LER 89-021-00:on 891218,when Operator Directed to Stop Svc Water Pump C by Positioning Handswitch to auto-after Stop Position,Pump Started,Causing ESF Actuation.Caused by Failed Circuit Board.Board replaced.W/900117 Ltr ML20005G1511990-01-0808 January 1990 LER 88-008-01:on 880607,AE (Gilbert Assoc) Notified Util of Design Defect Yielding Potential for Steam Propagation Path Which Could Affect Safe Shutdown Equipment.Caused by Design Error.Also Reportable Per Part 21.W/900108 Ltr ML20005E6941990-01-0202 January 1990 LER 89-019-00:on 891203,as Result of Plant Trip on 891202, Results of Reactor Coolant Sample Not Reviewed & Recognized as Being Out of Tolerance.Caused by Personnel Error.Another Sample of RCS Taken & Analyzed,Per Tech Spec.W/900102 Ltr ML20005E6611990-01-0202 January 1990 LER 89-020-00:on 891202,turbine Controls Failed to Respond to Attempt to Counter Loss of Load & Turbine Manually Tripped.Caused by Relay Contact Failure in Turbine Electrohydraulic Control circuitry.W/900102 Ltr ML20011D4691989-12-20020 December 1989 LER 89-015-02:on 890825,presssurizer Safety Valve Body Inlet Temp Increased to Greater than 450 F & Acoustic Leak Monitor Alarmed,Causing RCS to Depressurize & Reactor Trip. Caused by Loss of Loop Seal.Valve replaced.W/891220 Ltr ML19332F0131989-11-30030 November 1989 LER 89-018-00:on 891027,shift Engineer Observed That Control Room Alarm Did Not Occur When Sample Pumps Stopped.On 891031,radiation Monitors RM-A3 & RM-A4 Declared Inoperable. Caused by Inadequate procedures.W/891130 Ltr ML19327B4921989-10-24024 October 1989 LER 89-017-00:on 890918,responsible Engineer Reviewed Plant Parameters & Concluded That Initial Conditions Required by Surveillance Test Procedure 209.001 Not Satisfied.Caused by Personnel Error & Procedural inadequacy.W/891024 Ltr ML19327B3451989-10-24024 October 1989 LER 89-015-01:on 890825,pressurizer Safety Valve Body Inlet a Temp Increased to Greater than 450 F & Plant Shutdown Initiated.Cause Being Evaluated.Plant Parameters Monitored & Stabilized in Mode 3.W/891024 Ltr ML19325C6501989-10-0707 October 1989 LER 89-016-00:on 890908,shutdown Occurred Due to Inoperable Msiv.Caused by Crushed Conduit That Resulted in Short Circuit of Test Circuit Wiring.Conduit/Test Circuit Wiring repaired.W/891006 Ltr ML20006B2751989-06-27027 June 1989 LER 89-011-01:on 890528,manual Reactor Trip Initiated Following Failure of Pressurizer Safety Valve When Valve Became Unseated,Causing Rapid Depressurization of Rcs.Temp Detectors Installed on Safety valve.W/900123 Ltr ML20024F5131983-08-31031 August 1983 LER 83-091/03L-0:on 830802,while in Mode 1,borated Water Vol of Accumulator a Decreased to 7,354 Gallons.Caused by Valve Leakage in ECCS Check Valve Leakage Detection Sys.Valves Verified in Locked Position.Flange installed.W/830831 Ltr ML20024F4551983-08-31031 August 1983 LER 83-090/03L-0:on 830818,while Increasing Reactor/Turbine Power from 14 to 20%,rod Insertion Limit Violated.Caused by Operating Personnel Failure to Establish Plant Parameters. Emergency Boration initiated.W/830831 Ltr ML20024F2221983-08-31031 August 1983 LER 83-093/03L-0:on 830802,refueling Water Storage Tank Level Transmitter LT-991 Failed High.Caused by Internal Component Failure.Transmitter replaced.W/830831 Ltr ML20024F5901983-08-31031 August 1983 LER 83-092/03L-0:on 830817,east Wall Fire Barrier in Control Bldg Room CB-36-02 Declared Degraded When Unsealed Conduit Found in Newly Installed Juction Box.Caused by Personnel error.W/830831 Ltr ML20024D9111983-08-0101 August 1983 LER 83-075/03L-0:on 830703,emergency Feedwater Valve IFV-3536 to Steam Generator a Tripped Shut on High Flow & Failed to Reset.Caused by Signal Comparator Card Failure. Card replaced.W/830801 Ltr ML20024D8301983-08-0101 August 1983 LER 83-078/03L-0:on 830709,Th Inputs to Subcooling Monitor Channel a Declared Inoperable Due to Low