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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20045B3021993-06-11011 June 1993 LER 93-001-00:on 930513,discovered That One Channel of Rvlms Inoperable Since Probe Replaced in Oct 1992.On 930507, Discovered That Two Sensors in Rvlms Indicating Wet.Caused by Design Error.Wiring Polarity corrected.W/930611 Ltr ML20024H2281991-05-21021 May 1991 LER 91-003-00:on 910421,actuation of EFW Sys During Plant Heatup Occurred Due to Low Once Through Steam Generator Level.Caused by Leaking Feedwater Recirculation Valve.Plant Startup Procedure OP 1102.02 Will Be revised.W/910521 Ltr ML20024H0861991-05-10010 May 1991 LER 91-002-00:on 910410,inadvertent Actuations of Combined Control Emergency Ventilation Sys Occurred.Caused by Transient Noise Spike.Mod Will Be Completed by 910531 to Install Time Delay in Actuation circuitry.W/910510 Ltr ML20024G9781991-05-10010 May 1991 LER 90-004-01:on 900531,discovered Degraded Fire Barrier Penetration During Insp Per Generic Ltr 86-10.Caused by Failure to Identify Adequate Fire Barrier Seal During 1983 Plant Walkdown.Fire Watch posted.W/910510 Ltr ML20029C3771991-03-22022 March 1991 LER 91-006-00:on 910222,core Protection Calculator Reactor Coolant Sys Flow Channels Not Being Calibrated within Tech Spec.Caused by Personnel Error.Operations Manager Counseled Operators Involved in event.W/910322 Ltr ML20029B1331991-02-27027 February 1991 LER 91-004-00:on 910125,control Room Radiation Monitor Alarm/Trip Setpoint Greater than Normal.Caused by Personnel Error.Operations Manager Will Counsel Shift Supervisors & Night Order Will Be posted.W/910227 Ltr ML20028H6841991-01-21021 January 1991 LER 90-021-00:on 901222,potential RCS Leak Noted in Area of Pressurizer Upper Level Instrument Nozzle.Caused by Pure Water Stress Corrosion Cracking.New Nozzle Installed Into Penetration from Shell OD.W/910121 Ltr ML20043C6801990-05-31031 May 1990 LER 89-025-01:on 891221,identified That Portion of Wall Located in Auxiliary Bldg Had Not Been Previously Identified as Tech Spec Fire Barrier.Caused by Personnel Error.Wall Being Upgraded to Tech Spec status.W/900531 Ltr ML20043C3781990-05-30030 May 1990 LER 90-012-00:on 900430,18 Month Channel Calibr of Liquid Radwaste Effluent Line Flow Monitor Not Performed as Required.Caused by Inadequate Controls to Ensure Followup Actions Taken in Timely Manner.Amends revised.W/900530 Ltr ML20043C0361990-05-23023 May 1990 LER 90-003-01:on 900423,discovered That Incorrect Monitoring Instrumentation for Radiological Effluent Ventilation Sys Utilized to Comply W/Tech Specs.Caused by Mgt Oversight.Logs Process Monitors Will Not Be used.W/900523 Ltr ML20043A7411990-05-17017 May 1990 LER 90-004-01:on 900212,discovered That Backwater Valve in Floor Drain Pipe in Emergency Feedwater Pump Room Missing. Caused by Inadequate Configuration Control.Backwater Pumps Installed & Will Be Included in Maint program.W/900517 Ltr ML20042F7681990-05-0101 May 1990 LER 90-002-01:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Errors in Original Calculation Not Identified.Calibr Procedures revised.W/900501 Ltr ML20042F7751990-05-0101 May 1990 LER 90-010-00:on 900401,personnel Failed to Complete Control Element Assembly Position Log.Caused by Surveillance Program Deficiencies & Lack of Mgt Involvement.Shift Briefing Completed & Procedure Change incorporated.W/900501 Ltr ML20042E1981990-04-10010 April 1990 LER 90-008-00:on 900311,determined That Seal Leakage Test for Containment Personnel Air Lock Had Not Been Performed, Per Tech Specs.Caused by Personnel Error.Procedure Revs Initiated & Personnel counseled.W/900410 Ltr ML20012F5051990-04-0505 April 1990 LER 89-027-00:on 891005,determined That Leakage Rate for Containment Isolation Check Valve in Excess of Leakage Rate Allowed Per Tech Specs.Caused by Loose Weld Slag in Valve Seat Area.Valve Cleaned & reassembled.W/900405 Ltr ML20012F5031990-04-0505 April 1990 LER 90-007-00:on 900306,RCS Charging Line Rendered Inoperable Due to Deficient Piping Support Weld.Caused by Inadequate Work Controls & post-installation Insp Processes. Field Walkdowns & Weld Insps initiated.W/900405 Ltr ML20012F5741990-04-0404 April 1990 LER 90-006-00:on 900305,instrumentation Channels Declared Inoperable,Resulting in Manual Actuation of Reactor Protection Sys.Caused by Procedural Deficiencies.Functional Tests of Log Power Level Channels performed.W/900404 Ltr ML20012C7221990-03-14014 March 1990 LER 90-004-00:on 900212,identified That No Backwater Valve Located in Floor Drain Pipe in One of Emergency Feedwater Pump Rooms.Caused by Inadequate Configuration Control. Valves Installed on 900215.W/900314 Ltr ML20012C1821990-03-12012 March 1990 LER 85-029-00:on 850520,unusual Motor Vibrations Identified on Svc Water Pump 2PM4A.On 861028,high Vibrations Noted on Upper Motor Bearings of Pump 2PM4B.Caused by Improper Installation.New Bearings installed.W/900312 Ltr ML20012B7271990-03-0808 March 1990 LER 89-049-01:on 891220,discovered That Okonite T-95 Tape Not Used to Tape Internal Motor Lead Connections for Main Feedwater Containment Isolation Valves.Caused by Personnel Error.Valves Taped According to Design drawing.W/900308 Ltr ML20012B5701990-03-0505 March 1990 LER 90-003-00:on 