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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B4041993-07-28028 July 1993 LER 93-004-00:on 930629,identified Noncompliance W/Srs of TS 4.3.2.1,Table 3.3-3.8.b.Caused by Personnel Error.Retest Sucessfully Performed & Personnel Involved Have Taken Part in Discussion of Importance of Review process.W/930728 Ltr ML20046B1601993-07-28028 July 1993 LER 93-003-00:on 930628,TS Violation Occurred Due to Personnel Error Re non-licensed Operator Performing Evolution W/O Consulting Governing Procedure.Reactor Bldg Purge Supply Valves closed.W/930728 Ltr ML20028H4411990-12-27027 December 1990 LER 90-001-01:on 900209,Part 21 Rept Received from Gilbert Commonwealth Re Possible Loss of One Train of Chilled Water Sys in Event of High Energy Line Break.Conceptual Design Developed to Reduce Heat Load on coils.W/901231 Ltr ML20043F3941990-06-0404 June 1990 LER 90-008-00:on 900505,energizing of Sequencer Initiated Undervoltage Sequence Causing ESF Bus a to Deenergize. Caused by Incorrectly Installed Undervoltage Circuit Agastat Relay.Relay rewired.W/900604 Ltr ML20043B6031990-05-23023 May 1990 LER 90-007-00:on 900423,during Offsite Relay Testing,Oil Circuit Breaker Supplying Bus 3 Tripped Open,Resulting in Loss of Power to ESF Train B & Diesel Generator B Start. Caused by Deficient Procedure.Testing stopped.W/900523 Ltr ML20043A4231990-05-10010 May 1990 LER 90-006-00:on 900412,unplanned ESF Actuation Occurred When Train B Emergency Diesel Generator Automatically Started.Caused by Personnel Error.Feeder Breaker from Battery reopened.W/900510 Ltr ML20042G7691990-05-0808 May 1990 LER 90-005-00:on 900410,steam Generator Tube Eddy Current Exam Yielded Insp Category C-3 Results.Caused by Primary Water Stress Corrosion Cracking in Hot Leg Tubesheet Area. Defective Tubes Plugged or repaired.W/900508 Ltr ML20042G1761990-05-0707 May 1990 LER 90-003-00:on 900406,computer Software Error Caused Nonconservative Radiation Monitor Setpoints.Caused by Software Developer Personnel Error.Setpoints Readjusted & Procedures/Software evaluated.W/900507 Ltr ML20042G1791990-05-0707 May 1990 LER 90-004-00:on 881114,investigation Determined That Two Leads for Cabinet XPN-6002 Had Been Previously Disconnected in 881114 Refueling Outage,Rendering Transmitter LT-1976 Inoperable.Caused by Personnel error.W/900507 Ltr ML20042E1601990-04-11011 April 1990 LER 90-002-00:on 900318,inadvertent ESF Actuation Occurred When Emergency Start Signal Reset.Caused by Procedure Inadequacy When Emergency Start Signal Still Present on Train B.Sys Operating Procedure revised.W/900411 Ltr ML20012C4231990-03-12012 March 1990 LER 90-001-00:on 900209,Gilbert/Commonwealth,Inc Informed Util of Vendor Requirement to Rept Design Deficiency Re Failure of Safety Function,Per Part 21.Util Evaluating What Design Mods Can Be Made to Correct deficiency.W/900312 Ltr ML20006B1231990-01-26026 January 1990 LER 89-022-00:on 890913,discovered That Chilled Water Pump B Returned to Svc W/O Performing Adequate Section XI of ASME Boiler & Pressure Vessel Code Required post-maint Operability Test.Caused by Personnel error.W/900126 Ltr ML19354E1641990-01-17017 January 1990 LER 89-021-00:on 891218,when Operator Directed to Stop Svc Water Pump C by Positioning Handswitch to auto-after Stop Position,Pump Started,Causing ESF Actuation.Caused by Failed Circuit Board.Board replaced.W/900117 Ltr ML20005G1511990-01-0808 January 1990 LER 88-008-01:on 880607,AE (Gilbert Assoc) Notified Util of Design Defect Yielding Potential for Steam Propagation Path Which Could Affect Safe Shutdown Equipment.Caused by Design Error.Also Reportable Per Part 21.W/900108 Ltr ML20005E6941990-01-0202 January 1990 LER 89-019-00:on 891203,as Result of Plant Trip on 891202, Results of Reactor Coolant Sample Not Reviewed & Recognized as Being Out of Tolerance.Caused by Personnel Error.Another Sample of RCS Taken & Analyzed,Per Tech Spec.W/900102 Ltr ML20005E6611990-01-0202 January 1990 LER 89-020-00:on 891202,turbine Controls Failed to Respond to Attempt to Counter Loss of Load & Turbine Manually Tripped.Caused by Relay Contact Failure in Turbine Electrohydraulic Control circuitry.W/900102 Ltr ML20011D4691989-12-20020 December 1989 LER 89-015-02:on 890825,presssurizer Safety Valve Body Inlet Temp Increased to Greater than 450 F & Acoustic Leak Monitor Alarmed,Causing RCS to Depressurize & Reactor Trip. Caused by Loss of Loop Seal.Valve replaced.W/891220 Ltr ML19332F0131989-11-30030 November 1989 LER 89-018-00:on 891027,shift Engineer Observed That Control Room Alarm Did Not Occur When Sample Pumps Stopped.On 891031,radiation Monitors RM-A3 & RM-A4 Declared Inoperable. Caused by Inadequate procedures.W/891130 Ltr ML19327B4921989-10-24024 October 1989 LER 89-017-00:on 890918,responsible Engineer Reviewed Plant Parameters & Concluded That Initial Conditions Required by Surveillance Test Procedure 209.001 Not Satisfied.Caused by Personnel Error & Procedural inadequacy.W/891024 Ltr ML19327B3451989-10-24024 October 1989 LER 89-015-01:on 890825,pressurizer Safety Valve Body Inlet a Temp Increased to Greater than 450 F & Plant Shutdown Initiated.Cause Being Evaluated.Plant Parameters Monitored & Stabilized in Mode 3.W/891024 Ltr ML19325C6501989-10-0707 October 1989 LER 89-016-00:on 890908,shutdown Occurred Due to Inoperable Msiv.Caused by Crushed Conduit That Resulted in Short Circuit of Test Circuit Wiring.Conduit/Test Circuit Wiring repaired.W/891006 Ltr ML20006B2751989-06-27027 June 1989 LER 89-011-01:on 890528,manual Reactor Trip Initiated Following Failure of Pressurizer Safety Valve When Valve Became Unseated,Causing Rapid Depressurization of Rcs.Temp Detectors Installed on Safety valve.W/900123 Ltr ML20024F5131983-08-31031 August 1983 LER 83-091/03L-0:on 830802,while in Mode 1,borated Water Vol of Accumulator a Decreased to 7,354 Gallons.Caused