ML20028E009

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LER 82-060/03L-0:on 821215,Surveillance Requirement 4.3.3.6 Discovered Unperformed in Modes 1,2 & 3.Caused by Personnel Error.Procedure Revised
ML20028E009
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 01/14/1983
From: Mckinney C
SOUTH CAROLINA ELECTRIC & GAS CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20028D990 List:
References
LER-82-060-03L, LER-82-60-3L, NUDOCS 8301200240
Download: ML20028E009 (1)


Text

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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l 0 l2 j lOn December 15. 1982, with the Plant in Mode 1, the Licensee discovered that l l o l3 l l Surveillance Requirement 4.3.3.6, (Table 4.3-7, Item 22) had not been performed l l o l 4 l lwhile in P aes 1, 2 and 3. There were no adverse consequences from this event. l l o is l lUsing Sut eillance Test Procedure (STP) 135.001, the operability of the l

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS O27 l1l0llThe cause of the occurrence was due to personnel error. Surveillance Test l l 1 l 1 l l Procedure (STP) 135.001 was revised on December 21, 1982 to include the l l i l 2 l l verification of Pressurizer Safety Valve Position Indication on a monthly basis. l l 1 l 3 l l A satisfactorv nerformance of this orocedure was subsecuently completed. The l lildllticoncon n1nnn nn naditinnn1 nerinn in rnonrdn en thin nvent. =

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