Indications.Caused by Intermittent Opening on Input Connections.Connectors tightened.W/830801 Ltr ML20024D7981983-08-0101 August 1983 LER 83-076/03L-0:on 830707,during Mode 1,pressurizer Power Relief Valve PCV-444B-RC Failed to Stroke Fully.Caused by Low Pressure Nitrogen Reservoir Failing to Charge Up to Pressure.Valves Will Be Inspected & readjusted.W/830801 Ltr ML20024D6981983-07-29029 July 1983 LER 83-074/03L-0:on 830603,during Emergency Diesel Generator a Operability Surveillance Test,Normal 115 Kv Power Supply to Vital Bus Lost & Diesel Generator Output Breaker Tripped Open.Caused by Electrical surge.W/830729 Ltr ML20024D8571983-07-28028 July 1983 LER 83-072/03L-0:on 830701,smoke Detector SMK-CB-3,Zone W-W, Would Not Reset at Integrated Fire & Security Panel.Caused by Failure to Teletype Printed Control Board in Cathode Ray Tube Circuitry.Component replaced.W/830728 Ltr ML20024B6801983-07-0606 July 1983 LER 83-055/03L-0:on 830609 & 10,smoke Detectors in Control Bldg Zone a Failed.Caused by Welding in Area.Fire Watch Patrol Initiated & Affected Detectors & Deluge Resettled. W/830706 Ltr ML20024B7091983-07-0606 July 1983 Updated LER 83-054/03L-1:on 830601,power Failure Occurred, Defeating One Gpm Leakage Alarm for Reactor Bldg Sump.Caused by Loose Power Supply Module Fuse Holder Grounding Power Supply.Module replaced.W/830706 Ltr ML20024B7761983-07-0606 July 1983 LER 83-058/03L-0:on 830607,smoke Detector IXA-4993G Failed to Respond to Simulated Alarm.Caused by Broken Base Assembly in Detector Due to Open Circuit Preventing Alarm Condition. Component replaced.W/830706 Ltr ML20024B9821983-07-0101 July 1983 LER 83-056/03L-0:on 830606,feedwater Flow Transmitter (FT-468) Steam Generator B Failed Low.Caused by Failure of Power Supply Card.Card replaced.W/830701 Ltr ML20024C0371983-07-0101 July 1983 LER 83-057/03L-0:on 830606,nitrogen Low Pressure Alarm on Low Pressure Accumulator for PORV Received in Control Room. Caused by Valve Position Indicator Lights Not Showing Full Actual Position.Limit Switches adjusted.W/830701 Ltr ML20024C2601983-06-30030 June 1983 LER 83-54/03L-0:on 830601 Plant Auxiliary Relay Rack XPN-6034 Balance Declared Inoperable Due to Power Failure. Caused by Loose Fuse Holder on Power Supply Module Grounding Supply.Module replaced.W/830630 Ltr ML20024C1031983-06-22022 June 1983 LER 83-051/03L-0:on 830524,control Room Evacuation Panel Pressurizer Relief Tank Level Indicator ILI-470A Removed from Svc Due to Low Readings.Caused by Instrument Drift. Upgraded Electronic Cards installed.W/830622 Ltr ML20023D4561983-05-13013 May 1983 LER 83-036/03L-0:on 830414,during Performance of Channel Calibr,Pressurizer Safety Valve Position Indication on Valves Failed to Function Properly.Caused by Excessive Current Flow During Contact Closure.Switch Assembly Changed ML20023B6481983-04-29029 April 1983 LER 83-032/03L-0:on 830331,detection Zone Nnn in Control Bldg Failed to Respond to Simulated Smoke Condition During Investigation of Alarm.Alarm Previously Received on 830329. Caused by Short in Smoke Detector.Detector Reinstalled ML20023B4391983-04-29029 April 1983 LER 83-033/03L-0:on 830331,while in Mode 5,source Range Detectors N-31 & N-32 Lost for Approx 5 Minutes.Caused by Maint Personnel Error in Placing Trains of Solid State Protection Sys in Wrong Position.Personnel Cautioned ML20028G0861983-02-0101 February 1983 LER 83-001/01T-0:on 830119,w/plant in Mode 1,three Refueling Water Storage Tank Level Transmitters Failed High. Caused by Frozen Instrument Lines.Transmitters Thawed. Insulated Encls Will Be Installed ML20028F4721983-01-21021 January 1983 LER 82-065/03L-0:on 821222,electrical Power Lost to Train a Radiation Monitoring Sys.During Investigation of Loss of Power,Maint Personnel Accidently Short Circuited Train B. Caused by Blown Power Fuses Due to Personnel Error ML20028E0091983-01-14014 