ML19350C560

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Forwards Supplemental Response to IE Bulletin 80-06, Engineered Safety Feature (ESF) Reset Controls. Informs of Deficiency Discovered During Testing of Engineered Safety Feature Reset Controls Re HPCI Sys
ML19350C560
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 03/05/1981
From: Pasternak R
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
IEB-80-06, IEB-80-6, JAFP-81-0192, JAFP-81-192, NUDOCS 8104060015
Download: ML19350C560 (3)


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~ . . ' as POWER AUTHORITY CF THE STATE OF NEW YORK JAMES A. FIT 2 patrick NUCLEAR POWER PLANT RAYMOND J. PAsTERNAK Re:Went Meneger S P.O. BOX 41 Lycoming. New York 13093 315-342 3840 March 5, 1981 SERIAL: JAFP 81-0192 m to gs Boyce H. Grier, Director g United States Nuclear Regulatory Commission c}y 4p3 A Region I <

' L o.4 's O l (f 631 Park Avenue /Sg7 King of Prussia, PA. 19406 A i',  %

SUBJECT:

NRC I&E BULLETIN N0. 80-06 '

ENGINEERED SAFETY FEATURE (ESF) RESET C04( db -:

Reference:

Letter to Boyce H. Grier from Raymond J. Pasternak Dated July 1,1980 (Serial No. JAFP 80-538)

Dear Mr. Grier:

Based on discussions between members of Nuclear Regulatory Comission NRR staff, EG&G staff and Power Authority staff, on February 23, 1981, this supplemental response to the subject bulletin is provided.

During the discussions noted above, it became apparent that providing elementary diagrams of the Automatic Depressurization System to the EG&G staff reviewing Bulletin 80-06, responses could be of considerable assistance.- Accordingly, we have enclosed General Electric Drawing Number 791E453, Sheets 1 through 3 for that purpose. In addition, the FitzPatrick Plant staff noted that during testing of ESF reset functions conducted as part of the startup test program following the 1980 Refueling Outage, one (1) additional minor deficiency was discovered. This deficiency, which involves the High Pressure Coolant Injection (HPCI) System is described below.

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3 310.4060 _

Boyce H. Grier, Director March 5, 1981 United States Nuclear Regulatory Comission JAFP 81-0192

SUBJECT:

NRC I&E BULLETIN N0. 80-06 Page Following satisfaction of the HPCI initiation Logic, if the logic reset button is depressed inadverently the HPCI system will continue to operate normally except that the HPCI gland exhauster stops. To cause restart of the gland exhauster under these conditions, the control switch must be placed in the

" START" position.

Failure of the gland exhaust to restart would not result in any degradation of the HPCI system's capability to perform its safety function.

Some release of reactor steam from the HPCI turbine seals to the secondary containment would be expected. Since the deficiency is considered to be minor in nature and since licensed operations department personnel are aware of the deficiency and action to be taken, the FitzPatrick Plant does not plan to implement a modification to correct the deficiency until the 1981 Refueling Outage.

Very truly yours,.

,h ,. h ,

'RJP:VC:brp RAYM0ND J. PASTERNAK Enclosure RESIDENT MANAGER Subscribed and Sworn to before me this 5th day of March,1981 A ( AL _.

Notary Public DISTRIBUTION: (WITHENCLOSUREl g, ,

NRC Office of Inspection & Enforcement N$ $5$:$3Neu*n y Division of Reactor Operations Inspection My cemminh. Ex;;rcWuch 30,19_ ;.-

Washington, D.C. 20555 P. Polk, Licensing Project Manager U.S. Nuclear Regulatory Commission

" Washington, D.C. 20555 W.'Kountanis-EG&G, P.O. Box 204 San Ramon, CA. 94583

.NRC Resident Inspector NRCB 80-06 File y

Boyce H. Grier, Dir:ctor March 5, 1981 United States Nuclear Regulatory Commission JAFP 81-0192

SUBJECT:

NRC IAE BULLETIN N0. 80-06 Page DISTRIBUTION: (WITHOUT ENCLOSURE)

George T. Berry, PASNY, NY0 J. P. Bayne, PASNY, NY0 G. M. Wilverding, PASNY, NY0 M. C. Cosgrove, PASNY, JAF R. Baker, PASNY, JAF R. J. Converse, PASNY, JAF Document Control Center i

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