by Valve Leakage in ECCS Check Valve Leakage Detection Sys.Valves Verified in Locked Position.Flange installed.W/830831 Ltr ML20024F4551983-08-31031 August 1983 LER 83-090/03L-0:on 830818,while Increasing Reactor/Turbine Power from 14 to 20%,rod Insertion Limit Violated.Caused by Operating Personnel Failure to Establish Plant Parameters. Emergency Boration initiated.W/830831 Ltr ML20024F2221983-08-31031 August 1983 LER 83-093/03L-0:on 830802,refueling Water Storage Tank Level Transmitter LT-991 Failed High.Caused by Internal Component Failure.Transmitter replaced.W/830831 Ltr ML20024F5901983-08-31031 August 1983 LER 83-092/03L-0:on 830817,east Wall Fire Barrier in Control Bldg Room CB-36-02 Declared Degraded When Unsealed Conduit Found in Newly Installed Juction Box.Caused by Personnel error.W/830831 Ltr ML20024D9111983-08-0101 August 1983 LER 83-075/03L-0:on 830703,emergency Feedwater Valve IFV-3536 to Steam Generator a Tripped Shut on High Flow & Failed to Reset.Caused by Signal Comparator Card Failure. Card replaced.W/830801 Ltr ML20024D8301983-08-0101 August 1983 LER 83-078/03L-0:on 830709,Th Inputs to Subcooling Monitor Channel a Declared Inoperable Due to Low Indications.Caused by Intermittent Opening on Input Connections.Connectors tightened.W/830801 Ltr ML20024D7981983-08-0101 August 1983 LER 83-076/03L-0:on 830707,during Mode 1,pressurizer Power Relief Valve PCV-444B-RC Failed to Stroke Fully.Caused by Low Pressure Nitrogen Reservoir Failing to Charge Up to Pressure.Valves Will Be Inspected & readjusted.W/830801 Ltr ML20024D6981983-07-29029 July 1983 LER 83-074/03L-0:on 830603,during Emergency Diesel Generator a Operability Surveillance Test,Normal 115 Kv Power Supply to Vital Bus Lost & Diesel Generator Output Breaker Tripped Open.Caused by Electrical surge.W/830729 Ltr ML20024D8571983-07-28028 July 1983 LER 83-072/03L-0:on 830701,smoke Detector SMK-CB-3,Zone W-W, Would Not Reset at Integrated Fire & Security Panel.Caused by Failure to Teletype Printed Control Board in Cathode Ray Tube Circuitry.Component replaced.W/830728 Ltr ML20024B6801983-07-0606 July 1983 LER 83-055/03L-0:on 830609 & 10,smoke Detectors in Control Bldg Zone a Failed.Caused by Welding in Area.Fire Watch Patrol Initiated & Affected Detectors & Deluge Resettled. W/830706 Ltr ML20024B7091983-07-0606 July 1983 Updated LER 83-054/03L-1:on 830601,power Failure Occurred, Defeating One Gpm Leakage Alarm for Reactor Bldg Sump.Caused by Loose Power Supply Module Fuse Holder Grounding Power Supply.Module replaced.W/830706 Ltr ML20024B7761983-07-0606 July 1983 LER 83-058/03L-0:on 830607,smoke Detector IXA-4993G Failed to Respond to Simulated Alarm.Caused by Broken Base Assembly in Detector Due to Open Circuit Preventing Alarm Condition. Component replaced.W/830706 Ltr ML20024B9821983-07-0101 July 1983 LER 83-056/03L-0:on 830606,feedwater Flow Transmitter (FT-468) Steam Generator B Failed Low.Caused by Failure of Power Supply Card.Card replaced.W/830701 Ltr ML20024C0371983-07-0101 July 1983 LER 83-057/03L-0:on 830606,nitrogen Low Pressure Alarm on Low Pressure Accumulator for PORV Received in Control Room. Caused by Valve Position Indicator Lights Not Showing Full Actual Position.Limit Switches adjusted.W/830701 Ltr ML20024C2601983-06-30030 June 1983 LER 83-54/03L-0:on 830601 Plant Auxiliary Relay Rack XPN-6034 Balance Declared Inoperable Due to Power Failure. Caused by Loose Fuse Holder on Power Supply Module Grounding Supply.Module replaced.W/830630 Ltr ML20024C1031983-06-22022 June 1983 LER 83-051/03L-0:on 830524,control Room Evacuation Panel Pressurizer Relief Tank Level Indicator ILI-470A Removed from Svc Due to Low Readings.Caused by Instrument Drift. Upgraded Electronic Cards installed.W/830622 Ltr ML20023D4561983-05-13013 May 1983 LER 83-036/03L-0:on 830414,during Performance of Channel Calibr,Pressurizer Safety Valve Position Indication on Valves Failed to Function Properly.Caused by Excessive Current Flow During Contact Closure.Switch Assembly Changed ML20023B6481983-04-29029 April 1983 LER 83-032/03L-0:on 830331,detection Zone Nnn in Control Bldg Failed to Respond to Simulated Smoke Condition During Investigation of Alarm.Alarm Previously Received on 830329. Caused by Short in Smoke Detector.Detector Reinstalled ML20023B4391983-04-29029 April 1983 LER 83-033/03L-0:on 830331,while in Mode 5,source Range Detectors N-31 & N-32 Lost for Approx 5 Minutes.Caused by Maint Personnel Error in Placing Trains of Solid State Protection Sys in Wrong Position.Personnel Cautioned ML20028G0861983-02-0101 February 1983 LER 83-001/01T-0:on 830119,w/plant in Mode 1,three Refueling Water Storage Tank Level Transmitters Failed High. Caused by Frozen Instrument Lines.Transmitters Thawed. Insulated Encls Will Be Installed ML20028F4721983-01-21021 January 1983 LER 82-065/03L-0:on 821222,electrical Power Lost to Train a Radiation Monitoring Sys.During Investigation of Loss of Power,Maint Personnel Accidently Short Circuited Train B. Caused by Blown Power Fuses Due to Personnel Error ML20028E0091983-01-14014 January 1983 LER 82-060/03L-0:on 821215,Surveillance Requirement 4.3.3.6 Discovered Unperformed in Modes 1,2 & 3.Caused by Personnel Error.Procedure Revised ML20028E1831983-01-13013 January 1983 LER 82-059/03L-0:on 821215,w/plant in Mode 1,several Fire Doors Not Verified Closed.Caused by Doors Not Being Included in Auxiliary Operator Logs Rev & Therefore Not Checked.Log Being Revised to Ensure That Doors Checked ML20028E1301983-01-13013 January 1983 Revised LER 82-016/03L-2:on 821216,main Control Board Indicator PI-951 for Reactor Bldg Pressure Failed Low.Caused by Failure of Loop Power Supply Circuit Board When Exposed to Ambient Conditions.Circuit Board Replaced ML20028E0771983-01-13013 January 1983 LER 82-058/03L-0:on 821214,urgent Failure Alarm Due to Loss of Power Occurred During Restoration of Rod Control Sys Upon Completion of Power Operational Testing.Caused by Oxidation Between Fuse & Fuse Block Mating Surfaces ML20028E1241983-01-11011 January 1983 LER 82-057/03L-0:on 821213,turbine Bldg Sump Normal Discharge to Site Settling Ponds Temporarily Bypassed Via Auxiliary Pump & Fire Hose.Caused by Sump Pumps Becoming Clogged W/Debris from Const Repair Work Being Done ML20028D3231983-01-0707 January 1983 LER 82-056/03L-0:on 821209,surveillance Test Procedure, Nis Power Range Heat Balance, Not Performed in Specified Intervals.Caused by Personnel Oversight.Administrative Procedures for Control of Surveillances Revised ML20028D1161983-01-0505 January 1983 LER 82-053/03L-0:on 821206,during Mode 1,spurious High & Low Meter Indications Observed on Main Control Board Indicator FI-494 for Steam Generator C Flow.Caused by Failure of Circuit Board FY-494.Board Replaced 1993-07-28
