ML19289G225

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LER 79-053/03L-0 on 790713:control Room Air Conditioner Compressor Failed to Start from Control Room Panel.Caused by Casting Plug Lodged in Compressor Valve.Plug Removed,Unit Recharged & Declared Operable
ML19289G225
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 08/02/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19289G224 List:
References
LER-79-053-03L, LER-79-53-3L, NUDOCS 7908070551
Download: ML19289G225 (1)


Text

I NRC FORM 366 U. S NUCLE AR REGULATORY COMMISSION LICENSEE EVENT REPORT EXHIRIT A CONTROL 8 LOCK: l i l l l l l elh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) i o i l AIR A l Nl Q l 2lgl 0 l0 l UCENSENuusER -l0 l 0 [ 0l 0l0l- l0l0 l uCg< l1 [1l1 l1lgl l lg 8 9 UCENSEE CODE to 15 25 26 NSE tvPs JJ 67 C AT be CON'T f'o~lTI 7 8 . TG LL_J@l0 60 61 l s DOCKET 10 10 013161868 i@l NUMB ER 69 01EVENT 711l 31719 l@l 0l8HEPOHTDATE DATE 74 7S l 0l2 l 7 l 9l@ 80 EVENT DESCRIPTION AND PROBADLE CONSEQUENCES h o 2 I thiring Mode 1 overation. the Control Room Air Conditioner compressor, i Lo LU l 2VFT A. fni t ed to <; tart from the Control Room panel. The "B" Emergency I o 4 1 Air Conditioning System was verified operabic. This occurrence is similar n s Ito LER-50-368/79-050. l o s lThis occurrence is reportable per T.S. 6.9.1.9b. ,

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