January 1983 LER 82-060/03L-0:on 821215,Surveillance Requirement 4.3.3.6 Discovered Unperformed in Modes 1,2 & 3.Caused by Personnel Error.Procedure Revised ML20028E1831983-01-13013 January 1983 LER 82-059/03L-0:on 821215,w/plant in Mode 1,several Fire Doors Not Verified Closed.Caused by Doors Not Being Included in Auxiliary Operator Logs Rev & Therefore Not Checked.Log Being Revised to Ensure That Doors Checked ML20028E1301983-01-13013 January 1983 Revised LER 82-016/03L-2:on 821216,main Control Board Indicator PI-951 for Reactor Bldg Pressure Failed Low.Caused by Failure of Loop Power Supply Circuit Board When Exposed to Ambient Conditions.Circuit Board Replaced ML20028E0771983-01-13013 January 1983 LER 82-058/03L-0:on 821214,urgent Failure Alarm Due to Loss of Power Occurred During Restoration of Rod Control Sys Upon Completion of Power Operational Testing.Caused by Oxidation Between Fuse & Fuse Block Mating Surfaces ML20028E1241983-01-11011 January 1983 LER 82-057/03L-0:on 821213,turbine Bldg Sump Normal Discharge to Site Settling Ponds Temporarily Bypassed Via Auxiliary Pump & Fire Hose.Caused by Sump Pumps Becoming Clogged W/Debris from Const Repair Work Being Done ML20028D3231983-01-0707 January 1983 LER 82-056/03L-0:on 821209,surveillance Test Procedure, Nis Power Range Heat Balance, Not Performed in Specified Intervals.Caused by Personnel Oversight.Administrative Procedures for Control of Surveillances Revised ML20028D1161983-01-0505 January 1983 LER 82-053/03L-0:on 821206,during Mode 1,spurious High & Low Meter Indications Observed on Main Control Board Indicator FI-494 for Steam Generator C Flow.Caused by Failure of Circuit Board FY-494.Board Replaced 1993-07-28
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D6401999-10-31031 October 1999 Rev 2 to WCAP-15102, VC Summer Unit 1 Heatup & Cooldown Limit Curves for Normal Operation RC-99-0202, Monthly Operating Rept for Sept 1999 for VC Summer Nuclear Station.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for VC Summer Nuclear Station.With ML20216J4191999-09-24024 September 1999 Part 21 Rept Re 990806 Abb K-Line Breaker Defect After Repair.Vendor Notified of Shunt Trip Wiring Problem & Agreed to Modify Procedure for Refurbishment of Breakers RC-99-0180, Special Rept on 990807,electric Driven Fire Pump XPP0134A Was Declared Inoperable.Caused by Pump Discharge Relief Valve Failing to Open as Normally Expected.Two Temporary Fire Pumps Were Installed to Provide Backup Suppression1999-09-0808 September 1999 Special Rept on 990807,electric Driven Fire Pump XPP0134A Was Declared Inoperable.Caused by Pump Discharge Relief Valve Failing to Open as Normally Expected.Two Temporary Fire Pumps Were Installed to Provide Backup Suppression RC-99-0183, Monthly Operating Rept for Aug 1999 for Virgil C Summer Nuclear Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Virgil C Summer Nuclear Station,Unit 1.With ML20211K6161999-08-31031 August 1999 Rev 2 to VC Summer Nuclear Station,Colr for Cycle 12, Dtd Aug 1999 RC-99-0168, Special Rept:On 990804,electric Driven Fire Pump XPP0134A & Diesel Driven Fire Pump XPP0134B,were Removed from Svc to Allow for Plant Mod.Fire Pumps Were Returned to Operable Condition on 990818,after Mod Was Completed1999-08-19019 August 1999 Special Rept:On 990804,electric Driven Fire Pump XPP0134A & Diesel Driven Fire Pump XPP0134B,were Removed from Svc to Allow for Plant Mod.Fire Pumps Were Returned to Operable Condition on 990818,after Mod Was Completed ML20210M7071999-07-31031 July 1999 Rev 1 to VC Summer Nuclear Station COLR for Cycle 12 ML20211C2201999-07-31031 July 1999 Rev 1 to WCAP-15102, VC Summer Unit 1 Heatup & Cooldown Limit Curves for Normal Operation RC-99-0163, Monthly Operating Rept for July 1999 for VC Summer Nuclear Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0137, Monthly Operating Rept for June 1999 for VC Summer Nuclear Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0122, Monthly Operating Rept for May 1999 for VC Summer Nuclear Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for VC Summer Nuclear Station.With ML20206H2971999-05-0505 May 1999 Part 21 Rept Re Common Mode Failure for magne-blast Breakers.Vc Summer Nuclear Station Utilizes These Breakers in Many Applications,Including 7.2-kV EDG Electrical Buses RC-99-0103, Monthly Operating Rept for Apr 1999 for VC Summer Nuclear Station.