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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20045B3021993-06-11011 June 1993 LER 93-001-00:on 930513,discovered That One Channel of Rvlms Inoperable Since Probe Replaced in Oct 1992.On 930507, Discovered That Two Sensors in Rvlms Indicating Wet.Caused by Design Error.Wiring Polarity corrected.W/930611 Ltr ML20024H2281991-05-21021 May 1991 LER 91-003-00:on 910421,actuation of EFW Sys During Plant Heatup Occurred Due to Low Once Through Steam Generator Level.Caused by Leaking Feedwater Recirculation Valve.Plant Startup Procedure OP 1102.02 Will Be revised.W/910521 Ltr ML20024H0861991-05-10010 May 1991 LER 91-002-00:on 910410,inadvertent Actuations of Combined Control Emergency Ventilation Sys Occurred.Caused by Transient Noise Spike.Mod Will Be Completed by 910531 to Install Time Delay in Actuation circuitry.W/910510 Ltr ML20024G9781991-05-10010 May 1991 LER 90-004-01:on 900531,discovered Degraded Fire Barrier Penetration During Insp Per Generic Ltr 86-10.Caused by Failure to Identify Adequate Fire Barrier Seal During 1983 Plant Walkdown.Fire Watch posted.W/910510 Ltr ML20029C3771991-03-22022 March 1991 LER 91-006-00:on 910222,core Protection Calculator Reactor Coolant Sys Flow Channels Not Being Calibrated within Tech Spec.Caused by Personnel Error.Operations Manager Counseled Operators Involved in event.W/910322 Ltr ML20029B1331991-02-27027 February 1991 LER 91-004-00:on 910125,control Room Radiation Monitor Alarm/Trip Setpoint Greater than Normal.Caused by Personnel Error.Operations Manager Will Counsel Shift Supervisors & Night Order Will Be posted.W/910227 Ltr ML20028H6841991-01-21021 January 1991 LER 90-021-00:on 901222,potential RCS Leak Noted in Area of Pressurizer Upper Level Instrument Nozzle.Caused by Pure Water Stress Corrosion Cracking.New Nozzle Installed Into Penetration from Shell OD.W/910121 Ltr ML20043C6801990-05-31031 May 1990 LER 89-025-01:on 891221,identified That Portion of Wall Located in Auxiliary Bldg Had Not Been Previously Identified as Tech Spec Fire Barrier.Caused by Personnel Error.Wall Being Upgraded to Tech Spec status.W/900531 Ltr ML20043C3781990-05-30030 May 1990 LER 90-012-00:on 900430,18 Month Channel Calibr of Liquid Radwaste Effluent Line Flow Monitor Not Performed as Required.Caused by Inadequate Controls to Ensure Followup Actions Taken in Timely Manner.Amends revised.W/900530 Ltr ML20043C0361990-05-23023 May 1990 LER 90-003-01:on 900423,discovered That Incorrect Monitoring Instrumentation for Radiological Effluent Ventilation Sys Utilized to Comply W/Tech Specs.Caused by Mgt Oversight.Logs Process Monitors Will Not Be used.W/900523 Ltr ML20043A7411990-05-17017 May 1990 LER 90-004-01:on 900212,discovered That Backwater Valve in Floor Drain Pipe in Emergency Feedwater Pump Room Missing. Caused by Inadequate Configuration Control.Backwater Pumps Installed & Will Be Included in Maint program.W/900517 Ltr ML20042F7681990-05-0101 May 1990 LER 90-002-01:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Errors in Original Calculation Not Identified.Calibr Procedures revised.W/900501 Ltr ML20042F7751990-05-0101 May 1990 LER 90-010-00:on 900401,personnel Failed to Complete Control Element Assembly Position Log.Caused by Surveillance Program Deficiencies & Lack of Mgt Involvement.Shift Briefing Completed & Procedure Change incorporated.W/900501 Ltr ML20042E1981990-04-10010 April 1990 LER 90-008-00:on 900311,determined That Seal Leakage Test for Containment Personnel Air Lock Had Not Been Performed, Per Tech Specs.Caused by Personnel Error.Procedure Revs Initiated & Personnel counseled.W/900410 Ltr ML20012F5051990-04-0505 April 1990 LER 89-027-00:on 891005,determined That Leakage Rate for Containment Isolation Check Valve in Excess of Leakage Rate Allowed Per Tech Specs.Caused by Loose Weld Slag in Valve Seat Area.Valve Cleaned & reassembled.W/900405 Ltr ML20012F5031990-04-0505 April 1990 LER 90-007-00:on 900306,RCS Charging Line Rendered Inoperable Due to Deficient Piping Support Weld.Caused by Inadequate Work Controls & post-installation Insp Processes. Field Walkdowns & Weld Insps initiated.W/900405 Ltr ML20012F5741990-04-0404 April 1990 LER 90-006-00:on 900305,instrumentation Channels Declared Inoperable,Resulting in Manual Actuation of Reactor Protection Sys.Caused by Procedural Deficiencies.Functional Tests of Log Power Level Channels performed.W/900404 Ltr ML20012C7221990-03-14014 March 1990 LER 90-004-00:on 900212,identified That No Backwater Valve Located in Floor Drain Pipe in One of Emergency Feedwater Pump Rooms.Caused by Inadequate Configuration Control. Valves Installed on 900215.W/900314 Ltr ML20012C1821990-03-12012 March 1990 LER 85-029-00:on 850520,unusual Motor Vibrations Identified on Svc Water Pump 2PM4A.On 861028,high Vibrations Noted on Upper Motor Bearings of Pump 2PM4B.Caused by Improper Installation.New Bearings installed.W/900312 Ltr ML20012B7271990-03-0808 March 1990 LER 89-049-01:on 891220,discovered That Okonite T-95 Tape Not Used to Tape Internal Motor Lead Connections for Main Feedwater Containment Isolation Valves.Caused by Personnel Error.Valves Taped According to Design drawing.W/900308 Ltr ML20012B5701990-03-0505 March 1990 LER 90-003-00:on 900201,failure to Perform Monthly Source Check Surveillance on Three Radiation Process Monitors Occurred.Caused by Inadequate Procedure Change by Personnel. Source Check on Monthly