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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20045B3021993-06-11011 June 1993 LER 93-001-00:on 930513,discovered That One Channel of Rvlms Inoperable Since Probe Replaced in Oct 1992.On 930507, Discovered That Two Sensors in Rvlms Indicating Wet.Caused by Design Error.Wiring Polarity corrected.W/930611 Ltr ML20024H2281991-05-21021 May 1991 LER 91-003-00:on 910421,actuation of EFW Sys During Plant Heatup Occurred Due to Low Once Through Steam Generator Level.Caused by Leaking Feedwater Recirculation Valve.Plant Startup Procedure OP 1102.02 Will Be revised.W/910521 Ltr ML20024H0861991-05-10010 May 1991 LER 91-002-00:on 910410,inadvertent Actuations of Combined Control Emergency Ventilation Sys Occurred.Caused by Transient Noise Spike.Mod Will Be Completed by 910531 to Install Time Delay in Actuation circuitry.W/910510 Ltr ML20024G9781991-05-10010 May 1991 LER 90-004-01:on 900531,discovered Degraded Fire Barrier Penetration During Insp Per Generic Ltr 86-10.Caused by Failure to Identify Adequate Fire Barrier Seal During 1983 Plant Walkdown.Fire Watch posted.W/910510 Ltr ML20029C3771991-03-22022 March 1991 LER 91-006-00:on 910222,core Protection Calculator Reactor Coolant Sys Flow Channels Not Being Calibrated within Tech Spec.Caused by Personnel Error.Operations Manager Counseled Operators Involved in event.W/910322 Ltr ML20029B1331991-02-27027 February 1991 LER 91-004-00:on 910125,control Room Radiation Monitor Alarm/Trip Setpoint Greater than Normal.Caused by Personnel Error.Operations Manager Will Counsel Shift Supervisors & Night Order Will Be posted.W/910227 Ltr ML20028H6841991-01-21021 January 1991 LER 90-021-00:on 901222,potential RCS Leak Noted in Area of Pressurizer Upper Level Instrument Nozzle.Caused by Pure Water Stress Corrosion Cracking.New Nozzle Installed Into Penetration from Shell OD.W/910121 Ltr ML20043C6801990-05-31031 May 1990 LER 89-025-01:on 891221,identified That Portion of Wall Located in Auxiliary Bldg Had Not Been Previously Identified as Tech Spec Fire Barrier.Caused by Personnel Error.Wall Being Upgraded to Tech Spec status.W/900531 Ltr ML20043C3781990-05-30030 May 1990 LER 90-012-00:on 900430,18 Month Channel Calibr of Liquid Radwaste Effluent Line Flow Monitor Not Performed as Required.Caused by Inadequate Controls to Ensure Followup Actions Taken in Timely Manner.Amends revised.W/900530 Ltr ML20043C0361990-05-23023 May 1990 LER 90-003-01:on 900423,discovered That Incorrect Monitoring Instrumentation for Radiological Effluent Ventilation Sys Utilized to Comply W/Tech Specs.Caused by Mgt Oversight.Logs Process Monitors Will Not Be used.W/900523 Ltr ML20043A7411990-05-17017 May 1990 LER 90-004-01:on 900212,discovered That Backwater Valve in Floor Drain Pipe in Emergency Feedwater Pump Room Missing. Caused by Inadequate Configuration Control.Backwater Pumps Installed & Will Be Included in Maint program.W/900517 Ltr ML20042F7681990-05-0101 May 1990 LER 90-002-01:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Errors in Original Calculation Not Identified.Calibr Procedures revised.W/900501 Ltr ML20042F7751990-05-0101 May 1990 LER 90-010-00:on 900401,personnel Failed to Complete Control Element Assembly Position Log.Caused by Surveillance Program Deficiencies & Lack of Mgt Involvement.Shift Briefing Completed & Procedure Change incorporated.W/900501 Ltr ML20042E1981990-04-10010 April 1990 LER 90-008-00:on 900311,determined That Seal Leakage Test for Containment Personnel Air Lock Had Not Been Performed, Per Tech Specs.Caused by Personnel Error.Procedure Revs Initiated & Personnel counseled.W/900410 Ltr ML20012F5051990-04-0505 April 1990 LER 89-027-00:on 891005,determined That Leakage Rate for Containment Isolation Check Valve in Excess of Leakage Rate Allowed Per Tech Specs.Caused by Loose Weld Slag in Valve Seat Area.Valve Cleaned & reassembled.W/900405 Ltr ML20012F5031990-04-0505 April 1990 LER 90-007-00:on 900306,RCS Charging Line Rendered Inoperable Due to Deficient Piping Support Weld.Caused by Inadequate Work Controls & post-installation Insp Processes. Field Walkdowns & Weld Insps initiated.W/900405 Ltr ML20012F5741990-04-0404 April 1990 LER 90-006-00:on 900305,instrumentation Channels Declared Inoperable,Resulting in Manual Actuation of Reactor Protection Sys.Caused by Procedural Deficiencies.Functional Tests of Log Power Level Channels performed.W/900404 Ltr ML20012C7221990-03-14014 March 1990 LER 90-004-00:on 900212,identified That No Backwater Valve Located in Floor Drain Pipe in One of Emergency Feedwater Pump Rooms.Caused by Inadequate Configuration Control. Valves Installed on 900215.W/900314 Ltr ML20012C1821990-03-12012 March 1990 LER 85-029-00:on 850520,unusual Motor Vibrations Identified on Svc Water Pump 2PM4A.On 861028,high Vibrations Noted on Upper Motor Bearings of Pump 2PM4B.Caused by Improper Installation.New Bearings installed.W/900312 Ltr ML20012B7271990-03-0808 March 1990 LER 89-049-01:on 891220,discovered That Okonite T-95 Tape Not Used to Tape Internal Motor Lead Connections for Main Feedwater Containment Isolation Valves.Caused by Personnel Error.Valves Taped According to Design drawing.W/900308 Ltr ML20012B5701990-03-0505 March 1990 LER 90-003-00:on 900201,failure to Perform Monthly Source Check Surveillance on Three Radiation Process Monitors Occurred.Caused