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for VC Summer Nuclear Station.With ML20206K2421999-04-30030 April 1999 Rev 0 to COLR for Cycle 12 for Summer Nuclear Station RC-99-0087, Part 21 Interim Rept (SSH 99-0001) Re 990218 Failure of Circuit Breaker Located in Cubicle 14 of XSW1DB to Close During Surveillance Testing.Caused by Positive Interlock Angle Was Incorrect.Breaker Was Returned to GE Factory1999-04-15015 April 1999 Part 21 Interim Rept (SSH 99-0001) Re 990218 Failure of Circuit Breaker Located in Cubicle 14 of XSW1DB to Close During Surveillance Testing.Caused by Positive Interlock Angle Was Incorrect.Breaker Was Returned to GE Factory RC-99-0083, Monthly Operating Rept for Mar 1999 for VC Summer Nuclear Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0063, Special Rept:On 990302 & 16,meteorological Site Number One 10 Meter Temp Element Was Declared Inoperable.Caused by Erratic Operation.Cabling & 10 Meter Electrical Connectors Were Replaced1999-03-26026 March 1999 Special Rept:On 990302 & 16,meteorological Site Number One 10 Meter Temp Element Was Declared Inoperable.Caused by Erratic Operation.Cabling & 10 Meter Electrical Connectors Were Replaced ML20196K5421999-03-22022 March 1999 Rev 2 to VC Summer Nuclear Station,Training Simulator Quadrennial Certification Rept,1996-99, Books 1 & 2. Page 2 of 2 Section 2.4.4 (Rev 2) of Incoming Submittal Were Not Included RC-99-0055, Special Rept:On 990302,Meteorological Site Number One 10 Meter Temp Element (RTD) Was Declared Inoperable Due to Erratic Operation.Cause of Original RTD Failure Is Unknown. Equipment Was Declared Operable on 9903121999-03-16016 March 1999 Special Rept:On 990302,Meteorological Site Number One 10 Meter Temp Element (RTD) Was Declared Inoperable Due to Erratic Operation.Cause of Original RTD Failure Is Unknown. Equipment Was Declared Operable on 990312 RC-99-0050, Monthly Operating Rept for Feb 1999 for VC Summer Nuclear Station,Units 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for VC Summer Nuclear Station,Units 1.With ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML20203F4511999-02-12012 February 1999 SER Finding Licensee Adequately Addressed GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves, for Virgil C Summer Nuclear Station ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML20206R5241998-12-31031 December 1998 Santee Cooper 1998 Annual Rept RC-99-0052, Vsns 1998 Annual Operating Rept. with1998-12-31031 December 1998 Vsns 1998 Annual Operating Rept. with RC-99-0004, Monthly Operating Rept for Dec 1998 for VC Summer Nuclear Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for VC Summer Nuclear Station,Unit 1.With ML20206R5191998-12-31031 December 1998 Scana Corp 1998 Annual Rept ML20198F4241998-12-18018 December 1998 Safety Evaluation Granting Relief Request for Approval to Repair ASME Code Class 3 Service Water Piping Flaws in Accordance with GL 90-05 for VC Summer Nuclear Station RC-98-0223, Special Rept 98-001:on 981130,steam Line High Range Gamma Monitor (RMG-19C) Was Declared Inoperable Due to Indeterminate Alarm.Caused by Failures in Detector & Meter Reset Circuitry.Established Preplanned Alternate Method1998-12-16016 December 1998 Special Rept 98-001:on 981130,steam Line High Range Gamma Monitor (RMG-19C) Was Declared Inoperable Due to Indeterminate Alarm.Caused by Failures in