900201,failure to Perform Monthly Source Check Surveillance on Three Radiation Process Monitors Occurred.Caused by Inadequate Procedure Change by Personnel. Source Check on Monthly Basis implemented.W/900305 Ltr ML20011F6741990-03-0202 March 1990 LER 90-002-00:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Caused by Incorrect Static Pressure Assumption.Trip Setpoint Bistable increased.W/900302 Ltr ML20011F6781990-03-0101 March 1990 LER 89-026-00:on 891112,gaps in Piping Supports on Supply & Return Piping for Containment Coolers Identified.Caused by Inadequate Design Technique Used in Original Support Design. Shims Added Before Restart from outage.W/900301 Ltr ML20011F5831990-02-27027 February 1990 LER 89-022-01:on 891114,normal Offsite Power Feeder Breaker to 4,160-volt Ac ESF Bus Opened,Resulting in Loss of Power to Bus 2A3.Caused by Inadequate post-maint Test Controls. Test Switch Opened & Job Order changed.W/900227 Ltr ML20011F7311990-02-23023 February 1990 LER 90-001-00:on 900126,identified That Required Visual Insps of Containment Bldg After Entry Made Not Documented as Being Performed.Caused by Inadequate Procedural Guidance. Administrative Controls to Be established.W/900226 Ltr ML20006D7391990-02-0606 February 1990 LER 89-034-01:on 891031,determined That Tech Spec 3.9.1 Had Likely Been Violated Re Independent Circuits of Control Room Emergency Air Conditioning Sys.Caused by Inadequate Guidance Re Equipment Svc Removal.Procedures revised.W/900206 Ltr ML20011E2371990-01-31031 January 1990 LER 89-012-01:on 890626,RCS Backleakage Through Safety Injection Sys Check Valve Occurred Three Times.Caused by Missing Rollpins Which Connect Valve Disc to Valve Disc Shaft.Rollpins Replaced & Valves reassembled.W/900131 Ltr ML20011E2291990-01-31031 January 1990 LER 89-039-01:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Latch Mechanism Missing. Caused by Abnormally High Differential Pressure Across Door. Ventilation Sys Flow Balance performed.W/900131 Ltr ML20011E1451990-01-30030 January 1990 LER 89-024-00:on 891231,loose Terminal in Feedwater Control Sys Cabinet Resulted in Reactor Trip.Caused by Loose Connection on Terminal.Loose Connection Reterminated properly.W/900130 Ltr ML20006C1451990-01-29029 January 1990 LER 89-048-00:on 891228,automatic Reactor Trip & ESF Actuation Occurred as Result of Loss of All Main Feedwater Flow Due to Inadvertent Tripping of Main Feedwater Pump. Caused by Personnel error.O-rings replaced.W/900129 Ltr ML19354E3331990-01-22022 January 1990 LER 89-025-00:on 891221,two Piping Penetrations Located in Barrier Not Surveilled as Required by Tech Specs.Caused by Personnel Error.Fire Watch Posted When Necessary Per Tech Spec.W/900122 Ltr ML20006A8661990-01-22022 January 1990 LER 89-041-00:on 891221,automatic Actuation of Emergency Feedwater Sys Initiated.Caused by Lack of Adequate Procedural Guidance.Valve Positioners CV-2623 & CV-2673 Adjusted & Guidance Procedures developed.W/900122 Ltr ML20006A8671990-01-22022 January 1990 LER 89-042-01:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900122 Ltr ML20005F1551990-01-18018 January 1990 LER 89-023-01:on 891117,noted That Channel a Not Responding to Change in Power Level & Declared Inoperable.Caused by Defective Preamplifier.Evaluation of Sys Design & Channel Functional Test initiated.W/900108 Ltr ML20006B6461990-01-18018 January 1990 LER 89-047-00:on 891219,RCS Temp Increased Above 250 F W/ Oxygen Concentration Greater than Tech Specs Limit.Caused by Inadequate Procedural Guidance.Plant Startup Procedure Revised to Require Chemistry Dept signoff.W/900118 Ltr ML19354D8291990-01-15015 January 1990 LER 89-044-00:on 891214,incorrect Assumptions & Calculational Errors Identified for Low Pressure Injection & Reactor Bldg Spray Pumps When Aligned to Take Suction from Reactor Bldg sump.W/900115 Ltr ML20005G1681990-01-0909 January 1990 LER 89-045-00:on 891210,discovered That U-bolt Supports on Two Containment Isolation Valves in Containment Bldg Not Installed & Pressurizer Sample Lines & Valves Considered Inoperable.Missing U-bolts installed.W/900109 Ltr ML20005F1481990-01-0808 January 1990 LER 89-042-00:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900108 Ltr ML20005F1571990-01-0808 January 1990 LER 89-043-00:on 891208,discovered That Approx 50% of One Nut Ring Half Beneath Reactor Vessel Nozzle Flange Corroded Away.Caused by Gradual Deterioration of Gasket Matl.Design Change implemented.W/900108 Ltr ML20005F2071990-01-0404 January 1990 LER 89-040-00:on 891205 & 06,automatic Actuations of Emergency Diesel Generator Occurred as Result of Loss of Power to 480-volt ESF Bus.Caused by Personnel Error During Bus Transfer.Mgt Briefings conducted.W/900104 Ltr ML20005F0471990-01-0303 January 1990 LER 89-046-00:on 891204,reactor Bldg Isolation Valves Rendered Inoperable Due to Deficient Welds on Piping Supports Which Were Installed During Initial Plant Const. Deficient Supports Repaired Prior to restart.W/900103 Ltr ML20011D2521989-12-18018 December 1989 LER 89-039-00:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Missing Latch Mechanism. Caused by Extensive Use During 56-day Refueling Outage.More Frequent Insps of Door Condition to Be done.W/891218 Ltr ML20011D2501989-12-18018 December 1989 