[Table view] Category:RO)
MONTHYEARML20046B4041993-07-28028 July 1993 LER 93-004-00:on 930629,identified Noncompliance W/Srs of TS 4.3.2.1,Table 3.3-3.8.b.Caused by Personnel Error.Retest Sucessfully Performed & Personnel Involved Have Taken Part in Discussion of Importance of Review process.W/930728 Ltr ML20046B1601993-07-28028 July 1993 LER 93-003-00:on 930628,TS Violation Occurred Due to Personnel Error Re non-licensed Operator Performing Evolution W/O Consulting Governing Procedure.Reactor Bldg Purge Supply Valves closed.W/930728 Ltr ML20028H4411990-12-27027 December 1990 LER 90-001-01:on 900209,Part 21 Rept Received from Gilbert Commonwealth Re Possible Loss of One Train of Chilled Water Sys in Event of High Energy Line Break.Conceptual Design Developed to Reduce Heat Load on coils.W/901231 Ltr ML20043F3941990-06-0404 June 1990 LER 90-008-00:on 900505,energizing of Sequencer Initiated Undervoltage Sequence Causing ESF Bus a to Deenergize. Caused by Incorrectly Installed Undervoltage Circuit Agastat Relay.Relay rewired.W/900604 Ltr ML20043B6031990-05-23023 May 1990 LER 90-007-00:on 900423,during Offsite Relay Testing,Oil Circuit Breaker Supplying Bus 3 Tripped Open,Resulting in Loss of Power to ESF Train B & Diesel Generator B Start. Caused by Deficient Procedure.Testing stopped.W/900523 Ltr ML20043A4231990-05-10010 May 1990 LER 90-006-00:on 900412,unplanned ESF Actuation Occurred When Train B Emergency Diesel Generator Automatically Started.Caused by Personnel Error.Feeder Breaker from Battery reopened.W/900510 Ltr ML20042G7691990-05-0808 May 1990 LER 90-005-00:on 900410,steam Generator Tube Eddy Current Exam Yielded Insp Category C-3 Results.Caused by Primary Water Stress Corrosion Cracking in Hot Leg Tubesheet Area. Defective Tubes Plugged or repaired.W/900508 Ltr ML20042G1761990-05-0707 May 1990 LER 90-003-00:on 900406,computer Software Error Caused Nonconservative Radiation Monitor Setpoints.Caused by Software Developer Personnel Error.Setpoints Readjusted & Procedures/Software evaluated.W/900507 Ltr ML20042G1791990-05-0707 May 1990 LER 90-004-00:on 881114,investigation Determined That Two Leads for Cabinet XPN-6002 Had Been Previously Disconnected in 881114 Refueling Outage,Rendering Transmitter LT-1976 Inoperable.Caused by Personnel error.W/900507 Ltr ML20042E1601990-04-11011 April 1990 LER 90-002-00:on 900318,inadvertent ESF Actuation Occurred When Emergency Start Signal Reset.Caused by Procedure Inadequacy When Emergency Start Signal Still Present on Train B.Sys Operating Procedure revised.W/900411 Ltr ML20012C4231990-03-12012 March 1990 LER 90-001-00:on 900209,Gilbert/Commonwealth,Inc Informed Util of Vendor Requirement to Rept Design Deficiency Re Failure of Safety Function,Per Part 21.Util Evaluating What Design Mods Can Be Made to Correct deficiency.W/900312 Ltr ML20006B1231990-01-26026 January 1990 LER 89-022-00:on 890913,discovered That Chilled Water Pump B Returned to Svc W/O Performing Adequate Section XI of ASME Boiler & Pressure Vessel Code Required post-maint Operability Test.Caused by Personnel error.W/900126 Ltr ML19354E1641990-01-17017 January 1990 LER 89-021-00:on 891218,when Operator Directed to Stop Svc Water Pump C by Positioning Handswitch to auto-after Stop Position,Pump Started,Causing ESF Actuation.Caused by Failed Circuit Board.Board replaced.W/900117 Ltr ML20005G1511990-01-0808 January 1990 LER 88-008-01:on 880607,AE (Gilbert Assoc) Notified Util of Design Defect Yielding Potential for Steam Propagation Path Which Could Affect Safe Shutdown Equipment.Caused by Design Error.Also Reportable Per Part 21.W/900108 Ltr ML20005E6941990-01-0202 January 1990 LER 89-019-00:on 891203,as Result of Plant Trip on 891202, Results of Reactor Coolant Sample Not Reviewed & Recognized as Being Out of Tolerance.Caused by Personnel Error.Another Sample of RCS Taken & Analyzed,Per Tech Spec.W/900102 Ltr ML20005E6611990-01-0202 January 1990 LER 89-020-00:on 891202,turbine Controls Failed to Respond to Attempt to Counter Loss of Load & Turbine Manually Tripped.Caused by Relay Contact Failure in Turbine Electrohydraulic Control circuitry.W/900102 Ltr ML20011D4691989-12-20020 December 1989 LER 89-015-02:on 890825,presssurizer Safety Valve Body Inlet Temp Increased to Greater than 450 F & Acoustic Leak Monitor Alarmed,Causing RCS to Depressurize & Reactor Trip. Caused by Loss of Loop Seal.Valve replaced.W/891220 Ltr ML19332F0131989-11-30030 November 1989 LER 89-018-00:on 891027,shift Engineer Observed That Control Room Alarm Did Not Occur When Sample Pumps Stopped.On 891031,radiation Monitors RM-A3 & RM-A4 Declared Inoperable. Caused by Inadequate procedures.W/891130 Ltr ML19327B4921989-10-24024 October 1989 LER 89-017-00:on 890918,responsible Engineer Reviewed Plant Parameters & Concluded That Initial Conditions Required by Surveillance Test Procedure 209.001 Not Satisfied.Caused by Personnel Error & Procedural inadequacy.W/891024 Ltr ML19327B3451989-10-24024 October 1989 LER 89-015-01:on 890825,pressurizer