by Inadequate Procedure Change by Personnel. Source Check on Monthly Basis implemented.W/900305 Ltr ML20011F6741990-03-0202 March 1990 LER 90-002-00:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Caused by Incorrect Static Pressure Assumption.Trip Setpoint Bistable increased.W/900302 Ltr ML20011F6781990-03-0101 March 1990 LER 89-026-00:on 891112,gaps in Piping Supports on Supply & Return Piping for Containment Coolers Identified.Caused by Inadequate Design Technique Used in Original Support Design. Shims Added Before Restart from outage.W/900301 Ltr ML20011F5831990-02-27027 February 1990 LER 89-022-01:on 891114,normal Offsite Power Feeder Breaker to 4,160-volt Ac ESF Bus Opened,Resulting in Loss of Power to Bus 2A3.Caused by Inadequate post-maint Test Controls. Test Switch Opened & Job Order changed.W/900227 Ltr ML20011F7311990-02-23023 February 1990 LER 90-001-00:on 900126,identified That Required Visual Insps of Containment Bldg After Entry Made Not Documented as Being Performed.Caused by Inadequate Procedural Guidance. Administrative Controls to Be established.W/900226 Ltr ML20006D7391990-02-0606 February 1990 LER 89-034-01:on 891031,determined That Tech Spec 3.9.1 Had Likely Been Violated Re Independent Circuits of Control Room Emergency Air Conditioning Sys.Caused by Inadequate Guidance Re Equipment Svc Removal.Procedures revised.W/900206 Ltr ML20011E2371990-01-31031 January 1990 LER 89-012-01:on 890626,RCS Backleakage Through Safety Injection Sys Check Valve Occurred Three Times.Caused by Missing Rollpins Which Connect Valve Disc to Valve Disc Shaft.Rollpins Replaced & Valves reassembled.W/900131 Ltr ML20011E2291990-01-31031 January 1990 LER 89-039-01:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Latch Mechanism Missing. Caused by Abnormally High Differential Pressure Across Door. Ventilation Sys Flow Balance performed.W/900131 Ltr ML20011E1451990-01-30030 January 1990 LER 89-024-00:on 891231,loose Terminal in Feedwater Control Sys Cabinet Resulted in Reactor Trip.Caused by Loose Connection on Terminal.Loose Connection Reterminated properly.W/900130 Ltr ML20006C1451990-01-29029 January 1990 LER 89-048-00:on 891228,automatic Reactor Trip & ESF Actuation Occurred as Result of Loss of All Main Feedwater Flow Due to Inadvertent Tripping of Main Feedwater Pump. Caused by Personnel error.O-rings replaced.W/900129 Ltr ML19354E3331990-01-22022 January 1990 LER 89-025-00:on 891221,two Piping Penetrations Located in Barrier Not Surveilled as Required by Tech Specs.Caused by Personnel Error.Fire Watch Posted When Necessary Per Tech Spec.W/900122 Ltr ML20006A8661990-01-22022 January 1990 LER 89-041-00:on 891221,automatic Actuation of Emergency Feedwater Sys Initiated.Caused by Lack of Adequate Procedural Guidance.Valve Positioners CV-2623 & CV-2673 Adjusted & Guidance Procedures developed.W/900122 Ltr ML20006A8671990-01-22022 January 1990 LER 89-042-01:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900122 Ltr ML20005F1551990-01-18018 January 1990 LER 89-023-01:on 891117,noted That Channel a Not Responding to Change in Power Level & Declared Inoperable.Caused by Defective Preamplifier.Evaluation of Sys Design & Channel Functional Test initiated.W/900108 Ltr ML20006B6461990-01-18018 January 1990 LER 89-047-00:on 891219,RCS Temp Increased Above 250 F W/ Oxygen Concentration Greater than Tech Specs Limit.Caused by Inadequate Procedural Guidance.Plant Startup Procedure Revised to Require Chemistry Dept signoff.W/900118 Ltr ML19354D8291990-01-15015 January 1990 LER 89-044-00:on 891214,incorrect Assumptions & Calculational Errors Identified for Low Pressure Injection & Reactor Bldg Spray Pumps When Aligned to Take Suction from Reactor Bldg sump.W/900115 Ltr ML20005G1681990-01-0909 January 1990 LER 89-045-00:on 891210,discovered That U-bolt Supports on Two Containment Isolation Valves in Containment Bldg Not Installed & Pressurizer Sample Lines & Valves Considered Inoperable.Missing U-bolts installed.W/900109 Ltr ML20005F1481990-01-0808 January 1990 LER 89-042-00:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900108 Ltr ML20005F1571990-01-0808 January 1990 LER 89-043-00:on 891208,discovered That Approx 50% of One Nut Ring Half Beneath Reactor Vessel Nozzle Flange Corroded Away.Caused by Gradual Deterioration of Gasket Matl.Design Change implemented.W/900108 Ltr ML20005F2071990-01-0404 January 1990 LER 89-040-00:on 891205 & 06,automatic Actuations of Emergency Diesel Generator Occurred as Result of Loss of Power to 480-volt ESF Bus.Caused by Personnel Error During Bus Transfer.Mgt Briefings conducted.W/900104 Ltr ML20005F0471990-01-0303 January 1990 LER 89-046-00:on 891204,reactor Bldg Isolation Valves Rendered Inoperable Due to Deficient Welds on Piping Supports Which Were Installed During Initial Plant Const. Deficient Supports Repaired Prior to restart.W/900103 Ltr ML20011D2521989-12-18018 December 1989 LER 89-039-00:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Missing Latch Mechanism. Caused by Extensive Use During 56-day Refueling Outage.More Frequent Insps of Door Condition to Be done.W/891218 Ltr ML20011D2501989-12-18018 December 1989 LER 89-023-00:on 891117,approach to Criticality Commenced After Seventh Refueling Outage W/Logarithmic Power Level Channels Inoperable.Caused by Electrical Noise in Circuitry. Defective Preamplifier replaced.W/891218 