LER 89-023-00:on 891117,approach to Criticality Commenced After Seventh Refueling Outage W/Logarithmic Power Level Channels Inoperable.Caused by Electrical Noise in Circuitry. Defective Preamplifier replaced.W/891218 Ltr ML19351A6731989-12-14014 December 1989 LER 89-022-00:on 891114,inadequate post-maint Test Controls Resulted in de-energizing 4,160 Volt Ac ESFs Electric Bus Uexpectedly.Caused by Inadequate post-maint Test Controls. Job Order Instructions changed.W/891214 Ltr ML19354D5521989-12-14014 December 1989 LER 89-038-00:on 891114,reactor Trip Occurred as Result of Inadvertent Closure of Main Feedwater Isolation Valve.Caused by Personnel Error.Disciplinary Action Taken Against Individual & Senior Mgt Personnel Put on shift.W/891214 Ltr ML19351A4651989-12-11011 December 1989 LER 89-021-00:on 891111,when Low Level Radwaste Water in Waste Condensate Tank Aligned to Be Released,Discovered That Radiation Monitor Inoperable for Duration of Release.Caused by Personnel Error.Procedure revised.W/891211 Ltr ML19332F6171989-12-11011 December 1989 LER 89-037-00:on 891110,reactor Trip Occurred as Result of Inadvertent Grounding of Reactor Protection Sys Power Supply During Surveillance Testing.Caused by Inadequate Procedure. Procedures revised.W/891211 Ltr ML20005D6821989-12-0101 December 1989 LER 89-005-01:on 890518 & 25,damping Board Removed from Penetration Containing Cable Tray.On 890531,voids Noted in Penetration Seals.Caused by Erroneous Vendor Procedures. Penetrations Restored & Procedures revised.W/891201 Ltr ML19332E8611989-11-30030 November 1989 LER 89-034-00:on 891031,control Room Emergency Air Conditioning Sys Rendered Inoperable Due to Removing Independent Circuits from Svc.Caused by Inadequate Guidance.Procedures Revised & Circuits flagged.W/891130 Ltr 1998-10-22
[Table view] Category:RO)
MONTHYEARML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20045B3021993-06-11011 June 1993 LER 93-001-00:on 930513,discovered That One Channel of Rvlms Inoperable Since Probe Replaced in Oct 1992.On 930507, Discovered That Two Sensors in Rvlms Indicating Wet.Caused by Design Error.Wiring Polarity corrected.W/930611 Ltr ML20024H2281991-05-21021 May 1991 LER 91-003-00:on 910421,actuation of EFW Sys During Plant Heatup Occurred Due to Low Once Through Steam Generator Level.Caused by Leaking Feedwater Recirculation Valve.Plant Startup Procedure OP 1102.02 Will Be revised.W/910521 Ltr ML20024H0861991-05-10010 May 1991 LER 91-002-00:on 910410,inadvertent Actuations of Combined Control Emergency Ventilation Sys Occurred.Caused by Transient Noise Spike.Mod Will Be Completed by 910531 to Install Time Delay in Actuation circuitry.W/910510 Ltr ML20024G9781991-05-10010 May 1991 LER 90-004-01:on 900531,discovered Degraded Fire Barrier Penetration During Insp Per Generic Ltr 86-10.Caused by Failure to Identify Adequate Fire Barrier Seal During 1983 Plant Walkdown.Fire Watch posted.W/910510 Ltr ML20029C3771991-03-22022 March 1991 LER 91-006-00:on 910222,core Protection Calculator Reactor Coolant Sys Flow Channels Not Being Calibrated within Tech Spec.Caused by Personnel Error.Operations Manager Counseled Operators Involved in event.W/910322 Ltr ML20029B1331991-02-27027 February 1991 LER 91-004-00:on 910125,control Room Radiation Monitor Alarm/Trip Setpoint Greater than Normal.Caused by Personnel Error.Operations Manager Will Counsel Shift Supervisors & Night Order Will Be posted.W/910227 Ltr ML20028H6841991-01-21021 January 1991 LER 90-021-00:on 901222,potential RCS Leak Noted in Area of Pressurizer Upper Level Instrument Nozzle.Caused by Pure Water Stress Corrosion Cracking.New Nozzle Installed Into Penetration from Shell OD.W/910121 Ltr ML20043C6801990-05-31031 May 1990 LER 89-025-01:on 891221,identified That Portion of Wall Located in Auxiliary Bldg Had Not Been Previously Identified as Tech Spec Fire Barrier.Caused by Personnel Error.Wall Being Upgraded to Tech Spec status.W/900531 Ltr ML20043C3781990-05-30030 May 1990 LER 90-012-00:on 900430,18 Month Channel Calibr of Liquid Radwaste Effluent Line Flow Monitor Not Performed as Required.Caused by Inadequate Controls to Ensure Followup Actions Taken in Timely Manner.Amends revised.W/900530 Ltr ML20043C0361990-05-23023 May 1990 LER 90-003-01:on 900423,discovered That Incorrect Monitoring Instrumentation for Radiological Effluent Ventilation Sys Utilized to Comply W/Tech Specs.Caused by Mgt Oversight.Logs Process Monitors Will Not Be used.W/900523 Ltr ML20043A7411990-05-17017 May 1990 LER 90-004-01:on 900212,discovered That Backwater Valve in Floor Drain Pipe in Emergency Feedwater Pump Room Missing. Caused by Inadequate Configuration Control.Backwater Pumps Installed & Will Be Included in Maint program.W/900517 Ltr ML20042F7681990-05-0101 May 1990 LER 90-002-01:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Errors in Original Calculation Not Identified.Calibr Procedures revised.W/900501 Ltr ML20042F7751990-05-0101 May 1990 LER 90-010-00:on 900401,personnel Failed to Complete Control Element Assembly Position Log.Caused by Surveillance Program Deficiencies & Lack of Mgt Involvement.Shift Briefing Completed & Procedure Change incorporated.W/900501 Ltr ML20042E1981990-04-10010 April 1990 LER 90-008-00:on 900311,determined That