Basis implemented.W/900305 Ltr ML20011F6741990-03-0202 March 1990 LER 90-002-00:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Caused by Incorrect Static Pressure Assumption.Trip Setpoint Bistable increased.W/900302 Ltr ML20011F6781990-03-0101 March 1990 LER 89-026-00:on 891112,gaps in Piping Supports on Supply & Return Piping for Containment Coolers Identified.Caused by Inadequate Design Technique Used in Original Support Design. Shims Added Before Restart from outage.W/900301 Ltr ML20011F5831990-02-27027 February 1990 LER 89-022-01:on 891114,normal Offsite Power Feeder Breaker to 4,160-volt Ac ESF Bus Opened,Resulting in Loss of Power to Bus 2A3.Caused by Inadequate post-maint Test Controls. Test Switch Opened & Job Order changed.W/900227 Ltr ML20011F7311990-02-23023 February 1990 LER 90-001-00:on 900126,identified That Required Visual Insps of Containment Bldg After Entry Made Not Documented as Being Performed.Caused by Inadequate Procedural Guidance. Administrative Controls to Be established.W/900226 Ltr ML20006D7391990-02-0606 February 1990 LER 89-034-01:on 891031,determined That Tech Spec 3.9.1 Had Likely Been Violated Re Independent Circuits of Control Room Emergency Air Conditioning Sys.Caused by Inadequate Guidance Re Equipment Svc Removal.Procedures revised.W/900206 Ltr ML20011E2371990-01-31031 January 1990 LER 89-012-01:on 890626,RCS Backleakage Through Safety Injection Sys Check Valve Occurred Three Times.Caused by Missing Rollpins Which Connect Valve Disc to Valve Disc Shaft.Rollpins Replaced & Valves reassembled.W/900131 Ltr ML20011E2291990-01-31031 January 1990 LER 89-039-01:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Latch Mechanism Missing. Caused by Abnormally High Differential Pressure Across Door. Ventilation Sys Flow Balance performed.W/900131 Ltr ML20011E1451990-01-30030 January 1990 LER 89-024-00:on 891231,loose Terminal in Feedwater Control Sys Cabinet Resulted in Reactor Trip.Caused by Loose Connection on Terminal.Loose Connection Reterminated properly.W/900130 Ltr ML20006C1451990-01-29029 January 1990 LER 89-048-00:on 891228,automatic Reactor Trip & ESF Actuation Occurred as Result of Loss of All Main Feedwater Flow Due to Inadvertent Tripping of Main Feedwater Pump. Caused by Personnel error.O-rings replaced.W/900129 Ltr ML19354E3331990-01-22022 January 1990 LER 89-025-00:on 891221,two Piping Penetrations Located in Barrier Not Surveilled as Required by Tech Specs.Caused by Personnel Error.Fire Watch Posted When Necessary Per Tech Spec.W/900122 Ltr ML20006A8661990-01-22022 January 1990 LER 89-041-00:on 891221,automatic Actuation of Emergency Feedwater Sys Initiated.Caused by Lack of Adequate Procedural Guidance.Valve Positioners CV-2623 & CV-2673 Adjusted & Guidance Procedures developed.W/900122 Ltr ML20006A8671990-01-22022 January 1990 LER 89-042-01:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900122 Ltr ML20005F1551990-01-18018 January 1990 LER 89-023-01:on 891117,noted That Channel a Not Responding to Change in Power Level & Declared Inoperable.Caused by Defective Preamplifier.Evaluation of Sys Design & Channel Functional Test initiated.W/900108 Ltr ML20006B6461990-01-18018 January 1990 LER 89-047-00:on 891219,RCS Temp Increased Above 250 F W/ Oxygen Concentration Greater than Tech Specs Limit.Caused by Inadequate Procedural Guidance.Plant Startup Procedure Revised to Require Chemistry Dept signoff.W/900118 Ltr ML19354D8291990-01-15015 January 1990 LER 89-044-00:on 891214,incorrect Assumptions & Calculational Errors Identified for Low Pressure Injection & Reactor Bldg Spray Pumps When Aligned to Take Suction from Reactor Bldg sump.W/900115 Ltr ML20005G1681990-01-0909 January 1990 LER 89-045-00:on 891210,discovered That U-bolt Supports on Two Containment Isolation Valves in Containment Bldg Not Installed & Pressurizer Sample Lines & Valves Considered Inoperable.Missing U-bolts installed.W/900109 Ltr ML20005F1481990-01-0808 January 1990 LER 89-042-00:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900108 Ltr ML20005F1571990-01-0808 January 1990 LER 89-043-00:on 891208,discovered That Approx 50% of One Nut Ring Half Beneath Reactor Vessel Nozzle Flange Corroded Away.Caused by Gradual Deterioration of Gasket Matl.Design Change implemented.W/900108 Ltr ML20005F2071990-01-0404 January 1990 LER 89-040-00:on 891205 & 06,automatic Actuations of Emergency Diesel Generator Occurred as Result of Loss of Power to 480-volt ESF Bus.Caused by Personnel Error During Bus Transfer.Mgt Briefings conducted.W/900104 Ltr ML20005F0471990-01-0303 January 1990 LER 89-046-00:on 891204,reactor Bldg Isolation Valves Rendered Inoperable Due to Deficient Welds on Piping Supports Which Were Installed During Initial Plant Const. Deficient Supports Repaired Prior to restart.W/900103 Ltr ML20011D2521989-12-18018 December 1989 LER 89-039-00:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Missing Latch Mechanism. Caused by Extensive Use During 56-day Refueling Outage.More Frequent Insps of Door Condition to Be done.W/891218 Ltr ML20011D2501989-12-18018 December 1989 LER 89-023-00:on 891117,approach to Criticality Commenced After Seventh Refueling Outage W/Logarithmic Power Level Channels Inoperable.Caused by Electrical Noise in Circuitry. Defective Preamplifier replaced.W/891218 Ltr ML19351A6731989-12-14014 December 1989 LER 89-022-00:on 891114,inadequate post-maint Test Controls Resulted in de-energizing 4,160 Volt Ac