Ltr ML19351A6731989-12-14014 December 1989 LER 89-022-00:on 891114,inadequate post-maint Test Controls Resulted in de-energizing 4,160 Volt Ac ESFs Electric Bus Uexpectedly.Caused by Inadequate post-maint Test Controls. Job Order Instructions changed.W/891214 Ltr ML19354D5521989-12-14014 December 1989 LER 89-038-00:on 891114,reactor Trip Occurred as Result of Inadvertent Closure of Main Feedwater Isolation Valve.Caused by Personnel Error.Disciplinary Action Taken Against Individual & Senior Mgt Personnel Put on shift.W/891214 Ltr ML19351A4651989-12-11011 December 1989 LER 89-021-00:on 891111,when Low Level Radwaste Water in Waste Condensate Tank Aligned to Be Released,Discovered That Radiation Monitor Inoperable for Duration of Release.Caused by Personnel Error.Procedure revised.W/891211 Ltr ML19332F6171989-12-11011 December 1989 LER 89-037-00:on 891110,reactor Trip Occurred as Result of Inadvertent Grounding of Reactor Protection Sys Power Supply During Surveillance Testing.Caused by Inadequate Procedure. Procedures revised.W/891211 Ltr ML20005D6821989-12-0101 December 1989 LER 89-005-01:on 890518 & 25,damping Board Removed from Penetration Containing Cable Tray.On 890531,voids Noted in Penetration Seals.Caused by Erroneous Vendor Procedures. Penetrations Restored & Procedures revised.W/891201 Ltr ML19332E8611989-11-30030 November 1989 LER 89-034-00:on 891031,control Room Emergency Air Conditioning Sys Rendered Inoperable Due to Removing Independent Circuits from Svc.Caused by Inadequate Guidance.Procedures Revised & Circuits flagged.W/891130 Ltr 1998-10-22
[Table view] Category:RO)
MONTHYEARML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20045B3021993-06-11011 June 1993 LER 93-001-00:on 930513,discovered That One Channel of Rvlms Inoperable Since Probe Replaced in Oct 1992.On 930507, Discovered That Two Sensors in Rvlms Indicating Wet.Caused by Design Error.Wiring Polarity corrected.W/930611 Ltr ML20024H2281991-05-21021 May 1991 LER 91-003-00:on 910421,actuation of EFW Sys During Plant Heatup Occurred Due to Low Once Through Steam Generator Level.Caused by Leaking Feedwater Recirculation Valve.Plant Startup Procedure OP 1102.02 Will Be revised.W/910521 Ltr ML20024H0861991-05-10010 May 1991 LER 91-002-00:on 910410,inadvertent Actuations of Combined Control Emergency Ventilation Sys Occurred.Caused by Transient Noise Spike.Mod Will Be Completed by 910531 to Install Time Delay in Actuation circuitry.W/910510 Ltr ML20024G9781991-05-10010 May 1991 LER 90-004-01:on 900531,discovered Degraded Fire Barrier Penetration During Insp Per Generic Ltr 86-10.Caused by Failure to Identify Adequate Fire Barrier Seal During 1983 Plant Walkdown.Fire Watch posted.W/910510 Ltr ML20029C3771991-03-22022 March 1991 LER 91-006-00:on 910222,core Protection Calculator Reactor Coolant Sys Flow Channels Not Being Calibrated within Tech Spec.Caused by Personnel Error.Operations Manager Counseled Operators Involved in event.W/910322 Ltr ML20029B1331991-02-27027 February 1991 LER 91-004-00:on 910125,control Room Radiation Monitor Alarm/Trip Setpoint Greater than Normal.Caused by Personnel Error.Operations Manager Will Counsel Shift Supervisors & Night Order Will Be posted.W/910227 Ltr ML20028H6841991-01-21021 January 1991 LER 90-021-00:on 901222,potential RCS Leak Noted in Area of Pressurizer Upper Level Instrument Nozzle.Caused by Pure Water Stress Corrosion Cracking.New Nozzle Installed Into Penetration from Shell OD.W/910121 Ltr ML20043C6801990-05-31031 May 1990 LER 89-025-01:on 891221,identified That Portion of Wall Located in Auxiliary Bldg Had Not Been Previously Identified as Tech Spec Fire Barrier.Caused by Personnel Error.Wall Being Upgraded to Tech Spec status.W/900531 Ltr ML20043C3781990-05-30030 May 1990 LER 90-012-00:on 900430,18 Month Channel Calibr of Liquid Radwaste Effluent Line Flow Monitor Not Performed as Required.Caused by Inadequate Controls to Ensure Followup Actions Taken in Timely Manner.Amends revised.W/900530 Ltr ML20043C0361990-05-23023 May 1990 LER 90-003-01:on 900423,discovered That Incorrect Monitoring Instrumentation for Radiological Effluent Ventilation Sys Utilized to Comply W/Tech Specs.Caused by Mgt Oversight.Logs Process Monitors Will Not Be used.W/900523 Ltr ML20043A7411990-05-17017 May 1990 LER 90-004-01:on 900212,discovered That Backwater Valve in Floor Drain Pipe in Emergency Feedwater Pump Room Missing. Caused by Inadequate Configuration Control.Backwater Pumps Installed & Will Be Included in Maint program.W/900517 Ltr ML20042F7681990-05-0101 May 1990 LER 90-002-01:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Errors in Original Calculation Not Identified.Calibr Procedures revised.W/900501 Ltr ML20042F7751990-05-0101 May 1990 LER 90-010-00:on 900401,personnel Failed to Complete Control Element Assembly Position Log.Caused by Surveillance Program Deficiencies & Lack of Mgt Involvement.Shift Briefing Completed & Procedure Change incorporated.W/900501 Ltr ML20042E1981990-04-10010 April 1990 LER 90-008-00:on 900311,determined That Seal Leakage Test for Containment Personnel Air Lock Had Not Been Performed, Per Tech Specs.Caused by Personnel Error.Procedure Revs Initiated & Personnel counseled.W/900410 Ltr ML20012F5051990-04-0505 April 1990 LER 89-027-00:on 891005,determined That Leakage Rate for Containment Isolation Check Valve in Excess