Seal Leakage Test for Containment Personnel Air Lock Had Not Been Performed, Per Tech Specs.Caused by Personnel Error.Procedure Revs Initiated & Personnel counseled.W/900410 Ltr ML20012F5051990-04-0505 April 1990 LER 89-027-00:on 891005,determined That Leakage Rate for Containment Isolation Check Valve in Excess of Leakage Rate Allowed Per Tech Specs.Caused by Loose Weld Slag in Valve Seat Area.Valve Cleaned & reassembled.W/900405 Ltr ML20012F5031990-04-0505 April 1990 LER 90-007-00:on 900306,RCS Charging Line Rendered Inoperable Due to Deficient Piping Support Weld.Caused by Inadequate Work Controls & post-installation Insp Processes. Field Walkdowns & Weld Insps initiated.W/900405 Ltr ML20012F5741990-04-0404 April 1990 LER 90-006-00:on 900305,instrumentation Channels Declared Inoperable,Resulting in Manual Actuation of Reactor Protection Sys.Caused by Procedural Deficiencies.Functional Tests of Log Power Level Channels performed.W/900404 Ltr ML20012C7221990-03-14014 March 1990 LER 90-004-00:on 900212,identified That No Backwater Valve Located in Floor Drain Pipe in One of Emergency Feedwater Pump Rooms.Caused by Inadequate Configuration Control. Valves Installed on 900215.W/900314 Ltr ML20012C1821990-03-12012 March 1990 LER 85-029-00:on 850520,unusual Motor Vibrations Identified on Svc Water Pump 2PM4A.On 861028,high Vibrations Noted on Upper Motor Bearings of Pump 2PM4B.Caused by Improper Installation.New Bearings installed.W/900312 Ltr ML20012B7271990-03-0808 March 1990 LER 89-049-01:on 891220,discovered That Okonite T-95 Tape Not Used to Tape Internal Motor Lead Connections for Main Feedwater Containment Isolation Valves.Caused by Personnel Error.Valves Taped According to Design drawing.W/900308 Ltr ML20012B5701990-03-0505 March 1990 LER 90-003-00:on 900201,failure to Perform Monthly Source Check Surveillance on Three Radiation Process Monitors Occurred.Caused by Inadequate Procedure Change by Personnel. Source Check on Monthly Basis implemented.W/900305 Ltr ML20011F6741990-03-0202 March 1990 LER 90-002-00:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Caused by Incorrect Static Pressure Assumption.Trip Setpoint Bistable increased.W/900302 Ltr ML20011F6781990-03-0101 March 1990 LER 89-026-00:on 891112,gaps in Piping Supports on Supply & Return Piping for Containment Coolers Identified.Caused by Inadequate Design Technique Used in Original Support Design. Shims Added Before Restart from outage.W/900301 Ltr ML20011F5831990-02-27027 February 1990 LER 89-022-01:on 891114,normal Offsite Power Feeder Breaker to 4,160-volt Ac ESF Bus Opened,Resulting in Loss of Power to Bus 2A3.Caused by Inadequate post-maint Test Controls. Test Switch Opened & Job Order changed.W/900227 Ltr ML20011F7311990-02-23023 February 1990 LER 90-001-00:on 900126,identified That Required Visual Insps of Containment Bldg After Entry Made Not Documented as Being Performed.Caused by Inadequate Procedural Guidance. Administrative Controls to Be established.W/900226 Ltr ML20006D7391990-02-0606 February 1990 LER 89-034-01:on 891031,determined That Tech Spec 3.9.1 Had Likely Been Violated Re Independent Circuits of Control Room Emergency Air Conditioning Sys.Caused by Inadequate Guidance Re Equipment Svc Removal.Procedures revised.W/900206 Ltr ML20011E2371990-01-31031 January 1990 LER 89-012-01:on 890626,RCS Backleakage Through Safety Injection Sys Check Valve Occurred Three Times.Caused by Missing Rollpins Which Connect Valve Disc to Valve Disc Shaft.Rollpins Replaced & Valves reassembled.W/900131 Ltr ML20011E2291990-01-31031 January 1990 LER 89-039-01:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Latch Mechanism Missing. Caused by Abnormally High Differential Pressure Across Door. Ventilation Sys Flow Balance performed.W/900131 Ltr ML20011E1451990-01-30030 January 1990 LER 89-024-00:on 891231,loose Terminal in Feedwater Control Sys Cabinet Resulted in Reactor Trip.Caused by Loose Connection on Terminal.Loose Connection Reterminated properly.W/900130 Ltr ML20006C1451990-01-29029 January 1990 LER 89-048-00:on 891228,automatic Reactor Trip & ESF Actuation Occurred as Result of Loss of All Main Feedwater Flow Due to Inadvertent Tripping of Main Feedwater Pump. Caused by Personnel error.O-rings replaced.W/900129 Ltr ML19354E3331990-01-22022 January 1990 LER 89-025-00:on 891221,two Piping Penetrations Located in Barrier Not Surveilled as Required by Tech Specs.Caused by Personnel Error.Fire Watch Posted When Necessary Per Tech Spec.W/900122 Ltr ML20006A8661990-01-22022 January 1990 LER 89-041-00:on 891221,automatic Actuation of Emergency Feedwater Sys Initiated.Caused by Lack of Adequate Procedural Guidance.Valve Positioners CV-2623 & CV-2673 Adjusted & Guidance Procedures developed.W/900122 Ltr ML20006A8671990-01-22022 January 1990 LER 89-042-01:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900122 Ltr ML20005F1551990-01-18018 January 1990 LER 89-023-01:on 891117,noted That Channel a Not Responding to Change in Power Level & Declared Inoperable.Caused by Defective Preamplifier.Evaluation of Sys Design & Channel Functional Test initiated.W/900108 Ltr ML20006B6461990-01-18018 January 1990 LER 89-047-00:on 891219,RCS Temp Increased Above 250 F W/ Oxygen Concentration Greater than Tech Specs