ML19289G226

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LER 79-054/03L-0 on 790716:main Feedwater Valve a Failed Shut.Caused by Frozen Inboard Bearing on Valve Operator Motor.Bearing Replaced,Motor Reinstalled & Valve stroke-tested Satisfactorily.Valve Declared Operable
ML19289G226
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 08/02/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19289G224 List:
References
LER-79-054-03L, LER-79-54-3L, NUDOCS 7908070576
Download: ML19289G226 (1)


Text

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