of Leakage Rate Allowed Per Tech Specs.Caused by Loose Weld Slag in Valve Seat Area.Valve Cleaned & reassembled.W/900405 Ltr ML20012F5031990-04-0505 April 1990 LER 90-007-00:on 900306,RCS Charging Line Rendered Inoperable Due to Deficient Piping Support Weld.Caused by Inadequate Work Controls & post-installation Insp Processes. Field Walkdowns & Weld Insps initiated.W/900405 Ltr ML20012F5741990-04-0404 April 1990 LER 90-006-00:on 900305,instrumentation Channels Declared Inoperable,Resulting in Manual Actuation of Reactor Protection Sys.Caused by Procedural Deficiencies.Functional Tests of Log Power Level Channels performed.W/900404 Ltr ML20012C7221990-03-14014 March 1990 LER 90-004-00:on 900212,identified That No Backwater Valve Located in Floor Drain Pipe in One of Emergency Feedwater Pump Rooms.Caused by Inadequate Configuration Control. Valves Installed on 900215.W/900314 Ltr ML20012C1821990-03-12012 March 1990 LER 85-029-00:on 850520,unusual Motor Vibrations Identified on Svc Water Pump 2PM4A.On 861028,high Vibrations Noted on Upper Motor Bearings of Pump 2PM4B.Caused by Improper Installation.New Bearings installed.W/900312 Ltr ML20012B7271990-03-0808 March 1990 LER 89-049-01:on 891220,discovered That Okonite T-95 Tape Not Used to Tape Internal Motor Lead Connections for Main Feedwater Containment Isolation Valves.Caused by Personnel Error.Valves Taped According to Design drawing.W/900308 Ltr ML20012B5701990-03-0505 March 1990 LER 90-003-00:on 900201,failure to Perform Monthly Source Check Surveillance on Three Radiation Process Monitors Occurred.Caused by Inadequate Procedure Change by Personnel. Source Check on Monthly Basis implemented.W/900305 Ltr ML20011F6741990-03-0202 March 1990 LER 90-002-00:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Caused by Incorrect Static Pressure Assumption.Trip Setpoint Bistable increased.W/900302 Ltr ML20011F6781990-03-0101 March 1990 LER 89-026-00:on 891112,gaps in Piping Supports on Supply & Return Piping for Containment Coolers Identified.Caused by Inadequate Design Technique Used in Original Support Design. Shims Added Before Restart from outage.W/900301 Ltr ML20011F5831990-02-27027 February 1990 LER 89-022-01:on 891114,normal Offsite Power Feeder Breaker to 4,160-volt Ac ESF Bus Opened,Resulting in Loss of Power to Bus 2A3.Caused by Inadequate post-maint Test Controls. Test Switch Opened & Job Order changed.W/900227 Ltr ML20011F7311990-02-23023 February 1990 LER 90-001-00:on 900126,identified That Required Visual Insps of Containment Bldg After Entry Made Not Documented as Being Performed.Caused by Inadequate Procedural Guidance. Administrative Controls to Be established.W/900226 Ltr ML20006D7391990-02-0606 February 1990 LER 89-034-01:on 891031,determined That Tech Spec 3.9.1 Had Likely Been Violated Re Independent Circuits of Control Room Emergency Air Conditioning Sys.Caused by Inadequate Guidance Re Equipment Svc Removal.Procedures revised.W/900206 Ltr ML20011E2371990-01-31031 January 1990 LER 89-012-01:on 890626,RCS Backleakage Through Safety Injection Sys Check Valve Occurred Three Times.Caused by Missing Rollpins Which Connect Valve Disc to Valve Disc Shaft.Rollpins Replaced & Valves reassembled.W/900131 Ltr ML20011E2291990-01-31031 January 1990 LER 89-039-01:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Latch Mechanism Missing. Caused by Abnormally High Differential Pressure Across Door. Ventilation Sys Flow Balance performed.W/900131 Ltr ML20011E1451990-01-30030 January 1990 LER 89-024-00:on 891231,loose Terminal in Feedwater Control Sys Cabinet Resulted in Reactor Trip.Caused by Loose Connection on Terminal.Loose Connection Reterminated properly.W/900130 Ltr ML20006C1451990-01-29029 January 1990 LER 89-048-00:on 891228,automatic Reactor Trip & ESF Actuation Occurred as Result of Loss of All Main Feedwater Flow Due to Inadvertent Tripping of Main Feedwater Pump. Caused by Personnel error.O-rings replaced.W/900129 Ltr ML19354E3331990-01-22022 January 1990 LER 89-025-00:on 891221,two Piping Penetrations Located in Barrier Not Surveilled as Required by Tech Specs.Caused by Personnel Error.Fire Watch Posted When Necessary Per Tech Spec.W/900122 Ltr ML20006A8661990-01-22022 January 1990 LER 89-041-00:on 891221,automatic Actuation of Emergency Feedwater Sys Initiated.Caused by Lack of Adequate Procedural Guidance.Valve Positioners CV-2623 & CV-2673 Adjusted & Guidance Procedures developed.W/900122 Ltr ML20006A8671990-01-22022 January 1990 LER 89-042-01:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900122 Ltr ML20005F1551990-01-18018 January 1990 LER 89-023-01:on 891117,noted That Channel a Not Responding to Change in Power Level & Declared Inoperable.Caused by Defective Preamplifier.Evaluation of Sys Design & Channel Functional Test initiated.W/900108 Ltr ML20006B6461990-01-18018 January 1990 LER 89-047-00:on 891219,RCS Temp Increased Above 250 F W/ Oxygen Concentration Greater than Tech Specs Limit.Caused by Inadequate Procedural Guidance.Plant Startup Procedure Revised to Require Chemistry Dept signoff.W/900118 Ltr ML19354D8291990-01-15015 January 1990 LER 89-044-00:on 891214,incorrect Assumptions & Calculational Errors Identified for Low Pressure Injection & Reactor Bldg Spray Pumps When Aligned to Take Suction from Reactor Bldg sump.W/900115 Ltr ML20005G1681990-01-0909 January 1990 LER 89-045-00:on 