ML20028E124

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LER 82-057/03L-0:on 821213,turbine Bldg Sump Normal Discharge to Site Settling Ponds Temporarily Bypassed Via Auxiliary Pump & Fire Hose.Caused by Sump Pumps Becoming Clogged W/Debris from Const Repair Work Being Done
ML20028E124
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 01/11/1983
From: Fields H
SOUTH CAROLINA ELECTRIC & GAS CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20028E123 List:
References
LER-82-057-03L, LER-82-57-3L, NUDOCS 8301210009
Download: ML20028E124 (1)


Text

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EVENT DESCRIPTION / 7 PROBABLE CONSEQUENCES 010 l 0 l2 l lOn December 13, 1982, with the Plant in Mode 1, the Turbine Building sump normal l lo l3 l [ discharge to the site settling ponds was temporarily bypassed via an auxiliary l l o l4 l l pump and fire hose. This temporary path bypassed Radiation Monitor RM-L8 which l 10 ls l ln.onitors the normal discharge flou path. There were no adverse consequences as l l o l6 l lnrab sampleG were taken as required by the applicable Technical Specification l l o l 7 l l Action Statement. l lolatl I

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_ Wh (_Zj h 10 10 l0l 0l (_Jj h [lLj h l Alh lGl2l0l0l 4F 33 34 35 3. 5, 4. 4. 41 43 44 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1110 l lThe normal Turbine Buildinn sump pumps became clonned with debris from l l1l1ll construction repair work beine done. The sumos were cleaned in order to restore l l1 l 2 l lthe nnrmn1 unmn aiuchnron n14enmont. rnnnerncrinn will onenh11mh richent l

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, . i. j s NAME OF PREPARER /

  • d #~ PHONE: (80[)345-5209 H. G. Fields /F