Safety Valve Body Inlet a Temp Increased to Greater than 450 F & Plant Shutdown Initiated.Cause Being Evaluated.Plant Parameters Monitored & Stabilized in Mode 3.W/891024 Ltr ML19325C6501989-10-0707 October 1989 LER 89-016-00:on 890908,shutdown Occurred Due to Inoperable Msiv.Caused by Crushed Conduit That Resulted in Short Circuit of Test Circuit Wiring.Conduit/Test Circuit Wiring repaired.W/891006 Ltr ML20006B2751989-06-27027 June 1989 LER 89-011-01:on 890528,manual Reactor Trip Initiated Following Failure of Pressurizer Safety Valve When Valve Became Unseated,Causing Rapid Depressurization of Rcs.Temp Detectors Installed on Safety valve.W/900123 Ltr ML20024F5131983-08-31031 August 1983 LER 83-091/03L-0:on 830802,while in Mode 1,borated Water Vol of Accumulator a Decreased to 7,354 Gallons.Caused by Valve Leakage in ECCS Check Valve Leakage Detection Sys.Valves Verified in Locked Position.Flange installed.W/830831 Ltr ML20024F4551983-08-31031 August 1983 LER 83-090/03L-0:on 830818,while Increasing Reactor/Turbine Power from 14 to 20%,rod Insertion Limit Violated.Caused by Operating Personnel Failure to Establish Plant Parameters. Emergency Boration initiated.W/830831 Ltr ML20024F2221983-08-31031 August 1983 LER 83-093/03L-0:on 830802,refueling Water Storage Tank Level Transmitter LT-991 Failed High.Caused by Internal Component Failure.Transmitter replaced.W/830831 Ltr ML20024F5901983-08-31031 August 1983 LER 83-092/03L-0:on 830817,east Wall Fire Barrier in Control Bldg Room CB-36-02 Declared Degraded When Unsealed Conduit Found in Newly Installed Juction Box.Caused by Personnel error.W/830831 Ltr ML20024D9111983-08-0101 August 1983 LER 83-075/03L-0:on 830703,emergency Feedwater Valve IFV-3536 to Steam Generator a Tripped Shut on High Flow & Failed to Reset.Caused by Signal Comparator Card Failure. Card replaced.W/830801 Ltr ML20024D8301983-08-0101 August 1983 LER 83-078/03L-0:on 830709,Th Inputs to Subcooling Monitor Channel a Declared Inoperable Due to Low Indications.Caused by Intermittent Opening on Input Connections.Connectors tightened.W/830801 Ltr ML20024D7981983-08-0101 August 1983 LER 83-076/03L-0:on 830707,during Mode 1,pressurizer Power Relief Valve PCV-444B-RC Failed to Stroke Fully.Caused by Low Pressure Nitrogen Reservoir Failing to Charge Up to Pressure.Valves Will Be Inspected & readjusted.W/830801 Ltr ML20024D6981983-07-29029 July 1983 LER 83-074/03L-0:on 830603,during Emergency Diesel Generator a Operability Surveillance Test,Normal 115 Kv Power Supply to Vital Bus Lost & Diesel Generator Output Breaker Tripped Open.Caused by Electrical surge.W/830729 Ltr ML20024D8571983-07-28028 July 1983 LER 83-072/03L-0:on 830701,smoke Detector SMK-CB-3,Zone W-W, Would Not Reset at Integrated Fire & Security Panel.Caused by Failure to Teletype Printed Control Board in Cathode Ray Tube Circuitry.Component replaced.W/830728 Ltr ML20024B6801983-07-0606 July 1983 LER 83-055/03L-0:on 830609 & 10,smoke Detectors in Control Bldg Zone a Failed.Caused by Welding in Area.Fire Watch Patrol Initiated & Affected Detectors & Deluge Resettled. W/830706 Ltr ML20024B7091983-07-0606 July 1983 Updated LER 83-054/03L-1:on 830601,power Failure Occurred, Defeating One Gpm Leakage Alarm for Reactor Bldg Sump.Caused by Loose Power Supply Module Fuse Holder Grounding Power Supply.Module replaced.W/830706 Ltr ML20024B7761983-07-0606 July 1983 LER 83-058/03L-0:on 830607,smoke Detector IXA-4993G Failed to Respond to Simulated Alarm.Caused by Broken Base Assembly in Detector Due to Open Circuit Preventing Alarm Condition. Component replaced.W/830706 Ltr ML20024B9821983-07-0101 July 1983 LER 83-056/03L-0:on 830606,feedwater Flow Transmitter (FT-468) Steam Generator B Failed Low.Caused by Failure of Power Supply Card.Card replaced.W/830701 Ltr ML20024C0371983-07-0101 July 1983 LER 83-057/03L-0:on 830606,nitrogen Low Pressure Alarm on Low Pressure Accumulator for PORV Received in Control Room. Caused by Valve Position Indicator Lights Not Showing Full Actual Position.Limit Switches adjusted.W/830701 Ltr ML20024C2601983-06-30030 June 1983 LER 83-54/03L-0:on 830601 Plant Auxiliary Relay Rack XPN-6034 Balance Declared Inoperable Due to Power Failure. Caused by Loose Fuse Holder on Power Supply Module Grounding Supply.Module replaced.W/830630 Ltr ML20024C1031983-06-22022 June 1983 LER 83-051/03L-0:on 830524,control Room Evacuation Panel Pressurizer Relief Tank Level Indicator ILI-470A Removed from Svc Due to Low Readings.Caused by Instrument Drift. Upgraded Electronic Cards installed.W/830622 Ltr ML20023D4561983-05-13013 May 1983 LER 83-036/03L-0:on 830414,during Performance of Channel Calibr,Pressurizer Safety Valve Position Indication on Valves Failed to Function Properly.Caused by Excessive Current Flow During Contact Closure.Switch Assembly Changed ML20023B6481983-04-29029 April 1983 LER 83-032/03L-0:on 830331,detection Zone Nnn in Control Bldg Failed to Respond to Simulated Smoke Condition During Investigation of Alarm.Alarm Previously Received on 830329. Caused by Short in Smoke Detector.Detector Reinstalled ML20023B4391983-04-29029 April 1983 LER 83-033/03L-0:on 830331,while in Mode 5,source Range Detectors N-31 & N-32 Lost for Approx 5 Minutes.Caused by Maint Personnel Error in Placing Trains of Solid State Protection Sys in Wrong Position.Personnel Cautioned ML20028G0861983-02-0101 February 1983 LER 83-001/01T-0:on 830119,w/plant in Mode 1,three Refueling Water Storage Tank Level Transmitters Failed High. Caused by Frozen Instrument Lines.Transmitters Thawed. Insulated Encls Will Be Installed ML20028F4721983-01-21021 January 1983 LER 82-065/03L-0:on 821222,electrical Power Lost to Train a Radiation Monitoring Sys.During Investigation of Loss of Power,Maint Personnel Accidently Short Circuited Train B. Caused by Blown Power Fuses Due to Personnel Error ML20028E0091983-01-14014 January 1983 LER 