891210,discovered That U-bolt Supports on Two Containment Isolation Valves in Containment Bldg Not Installed & Pressurizer Sample Lines & Valves Considered Inoperable.Missing U-bolts installed.W/900109 Ltr ML20005F1481990-01-0808 January 1990 LER 89-042-00:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900108 Ltr ML20005F1571990-01-0808 January 1990 LER 89-043-00:on 891208,discovered That Approx 50% of One Nut Ring Half Beneath Reactor Vessel Nozzle Flange Corroded Away.Caused by Gradual Deterioration of Gasket Matl.Design Change implemented.W/900108 Ltr ML20005F2071990-01-0404 January 1990 LER 89-040-00:on 891205 & 06,automatic Actuations of Emergency Diesel Generator Occurred as Result of Loss of Power to 480-volt ESF Bus.Caused by Personnel Error During Bus Transfer.Mgt Briefings conducted.W/900104 Ltr ML20005F0471990-01-0303 January 1990 LER 89-046-00:on 891204,reactor Bldg Isolation Valves Rendered Inoperable Due to Deficient Welds on Piping Supports Which Were Installed During Initial Plant Const. Deficient Supports Repaired Prior to restart.W/900103 Ltr ML20011D2521989-12-18018 December 1989 LER 89-039-00:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Missing Latch Mechanism. Caused by Extensive Use During 56-day Refueling Outage.More Frequent Insps of Door Condition to Be done.W/891218 Ltr ML20011D2501989-12-18018 December 1989 LER 89-023-00:on 891117,approach to Criticality Commenced After Seventh Refueling Outage W/Logarithmic Power Level Channels Inoperable.Caused by Electrical Noise in Circuitry. Defective Preamplifier replaced.W/891218 Ltr ML19351A6731989-12-14014 December 1989 LER 89-022-00:on 891114,inadequate post-maint Test Controls Resulted in de-energizing 4,160 Volt Ac ESFs Electric Bus Uexpectedly.Caused by Inadequate post-maint Test Controls. Job Order Instructions changed.W/891214 Ltr ML19354D5521989-12-14014 December 1989 LER 89-038-00:on 891114,reactor Trip Occurred as Result of Inadvertent Closure of Main Feedwater Isolation Valve.Caused by Personnel Error.Disciplinary Action Taken Against Individual & Senior Mgt Personnel Put on shift.W/891214 Ltr ML19351A4651989-12-11011 December 1989 LER 89-021-00:on 891111,when Low Level Radwaste Water in Waste Condensate Tank Aligned to Be Released,Discovered That Radiation Monitor Inoperable for Duration of Release.Caused by Personnel Error.Procedure revised.W/891211 Ltr ML19332F6171989-12-11011 December 1989 LER 89-037-00:on 891110,reactor Trip Occurred as Result of Inadvertent Grounding of Reactor Protection Sys Power Supply During Surveillance Testing.Caused by Inadequate Procedure. Procedures revised.W/891211 Ltr ML20005D6821989-12-0101 December 1989 LER 89-005-01:on 890518 & 25,damping Board Removed from Penetration Containing Cable Tray.On 890531,voids Noted in Penetration Seals.Caused by Erroneous Vendor Procedures. Penetrations Restored & Procedures revised.W/891201 Ltr ML19332E8611989-11-30030 November 1989 LER 89-034-00:on 891031,control Room Emergency Air Conditioning Sys Rendered Inoperable Due to Removing Independent Circuits from Svc.Caused by Inadequate Guidance.Procedures Revised & Circuits flagged.W/891130 Ltr 1998-10-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L8931999-10-31031 October 1999 Rev 1 to BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs ML20212L1141999-10-0101 October 1999 Safety Evaluation Granting Request for Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c 0CAN109902, Monthly Operating Repts for Sept 1999 for Arkansas Nuclear One,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Arkansas Nuclear One,Units 1 & 2.With ML20216J6271999-09-27027 September 1999 Rev 0 to CALC-98-R-1020-04, ANO-1 Cycle 16 Colr ML20212F5261999-09-22022 September 1999 SER Approving Request Reliefs 1-98-001 & 1-98-200,parts 1,2 & 3 for Second 10-year ISI Interval at Arkansas Nuclear One, Unit 1 0CAN099907, Monthly Operating Repts for Aug 1999 for Ano,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ano,Units 1 & 2. with ML20211F4281999-08-25025 August 1999 Safety Evaluation Concluding That Licensee Provided Acceptable Alternative to Requirements of ASME Code Section XI & That Authorization of Proposed Alternative Would Provide Acceptable Level of Quality & Safety 0CAN089904, Monthly Operating Repts for July 1999 for Ano,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ano,Units 1 & 2. with ML20210K8831999-07-29029 July 1999 Non-proprietary Addendum B to BAW-2346P,Rev 0 Re ANO-1 Specific MSLB Leak Rates 0CAN079903, Monthly Operating Repts for June 1999 for Ano,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Ano,Units 1 & 2. with ML20207E7231999-06-0202 June 1999 Safety Evaluation Authorizing Proposed Alternative Exam Methods Proposed in Alternative Exam 99-0-002 to Perform General Visual Exam of Accessible Areas & Detailed Visual Exam of Areas Determined to Be Suspect ML20196A0191999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Arkansas Nuclear One,Units 1 & 2.With ML20196A6251999-05-31031 May 1999 Non-proprietary Rev 0 to TR BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs ML20195D1991999-05-28028 May 1999 Probabilistic Operational Assessment of ANO-2 SG Tubing for Cycle 14 ML20206M7711999-05-11011 May 1999 SER Accepting Relief Request from ASME Code Section XI Requirements for Plant,Units 1 & 2 0CAN059903, Monthly Operating Repts for Apr 