Detector & Meter Reset Circuitry.Established Preplanned Alternate Method RC-98-0222, Monthly Operating Rept for Nov 1998 for VC Summer Nuclear Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for VC Summer Nuclear Station,Unit 1.With ML20155G4551998-11-0404 November 1998 Safety Evaluation Accepting Licensee Proposed Alternative to Use Code Case N-416-1 with Licensee Proposed Addl Exams RC-98-0208, Monthly Operating Rept for Oct 1998 for VC Summer Nuclear Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for VC Summer Nuclear Station,Unit 1.With ML20207J5701998-10-31031 October 1998 Non-proprietary Rev 1 to WCAP-14955, Probabilistic & Economic Evaluation of Rv Closure Head Penetration Integrity for VC Summer Nuclear Plant ML20154Q9571998-10-21021 October 1998 SER Accepting Request Seeking Approval to Use Alternative Rules of ASME Code Case N-498-1 for Class 1,2 or 3 Sys ML20154K7901998-09-30030 September 1998 Non-proprietary Rev 0 to WCAP-15101, Analysis of Capsule W from Sceg VC Summer Unit 1 Rv Radiation Surveillance Program RC-98-0184, Monthly Operating Rept for Sept 1998 for VC Summer Nuclear Station.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for VC Summer Nuclear Station.With ML20154K8041998-09-30030 September 1998 Non-proprietary Rev 0 to WCAP-15103, Evaluation of Pressurized Thermal Shock for VC Summer Unit 1 RC-98-0166, Monthly Operating Rept for Aug 1998 for VC Summer Nuclear Station,Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for VC Summer Nuclear Station,Unit 1.With ML20237A7181998-08-13013 August 1998 SER Accepting Util Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves RC-98-0153, Monthly Operating Rept for July 1998 for VC Summer Nuclear Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for VC Summer Nuclear Station,Unit 1 RC-98-0131, Monthly Operating Rept for June 1998 for VC Summer Nuclear Station1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for VC Summer Nuclear Station ML20248J0191998-06-0404 June 1998 Safety Evaluation Accepting Licensee Inservice Testing Program Interim Pump Relief Request Per 10CFR50.55a(a)(3) (II) RC-98-0113, Monthly Operating Rept for May 1998 for VC Summer Nuclear Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for VC Summer Nuclear Station,Unit 1 RC-98-0100, Monthly Operating Rept for Apr 1998 for VC Summer Nuclear Station,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for VC Summer Nuclear Station,Unit 1 ML20217G7411998-04-22022 April 1998 Rev 1 to VC Summer Nuclear Station COLR for Cycle 11 RC-98-0076, Final Part 21 Rept Re a DG EG-B for Vsns,As Followup to .Power Control Svcs of Engine Sys,Inc Provided Response on 980318.Evaluation Concludes That Failure of EG-B Is one-time non-repeatable Failure1998-04-17017 April 1998 Final Part 21 Rept Re a DG EG-B for Vsns,As Followup to .Power Control Svcs of Engine Sys,Inc Provided Response on 980318.Evaluation Concludes That Failure of EG-B Is one-time non-repeatable Failure RC-98-0084, Monthly Operating Rept for Mar 1998 for Virgil C Summer Nuclear Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Virgil C Summer Nuclear Station,Unit 1 ML20212H1421998-03-0202 March 1998 Interim Part 21 Rept SSH 98-002 Re EG-B Unit That Was Sent to Power Control Svcs for Determination of Instability & Refurbishment of a Dg.Cause of Speed Oscillations Unknown. Completed Hot Bore Checks on Power Case 1999-09-08
[Table view] |
Text
. .
10CFR50.73 .
Bo th Carolina Electr'ic & G:s C::mpany ' tile S.iredt ern .
Jenkinsville, SC 29065 Nuclear Operatior.s :
(803) 3454 040 1
SCE&G_
mn-January 23, 1990 1
l J
Document Control Desk 4
U. S. Nuclear Regulatory Commission Washington,-DC 20555:
.i
Subject:
Virgil C. Summer Nuclear. Station Docket No. 50/395 -l Operating License No. NPF-12 i LER 89-011.. Revision 1 I
Gentlemen:
Attached is Revision 1 to Licensee Event Report No.89-011 for the Virgil C.