Limit.Caused by Inadequate Procedural Guidance.Plant Startup Procedure Revised to Require Chemistry Dept signoff.W/900118 Ltr ML19354D8291990-01-15015 January 1990 LER 89-044-00:on 891214,incorrect Assumptions & Calculational Errors Identified for Low Pressure Injection & Reactor Bldg Spray Pumps When Aligned to Take Suction from Reactor Bldg sump.W/900115 Ltr ML20005G1681990-01-0909 January 1990 LER 89-045-00:on 891210,discovered That U-bolt Supports on Two Containment Isolation Valves in Containment Bldg Not Installed & Pressurizer Sample Lines & Valves Considered Inoperable.Missing U-bolts installed.W/900109 Ltr ML20005F1481990-01-0808 January 1990 LER 89-042-00:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900108 Ltr ML20005F1571990-01-0808 January 1990 LER 89-043-00:on 891208,discovered That Approx 50% of One Nut Ring Half Beneath Reactor Vessel Nozzle Flange Corroded Away.Caused by Gradual Deterioration of Gasket Matl.Design Change implemented.W/900108 Ltr ML20005F2071990-01-0404 January 1990 LER 89-040-00:on 891205 & 06,automatic Actuations of Emergency Diesel Generator Occurred as Result of Loss of Power to 480-volt ESF Bus.Caused by Personnel Error During Bus Transfer.Mgt Briefings conducted.W/900104 Ltr ML20005F0471990-01-0303 January 1990 LER 89-046-00:on 891204,reactor Bldg Isolation Valves Rendered Inoperable Due to Deficient Welds on Piping Supports Which Were Installed During Initial Plant Const. Deficient Supports Repaired Prior to restart.W/900103 Ltr ML20011D2521989-12-18018 December 1989 LER 89-039-00:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Missing Latch Mechanism. Caused by Extensive Use During 56-day Refueling Outage.More Frequent Insps of Door Condition to Be done.W/891218 Ltr ML20011D2501989-12-18018 December 1989 LER 89-023-00:on 891117,approach to Criticality Commenced After Seventh Refueling Outage W/Logarithmic Power Level Channels Inoperable.Caused by Electrical Noise in Circuitry. Defective Preamplifier replaced.W/891218 Ltr ML19351A6731989-12-14014 December 1989 LER 89-022-00:on 891114,inadequate post-maint Test Controls Resulted in de-energizing 4,160 Volt Ac ESFs Electric Bus Uexpectedly.Caused by Inadequate post-maint Test Controls. Job Order Instructions changed.W/891214 Ltr ML19354D5521989-12-14014 December 1989 LER 89-038-00:on 891114,reactor Trip Occurred as Result of Inadvertent Closure of Main Feedwater Isolation Valve.Caused by Personnel Error.Disciplinary Action Taken Against Individual & Senior Mgt Personnel Put on shift.W/891214 Ltr ML19351A4651989-12-11011 December 1989 LER 89-021-00:on 891111,when Low Level Radwaste Water in Waste Condensate Tank Aligned to Be Released,Discovered That Radiation Monitor Inoperable for Duration of Release.Caused by Personnel Error.Procedure revised.W/891211 Ltr ML19332F6171989-12-11011 December 1989 LER 89-037-00:on 891110,reactor Trip Occurred as Result of Inadvertent Grounding of Reactor Protection Sys Power Supply During Surveillance Testing.Caused by Inadequate Procedure. Procedures revised.W/891211 Ltr ML20005D6821989-12-0101 December 1989 LER 89-005-01:on 890518 & 25,damping Board Removed from Penetration Containing Cable Tray.On 890531,voids Noted in Penetration Seals.Caused by Erroneous Vendor Procedures. Penetrations Restored & Procedures revised.W/891201 Ltr ML19332E8611989-11-30030 November 1989 LER 89-034-00:on 891031,control Room Emergency Air Conditioning Sys Rendered Inoperable Due to Removing Independent Circuits from Svc.Caused by Inadequate Guidance.Procedures Revised & Circuits flagged.W/891130 Ltr 1998-10-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L8931999-10-31031 October 1999 Rev 1 to BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs ML20212L1141999-10-0101 October 1999 Safety Evaluation Granting Request for Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c 0CAN109902, Monthly Operating Repts for Sept 1999 for Arkansas Nuclear One,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Arkansas Nuclear One,Units 1 & 2.With ML20216J6271999-09-27027 September 1999 Rev 0 to CALC-98-R-1020-04, ANO-1 Cycle 16 Colr ML20212F5261999-09-22022 September 1999 SER Approving Request Reliefs 1-98-001 & 1-98-200,parts 1,2 & 3 for Second 10-year ISI Interval at Arkansas Nuclear One, Unit 1 0CAN099907, Monthly Operating Repts for Aug 1999 for Ano,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ano,Units 1 & 2. with ML20211F4281999-08-25025 August 1999 Safety Evaluation Concluding That Licensee Provided Acceptable Alternative to Requirements of ASME Code Section XI & That Authorization of Proposed Alternative Would Provide Acceptable Level of Quality & Safety 0CAN089904, Monthly Operating Repts for July 1999 for Ano,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ano,Units 1 & 2. with ML20210K8831999-07-29029 July 1999 Non-proprietary Addendum B to BAW-2346P,Rev 0 Re ANO-1 Specific MSLB Leak Rates 0CAN079903, Monthly Operating Repts for June 1999 for Ano,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Ano,Units 1 & 2. with ML20207E7231999-06-0202 June 1999 Safety Evaluation Authorizing Proposed Alternative Exam Methods Proposed in Alternative Exam 99-0-002 to Perform General Visual Exam of Accessible Areas & Detailed Visual Exam of Areas