1999 for Ano,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ano,Units 1 & 2. with ML20206F0691999-04-29029 April 1999 Safety Evaluation Accepting Licensee Re ISI Plan for Third 10-year Interval & Associated Requests for Alternatives for Plant,Unit 1 ML20205M6941999-04-12012 April 1999 Safety Evaluation Granting Relief for Second 10-yr Inservice Inspection Interval for Plant,Unit 1 ML20205D6061999-03-31031 March 1999 Safety Evaluation Supporting Licensee Proposed Approach Acceptable to Perform Future Structural Integrity & Operability Assessments of Carbon Steel ML20205R6351999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Ano,Units 1 & 2. with ML20205D4711999-03-26026 March 1999 SER Accepting Util Proposed Alternative to Employ Alternative Welding Matls of Code Cases 2142-1 & 2143-1 for Reactor Coolant System to Facilitate Replacement of Steam Generators at Arkansas Nuclear One,Unit 2 ML20204B1861999-03-15015 March 1999 Safety Evaluation Authorizing Licensee Request for Alternative to Augmented Exam of Certain Reactor Vessel Shell Welds,Per Provisions of 10CFR50.55a(g)(6)(ii)(A)(5) 0CAN039904, Monthly Operating Repts for Feb 1999 for Ano,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Ano,Units 1 & 2. with ML20212G6381999-02-25025 February 1999 Ano,Unit 2 10CFR50.59 Rept for 980411-990225 ML20203E4891999-02-11011 February 1999 Rev 1 to 97-R-2018-03, ANO-2,COLR for Cycle 14 ML20199F0351998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Ano,Units 1 & 2 ML20198M7841998-12-29029 December 1998 SER Accepting Util Proposal to Use ASME Code Case N-578 as Alternative to ASME Code Section Xi,Table IWX-2500 for Arkansas Nuclear One,Unit 2 0CAN129805, LER 98-S02-00:on 981124,security Officer Found Not to Have Had Control of Weapon for Period of Approx 3 Minutes Due to Inadequate self-checking to Ensure That Weapon Remained Secure.All Security Officers Briefed.With1998-12-11011 December 1998 LER 98-S02-00:on 981124,security Officer Found Not to Have Had Control of Weapon for Period of Approx 3 Minutes Due to Inadequate self-checking to Ensure That Weapon Remained Secure.All Security Officers Briefed.With ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20198D2441998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Ano,Units 1 & 2. with ML20199F7401998-11-16016 November 1998 Rev 9 to ANO-1 Simulator Operability Test,Year 9 (First Cycle) ML20195B4801998-11-0707 November 1998 Rev 20 to ANO QA Manual Operations ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program 0CAN119808, Monthly Operating Repts for Oct 1998 for Ano,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Ano,Units 1 & 2. with ML20197H0741998-10-29029 October 1998 Rev 1 to Third Interval ISI Program for ANO-1 ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual ML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20154J2471998-10-0909 October 1998 SER Accepting Inservice Testing Program,Third ten-year Interval for License DPR-51,Arkansas Nuclear One,Unit 1 0CAN109806, Monthly Operating Repts for Sept 1998 for ANO Units 1 & 2. with1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for ANO Units 1 & 2. with ML20154E2171998-09-28028 September 1998 Follow-up Part 21 Rept Re Defect with 1200AC & 1200BC Recorders Built Under Westronics 10CFR50 App B Program. Westronics Has Notified Bvps,Ano & RBS & Is Currently Making Arrangements to Implement Design Mods 0CAN099803, Monthly Operating Repts for Aug 1998 for ANO Units 1 & 2. with1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for ANO Units 1 & 2. with ML20237B7671998-08-19019 August 1998 ANO REX-98 Exercise for 980819 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20236X2351998-08-0505 August 1998 Part 21 Rept Re Defect Associated W/Westronics 1200AC & 1200BC Recorders Built Under Westronics 10CFR50,App B Program.Beaver Valley,Arkansas Nuclear One & River Bend Station Notified.Design Mod Is Being Developed 0CAN089804, Monthly Operating Repts for July 1998 for Ano,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Ano,Units 1 & 2 ML20196C7831998-07-30030 July 1998 Summary Rept of Results for ASME Class 1 & 2 Pressure Retaining Components & Support for ANO-1 ML20155H7161998-07-15015 July 1998 Rev 1 to 96-R-2030-02, Revised Reactor Vessel Fluence Determination ML20236R0531998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Ano,Units 1 & 2 ML20249B7791998-06-22022 June 1998 Part 21 Rept Re Findings,Resolutions & Conclusions Re Failure of Safety Related Siemens 4KV,350 MVA,1200 a Circuit Breakers to Latch Closed ML20249B5091998-06-15015 June 1998 SG ISI Results for Fourteenth Refueling Outage 1999-09-30
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l s Arkansas Power & Ught Company l
, . 42 V cs!Captal l Lee Rack AR 72203 l Tel 501377 4000 j H
1 l
March 1, 1990 l 2CAN639004 ;
i U. S. Nuclear Regulatory Commission Document Control Desk Mail Station P1-137 l Washington, D. C. 20555
SUBJECT:
Arkansas Nuclear One - Unit 2 #
Docket No. 50-368 License No. NPF-6 Licensee Event Report No. 50-368/89-026-00 Gentlemen: ,
In accordance with 10CFR50.73(a)(2)(ii)(B), attached is the subject report concerning reactor building cooler nozzles which could be subjected to ;
unacceptable stresses during a seismic event due to excessive gaps in piping supports which resulted from an inadequate design technique. >
Very truly yours, I .)