ESFs Electric Bus Uexpectedly.Caused by Inadequate post-maint Test Controls. Job Order Instructions changed.W/891214 Ltr ML19354D5521989-12-14014 December 1989 LER 89-038-00:on 891114,reactor Trip Occurred as Result of Inadvertent Closure of Main Feedwater Isolation Valve.Caused by Personnel Error.Disciplinary Action Taken Against Individual & Senior Mgt Personnel Put on shift.W/891214 Ltr ML19351A4651989-12-11011 December 1989 LER 89-021-00:on 891111,when Low Level Radwaste Water in Waste Condensate Tank Aligned to Be Released,Discovered That Radiation Monitor Inoperable for Duration of Release.Caused by Personnel Error.Procedure revised.W/891211 Ltr ML19332F6171989-12-11011 December 1989 LER 89-037-00:on 891110,reactor Trip Occurred as Result of Inadvertent Grounding of Reactor Protection Sys Power Supply During Surveillance Testing.Caused by Inadequate Procedure. Procedures revised.W/891211 Ltr ML20005D6821989-12-0101 December 1989 LER 89-005-01:on 890518 & 25,damping Board Removed from Penetration Containing Cable Tray.On 890531,voids Noted in Penetration Seals.Caused by Erroneous Vendor Procedures. Penetrations Restored & Procedures revised.W/891201 Ltr ML19332E8611989-11-30030 November 1989 LER 89-034-00:on 891031,control Room Emergency Air Conditioning Sys Rendered Inoperable Due to Removing Independent Circuits from Svc.Caused by Inadequate Guidance.Procedures Revised & Circuits flagged.W/891130 Ltr 1998-10-22
[Table view] Category:RO)
MONTHYEARML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20045B3021993-06-11011 June 1993 LER 93-001-00:on 930513,discovered That One Channel of Rvlms Inoperable Since Probe Replaced in Oct 1992.On 930507, Discovered That Two Sensors in Rvlms Indicating Wet.Caused by Design Error.Wiring Polarity corrected.W/930611 Ltr ML20024H2281991-05-21021 May 1991 LER 91-003-00:on 910421,actuation of EFW Sys During Plant Heatup Occurred Due to Low Once Through Steam Generator Level.Caused by Leaking Feedwater Recirculation Valve.Plant Startup Procedure OP 1102.02 Will Be revised.W/910521 Ltr ML20024H0861991-05-10010 May 1991 LER 91-002-00:on 910410,inadvertent Actuations of Combined Control Emergency Ventilation Sys Occurred.Caused by Transient Noise Spike.Mod Will Be Completed by 910531 to Install Time Delay in Actuation circuitry.W/910510 Ltr ML20024G9781991-05-10010 May 1991 LER 90-004-01:on 900531,discovered Degraded Fire Barrier Penetration During Insp Per Generic Ltr 86-10.Caused by Failure to Identify Adequate Fire Barrier Seal During 1983 Plant Walkdown.Fire Watch posted.W/910510 Ltr ML20029C3771991-03-22022 March 1991 LER 91-006-00:on 910222,core Protection Calculator Reactor Coolant Sys Flow Channels Not Being Calibrated within Tech Spec.Caused by Personnel Error.Operations Manager Counseled Operators Involved in event.W/910322 Ltr ML20029B1331991-02-27027 February 1991 LER 91-004-00:on 910125,control Room Radiation Monitor Alarm/Trip Setpoint Greater than Normal.Caused by Personnel Error.Operations Manager Will Counsel Shift Supervisors & Night Order Will Be posted.W/910227 Ltr ML20028H6841991-01-21021 January 1991 LER 90-021-00:on 901222,potential RCS Leak Noted in Area of Pressurizer Upper Level Instrument Nozzle.Caused by Pure Water Stress Corrosion Cracking.New Nozzle Installed Into Penetration from Shell OD.W/910121 Ltr ML20043C6801990-05-31031 May 1990 LER 89-025-01:on 891221,identified That Portion of Wall Located in Auxiliary Bldg Had Not Been Previously Identified as Tech Spec Fire Barrier.Caused by Personnel Error.Wall Being Upgraded to Tech Spec status.W/900531 Ltr ML20043C3781990-05-30030 May 1990 LER 90-012-00:on 900430,18 Month Channel Calibr of Liquid Radwaste Effluent Line Flow Monitor Not Performed as Required.Caused by Inadequate Controls to Ensure Followup Actions Taken in Timely Manner.Amends revised.W/900530 Ltr ML20043C0361990-05-23023 May 1990 LER 90-003-01:on 900423,discovered That Incorrect Monitoring Instrumentation for Radiological Effluent Ventilation Sys Utilized to Comply W/Tech Specs.Caused by Mgt Oversight.Logs Process Monitors Will Not Be used.W/900523 Ltr ML20043A7411990-05-17017 May 1990 LER 90-004-01:on 900212,discovered That Backwater Valve in Floor Drain Pipe in Emergency Feedwater Pump Room Missing. Caused by Inadequate Configuration Control.Backwater Pumps Installed & Will Be Included in Maint program.W/900517 Ltr ML20042F7681990-05-0101 May 1990 LER 90-002-01:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Errors in Original Calculation Not Identified.Calibr Procedures revised.W/900501 Ltr ML20042F7751990-05-0101 May 1990 LER 90-010-00:on 900401,personnel Failed to Complete Control Element Assembly Position Log.Caused by Surveillance Program Deficiencies & Lack of Mgt Involvement.Shift Briefing Completed & Procedure Change incorporated.W/900501 Ltr ML20042E1981990-04-10010 April 1990 LER 90-008-00:on 900311,determined That Seal Leakage Test for Containment Personnel Air Lock Had Not Been Performed, Per Tech Specs.Caused by Personnel Error.Procedure Revs Initiated & Personnel counseled.W/900410 Ltr ML20012F5051990-04-0505 April 1990 LER 89-027-00:on 891005,determined That Leakage Rate for Containment Isolation Check Valve in Excess of Leakage Rate Allowed Per Tech Specs.Caused by Loose Weld Slag in Valve Seat Area.Valve Cleaned & reassembled.W/900405 Ltr ML20012F5031990-04-0505 April 1990 LER 90-007-00:on 900306,RCS Charging Line Rendered Inoperable Due