Determined to Be Suspect ML20196A0191999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Arkansas Nuclear One,Units 1 & 2.With ML20196A6251999-05-31031 May 1999 Non-proprietary Rev 0 to TR BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs ML20195D1991999-05-28028 May 1999 Probabilistic Operational Assessment of ANO-2 SG Tubing for Cycle 14 ML20206M7711999-05-11011 May 1999 SER Accepting Relief Request from ASME Code Section XI Requirements for Plant,Units 1 & 2 0CAN059903, Monthly Operating Repts for Apr 1999 for Ano,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ano,Units 1 & 2. with ML20206F0691999-04-29029 April 1999 Safety Evaluation Accepting Licensee Re ISI Plan for Third 10-year Interval & Associated Requests for Alternatives for Plant,Unit 1 ML20205M6941999-04-12012 April 1999 Safety Evaluation Granting Relief for Second 10-yr Inservice Inspection Interval for Plant,Unit 1 ML20205D6061999-03-31031 March 1999 Safety Evaluation Supporting Licensee Proposed Approach Acceptable to Perform Future Structural Integrity & Operability Assessments of Carbon Steel ML20205R6351999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Ano,Units 1 & 2. with ML20205D4711999-03-26026 March 1999 SER Accepting Util Proposed Alternative to Employ Alternative Welding Matls of Code Cases 2142-1 & 2143-1 for Reactor Coolant System to Facilitate Replacement of Steam Generators at Arkansas Nuclear One,Unit 2 ML20204B1861999-03-15015 March 1999 Safety Evaluation Authorizing Licensee Request for Alternative to Augmented Exam of Certain Reactor Vessel Shell Welds,Per Provisions of 10CFR50.55a(g)(6)(ii)(A)(5) 0CAN039904, Monthly Operating Repts for Feb 1999 for Ano,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Ano,Units 1 & 2. with ML20212G6381999-02-25025 February 1999 Ano,Unit 2 10CFR50.59 Rept for 980411-990225 ML20203E4891999-02-11011 February 1999 Rev 1 to 97-R-2018-03, ANO-2,COLR for Cycle 14 ML20199F0351998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Ano,Units 1 & 2 ML20198M7841998-12-29029 December 1998 SER Accepting Util Proposal to Use ASME Code Case N-578 as Alternative to ASME Code Section Xi,Table IWX-2500 for Arkansas Nuclear One,Unit 2 0CAN129805, LER 98-S02-00:on 981124,security Officer Found Not to Have Had Control of Weapon for Period of Approx 3 Minutes Due to Inadequate self-checking to Ensure That Weapon Remained Secure.All Security Officers Briefed.With1998-12-11011 December 1998 LER 98-S02-00:on 981124,security Officer Found Not to Have Had Control of Weapon for Period of Approx 3 Minutes Due to Inadequate self-checking to Ensure That Weapon Remained Secure.All Security Officers Briefed.With ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20198D2441998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Ano,Units 1 & 2. with ML20199F7401998-11-16016 November 1998 Rev 9 to ANO-1 Simulator Operability Test,Year 9 (First Cycle) ML20195B4801998-11-0707 November 1998 Rev 20 to ANO QA Manual Operations ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program 0CAN119808, Monthly Operating Repts for Oct 1998 for Ano,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Ano,Units 1 & 2. with ML20197H0741998-10-29029 October 1998 Rev 1 to Third Interval ISI Program for ANO-1 ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual ML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20154J2471998-10-0909 October 1998 SER Accepting Inservice Testing Program,Third ten-year Interval for License DPR-51,Arkansas Nuclear One,Unit 1 0CAN109806, Monthly Operating Repts for Sept 1998 for ANO Units 1 & 2. with1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for ANO Units 1 & 2. with ML20154E2171998-09-28028 September 1998 Follow-up Part 21 Rept Re Defect with 1200AC & 1200BC Recorders Built Under Westronics 10CFR50 App B Program. Westronics Has Notified Bvps,Ano & RBS & Is Currently Making Arrangements to Implement Design Mods 0CAN099803, Monthly Operating Repts for Aug 1998 for ANO Units 1 & 2. with1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for ANO Units 1 & 2. with ML20237B7671998-08-19019 August 1998 ANO REX-98 Exercise for 980819 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20236X2351998-08-0505 August 1998 Part 21 Rept Re Defect Associated W/Westronics 1200AC & 1200BC Recorders Built Under Westronics 10CFR50,App B Program.Beaver Valley,Arkansas Nuclear One & River Bend Station Notified.Design Mod Is Being Developed 0CAN089804, Monthly Operating Repts for July 1998 for Ano,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Ano,Units 1 & 2 ML20196C7831998-07-30030 July 1998 Summary Rept of Results for ASME Class 1 & 2 Pressure Retaining Components & Support for ANO-1 ML20155H7161998-07-15015 July 1998 Rev 1 to 96-R-2030-02, Revised Reactor Vessel Fluence Determination ML20236R0531998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Ano,Units 1 & 2 ML20249B7791998-06-22022 June 1998 Part 21 Rept Re Findings,Resolutions & Conclusions Re Failure of Safety Related Siemens 4KV,350 MVA,1200 a Circuit Breakers to Latch Closed ML20249B5091998-06-15015 June 1998 SG ISI Results for Fourteenth Refueling Outage 1999-09-30
[Table view] |
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+ i Arkansas Power & Ught Company .