82-060/03L-0:on 821215,Surveillance Requirement 4.3.3.6 Discovered Unperformed in Modes 1,2 & 3.Caused by Personnel Error.Procedure Revised ML20028E1831983-01-13013 January 1983 LER 82-059/03L-0:on 821215,w/plant in Mode 1,several Fire Doors Not Verified Closed.Caused by Doors Not Being Included in Auxiliary Operator Logs Rev & Therefore Not Checked.Log Being Revised to Ensure That Doors Checked ML20028E1301983-01-13013 January 1983 Revised LER 82-016/03L-2:on 821216,main Control Board Indicator PI-951 for Reactor Bldg Pressure Failed Low.Caused by Failure of Loop Power Supply Circuit Board When Exposed to Ambient Conditions.Circuit Board Replaced ML20028E0771983-01-13013 January 1983 LER 82-058/03L-0:on 821214,urgent Failure Alarm Due to Loss of Power Occurred During Restoration of Rod Control Sys Upon Completion of Power Operational Testing.Caused by Oxidation Between Fuse & Fuse Block Mating Surfaces ML20028E1241983-01-11011 January 1983 LER 82-057/03L-0:on 821213,turbine Bldg Sump Normal Discharge to Site Settling Ponds Temporarily Bypassed Via Auxiliary Pump & Fire Hose.Caused by Sump Pumps Becoming Clogged W/Debris from Const Repair Work Being Done ML20028D3231983-01-0707 January 1983 LER 82-056/03L-0:on 821209,surveillance Test Procedure, Nis Power Range Heat Balance, Not Performed in Specified Intervals.Caused by Personnel Oversight.Administrative Procedures for Control of Surveillances Revised ML20028D1161983-01-0505 January 1983 LER 82-053/03L-0:on 821206,during Mode 1,spurious High & Low Meter Indications Observed on Main Control Board Indicator FI-494 for Steam Generator C Flow.Caused by Failure of Circuit Board FY-494.Board Replaced 1993-07-28
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D6401999-10-31031 October 1999 Rev 2 to WCAP-15102, VC Summer Unit 1 Heatup & Cooldown Limit Curves for Normal Operation RC-99-0202, Monthly Operating Rept for Sept 1999 for VC Summer Nuclear Station.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for VC Summer Nuclear Station.With ML20216J4191999-09-24024 September 1999 Part 21 Rept Re 990806 Abb K-Line Breaker Defect After Repair.Vendor Notified of Shunt Trip Wiring Problem & Agreed to Modify Procedure for Refurbishment of Breakers RC-99-0180, Special Rept on 990807,electric Driven Fire Pump XPP0134A Was Declared Inoperable.Caused by Pump Discharge Relief Valve Failing to Open as Normally Expected.Two Temporary Fire Pumps Were Installed to Provide Backup Suppression1999-09-0808 September 1999 Special Rept on 990807,electric Driven Fire Pump XPP0134A Was Declared Inoperable.Caused by Pump Discharge Relief Valve Failing to Open as Normally Expected.Two Temporary Fire Pumps Were Installed to Provide Backup Suppression RC-99-0183, Monthly Operating Rept for Aug 1999 for Virgil C Summer Nuclear Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Virgil C Summer Nuclear Station,Unit 1.With ML20211K6161999-08-31031 August 1999 Rev 2 to VC Summer Nuclear Station,Colr for Cycle 12, Dtd Aug 1999 RC-99-0168, Special Rept:On 990804,electric Driven Fire Pump XPP0134A & Diesel Driven Fire Pump XPP0134B,were Removed from Svc to Allow for Plant Mod.Fire Pumps Were Returned to Operable Condition on 990818,after Mod Was Completed1999-08-19019 August 1999 Special Rept:On 990804,electric Driven Fire Pump XPP0134A & Diesel Driven Fire Pump XPP0134B,were Removed from Svc to Allow for Plant Mod.Fire Pumps Were Returned to Operable Condition on 990818,after Mod Was Completed ML20210M7071999-07-31031 July 1999 Rev 1 to VC Summer Nuclear Station COLR for Cycle 12 ML20211C2201999-07-31031 July 1999 Rev 1 to WCAP-15102, VC Summer Unit 1 Heatup & Cooldown Limit Curves for Normal Operation RC-99-0163, Monthly Operating Rept for July 1999 for VC Summer Nuclear Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0137, Monthly Operating Rept for June 1999 for VC Summer Nuclear Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0122, Monthly Operating Rept for May 1999 for VC Summer Nuclear Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for VC Summer Nuclear Station.With ML20206H2971999-05-0505 May 1999 Part 21 Rept Re Common Mode Failure for magne-blast Breakers.Vc Summer Nuclear Station Utilizes These Breakers in Many Applications,Including 7.2-kV EDG Electrical Buses RC-99-0103, Monthly Operating Rept for Apr 1999 for VC Summer Nuclear Station.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for VC Summer Nuclear Station.With ML20206K2421999-04-30030 April 1999 Rev 0 to COLR for Cycle 12 for Summer Nuclear Station RC-99-0087, Part 21 Interim Rept (SSH 99-0001) Re 990218 Failure of Circuit Breaker Located in Cubicle 14 of XSW1DB to Close During Surveillance Testing.Caused by Positive Interlock Angle Was Incorrect.Breaker Was Returned to GE Factory1999-04-15015 April 1999 Part 21 Interim Rept (SSH 99-0001) Re 990218 Failure of Circuit Breaker Located in Cubicle 14 of XSW1DB to Close During Surveillance Testing.Caused by Positive Interlock Angle Was Incorrect.Breaker Was Returned to GE Factory RC-99-0083, Monthly Operating Rept for Mar 1999 for VC Summer Nuclear Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0063, Special Rept:On 990302 & 16,meteorological Site Number One 10 Meter Temp Element Was Declared Inoperable.Caused by Erratic Operation.Cabling & 10 Meter Electrical Connectors Were Replaced1999-03-26026 March 1999 Special Rept:On 990302 & 16,meteorological Site Number One 10 Meter Temp Element Was Declared Inoperable.Caused by Erratic Operation.Cabling & 10 Meter Electrical Connectors Were Replaced ML20196K5421999-03-22022 March 1999 Rev 2 to VC Summer Nuclear Station,Training Simulator Quadrennial Certification Rept,1996-99, Books 1 & 2. Page 2 of 2 Section 2.4.4 (Rev 2) of Incoming Submittal Were Not Included RC-99-0055, Special Rept:On 990302,Meteorological Site Number One 10 Meter Temp Element (RTD) Was Declared Inoperable