to Deficient Piping Support Weld.Caused by Inadequate Work Controls & post-installation Insp Processes. Field Walkdowns & Weld Insps initiated.W/900405 Ltr ML20012F5741990-04-0404 April 1990 LER 90-006-00:on 900305,instrumentation Channels Declared Inoperable,Resulting in Manual Actuation of Reactor Protection Sys.Caused by Procedural Deficiencies.Functional Tests of Log Power Level Channels performed.W/900404 Ltr ML20012C7221990-03-14014 March 1990 LER 90-004-00:on 900212,identified That No Backwater Valve Located in Floor Drain Pipe in One of Emergency Feedwater Pump Rooms.Caused by Inadequate Configuration Control. Valves Installed on 900215.W/900314 Ltr ML20012C1821990-03-12012 March 1990 LER 85-029-00:on 850520,unusual Motor Vibrations Identified on Svc Water Pump 2PM4A.On 861028,high Vibrations Noted on Upper Motor Bearings of Pump 2PM4B.Caused by Improper Installation.New Bearings installed.W/900312 Ltr ML20012B7271990-03-0808 March 1990 LER 89-049-01:on 891220,discovered That Okonite T-95 Tape Not Used to Tape Internal Motor Lead Connections for Main Feedwater Containment Isolation Valves.Caused by Personnel Error.Valves Taped According to Design drawing.W/900308 Ltr ML20012B5701990-03-0505 March 1990 LER 90-003-00:on 900201,failure to Perform Monthly Source Check Surveillance on Three Radiation Process Monitors Occurred.Caused by Inadequate Procedure Change by Personnel. Source Check on Monthly Basis implemented.W/900305 Ltr ML20011F6741990-03-0202 March 1990 LER 90-002-00:on 900131,errors Identified in Calculation Used to Establish Calibr Tables for Steam Generator Water Level Transmitters.Caused by Incorrect Static Pressure Assumption.Trip Setpoint Bistable increased.W/900302 Ltr ML20011F6781990-03-0101 March 1990 LER 89-026-00:on 891112,gaps in Piping Supports on Supply & Return Piping for Containment Coolers Identified.Caused by Inadequate Design Technique Used in Original Support Design. Shims Added Before Restart from outage.W/900301 Ltr ML20011F5831990-02-27027 February 1990 LER 89-022-01:on 891114,normal Offsite Power Feeder Breaker to 4,160-volt Ac ESF Bus Opened,Resulting in Loss of Power to Bus 2A3.Caused by Inadequate post-maint Test Controls. Test Switch Opened & Job Order changed.W/900227 Ltr ML20011F7311990-02-23023 February 1990 LER 90-001-00:on 900126,identified That Required Visual Insps of Containment Bldg After Entry Made Not Documented as Being Performed.Caused by Inadequate Procedural Guidance. Administrative Controls to Be established.W/900226 Ltr ML20006D7391990-02-0606 February 1990 LER 89-034-01:on 891031,determined That Tech Spec 3.9.1 Had Likely Been Violated Re Independent Circuits of Control Room Emergency Air Conditioning Sys.Caused by Inadequate Guidance Re Equipment Svc Removal.Procedures revised.W/900206 Ltr ML20011E2371990-01-31031 January 1990 LER 89-012-01:on 890626,RCS Backleakage Through Safety Injection Sys Check Valve Occurred Three Times.Caused by Missing Rollpins Which Connect Valve Disc to Valve Disc Shaft.Rollpins Replaced & Valves reassembled.W/900131 Ltr ML20011E2291990-01-31031 January 1990 LER 89-039-01:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Latch Mechanism Missing. Caused by Abnormally High Differential Pressure Across Door. Ventilation Sys Flow Balance performed.W/900131 Ltr ML20011E1451990-01-30030 January 1990 LER 89-024-00:on 891231,loose Terminal in Feedwater Control Sys Cabinet Resulted in Reactor Trip.Caused by Loose Connection on Terminal.Loose Connection Reterminated properly.W/900130 Ltr ML20006C1451990-01-29029 January 1990 LER 89-048-00:on 891228,automatic Reactor Trip & ESF Actuation Occurred as Result of Loss of All Main Feedwater Flow Due to Inadvertent Tripping of Main Feedwater Pump. Caused by Personnel error.O-rings replaced.W/900129 Ltr ML19354E3331990-01-22022 January 1990 LER 89-025-00:on 891221,two Piping Penetrations Located in Barrier Not Surveilled as Required by Tech Specs.Caused by Personnel Error.Fire Watch Posted When Necessary Per Tech Spec.W/900122 Ltr ML20006A8661990-01-22022 January 1990 LER 89-041-00:on 891221,automatic Actuation of Emergency Feedwater Sys Initiated.Caused by Lack of Adequate Procedural Guidance.Valve Positioners CV-2623 & CV-2673 Adjusted & Guidance Procedures developed.W/900122 Ltr ML20006A8671990-01-22022 January 1990 LER 89-042-01:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900122 Ltr ML20005F1551990-01-18018 January 1990 LER 89-023-01:on 891117,noted That Channel a Not Responding to Change in Power Level & Declared Inoperable.Caused by Defective Preamplifier.Evaluation of Sys Design & Channel Functional Test initiated.W/900108 Ltr ML20006B6461990-01-18018 January 1990 LER 89-047-00:on 891219,RCS Temp Increased Above 250 F W/ Oxygen Concentration Greater than Tech Specs Limit.Caused by Inadequate Procedural Guidance.Plant Startup Procedure Revised to Require Chemistry Dept signoff.W/900118 Ltr ML19354D8291990-01-15015 January 1990 LER 89-044-00:on 891214,incorrect Assumptions & Calculational Errors Identified for Low Pressure Injection & Reactor Bldg Spray Pumps When Aligned to Take Suction from Reactor Bldg sump.W/900115 Ltr ML20005G1681990-01-0909 January 1990 LER 89-045-00:on 891210,discovered That U-bolt Supports on Two Containment Isolation Valves in Containment Bldg Not Installed & Pressurizer Sample Lines & Valves Considered Inoperable.Missing U-bolts installed.W/900109 Ltr ML20005F1481990-01-0808 January 