ML20024C037

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LER 83-057/03L-0:on 830606,nitrogen Low Pressure Alarm on Low Pressure Accumulator for PORV Received in Control Room. Caused by Valve Position Indicator Lights Not Showing Full Actual Position.Limit Switches adjusted.W/830701 Ltr
ML20024C037
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 07/01/1983
From: Dixon O, Kolb L
SOUTH CAROLINA ELECTRIC & GAS CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
LER-83-057-03L, LER-83-57-3L, NUDOCS 8307120196
Download: ML20024C037 (3)


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EVENT DESCRIPTION AND PROSABLE CON 3EQUENCES h o2 l On June 6.1983. at 1905 hours0.022 days <br />0.529 hours <br />0.00315 weeks <br />7.248525e-4 months <br />. with the Plant in Mncio 1; n Ni tervon im, pnnnnunn l E l Alann on the Low Pressure Accumtilator for Pressurizer Power Ooerated Relief Valve l ,

o4 I (PORV) (PCV-445A-RC) was received in the Control Roon. PCV-445A-RC would not ooen!

[o lTl l fran the Main Control Board. 'Ihere were no adverse consecuences as the Plant ms l oe I in canplaince with Technical Specification 3.4.4. Action Statment (at and l l o l, l l Technical Specification 3.3.3.6, Table 3.3-10, Item 20, and the redundlnt train l l o I e . I was OPERABIE. l

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NAME OF PREPARE ' PHONE: ( 035345-5209 L / E. Kolb

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Mr. James P. O'Reilly LER No.83-057 Page Twc July 1, 18 3 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES On June 6,1983, at 1305 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.965525e-4 months <br />, with the Plant in Mode 1, Nitrogen Low Pressure Alarm 1x1 the Low Pressure Accumulator for Pressurizer Power Operated Relief Valve (PORV) POV-445A-RC was received in the Control Room. PCV-445A-RC would not open from the Main Control Board. Within 15 minutes af ter receipt of the alarm, the block valve for POV-445A-RC (8000A) was closed and power removed.

Technical Specification 3.4.4, Action Statement (a), requires that with one (1) or more PORV(s) inoperable, within one (1) hour either restore the PORV(s) to OPERABLE status or close the associated block valve (s) and remove power from the block' valve (s); otherwise, be in at least HOT STANDBY within the next six (6) hours and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

In addition to the above referenced Specification, Technical Specification 3 3.3.6, Table 3 3-10, Item 20, is also applicable but not required when the associated block valve is closed.

There were no adverse consequences as the Plant was in compliance with the applicable Technical Specification Action Statement, and the redunaant train was OPERABLE.

CAUSE AND CORRECTIVE ACTIONS The cause of the occurrence has been attributed to low operating pressure for PORV POV-445A-RC. In addition to the above problem, it was determined that the valve position indicator lights on the Main Control Board were not showing full actual position. The cause of this second problem has been attributed to the valve limit switches being out of adjustment.

Nitrogen Supply Header Pressure Control Regulator (IPV-6307A) for PORV POV-445A-RC was adjusted to allow full valve stroking. The valve limit. switches were adjusted to give proper Main Control Board Indication. Before being returned to' service on June 19, 1983, at 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br />, a Surveillance Valve Operability Test was performed satisfactorily.

No further action is planned other than normal surveillance testing.

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v ........ , g3 g "I nu.t... o .ari.~* July 1, 1983 Mr. James P. O'Reilly Regional Administrator U.S. Nuclear Regulatory Commission Region II, Suite 2900 101 Marietta Street, N.W. Atlanta, Georgia 30303

SUBJECT:

Virgil C. Summer Nuclear Station Docket No. 50/395 Operating License No. NPF-12 Thirty Day Written Report LER 83-057

Dear Mr. O'Reilly:

Please find attached Licensee Event Report #83-057 for Virgil C. Summer Nuclear Station. This Thirty Day Report is required by Technical Specification 6.9.1.13.(b) as a result of entry into Action Statenent (a) of Technical Specification 3.4.4, "Relier Valves," on June 6,1983 Should there be any questions, please call us at your convenience. Very truly yours, O. W. Dixon, Jr. LEK:0WD/dwr i Attachment cc: V. C. Sumner C. L. Ligon (NSRC) l E. H. Crews, Jr. G. J. Braddick l T. C. Nichols, Jr. ,/0. W. Dixon, Jr. J. C. Miller E. C. Roberts J. L. Skolds H. N. Cyrus J. B. Knotts, Jr. Group / General Managers I&E (Washington) O. S. Bradham Document Management Branch l R. B. Clary l C. A. Price INPO Records Center A. R. Koon NPCF D. A. Lavigne File (Lic./Eng.) l l l OFFICIAE COPT \ fraL l lll

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