. C. Ewihg r
- i. General Manager, '
l Technical Support and Assessment l
l ECE/RHS/sgw l attachment cc: Regional Administrator l Region IV '
U. S. Nuclear Regulatory Commission 611 Ryan Plaza Drive, Suite 1000 Arlington, TX 76011 INPO Records Center 1500 Circle 75 Parkway Atlanta, GA 30339-3064 9003070138 900301 h 413 N
l PDR ADOCK 05000368 d l
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PDC F
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?.. F m 1062.01A e .
NRC Fona 366 (9-83) U.S. Nuclear Regulatory C ssion Approved OMB No. 315 0104 Expires: 8/31/85 LICENSEE EVENT REPORT (L E R)
FACILITY NAME (1) Arkansas Nuclear One, Unit Two l DOCKET NUltER (2) lPAGE (3) 10151010101 31 61 Bill 0Fl013 TITLE (4) Reactor Building Cooler Nozzles Could be Subjected to Unacceptale 5 tresses During a Seisele Event Due to Excessive Gaps in Piping Supports Which Resulted From an Inadequate Design Technique
_ EVENT DATE (5) ,ER NUIWER (6) REPORT DATJ (7) 6 g I hiequentiell 1 Revision OTHER FACILITIE5 INVOLVED (8) l Month Day Year Year Number Month, Day l
i Number Year Facility Names Docket Nunber(s1 i i 0 5 0 0 0 11 1 11 2 81 9 81 9 --
' Of 21 6 --I 01 0 01 3 l 01 1 1 91 Of DPERA ING 0 5 0 0 0 lTH MODE J9) 5 5 RLFUMI 15 Summa ILU PUR5UANT D THE REQUIntntnis OF 10 CFR 5:
- PDWER (Check one or more of the followino) (11) -
20.402(b) l 20,405(c) 50.73(a)(2)(iv) l 73,71(b)
C i
LEVEll. 20.405(a)(1)(1)
-(10) 1 010101 1 20.405(a)(1)(11)
_t 50 36(c)(1)
[ 50.73(a)(2)(v) [l73.71(c)
_1 50.36(c)(2) 1 50.73(a)(2)(v11) Other (Specify in I l 20.40$(a)(1)(iii) l
~l 50.73(a)(2)(1) ~ l 50.73(a)(2)(v111)(A). ~l Abstract below and I 20.405(a)(1)(iv) 1
~ l 50.73(a)(2)(vi11)(B)l in Text, NRC Form Il[I20.405(a)(1)(v) l3l150.73(a)(2)11) 50.73 :a)(2) 111) l~l 50.73(a)(2)(x) l 366A)
Name LICENSEE CONTACT FOR THIS LER (12) l _ Telephone Number Area l Larry A. Taylor, Nuclear Safety and Licensing Specialist Code 51011 916141 13l11010 COMPLETE ONE LINE FOR EACH COMPONtKT FAILURE DE5CRIBED IN THIS REPORT (h3)
Reportable '
) Reportable Cause Systee Component Manufacturer to NPROS Cause System Component Manufacturer. to NPROS !
I I l i I I I I I I l l 1 I l l I I 1 I I I l I i l I i SUPI LRtNT ret' ORT EXPECTED (14) EXPECTED Month Day (Year l~l Yes (if ves, complete Expected Submission Date) lifl No SUBMISSION L DATE (15) 11 I I AB5 TRACT (Limit to 1400 spaces, f.e., approximately fifteen single-space typewrf, ten lines) (L6)
On November 12, 1989, while performing an as built walkdown of the Service Water systes piping in the Reactor Building (RB) during refueling outage 2R7, Engineering personnel identified gaps in the piping supports on the supply and return piping for the containment coolers which were in excess of the original design gap allowables. An initial engineering review of the condition, which considered that the affected piping was a low temperature system (i.e., design temperature of 150 degrees), determined that the system remained operable pending further engineering evaluation. However, the identified niping support gap deficiencies were corrected by the addition of shims before restart from the outage.
the subsequent engineering evaluation, which was completed on January 30, 1990, determined that the ,
inlet nozzles on 2VCC-2A and the outlet nozzles on 2VCC-2B could have experienced higher loads than -
they were designed for if a design basis seistic event had occurred while the gaps existed. The cause of this condition was determined to be an inadequate design technique used in the original design of the piping supports. This technique provided support gaps to allow for free thermal growth during i
heatup, but failed position after to consider that the system piping could not be relied upon to return to its original cooldown.