1990 LER 89-042-00:on 891209,inadvertent Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Keying of Hand Held Radio in Vicinity of Chlorine Monitors by Technician.Technician counseled.W/900108 Ltr ML20005F1571990-01-0808 January 1990 LER 89-043-00:on 891208,discovered That Approx 50% of One Nut Ring Half Beneath Reactor Vessel Nozzle Flange Corroded Away.Caused by Gradual Deterioration of Gasket Matl.Design Change implemented.W/900108 Ltr ML20005F2071990-01-0404 January 1990 LER 89-040-00:on 891205 & 06,automatic Actuations of Emergency Diesel Generator Occurred as Result of Loss of Power to 480-volt ESF Bus.Caused by Personnel Error During Bus Transfer.Mgt Briefings conducted.W/900104 Ltr ML20005F0471990-01-0303 January 1990 LER 89-046-00:on 891204,reactor Bldg Isolation Valves Rendered Inoperable Due to Deficient Welds on Piping Supports Which Were Installed During Initial Plant Const. Deficient Supports Repaired Prior to restart.W/900103 Ltr ML20011D2521989-12-18018 December 1989 LER 89-039-00:on 891116,discovered That Door for Upper North Electrical Penetration Room Open & Missing Latch Mechanism. Caused by Extensive Use During 56-day Refueling Outage.More Frequent Insps of Door Condition to Be done.W/891218 Ltr ML20011D2501989-12-18018 December 1989 LER 89-023-00:on 891117,approach to Criticality Commenced After Seventh Refueling Outage W/Logarithmic Power Level Channels Inoperable.Caused by Electrical Noise in Circuitry. Defective Preamplifier replaced.W/891218 Ltr ML19351A6731989-12-14014 December 1989 LER 89-022-00:on 891114,inadequate post-maint Test Controls Resulted in de-energizing 4,160 Volt Ac ESFs Electric Bus Uexpectedly.Caused by Inadequate post-maint Test Controls. Job Order Instructions changed.W/891214 Ltr ML19354D5521989-12-14014 December 1989 LER 89-038-00:on 891114,reactor Trip Occurred as Result of Inadvertent Closure of Main Feedwater Isolation Valve.Caused by Personnel Error.Disciplinary Action Taken Against Individual & Senior Mgt Personnel Put on shift.W/891214 Ltr ML19351A4651989-12-11011 December 1989 LER 89-021-00:on 891111,when Low Level Radwaste Water in Waste Condensate Tank Aligned to Be Released,Discovered That Radiation Monitor Inoperable for Duration of Release.Caused by Personnel Error.Procedure revised.W/891211 Ltr ML19332F6171989-12-11011 December 1989 LER 89-037-00:on 891110,reactor Trip Occurred as Result of Inadvertent Grounding of Reactor Protection Sys Power Supply During Surveillance Testing.Caused by Inadequate Procedure. Procedures revised.W/891211 Ltr ML20005D6821989-12-0101 December 1989 LER 89-005-01:on 890518 & 25,damping Board Removed from Penetration Containing Cable Tray.On 890531,voids Noted in Penetration Seals.Caused by Erroneous Vendor Procedures. Penetrations Restored & Procedures revised.W/891201 Ltr ML19332E8611989-11-30030 November 1989 LER 89-034-00:on 891031,control Room Emergency Air Conditioning Sys Rendered Inoperable Due to Removing Independent Circuits from Svc.Caused by Inadequate Guidance.Procedures Revised & Circuits flagged.W/891130 Ltr 1998-10-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L8931999-10-31031 October 1999 Rev 1 to BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs ML20212L1141999-10-0101 October 1999 Safety Evaluation Granting Request for Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c 0CAN109902, Monthly Operating Repts for Sept 1999 for Arkansas Nuclear One,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Arkansas Nuclear One,Units 1 & 2.With ML20216J6271999-09-27027 September 1999 Rev 0 to CALC-98-R-1020-04, ANO-1 Cycle 16 Colr ML20212F5261999-09-22022 September 1999 SER Approving Request Reliefs 1-98-001 & 1-98-200,parts 1,2 & 3 for Second 10-year ISI Interval at Arkansas Nuclear One, Unit 1 0CAN099907, Monthly Operating Repts for Aug 1999 for Ano,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ano,Units 1 & 2. with ML20211F4281999-08-25025 August 1999 Safety Evaluation Concluding That Licensee Provided Acceptable Alternative to Requirements of ASME Code Section XI & That Authorization of Proposed Alternative Would Provide Acceptable Level of Quality & Safety 0CAN089904, Monthly Operating Repts for July 1999 for Ano,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ano,Units 1 & 2. with ML20210K8831999-07-29029 July 1999 Non-proprietary Addendum B to BAW-2346P,Rev 0 Re ANO-1 Specific MSLB Leak Rates 0CAN079903, Monthly Operating Repts for June 1999 for Ano,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Ano,Units 1 & 2. with ML20207E7231999-06-0202 June 1999 Safety Evaluation Authorizing Proposed Alternative Exam Methods Proposed in Alternative Exam 99-0-002 to Perform General Visual Exam of Accessible Areas & Detailed Visual Exam of Areas Determined to Be Suspect ML20196A0191999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Arkansas Nuclear One,Units 1 & 2.With ML20196A6251999-05-31031 May 1999 Non-proprietary Rev 0 to TR BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs ML20195D1991999-05-28028 May 1999 Probabilistic Operational Assessment of ANO-2 SG Tubing for Cycle 14 ML20206M7711999-05-11011 May 1999 SER Accepting Relief Request from ASME Code Section XI Requirements for Plant,Units 1 & 2 0CAN059903, Monthly Operating Repts for Apr 1999 for Ano,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ano,Units 1 & 2. with ML20206F0691999-04-29029 April 1999 Safety Evaluation Accepting Licensee Re