4 Summer _ Nuclear Station. Specifically, the revision identifies the cause of.
the May 28, 1989, pressurizer safety valve'misoperation and supplements the j
" Additional Corrective Action " section. Additionally, the pressure at which the manual reactor trip was initiated has been revised to 2000 psig.- This i number is in better agreement with engineering analysis and-the Technical l Support Center event printout than the 1900 psig previously reported. This .
report is submitted pursuant to the requirements of 10CFR50.73(a)(2)(iv).- '
Should there be any questions, please call us at your convenience'.
Very truly yours,
- 0. S. Bradham i
EWR/0SB: led Attachment 1
c: D. A. Nauman/0. W.'Dixon, Jr./T. C. Nichols, Jr.
E. C. Roberts !
R. V. Tanner J. C. Snelson i S. D. Ebneter R. L. Prevatte J. J. Hayes, Jr. l J. B. Knotts, Jr. ;
General Managers INP0 Records Center i C. A. Price ANI Library !
G. J. Taylor Marsh & McLennan J. R. Proper 4
.NSRC !
R. B. Clary NPCF ;
F. H. Zander RTS (ON0 0 0047)
T. L. Matlosz Files (818.05&818.07)
K. E. Nodland i, 9002010227 890627 /
PDR .ADOCK 05000395 /
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At 0252 hours0.00292 days <br />0.07 hours <br />4.166667e-4 weeks <br />9.5886e-5 months <br />, May 28, 1989, a manual Reactor Trip was initiated following the l failure of a Pressurizer Safety Valve. The valve (XVS-8010-C) became-unseated i causing a rapid depressurization of the Reactor Coolant System. The manual Reactor i
Trip was initiated at approximately 2000 psig and the safety valve reseated prior to reaching the Safety Injection setpoint of 1850 psig. The Reactor Coolant System
! pressure recovered and was stabilized at approximately 2000 psig.
l During the transient, a condenser steam dump valve failed to close and an operator had to fail the air to the valve for closure.
Pressurizer Safety Valves (XVS-8010-B and C) were replaced and the reactor was restarted at 0049 hours5.671296e-4 days <br />0.0136 hours <br />8.101852e-5 weeks <br />1.86445e-5 months <br />, June 11, 1989. Note: Valve 8010 B was replaced due to minor leakage past the seat.
The Licensee has determined that the reason for the misoperation of XVS-8010-C is that the expected margin between normal operating pressure and the pressurizer safety valve relief setpoint pressure was reduced to zero. It was also determined that the most prevalent factor in this margin reduction was a loop seal discharge.
This discharge resulted in a reduced valve setpoint because of the steam medium imposed on the valve. As such, the Licensee is focusing the corrective action plan on the elimination of loop seal capability for the pressurizer safety valves.
NOTE: A subsequent report (LER 89-015 dated September 20,1989) documents a similar i event involving pressurizer safety valve XVS-8010-A. The Licensee has determined l that a loss of loop seal was the cause for the misoperation of XVS-8010-A. ;
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"' LICENSEE EVENT REPORT (LER) TEXT CONTINUATION ' urnoveo oue so mo-otm r
i l. EXPIRES 8/31/85 - ,
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Plant Identification i
Westinghouse - Pressurized Water Reactor i E_auipment Identification J Pressurizer Safety Valve - EIIS - None U
.~ Identification of Event A Pressurizer Safety Valve became unseated causing a rapid decrease in Reactor Coolant :
System (RCS) pressure. A manual Reactor Trip was initiated at approximately 2000 psig. [.
Event Date ,
May 28, 1989 .
Discovery Date May 28. 1989 -'
' a~
Report Date June 27, 1989 This report was initiated by Off-Normal Occurrence Report 89-47.
Condition Prior to Event .
Mode 1 - 100 percent .:
1 Description of Event .
I a At 0252 hours0.00292 days <br />0.07 hours <br />4.166667e-4 weeks <br />9.5886e-5 months <br />, May 28, 1989, a manual Reactor Trip was initiated following the failure-of a Pressurizer Safety Valve. The valve (XVS-8010-C) became unseated causing a. rapid depressurization of the Reactor Coolant System (RCS). The. manual Reactor Trip was initiated at approximately 2000 psig and the safety valve reseated prior to reaching the l Safety Injection setpoint of 1850 psig. The RCS recovered and was stabilized at-approximately 2000 psig.