! Arkansas Near One RoJe S. Da 137 G Russenedie, AR 70N)1 Tel 501964 3100 i
February 26, 1990 r 2CAN629007 p
U. S. Nuclear Regulatory Commission Document Control Desk Mail Station P1-137 Washington, D. C. 20555
$UBJECT: Arkansas Nuclear One - Unit 2 i
Docket No. 50-368 b License No. NPF-6 License Event Report No. 50-368/90-001-00 l
Gentlemen:
In accordance with 10CFR50.73(a)(2)(1)(B), attached is the subject report concerning inadequate procedural guidance. This condition resulted in the failure to perform a visual inspection as required by Technical Specification 4.5.2.c.2. The visual inspection verifies that no loose debris is present in the affected areas of the containment building after entry when containment integrity is established.
Very truly yours, E. C. Ewing General Manager, Technical Support and Assetsment ECE/0M/sgw attac'.iment cc: Regional Administrator Region IV U. S. Nuclear Regulatory Commission 611 Ryan Plaza Drive, Suite 1000 Arlington, TX 76011 INP0 Records Center 1500 Circle 75 Parkway Atlanta, GA 30339-3064 #
900307o33o 900223 D 11l PDR ADOCK 05000368 tb R- prge An Entergy Compaw E:
r l Fom 1062.01A NRC Form 366 U.S. Nuclear Regulatory Comeission ,
(9 83) Approved OMB No. 3150-0104 Expires: 8/31/85 LICENSEE EVENT REPORT (L E R)
FACILITY NAMI (1) Arkansas huclear One, Unit Two jDDCLET NUPSER (2) (PAGE (3) 10151010!01 31 61 81110Fl013 TITLE (4) Insoequate Procedural Guidance Resultto in Failure to Perform a Visuai Inspection as Required by Technical Specifications of Affected Areas in Containment After a Containment Entry when containsient Integrity was Established
~IVENT DATE (5) .ERWR) REPORT DATL (7) OTHFR FAC] LIT]E5 INVOLVED (8) ,
l l lJequntiell ikevision l l Monthi Day ,1 Year Year i Nunter Number ' Month Day ' Year l Facility Names Docket Number (sh i .
l j 0 5 0 0 0 01 11 21 6 0 0 91 01--l Of 01 1 --I Of U 01 21 21 31 91 01 0 5 0 0 0 '
DTTRATING TH.5 REPORT 15 5U5MITTLD PUR5UANT "O THE RIQUIREMENT5 0F 10 CFR 5:
MODE (9) I1 (Check one or more of the fellowino) (11)
POWERI l 20.402(b) l l 20.405(c) t,,,,,1 bO.73(a)(2)(iv) l~ { 73.71(b)
LEVELI l_ 20.40$(a)(1)(1) l[l50.36(c)(1) 1,,_,1 50.73(a)(2)(v) l l 73.71(c) i (10) 1110101_i 1 20.405(a)(1)(11) l 50.36(c)(2) l_l 50.73(a)(2)(vil) l ' 'f l _ l 20.405(a)(1)(111) Ql150.73(a)(2)(1) l_l 50.73(a)(2)(v111)(A)l_l Other (Specify in Abstract below and l_ l 20.40$(a)(1)(iv) l_ l 50.73(a)(2)(ii) in Text. NRC Form I l 20,405(a)(1)(v) I i 50.73da)(2)(iii) il_I 50.7?(a)(2)(x)l 50.73(a)(2)(v111)(B)l I 366A) t1CENSEE CONTACT FOR THIS LER (1?)
Name l Telephone Number l Area l Dana N111er, Nuclear Safety and Licensing Specialist l Code i 1510111916141-13111010 COMPLI TE ONE LINE FOR EACH COMPONEh7 FAILURE DESCRIBFD IN THlh REPORT C3) l l ,
i Reportablel l l l 1,Reportablel '
Causel$ystem Component IManufacturer to NPRDS Cause System Component Manufacturer to NPRDS i i i i I I I I I I I e I 1 I i 1 1 I I i
_ 1 I I I I i i l i l 1 I o I l l l l l l l l 1 SUPPLEMEN" kEPORT EkPECTLD (14) l EXPECTED Honth Day Year i SUBMISSION l 6 1 Yes (If yes complete Expected Submission Date) lil No l DATE (15) I*I h I I I D ACl (Limit to 1400 spaces, i.e., approximatel/ fifteen single-space typewritten lines) (16)
Technical Specifications require that a visual inspection of the effected areas of the containment building be performed after an entry is made while containment integrity is established. The intent of the inspection is to ensure there is no loose debris lef t in the containment building which could ,
collect in the containment building sump and cause restriction of pump suctions during LOCA conditions. ;
On January 26, 1990, it was identified that the required inspections had not been documented as being '
perfomed. The failure to document the completion of the surveillance requirement had existed since plant construction. Current ANO administrative housekeeping procedures direct employees to remove any tools, equipment, materials, trash or debris upon completion of a work activity. Therefore, the controls were in place to minimize debris or other materials when a work activity was completed in
. containment. No significant safety concerns have been identified. The root cause of this event was inadequate procedural guidance. The form used to perform containment building visual inspections was a part of the plant heatup procedure and no guidance was given in other procedures to use the form at times when containment building entries were made with containment integrity established. Administrative controls will be established to ensure a visual inspection is performed as required by Technical Specifications. This event is reportable pursuant to 10CFR$0.73(a)(2)(1)(B).