ISI Plan for Third 10-year Interval & Associated Requests for Alternatives for Plant,Unit 1 ML20205M6941999-04-12012 April 1999 Safety Evaluation Granting Relief for Second 10-yr Inservice Inspection Interval for Plant,Unit 1 ML20205D6061999-03-31031 March 1999 Safety Evaluation Supporting Licensee Proposed Approach Acceptable to Perform Future Structural Integrity & Operability Assessments of Carbon Steel ML20205R6351999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Ano,Units 1 & 2. with ML20205D4711999-03-26026 March 1999 SER Accepting Util Proposed Alternative to Employ Alternative Welding Matls of Code Cases 2142-1 & 2143-1 for Reactor Coolant System to Facilitate Replacement of Steam Generators at Arkansas Nuclear One,Unit 2 ML20204B1861999-03-15015 March 1999 Safety Evaluation Authorizing Licensee Request for Alternative to Augmented Exam of Certain Reactor Vessel Shell Welds,Per Provisions of 10CFR50.55a(g)(6)(ii)(A)(5) 0CAN039904, Monthly Operating Repts for Feb 1999 for Ano,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Ano,Units 1 & 2. with ML20212G6381999-02-25025 February 1999 Ano,Unit 2 10CFR50.59 Rept for 980411-990225 ML20203E4891999-02-11011 February 1999 Rev 1 to 97-R-2018-03, ANO-2,COLR for Cycle 14 ML20199F0351998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Ano,Units 1 & 2 ML20198M7841998-12-29029 December 1998 SER Accepting Util Proposal to Use ASME Code Case N-578 as Alternative to ASME Code Section Xi,Table IWX-2500 for Arkansas Nuclear One,Unit 2 0CAN129805, LER 98-S02-00:on 981124,security Officer Found Not to Have Had Control of Weapon for Period of Approx 3 Minutes Due to Inadequate self-checking to Ensure That Weapon Remained Secure.All Security Officers Briefed.With1998-12-11011 December 1998 LER 98-S02-00:on 981124,security Officer Found Not to Have Had Control of Weapon for Period of Approx 3 Minutes Due to Inadequate self-checking to Ensure That Weapon Remained Secure.All Security Officers Briefed.With ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20198D2441998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Ano,Units 1 & 2. with ML20199F7401998-11-16016 November 1998 Rev 9 to ANO-1 Simulator Operability Test,Year 9 (First Cycle) ML20195B4801998-11-0707 November 1998 Rev 20 to ANO QA Manual Operations ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program 0CAN119808, Monthly Operating Repts for Oct 1998 for Ano,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Ano,Units 1 & 2. with ML20197H0741998-10-29029 October 1998 Rev 1 to Third Interval ISI Program for ANO-1 ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual ML17335A7641998-10-22022 October 1998 LER 98-004-00:on 980923,inadvertent Actuation of Efs Occurred During Surveillance Testing.Caused by Personnel Error.Personnel Involved with Event Were Counseled & Procedure Changes Were Implemented.With 981022 Ltr ML20154J2471998-10-0909 October 1998 SER Accepting Inservice Testing Program,Third ten-year Interval for License DPR-51,Arkansas Nuclear One,Unit 1 0CAN109806, Monthly Operating Repts for Sept 1998 for ANO Units 1 & 2. with1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for ANO Units 1 & 2. with ML20154E2171998-09-28028 September 1998 Follow-up Part 21 Rept Re Defect with 1200AC & 1200BC Recorders Built Under Westronics 10CFR50 App B Program. Westronics Has Notified Bvps,Ano & RBS & Is Currently Making Arrangements to Implement Design Mods 0CAN099803, Monthly Operating Repts for Aug 1998 for ANO Units 1 & 2. with1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for ANO Units 1 & 2. with ML20237B7671998-08-19019 August 1998 ANO REX-98 Exercise for 980819 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20236X2351998-08-0505 August 1998 Part 21 Rept Re Defect Associated W/Westronics 1200AC & 1200BC Recorders Built Under Westronics 10CFR50,App B Program.Beaver Valley,Arkansas Nuclear One & River Bend Station Notified.Design Mod Is Being Developed 0CAN089804, Monthly Operating Repts for July 1998 for Ano,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Ano,Units 1 & 2 ML20196C7831998-07-30030 July 1998 Summary Rept of Results for ASME Class 1 & 2 Pressure Retaining Components & Support for ANO-1 ML20155H7161998-07-15015 July 1998 Rev 1 to 96-R-2030-02, Revised Reactor Vessel Fluence Determination ML20236R0531998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Ano,Units 1 & 2 ML20249B7791998-06-22022 June 1998 Part 21 Rept Re Findings,Resolutions & Conclusions Re Failure of Safety Related Siemens 4KV,350 MVA,1200 a Circuit Breakers to Latch Closed ML20249B5091998-06-15015 June 1998 SG ISI Results for Fourteenth Refueling Outage 1999-09-30
[Table view] |
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I jl Atkin6H Power & 13ght Company l ,/ A Aansas Nathw Om:
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L March 12, 1990 2CANO39008 l
U. S. Nuclear Regulatory Commission Document Control Desk Mail Station P1-137 Washington, D. C. 20555
SUBJECT:
Arkansas Nuclear One - Unit 2 Docket No. 50-368 License No. NPF-6 Licensee Event Report No. 50-368/85-029-00 Gentlemen:
In accordance with 10CFR50.73(a)(2)(v), attached is the ' subject report- '
concerning inadequate quality control:by'the vendor which resulted in the !
improper installation of service water pump motor bearings. This caused a condition which could have prevented the fulfillment of the safety function of the Service Water system.