Due to Erratic Operation.Cause of Original RTD Failure Is Unknown. Equipment Was Declared Operable on 9903121999-03-16016 March 1999 Special Rept:On 990302,Meteorological Site Number One 10 Meter Temp Element (RTD) Was Declared Inoperable Due to Erratic Operation.Cause of Original RTD Failure Is Unknown. Equipment Was Declared Operable on 990312 RC-99-0050, Monthly Operating Rept for Feb 1999 for VC Summer Nuclear Station,Units 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for VC Summer Nuclear Station,Units 1.With ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML20203F4511999-02-12012 February 1999 SER Finding Licensee Adequately Addressed GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves, for Virgil C Summer Nuclear Station ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML20206R5241998-12-31031 December 1998 Santee Cooper 1998 Annual Rept RC-99-0052, Vsns 1998 Annual Operating Rept. with1998-12-31031 December 1998 Vsns 1998 Annual Operating Rept. with RC-99-0004, Monthly Operating Rept for Dec 1998 for VC Summer Nuclear Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for VC Summer Nuclear Station,Unit 1.With ML20206R5191998-12-31031 December 1998 Scana Corp 1998 Annual Rept ML20198F4241998-12-18018 December 1998 Safety Evaluation Granting Relief Request for Approval to Repair ASME Code Class 3 Service Water Piping Flaws in Accordance with GL 90-05 for VC Summer Nuclear Station RC-98-0223, Special Rept 98-001:on 981130,steam Line High Range Gamma Monitor (RMG-19C) Was Declared Inoperable Due to Indeterminate Alarm.Caused by Failures in Detector & Meter Reset Circuitry.Established Preplanned Alternate Method1998-12-16016 December 1998 Special Rept 98-001:on 981130,steam Line High Range Gamma Monitor (RMG-19C) Was Declared Inoperable Due to Indeterminate Alarm.Caused by Failures in Detector & Meter Reset Circuitry.Established Preplanned Alternate Method RC-98-0222, Monthly Operating Rept for Nov 1998 for VC Summer Nuclear Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for VC Summer Nuclear Station,Unit 1.With ML20155G4551998-11-0404 November 1998 Safety Evaluation Accepting Licensee Proposed Alternative to Use Code Case N-416-1 with Licensee Proposed Addl Exams RC-98-0208, Monthly Operating Rept for Oct 1998 for VC Summer Nuclear Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for VC Summer Nuclear Station,Unit 1.With ML20207J5701998-10-31031 October 1998 Non-proprietary Rev 1 to WCAP-14955, Probabilistic & Economic Evaluation of Rv Closure Head Penetration Integrity for VC Summer Nuclear Plant ML20154Q9571998-10-21021 October 1998 SER Accepting Request Seeking Approval to Use Alternative Rules of ASME Code Case N-498-1 for Class 1,2 or 3 Sys ML20154K7901998-09-30030 September 1998 Non-proprietary Rev 0 to WCAP-15101, Analysis of Capsule W from Sceg VC Summer Unit 1 Rv Radiation Surveillance Program RC-98-0184, Monthly Operating Rept for Sept 1998 for VC Summer Nuclear Station.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for VC Summer Nuclear Station.With ML20154K8041998-09-30030 September 1998 Non-proprietary Rev 0 to WCAP-15103, Evaluation of Pressurized Thermal Shock for VC Summer Unit 1 RC-98-0166, Monthly Operating Rept for Aug 1998 for VC Summer Nuclear Station,Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for VC Summer Nuclear Station,Unit 1.With ML20237A7181998-08-13013 August 1998 SER Accepting Util Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves RC-98-0153, Monthly Operating Rept for July 1998 for VC Summer Nuclear Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for VC Summer Nuclear Station,Unit 1 RC-98-0131, Monthly Operating Rept for June 1998 for VC Summer Nuclear Station1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for VC Summer Nuclear Station ML20248J0191998-06-0404 June 1998 Safety Evaluation Accepting Licensee Inservice Testing Program Interim Pump Relief Request Per 10CFR50.55a(a)(3) (II) RC-98-0113, Monthly Operating Rept for May 1998 for VC Summer Nuclear Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for VC Summer Nuclear Station,Unit 1 RC-98-0100, Monthly Operating Rept for Apr 1998 for VC Summer Nuclear Station,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for VC Summer Nuclear Station,Unit 1 ML20217G7411998-04-22022 April 1998 Rev 1 to VC Summer Nuclear Station COLR for Cycle 11 RC-98-0076, Final Part 21 Rept Re a DG EG-B for Vsns,As Followup to .Power Control Svcs of Engine Sys,Inc Provided Response on 980318.Evaluation Concludes That Failure of EG-B Is one-time non-repeatable Failure1998-04-17017 April 1998 Final Part 21 Rept Re a DG EG-B for Vsns,As Followup to .Power Control Svcs of Engine Sys,Inc Provided Response on 980318.Evaluation Concludes That Failure of EG-B Is one-time non-repeatable Failure RC-98-0084, Monthly Operating Rept for Mar 1998 for Virgil C Summer Nuclear Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Virgil C Summer Nuclear Station,Unit 1 ML20212H1421998-03-0202 March 1998 Interim Part 21 Rept SSH 98-002 Re EG-B Unit That Was Sent to Power Control Svcs for Determination of Instability & Refurbishment of a Dg.Cause of Speed Oscillations Unknown. Completed Hot Bore Checks on Power Case 1999-09-08
[Table view] |
Text
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s:uth C!.rolina Etctric & cas CImpany..- 0110 S. Bradham '
O/; .:.- P.O. Box 88 - Vice Prtsidtnt l WF- - Jenkinsvilb, SC 29065 Nuclear Operttions :
s;av '3803) 3454 040 g -;' SCEAG 39 w%
- January 2, 1990 a s t,
Document Control Desk
, .U.-S. Nuclear Regulatory Commission Washington, DC 20555
SUBJECT:
Virgil C. Summer Nuclear Station y Docket No. 50/395 Opereting License No. NPF-12 LER 89-020 Gentlemen:
-Attached is Licensee Event Report No.89-020 for the Virgil C. Summer Nuclear
, Station.. This= report is submitted pursuant to the requirements of
- 10CFR50.73(a)(2)(iv). .