1 Indication of a possible safety valve problem had bleh noted at 0024 and 0034-hours upon intermittent actuation of the " Pressurizer Safety Valve Open" annunciator on the Main Control Board and changes in the Safety Valve tailpipe temperature. Instrument'and Controls (I&C) personnel were requested to install multichannel recorders'on the Pressurizer Safety Acoustic Monitor to aid the operators in determining the extent of the-
' problem. During the installation of the recorder, two additional events occurred at 0133 and 0206 hours0.00238 days <br />0.0572 hours <br />3.406085e-4 weeks <br />7.8383e-5 months <br />. At 0252 hours0.00292 days <br />0.07 hours <br />4.166667e-4 weeks <br />9.5886e-5 months <br />, the fifth event occurred which resulted in the depressurization of the RCS and the initiation of a manual Reactor Trip. The previous- L g,oa u..
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATIO'N' urnoveo ous No. sno-om -:
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l l events had produced no corresponding decrease in RCS. pressure or increase .in the.
Pressurizer Relief Tank pressure and temperature.
During the transient, a condenser steam dump valve failed to close and an operator had to fail the air to the valve for closure.
Cause of Event The Licensee has performed a Root Cause Analysis and h'as determined that the basic reason $
for the misoperation.of XVS-8010-C is that the expected margin of 250 psi (10 percent) . ')
between the normal operating pressure and the safety valve'setpoint pressure was reduced .
to zero. The Licensee has divided the contributing factors'in this margin elimination -
into two categories:. 1) valve-specific factors, and 2) non valve-specific-factors. Of-the 10 percent margin reduction, the analysis has quantified approximately 6.6 percent, and has identified factors which-contribute-to the remaining margin but:cannot be-quantified.
The valve-specific contributing factors are those factors which have'been tested and analyzed for XVS-8010-C. These valve-specific contributing factors, which make up approximately 6 percent of the eliminated 10 percent margin, are: 1)iloop seal discharge:
and 2) cetpoint variations. While the analysis was performed specifically for XVS-8014 C, the factors identified are expected to be generic to allisafety valves .but the numerical results are unlikely to be duplicated . !
The first valve-specific factor contributing to the margin reduction is^the loss of loop.
seal on the valve. A test was performed on XVS-8010-C to measure the pressure-where' 1
' valve leakage exceeded condensation into the loop seal. This test, which is a sicw pressure increase ramp test performed on the test stand, is important because it specifies the pressure at which loop seal discharge occurs. For XVS-8010-C. this. -
pressure was found to be 118 psig (4.7 percent)~below the setpoint pressure of 2485 psig.
The second valve-specific factor identified by the Licensee is the setpoint variation which XVS-80.10-C exhibits when the valve body temperature is increased. A setpoint .
reduction of 22 psig (1 percent) was measured during a steam soak test using the Setpoint I Verification Device (SPVD) with the loop seal in place. This setpoint change is due to valve stem motion as the valve body temperature increases. This setpoint reduction may.
not be evident when the valve setpoint is established under ambient operating conditions. ,
The two valve-specific factors identified above combine for a reduction in setpoint of. '
5.7 percent. This agrees with other testing on XVS-8010-C which shows the valve has a l lower lift pressure (in excess of 150 psig) when exposed to steam rather than water.
Once the loop seal is lost, the valve is exposed to steam. Since a steam medium on the valve results in a setpoint change of approximately 6 percent (150 psig), this value is i used in quantifying the setpoint change. The 4.7. percent from loop seal. discharge and the 1.0 percent from setpoint variations are included in the 6 percent.
The second category in which the Licensee has divided the contributing factors for the !
valve misoperation is the "non-valve specific category." This category contains the- '
. factors which depend on components other than the pressurizer safety valves. These unc ,ono m.
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factors, therefore, will impact all of the' pressurizer safety. valves.' In this category, 5 only one factor. instrumentation calibration, can be quantified as- to its effects on the
'setpoint reduction.
Instrumentation calibration checks of "As Found" conditions after-the event and subsequent evaluations have resulted in a best estimate that the pressure I.
control instrumentation may have been a maximum of 0.6 percent low in indication / control. a
'A 0.6 percent loss of setpoint margin.is therefore attributed'to pressure-instrumentation l calibration.
i Other non-valve specific contributing factors identified as having a potential for- J resulting in a setpoint margin loss but which could not be quantified are:. .