Very truly yours, arly C. Ewing General Manager, Technical Support l and Assessment t ECE/DM/abw cc: Regional Administrator Region IV U. S. Nuclear Regulatory Commission
, 611 Ryan Plaza Drive, Suite 1000 Arlington, TX 76011 INP0 Records Center Suite 1500 '
1100 Circle 75 Parkway Atlanta, GA 30339-3064 j,'gRo3200240 900312 g ADOCK 05000368 2
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Form 1062.01A
' NRC Fem '36'6 U.S. Nuclear Regulatory Commission
.(9 83) e proved OM8 No. 3150 0104 L1CENSEE EVENT REPORT (L E R)
FACILITY NAME (1) Arkansas huclear One, Unit Two IDDCAET NUMBER (2) lFAGE (3) 10151010101 31 61 Bill 0Fl013 TITLE (4) Inadequate Quality Control by tee ** Vendor Resulted in Improper Instal?ation of Service Water Pump Motor tB arings Causing a Condition Which Could Have Prevented the Fulfillment of the Safety Tunction of the Service Water System EVENT DATE (5) ER NUMBER (61 REPORT DATE (7) OTHER FACILII]E5 INVOLVED (B) 1 Jequentiali l Revision Month Day Year Year Number Number Month Day Facility Names Year Docket Number (sl 0 b 0 0 0
_ 01 5 21 0 8 5 81 5 --
- 01 21 9 -I 01 0 01 3" 11 21 91 01 0 5 0 0 0 OPERA"ING TH;5 REPORT 15 5UBMITTED PUR5UANT O THE REQUIREMENT 5 OF 10 CFR 5:
MODE L9) 5 (Check one or more of the follt. wino) (11)
F0wtR 20.402(b) 20.40b(c)
LEVEL
~
o~, 50.36(c)(1) i 50.73(a (2)(iv) l l 73.71(b)
~ L 20.405(a)(1)(1) ~ ;
~7 50.73(a (2)(v) ~l 73.71(c)
(10) 1 01010 20.405(a) 1)(11) ~1 50.36(c)(2)
~
~l Other ($pecify in l~~l 50.73(a)(2)(vii)
- 20.405(a) 1)(111) ~~
1 50.73(a)(2)(i) ~
I 50.73(a (vitt (A) Abstract below and
~ 20.405(a)(1)(lv) ~ l 50.73(a)(2)(11) '"~ $0.73(a (viii (B) in Text NRC Fore 20.405(a)(1)(v) l 50.73(a)(2)(4'i) $0.73(a)(2)(x) 3664)
LICEN5EE CONTALT FOR THIS LER (12)
Name Telephone humber Area Dana Millar, Nuclear $afety and Licensing Specialist , Code
' 51011 916f41-13111010 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (L3)
Reportablei l .
l Reportable,I Caust System Component Manufacturer to NPRDS Cause System Component Manufacturer. to NPRD$
0 Bl i NI Of f GI 61 81 3 i l' j l l l l 1 i
I l l I l l 1 1 I I i I I i l l l SUPPLEMEN" REPORT EXPECTFD (14) EXPECTED Month Day tear SUBMIS$10N ,
l~l Yes (if ves. Complete Expected Submission Date) lIl No DATE (15) I l I i AB5TRACI (Limit to 1400 spaces, i.e. , approximately fif teen single space typewristen lines) (: 6)
As a result of a detailed review of the Service Water (SW) system during an NRC inspection, Arkansas Nuclear One (ANO) has performed a historical review of these events and conservatively detemin6J them to be reportable. On April 10, 1985, a motor, which had newly installed bearings and had been rewound by the vendor, General Electric (GE), was installed on 'A' SW pump (2P4A). After approximately 40 days of pump operation on May 20, 1985, unusual motor vibrations were identified on 2PM4A. It was determined that the upper motor bearings were degraded. The bearings were replaced and the pump returned to service on May 21, 1985. On May 25, 1985, a motor, which GE had returned after rewinding and replacing the motor bearings, was installed on 2P48. On October 28, 1986, high vibrations were identified on the upper actor bearings of 2PM4B. The bearings which were degraded were replaced and the pump returned to service. The root cause of the failure of the bearings on 2PM4A was the installation of the incorrect bearings by CE at the service facility. The failure of the bearings in 2PM4B was due to improper {
installation (incorrect orientation) of the bearings at the GE service facility. Bearing replacements have been performed by AND maintenance personnel since 1985. In each failure the redundant train of SW was avaliable to shutdown the plant, therefore, this event was not safety significant.
i
Form 1062.01B NRC Fem 366A ** U.S. Nuclear Regulatory Commission (9 83) Approved DMB No. 3150-0104 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1) lDOCAET NUMBER (2) l LER NUMBER (6) l FAGE (3) l l l 15tquentiall l Revision!
Arkansas Nuclear One, Unit Two l l Year Number Number l 1015I010101 31 61 81 61 F --
01 21 9 --
01 0101210F1013 ItU (If more space is required, use additional NRC Form 366A's) (17)
A. Plant $tatus At the time of occurrence of this event. Arkansas Nuclear One Unit Two (ANO-2) was operating in Mode 5 (Cold Shutdown). A plant heatup was in progress from 2R4 refueling outage (March 15, 1985 to May 26, 1985).
