05000395/LER-1982-060-03, /03L-0:on 821215,Surveillance Requirement 4.3.3.6 Discovered Unperformed in Modes 1,2 & 3.Caused by Personnel Error.Procedure Revised

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/03L-0:on 821215,Surveillance Requirement 4.3.3.6 Discovered Unperformed in Modes 1,2 & 3.Caused by Personnel Error.Procedure Revised
ML20028E009
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 01/14/1983
From: Mckinney C
SOUTH CAROLINA ELECTRIC & GAS CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20028D990 List:
References
LER-82-060-03L, LER-82-60-3L, NUDOCS 8301200240
Download: ML20028E009 (1)


LER-1982-060, /03L-0:on 821215,Surveillance Requirement 4.3.3.6 Discovered Unperformed in Modes 1,2 & 3.Caused by Personnel Error.Procedure Revised
Event date:
Report date:
3951982060R03 - NRC Website

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REP Rro.rE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l 0 l2 j lOn December 15. 1982, with the Plant in Mode 1, the Licensee discovered that l

l o l3 l l Surveillance Requirement 4.3.3.6, (Table 4.3-7, Item 22) had not been performed l

l o l 4 l lwhile in P aes 1, 2 and 3.

There were no adverse consequences from this event.

l l o is l lUsing Sut eillance Test Procedure (STP) 135.001, the operability of the l

[ o l6 l l Acoustic Monitor, which would have activated an alarm in the Control Room if l

i l o l 7 l l flow had been detected downstream of the safety vnives, has been verified.

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS O27 l1l0llThe cause of the occurrence was due to personnel error.

Surveillance Test l

l 1 l 1 l l Procedure (STP) 135.001 was revised on December 21, 1982 to include the l

l i l 2 l l verification of Pressurizer Safety Valve Position Indication on a monthly basis.

l l 1 l 3 l l A satisfactorv nerformance of this orocedure was subsecuently completed. The l

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% POW E R OTHER ST ATUS l.COVERY DISCOVERY DESCRIPTION l115llB l @ l 0 ] 4l8 l@l N/A l

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NAME OF PREPARER A[

PHONE:

(8 3) 345-5209 y/J. McKinney

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