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< ' l' Fom 1062.01B NRC f ore 366A U.S. Nuclear Regulatory Commission (9-83) Approved OMB ho. 3150-0104 Expires: 8/31/85 i
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LICENSE: EVENT REPORT (LER) TEXT CONTINUATION TATTUh nAMt (1) ipocKr1 NJgbER (2) l LfR NJ4MR (6) i FAGt (3) l l t 15equentiali IRevision)
Arkansas Nuclear One, Unit Two l Number LYear -- '
humber i 10151010101 31 61 81 91 0 01 01 1 -- 01 0101210F1013 ItK1 (If more space is requitec, use t.acitional NRC Form 3664's) (17)
A. Plant Status i At the time of occurrence of this event Arkansas Nuclear One, Unit Two (AND-2) was operating at 100 percent of rated thersal power in Mode 1 (Power Operation). Reactor Coolant System (RC5) [AB) '
pressure was approximately 2250 psia and RCS temperature about 580 degrees Fahrenheit.
8, Event Description Following the completion of a containment building entry when containment building integrity is established, Technicel Specification 4.5.2.c.2 requires that a visual inspection be performed, lhe intent of this inspection is to verify that no loose debris is present in the containment butiding which could be transported to the containment building sump and cause restriction of the ;
pump suctions (i.e., High Pressure Safety Injection (HPSI) [BQJ or Low Pressure Safety injection r (LPSI) [BP) or Containment Spray (CS) [BE) pumps) during Loss of Coolant Accident (LOCA) conditions, i t- The inspection should be performed in the areas of the containment building where loose debris may be present as a result of a maintenance activity which was performed. On January 26, 1990, while reviewing Technical Specification 3.5.2 (Emergency Core Cooling System (ECCS) subsystems) and the associated surveillance requirements, as part of the operations requalification traiaing program, it was discovered that the requirements of Technjcal Specification 4.5.2.c.2 were not being documented as having been performed. Although, visual inspections of the containment building have not been documented, the operators have routinely performed inspections as a good operating practice, however, not to comply with Technical Specifications. The failure to properly document the performance of this surveillance requirement has existed since plant construction.
C. Safety Significance The primary concern related to this condition was the potential for loose debris collecting in the containment building sump which could cause restriction of pump suctions during LOCA conditions.
l Prior to a plant bestup following a refueling outage or a maintenance outage, a containment i building visual inspection is performed by the operations staff. The purpose of the inspection is to ensure the containment building and the containment building sump suction lines are free of '
debris and other areas of the building are pruperly prepared for heatup. The visual inspection performed as part of the plant heatup is documented on a fem included in an ANO operations procedure used only during plant heatups. An ANO plant administrative procedure, governing plant housekeeping practices, provides guidance to employees regarding their responsibilities. The procedure states that it is the responsibility of each individual to ensure he removes any tools,
[ equipment, materials, trash or debris upon completion of hit work activity. Since a visual ;
inspection is perforsed prior to a plant heatup which verifles that the entire containment .
building is free of debris, only the work area would t e of concern wha 7 an entry is made with I containment integrity established. Current practices based on the plan 6 housekeeping procedure provide a level of assurance that the affected area of the contoineent building is left in a clean
( condition upon containment 6xit. Therefore, as a result of this condition, no significant safety concerns exist.
L D. Root Cause l
The root cause of this event was procedural inadequacy. During the initial review of Technical Specification surveillence requirements a fors was created to perform a visual inspection of the containment building. The fore was incorporated in a procedure which was used only during plant heatups. When a containment building entry was made with containment building integrity established there was no procedural guidance to use the existing fore or to direct the operator to the plant heatup procedure. The lack of procedural guidance resulted in a failure to properly document and verify that a visual inspection of the affected area in the containment building had been performed when containment integrity was established.
E. Basis for Reportability ~
)
Technical Specification 4.0.3 states that the failure to perform a surveillance requirement within the specified time interval shall constitute a failure to meet the operability requirements for a Limiting Condition for Operation. Since it has not been documented that a visual inspection of the affected areas in the containment building has been performed when a containment building entry was made and containment building integrity established, the operability requirements for the ECCS subsystems were technically not satisfied. Therefore, this event is reportable pursuant to 10CFR50.73(a)(2)(1)(B), operation prohibited by Technical Specifications.
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di Form 1062.01B NRC Fore 366A U.$. Nuclear Regulatory Commission (9 83) . Approved DMB ho. 3150-01D4 i Expires: 8/31/&5 i LICENSEE fvtNT REPORT (LER) TEXT CONTIN 0ATION FACILITY R4ME (1) lDOCKEl NUMBER (2) l .ER WOMBER (6) l PAGE (3) l l l lJequentiall l Revision l Arkansas Nuclear One, Unit Two l l Yearl Number Number l 10151010101 31 61 81 IT 01-- oi 0 1 -- Di ol013lOr1013 TEK1 (If more space is required, use additional NRC Fore 366A's) (17)
F. Corrective Actions Additionel administrative controls will be established to ensure a visual inspection of the affected areas [
in the containment building is performed at the completion of a containment building entry when containment -
integrity is established. This should ensure that the surveillance is properly performed and documented 4A
- required. The procedure revision will be completed by April 15, 1990.
G. Additional Infore.ation Previously reported events in which inadequate procedural guidance resulted in the failure to perform a required Technical Specification surveillance were reported in LERs 50-313/89 032-00, 50-313/89-033-00 and 50 368/86-015-00.
Energy Industry Identification System (EII$) codes are identified in the text 4s [XX). ,
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