ML19289G227

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LER 79-055/03L-0 on 790719:main Feedwater Controller B Malfunctioned.Caused by Water in Steam Supply Line.Water Blown from Steam Line & Tested Successfully
ML19289G227
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 08/02/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19289G224 List:
References
LER-79-055-03L, LER-79-55-3L, NUDOCS 7908070592
Download: ML19289G227 (1)


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NRC FORM 366 (7 77) U. S. NUCLE AR REGUL ATORY COMMISSION LICENSEE EVENT REPORT EXHLBIT A CONTROL BLOCK: l 6

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6 h (PLEASE PRINT OR TYPE ALL REQUtr.lO INFORMATIONI 8 iAlRlAl 7 8 9 Njdl 21@15l 0l0 l-l0 10l 0l Oj0l- l0l0 l gUCLNSE L8CENSEE CODE le UCENSE NvveEH 25 2G l1 tl1l1 vPE JO l1lgl l lg 57 CAT 5m CON *T i

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60 61 OOCKET NUMBER EVENT OATE 24 75 HEPOHTDATE to EVENT DESCRIPTION AND PROBADLE CONSEQUENCES h FETTl I During Mode 1 operation. the "B" Main Feedwater Controller malfunctioned, I F6Til I reouirine Emercency Feedwater. EFW pump steam turbine driver, 2K3, for 10lai tpump 2P7A tripped on overspeed upon receipt of EFAS sinna1, resulting in i n

5 I nn finw frnm ?P7A. Finw was established with the electric driven EFW I O s pump. 2P7R. There hwe been nn sinilar occurrences.

A This cecurrence is reportable per T.S. 6.9.1.9b. I O as l 7 8 9 Sv$1EM CAubt CAUSE 80 CCDE LCCE SUBCODE COvP vatvE LOMPONENT COut AUW %E 8

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4f 43 44 4, CAUSE DESCRIPTION AND CORRECflVE ACTIONS h i O Investication revealed overspeed trip was due to water in the steam i i i i sunniv line. The water was blown from the steam line and 2P7A was i ii 121 I successfully started three times. Onerations has initiated a steam i 13131 1 line blowdown once per shift. Engineering is evaluating the steam I L, il *J 8 .

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