- 1. Loss of clearance between the tailpipe flange.and' mounting plate.- :
By analyzing the deformation of the irregular flame cut surfaces of the mounting. t plate where the plate contacted the tailpipe flange, stress levels in the valve body ~
were calculated to be 4,925 psi. Although this stress level is cnly approximately: g 18 percent of allowable, some disc-to-nozzle misalignment probably.resulted.' The non-symmetrical pattern of degradation of the disc and nozzle seating surfaces-identified during valve disassembly also confirm that.some misalignment was present.
- 2. Elevated temperature of the valve body'due to the insulation configuration results in body expansion that can reduce the setpoint by-moving the spring compressed disc '
in a direction to reduce spring compression of the tiisc-to-nozzle.
- 3. A correlation of indicated tailpipe temperature' variations with pumping-the-Pressurizer Relief Tank has been made. Recent close_ monitoring indicates a direct ;
correlation between pumping the tank and minor temperature excursions on the i tailpipe of a leaking safety valve. The exact cause of this pattern has not been:
- identified, and at this time it appears to be only a. minor contributor.
- 4. Hydrogen concentrations in the pressurizer vapor space.-
2 Preliminary information indicates concentrations of H2 which may-alter the thermal characteristics of the valve. Hydrogen concentrations in the vapor space impact the condensation rate into the loop seal, the leak tightness of the valve (H2 vs. ,
water / steam), the control response of the pressurizer heater / spray-controls,,and.
other chemical degradation effects.
1 To summarize, the reason for the misoperation of XVS-8010-C is that the expected margin between normal operating pressure and the safety valve relief setpointt pressure was reduced to zero. Several contributing factors in the margin elimination for XVS-8010-C have been identified. Approximately 6 percent of the 10 percent reduction-has been-attributed to the difference in setpoint between steam and water. This difference occurred on XVS-8010-C when the loop seal was discharged. Because loop seal discharge '
and the resulting impact of the water /tteam difference is the most impacting of the quantifiable factors, the Licensee is focusing the corrective action plan on the loop seal system. The factors identified are expected to be applicable to all. safety valves. '
The numerical results are expected to be slightly different for each valve. -
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--_.3, CC' Form 366A - U.S. NUCLE .2 KEIULAtoRY CoMMl881oh i
- " 2 y LICENSEE EVENT REPORT (LER) TEXT CONTINUATION . " u,Rovfo ous Noso-osu : !
,7y , EXPIRE 3. 8/31 C6 FACILITY NAMt,14 DOCKET NUMSER (2) LER NUMeER (6) PAGE (31 VIAR :
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Analysis of Event i
The safety significance of this event was moderate in that if the safety valve had'not' seated following the Reactor Trip, the Safety Injection System would.have been-challenged.
^
Immediate Corrective Action -
Immediate corrective action taken was the initiation of the manual: Reactor Trip. The ;
operators monitored RCS pressure and were prepared :to initiate Safety Injection. Plant "
parameters were monitored and the plant was stabilized in Mode 3 at'a reduced; operating-pressure of approximately 2000 psig. The plant was subsequently taken to Mode 5 for. l removal and replacement of the: safety valves XVS 8010 B and C.-
Additional Corrective Action:
The Licensee has temporarily installed temperature detectors on the pressurizer' safety valves to' facilitate monitoring of the valve body inlet temperatures. The Licensee-has-
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issued a special instruction detailing the monitoring of;these temperatures and the initiation of a plant shutdown should a valve body. inlet temperature reach 450*F. j NOTE: As the result of a subsequent pressurizer safety valve misoperation on August 25 s i 1989, noted in LER 89-015, the Licensee has revised.the shutdown temperature'to 390*F.-
L Additionally, at 350*F action will be taken to develop a plan for plant shutdown.taking into account, among other variables, the rate of change of temperature. 'The Licensee's.
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management and the Resident NRC Inspector-will be notified when the safetyLvalve temperature reaches 350*F.
The Licensee intends to: 1) modify the pressurizer safety valves' internals for. steam application, and 2) eliminate loop seal capability on the pressurizer safety' valves.
.This modification is scheduled for the fifth refueling outage'(currently scheduled to I begin March 23,1990) and is contingent upon receiving the required materials in time for implementation.
Safety valves XVS-8010-B and C were replaced with spare valves. Valve'8010-B was.
replaced because it was experiencing minor leakage past the seat. Setpoints'for all three safeties were verified in Mode 3 prior to restart. <
Troubleshooting identified that the ralfunction of the condenser steam-dump valve was attributed to the current / pressure convertor being out of adjustment. Adjustments were made and the valve satisfactorily tested and declared operable.
Prior Event None -
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