B. Event Description ,
The Service Water (SW) system [BI) consists of two independent, but interconnected, seismic Category 1, redundant flow paths which furnish cooling water to two independent trains of Engineered Safety Feature (ESF) equipment under normal and emergency conditions. Three pumps are provided such that each is capable of supplying 100 percent of the required cooling water supply for one train of ESF equipment during a Design Basis Accident (i.e., Loss of Coolant Accident with a Concurrent Loss of Offsite Power). Examples of E!F systems supplied with SW include: Containment Cooling (BK), Emergency Diesel Generator (EK), High Pressure Safety injection (BQ), and Low Pressurs SafetyInjection[EP). The normal water supply to the SW system is from the Lake Dardanelle Reservoir.
The SW pump motors are vertical high thrust motors manufactured by General Electric (CE) [Gef3).
The motors are designed with two upper bearings mounted in tendem for a high continuous downward thrust application and with a lower bearing which functions as a guide bearing. The upper bearings are angular contact ball bearings and the lower bearing is a radial bearing. The motor is designed for a continuous downward thrust and a momentary upthrust.
On April 10, 1985, 6 motor, which had newly installed baurings and had been rewound by the vendor L (CE), was installed on 2P4A and the pump was placed in service. After approximately forty days of
, pump operation on May 20, 1985, unusual vibrations were identified on 'A' SW pump motor (2PM4A).
l The pump, which was running at the time, was secured. Af ter an inspection it was determined that j the upper motor bearings had degraded causing the high vibrations. A subsequent evaluation revealed that the incorrect bearings had been installed in the motor during work performed at the
! GE service facility. The upper motor bearings were replaced with the correct bearings and the pump l returned to service on May 21, 1985.
l t
On May 25, 1985, a motor, which GE had returned af ter rewinding and replacing the motor bearings, was installed on 2P4B. With the plant operating in Mode 1. on October 28, 1986, high vibrations l were identified on the upper motor bearings of 2PM48. The bearings which were degraded were replaced and the pump returned to service.
C. Safety Significance The SW system serves two identical full capacity trains of ESF equipment. Only one train of ESF equipseent is required for shutdown of the plant af ter any postulated accident condition. Each $W I system train is capable of supplying 100 percent of the required cooling water flows thus meeting l the single failure criterion. If one SW pump falls, the standby pump, if available, may be l brought into service to provide 100 percent of the required cooling water flow for that train.
In the May 1985 event and October 1986 event with the failure of the upper motor bearings on 2PM4A and 2PM48, respectively, only one train of the SW system was affected. If a failure of a SW pump on the redundant train had occurred, this event would be considered safety significant.
However, one train of SW remained operable throughout both events, therefore, this event was not l safety significant.
I D. Root Cause The root cause of the failure (May 1985) of the upper motor bearings on 2PM4A was that the incorrect motor bearings were installed by GE apparently due to inadequate quality control measures at the service facility.
The cause of the October 1986 failure of the upper motor bearings on 2PM4B was also attributed to inadequate quality control by GE. When the motor was received from GE and installed in May 1985, the upper motor bearings had been installed in the incorrect orientation.
E
Fore 1062.01B NRC Fore 366A' ', . U.S. huelear Regulatory Commission (9-83) Approved OMB No. 3150-01D4 Expires: 8/31/85 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY KAME (1) lDOCAET NUMBER (2) l ;[R NOMF.f R (6) l PAGE (3) l l l lJequential '
l Revision)
Arkansas Nuclear One, Unit Two i l_Yearl Number Number l 10I51010f01 31 61 81 81 bi-- 01 21 9 --
01 Ol01310F1013 TEXT (If more space is. required, use edditional NRC Form 366A's) (17)
E. Basis for Reportability As a result of a detailed review of the $V system during an NRC inspection, AND performed a historical review of these events. On February 9, 1990, these events were conservatively determined to be reportable pursuant to 10CFR50.73(a)(2)(v) as a condition that alone could have prevented the fulfillment of the safety function of the SW system. The failure of a train of the SW system results in a loss of a full train of ESF equipment.
F. Corrective Action
, The correct bearings were installed in 2PM4A after the bearing failures. The bearings in 2PM4B were installed in the correct orientation af ter the bearing f ailures.
The pump motors were sent to the GE service facility for rewinding of the motors. AND also requested that new bearings be installed. Af ter the beering f ailure (May 1985 event) AND apparently did not notify GE of the installation of the incorrect bearings, therefore, 90 actions were taken by CE. At the time of occurrence CE's tuality assurance program was acceptable. The AND Quality Assurance group will evaluate the GE quality assurance program specific to this situation for generic implications. The results of the evaluation will be completed by June 1,1990. Maintenance activities on the $W pump motors (i.e., bearing replacement) have been performed by AND maintenance personnel since the May 1985 and October 1986 bearing failures.
Following the failure of the upper motor bearings on 2PM4B which had been serviced by GE, the GE designers were consulted. It was concluded after further Investigation that the SW pump motors were designed for a face to back bearing orientation. This design configuration allows for two load carrying surfaces for the downward thrusts experienced by the bearings. The original ANO maintenance procedure for bearing installation in the SW pump motors did not depict a specific orientation for the installation of the bearings. The standard maintenance practice for bearing installation was to place the new bearings in the motor in the same orientation as the old bearings were found. This did not provide an assurance that the bearings were being properly installed.
The AND maintenance procedures for bearing installation in the SW pump motors were revised in October 1986 to reflect the correct orientation for bearing installation and to provide an assurance that the bearings would be correctly installed in the future.
G. Additional Information
+There are no previously reported events concerning incorrect bearing installations on 5W pump motors.
Energy Industry Identificotion System (Ell 5) codes are identified in the text as (XX].
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