=Should there be any questions', please call us at your convenience. ;
Very truly yours,
/
- 0. S. Bradham CJM/OSB: led Attachment c: D. A. Nauman/0. W. Dixon, Jr./T. C. Nichols, Jr.
c E. C. Roberts
,R. V. Tanner J. C. Snelson S. D. Ebneter R. L. Prevatte J. J. Hayes, Jr. J. B. Knotts, Jr.
General Managers INP0 Records Center ;
C. A. Price ANI Library '
G. J. Taylor Marsh & McLennan 1 J. R. Proper NSRC R. B. Clary NPCF F. H. Zander RTS (ON0 890107)
T. L. Matlosz Files (818.05 & 818.07) l L K. E. Nodland i
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- ActLITY 8 eases N . DOCKSTasueGGR431 FAGE W Virail C. Summer Nuclear station 0 Is l o lo l o l 31915 i loFl 015 TITit tel Reactor Trip on Low-Low Steam Generator Level Followina Turbine Trin sygeff Daft Isl Lan NynetR 404 RGPORT Daft (T) OTMSA f ACILITitS 18ev0Lvt0 21
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" C E s CAUSE SYSTEM COMPONENT MkAjN8 CAUSS SYSTEM ConsPONGNT N g ",TpA s B JJi RLYi i i G i q80 i N i i i i i i i E Ell' B l KI RI Gl 01810 N I l I I I I I '
GUPPLEMENTAL PGPORT EXPECTRO Hel MONTM DAY YEAR YES fid v.e. semgHne LX.tCTfD SUentIS$10N De tti NO l l l AssinACT ,u ,= ,. A. = .. .- ev, , nel On December 2, 1989, at approximately 2202 hours0.0255 days <br />0.612 hours <br />0.00364 weeks <br />8.37861e-4 months <br />, operations personnel started a load reduction to 90% power for the monthly turbine control valve testing. When the operator pushed.the load selector decrease button for the second 2% reduction in power the turbine commenced a rapid power decrease (2209 hours0.0256 days <br />0.614 hours <br />0.00365 weeks <br />8.405245e-4 months <br />). Operations personnel attempted to counter the loss of load by selecting manual increase; )
however, the turbine controls failed to respono and the turbine was manually tripped 1 when turbine power decreased below P-9 (Power Permissive < 50% Rated Thermal Power). 1 The exciter field breaker initially failed to open from the Main Control Board (MCB).
An operator was immediately dispatched to locally open the breaker. The breaker finally opened after several attempts to cycle the breaker from the MCB.
Main feedwater was manually secured /1t 2220 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.4471e-4 months <br /> when the turbine runback transient caused a high level in the deareater (DA). When main feedwater was restored at 2221 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.450905e-4 months <br />, the addition _of cooler (280"F) water caused a rapid RCS cooldown and steam generator levels to shrink to below the low-low steam generator level reactor trip l setpoints. A reactor trip occurred at 2222 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.45471e-4 months <br /> on C" Steam Generator low-low level. With the exception of the previously mentioned problems the plant response was normal. A failed turbine control circuit board was replaced and the exciter field breaker PM'd prior to authorizing the plant restart.
Additional actions have been initiated by SCE&G to modify the turbine control circuit and increase the PM frequency on the exciter field breaker, gag, =
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PLANT-IDENTIFICATION:
Westinghouse 2 Pressurized Water Reactor =
+
EQUIPMENT IDENTIFICATION:
Electrohydraulic Control Panel. Relay. - EIIS - JJ
- w. ,
Alterex-Exciter Field Breaker - EIIS - EL 4
IDENTIFICATION OF EVENT:
' On December 2,:1989, at-approximately.2209 hours0.0256 days <br />0.614 hours <br />0.00365 weeks <br />8.405245e-4 months <br />, the turbine commenced a rapid-power decrease due'to a failure;in the turbine control system. At the time of the-occurrence,vpower was.being-decreased to approximately 90% for routine turbine-control: valve testing. . At 2217 hours0.0257 days <br />0.616 hours <br />0.00367 weeks <br />8.435685e-4 months <br /> the main generator breaker and the turbine were manually tripped.after power had decreased below P-9-(Power Permissive < 50%
Rated Thermal Power). A reactor trip occurred at 2222 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.45471e-4 months <br /> on low-low steam generator _ level during-restoration of main feedwater f. low to-the steam generators.
The increased flow in.feedwater at a temperature of 280*F caused a rapid shrink. in all' steam' generator-levels.
- EVENT'DATE:
December 2, 1989,-at' 2222 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.45471e-4 months <br /> REPORT DATE: January 2, 1990 This report.was initiated by Off-Normal Occurrence Number 89-107.
' CONDITION PRIOR TO EVENT:
i Mode 1 - 100% Power DESCRIPTION OF EVENT:
On' December.2, 1989, at approximately 2202 hours0.0255 days <br />0.612 hours <br />0.00364 weeks <br />8.37861e-4 months <br />, operations personnel started a loadoperator
'the reduction to 90%
pushed thepower load sel for the monthly turbine control valve testing. When ector decrease button for the second 2% reduction
- in power, the turbine commenced a rapid power decrease (2209 hours0.0256 days <br />0.614 hours <br />0.00365 weeks <br />8.405245e-4 months <br />). This turbine runback resulted in an actuation of all fourteen steam dumps (including the PORV's to the atmosphere) and automatic rod insertion to compensate for the turbine runback.