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. i Form 1062.01B i NRC Fors 366A U.S. Nuclear Regulatory Commission 1 (9-83) Approved OMB No. 3150-0104 Expires: 8/31/85 LICENSEE EVENT REPORT (LER) TEXT CONTINUATIDN i FACILITY NAME (1) lDD RET NJEER (2) l JR NUMBER (61 l FAGE (3) [
l l l 1 5eouentiali i Revisioni '
Arkansas Nuclear One, Unit Two l l Year Number Number l 101510!0101 31 61 BI 86 9 --
01 21 6 --
01 of01210Fl013 TEXT (If mo n space is required, use additional NRC form 366A's) (17) j A. Plant Status 1 At the time of discovery of this condition, Arkansas Nuclear One, Unit Two (ANO-2) was in the cold ,
shutdown condition (Mode 5). Refueling outage 2R7 was in progress, f B. Event Description On November 12, 1989, while performing an as built walkdown of the Service Water system (SW) [BI) l piping in the Reactor Building (RB) in accordance with the Isometric Update Project, Engineering e personnel identified gaps in the piping supports on the supply and return piping for the containment ;
coolers (2VCC-2A, B, C, and D) which were in excess of the original design pap allowables. An initial engineering review of the condition, which considered that the affacted piping was a low temperature system (i.e., design temperature of 150 degrees) and excessive thermal stresses were ,
not likely, determined that the system remained operable pending further engineering evaluation. l However, prior to restart from the outage, the support gap deficiencies were corrected to bring ,
them within original seismic design values. The subsequent engineering evalu; tion, which was completed on January 30, 1990, detersined that the inlet nozzles on 2VCC 2A and the outlet nozzles on 2VCC 28 could have experienced higher loads than design if a design balls seismic event had occurred while the gaps existed.
Three of the supports on the inlet piping for 2VCC-2A which had excessive gaps were located near each other and also close to the cooler inlet nozzles. The evaluation determined that the loads from these supports would most likely be transferred to the cooler inlet nozzles during a seismic event and that these loads could exceed acceptable levels.
There were six supports on the return line from 2VCC-2B which were identified as having excessive gaps. Three of these supports were located close to the cooler. The evaluation determined thet during a seismic event the loads from these supports would probably be transferred to the cooler ,
outlet nozzles, resultIng in stresses in excess of acceptable levels.
Considering the probable transfer of loads from the piping supports to the cooler nozzles during a seismic event, ANO determined (using engineering judgement) that these lines did not meet load allowables while the gaps existed. This judgement was made based on the assumption that the cooler nozzles would not have met load allowables if the supports with excessive gaps were removed from the analysis. It is possible that a detailed computer analysis could prove the system to be operable, however, it was conservatively declared inoperable.
C. Safety $1gnificance The Reactor Building Heat Removal Systems consist of the four 25 percent capacity containment coolers and two 50 percent capacity containment spray pumps and their associated spray headers.
These cooling systems are designed with sufficient redundancy so that any of the following combinations of equipment will provide adequate heat removal to attenuate the post accident temperature and pressure conditions which would be imposed upon the RB following a Loss of Coolant Accident (LOCA) or a Main Steam Line Break (MSLB).
- All four containment coolers
- Both Reactor Building Spray systems
The significance of this condition is minimized by the fact that sufficient cooling system redundancy is available to adequately cool the RB following a LOCA or MSLB, even if 2VCC-2A and B were unavailable. In addition, the plant's safety analysis does not consider the occurrence of a LOCA or MSLB, which would require RB cooler operation, concurrent with a seismic event.
D. Root Cause The root cause of this condition was determined to be inadequate design of the piping supports.
A review of the original qualifying calculation for the SW system indicated that many of the piping supports were designed with specific gaps which would allow free thermal growth during heatup but would restrain the pipe during a seismic event. The original design attempted this by limiting gaps to a maximum of 1/8 inch and a minimum of 1/16 inch. Caps were specified on a
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~ . . s Fore 1062.018 .
NRC Fom 366A U.S. Nuclear Regulatory Commission (9 83) Approved Ole No. 3150-010*,
LICENSEE EVENT REPORT (LER) TEXT CONT!NUAT!DN ,
i FACILITY PURE (1) l DOCKET N M R (2) l LER NMR (6) l PAGE (3) '
l l 1 l%quentiall l Revision l Arkansas Nuclear One, Unit Two l l Year Number Number l ,
10151010101 31 61 81 81 9 --
01 21 6 --
01 Ol013IDF1013 T[KT (If more space is required, use additional NRC Fom 366A's) (17) particular side of the piping based on the predicted direction of themal movement. This design didn't consider that piping systems tend to ' creep' during their heatup and cooldown cycles and cannot be relied upon to return to the exact position in which they were installed. This technique of modeling piping systees to take credit for gaps in the pipe supports is unique to the piping system discussed in this report. ANO has not identified the use of this piping system modeling technique (i.e., taking credit for gaps in piping supports) in the design of other plant systems.
E. Basis for Reportability
$1nce the excessive piping support gaps resulted in a condition in which the cooler nozzles could have experienced loads greater than design during a seismic event, this event is considered !
reportable pursuant to 10CFR50.73(a)(2)(11)(B) as a condition outside the design basis of the i plant. .
This condition was also reported in accordance with 20CFR50.72 on January 30, 1990.
F. Corrective Action The isometric update project, which identified the deficiencies discussed in this report, was initiated in 1987 to identify and resolve ex16 ting discrepancies between design drawings and the as-built condition of the plant. This project utilizes field walkdowns of piping systems as well as piping analyses reviews and has been proven effective in identifying suppcrt deficiencies.
All of the identified piping support gap deficiencies were corrected by the addition cf shiss [
before restart from the 2R7 outage.
Although the current configuration is judged to be operable, the design of this piping system will be evaluated using conventional design techniques to eliminate this unique model'ing approtch.
G Additional Information A similar event in which an inadequate modeling technique resulted in inadequate piping supports was reported in LER 50 313/88 030-00.
Energy Industry Identification System (E!!S) codes are indicated in the text as (xx). r I !