Operations personnel attempted to counter the loss of load by selecting manual increase; however, the turbine controls failed to respond and the turbine was manually tripped at 2217 hours0.0257 days <br />0.616 hours <br />0.00367 weeks <br />8.435685e-4 months <br /> when g ag ,oa .
7 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION areR6vEo ous no siso-oio4
- 4 EXPIRES 8'31/86 F ACl4tTV NAME (15 ' DOCKET NUMBER (28 LER NUMBER 16) PAGE (3) v8Aa -
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power had decreased below the P-9 setpoint. An additional problem occurred when-the' exciter _ field breaker initially failed to open from the Main Control Board (MCB)-following the' trip. An operator was immediately dispatched to locally open the breaker. The breaker finally opened after several_ attempts to cycle it from ;
.the MCB. l Main feedwater was manually. secured by operations at 2220 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.4471e-4 months <br /> when the turbine runback transient caused a high level in the deareater (DA). The rapid increase in l DA level led to a manual trip of the "B" condensate pump and the automatic tripping I of."A" condensate pump.. The condensate system was then aligned for restart and the '
"A" :ondensate pump was started. When main feedwater was restored at 2221 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.450905e-4 months <br />,
-the addition of cooler (280*F) water caused a rapid RCS cooldown and steam generator levels to shrink to below the low-low steam generator level reactor trip setpoints. A reactor trip occurred at 2222 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.45471e-4 months <br /> on "C" Steam Generator low-low level.. With the exception of_the previously mentioned problems, the plant response was normal. The plant was stabilized in Mode 3 until the cause of the malfunctions
'could be determined and corrected.
CAUSE OF EVENT:
The cause of the turbine runback was a relay contact failure in the turbine electrohydraulic control (EHC) load reference circuitry. Relay contacts for stator water cooling runback had shorted and remained closed when the operator pressed the load decrease button on the MCB. Instrumentation personnel replaced the circuit board which contained the defective component and returned the EHC system to operable status for a plant restart on December 3, 1989.
Subsequent investigations by engineering personnel determined that the component malfunction appeared to have resulted from a design deficiency. It is standard practice to connect a reverse biased diode across relay coils in the EHC circuitry to prevent high inductive voltages from being produced. A review of the runback circuit, which was modified in April of 1987, determined that a 24 VDC relay coil was connected to the failed contact without diodes. The contacts are rated for 500 volts; however, in a test on December 7, 1989 the vendor and South Carolina Electric & Gas Company (SCE&G) engineering personnel observed spikes of over 400 volts and that the contacts easily arced. The test confirmed that the contacts could short and cause the runback which occurred on December 2, 1989.
The failure of the Alterex exciter field breaker to open is a repeat occurrence.
The previous failure which was noted in LER 88-002 dated March 11, 1988, was due to solidification of grease, whereas the latest failure was determined to have resulted from a lack of lubrication. The cause of the repeat failure was either due to personnel error or too long of a period between lubrications. Following the previous event, the type of grease applied for lubrication of this breaker was changed to prevent binding per the recommendations of IE Information Notice 87-12
" Potential Problems with Metal Clad Circuit Breakers, General Electric Type AKF 25," and the frequency of preventative maintenance (PM) was set for every refueling outage. During an outage in November of 1988, the breaker was sent to a vendor for ungonu ma
7 f32: l F aenc Form asea c U.S NUCL6f.R 7.40VLATORY COMMISSION
'@ "9 s y - LICENSEE EVENT REPORT (LER) TEXT CONTINUATION-Arenoveo oms No. siso-oio4 9 EXPIRE 8 8/31/65
'[iI P ACILITY NAME (1)I DOCKET NUMOtR IM WR NUMSER W ,Mm I TIA" -
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-refurbishment and on installation the PM was rescheduled for the next outage in -
1990.. -1
-1 ANADSIS ~ OF' EVENT:
1 This report is being submitted pursuant to the requirements of 10CFR50.73(2)(a)(iv). Notification to the NRC Operations Center via the Emergency- l Notification System was made at 0030 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> on December 3, 1989, per the requirementsof10CFR50.72(b)(2)(ii).
'With the exception of the Alterex. exciter field breaker, the plant responded as expected to the turbine runback and subsequent reactor trip. During the runback, reactor-power was decreased through rod-insertion and emergency boration. As previously stated, increasing levels in the DA following the manual trip of the turbine.resulted.in loss of condensate pumps, and during the recovery process the ,
addition of' main feedwater led to a shrink in steam generator levels and subsequent :
- reactor _ trip from approximately 5% RTP. The turbine driven emergency feedwater
_(TDEFW) pump started when the trip occurred due to the low-low level in all three steam generators and operated for approximately five minutes before being manually-tripped:by the operator. The plant cooled down to 530 F during the transient and was. stabilized in Mode 3.
Because of minor primary to secondary leakage in the steam generators, the TDEFW pump-and the power operated relief valve operations resulted in a release of gaseous effluents. Calculations performed in accordance with Technical Specification 3.11.2.1 determined that the release was neligible (<0.1% of allowable releases / year).
IMMEDIATE CORRECTIVE ACTION:
. Following t'he reactor trip, the operating shift placed the plant in a stable
- condition in accordance with Emergency Operating Procedure (EOP) 1.0, " Reactor p -Trip / Safety Injection Actuation," and E0P-1.1, " Reactor Trip Recovery."
l Maintenance was then directed to investigate and repair the noted equipment failures. The EHC card was replaced and the exciter field breaker PM'd prior to authorizing the plant restart.
p ADDITIONAL CORRECTIVE ACTION:
L L The following additional actions were initiated by SCE&G to prevent a similar reoccurrence:
- 1. The circuitry of the EHC card was analyzed and determined to contain a design deficiency in that diodes were not installed to prevent high inductive voltages. This deficiency was confirmed through testing on December 7, 1989.
- 2. A modification to install diodes in the circuitry was performed on December 29, 1989.
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TEXT tot more spese n tw, one natheonn! NMC form 366Knl(11) r.
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- 3. Maintenance has been directed to inspect and lubricate if necessary the exciter field breaker at approximately six month intervals (actual time is
' dependent on frequency of outages) until the reliability of the breaker can be established. i PRIOR OCCURRENCES:
LER 88-002, dated March 11,'1988 t
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1 NRC FORM 366A i 69 831